Tag Archives: staining

Refreshing a Comoy’s Made in London, England Bent Bulldog


Blog by Dal Stanton

I saw this Comoy’s Bent Bulldog as a charity listing on eBay for the Akron Art Museum, in Akron, Ohio.  The seller, like me, was providing pipes for a good cause and I like that.  I also liked the Bulldog I saw in the pictures the seller provided and by the description, it seemed the seller was a pipe person.  The nuts and bolts description:

A classic bulldog! About 5 1/4” long, bowl is 1 1/2” tall, 1 5/8” wide tapering to 1 1/8” at rim. ID 13/16”, depth 1 5/16”. Marked on one side of shank COMOY’S, other side MADE IN LONDON ENGLAND in circular fashion 4097, beneath shank a capital H. A capital C stamped on side of bit. No other marks detected.

Diamond saddle bit is well-seated push fit, cleaned and polished, showing some bite wear but no holes through. Some oxidation as well. Stummel is well hand worn and smoothed, some dings and scratches, scorch on rim, light cake in bowl. Though the pipe is smokable as is, this one has the possibility of being a real beauty with some TLC!

I took the gambit dangled in the last sentence regarding this Bulldog’s possible condition with some TLC.  My bid on the auction block was sufficient, I supported the Akron Art Museum, and now this Comoy’s Bent Bulldog is on the worktable here in Sofia, Bulgaria, on track to benefit the Daughters of Bulgaria, my favorite cause.  This was the second pipe that Stephen commissioned along with a Custom-Bilt Rusticated Panel.  Here’s the picture I saw on eBay which got Stephen’s attention in the For ‘Pipe Dreamers’ Only! collection:Now on my worktable, I take more pictures to get a closer look at the condition of this Comoy’s Bent Bulldog. The nomenclature on the Bulldog’s diamond shank is clear.  On the upper left shank is stamped ‘Comoy’s’.  The right upper shank has encircled, ‘MADE’ with ‘IN’ in the center and ‘LONDON’ on the bottom.  Underneath the circle is ‘ENGLAND’ in straight script.  To the right is shape number ‘409 7’.  Underneath this on the lower right shank panel is stamped ‘H’.  All indicators of the nomenclature point to a Cadogan era pipe which began in 1979 with the merger absorbing Comoy’s.  The simple ‘C’ stem stamp confirms this without the classic 3 piece inlaid ‘C’.  The shape number of 409 has historically indicated a Bulldog on earlier shape charts with a slight quarter bend.  The addition of the ‘7’ on this Bulldog I’m not clear on this, except that during the Cadogan era they added a 4th number to the shapes according to the Pipepedia article on shapes. I would say that this Comoy’s Bent Bulldog has been lovingly enjoyed over the years.  He’s got quite a few scrapes and bruises for the wear, mainly on his dome and circling the double grooves.  I took quite a few pictures of these above.  I’ll need to do some repairs especially on the back side of the dome where there are several small concentrated dents.  The front of the rim has been scorched from lighting practices it appears.  The dome grooves need to be cleaned and I detect a few chips of briar on the back-right side along the grooves.  Also, of interest are two huge fills on the right side of the bowl as it tapers down.  I’ll need to take a good long look at these.  The stem has oxidation and typical tooth chatter and compression dents on the button lip and just before the button.  The former steward was a clencher.

I begin the restoration of this Comoy’s Bulldog by placing the stem in a soak of Before & After Deoxidizer along with other pipes and stems in the queue.  Whoops, I include the original seller’s pictures – I forgot to take pictures of the original stem’s condition before putting the stem into the soak. After some hours of soaking, I remove the Bulldog stem and using a cotton cloth wetted with alcohol, I wipe down the stem removing the raised oxidation.  I follow this by wetting a cotton pad with light paraffin oil (mineral oil) and continue to wipe off the oxidation and the oil helps rejuvenate the vulcanite.After the soak wiping and the stem dries, I can still detect oxidation on the stem which requires more attention.  Before I start sanding the stem, I use Before & After Fine and Extra Fine Polishes to work on the oxidation.  It is advertised to continue the raising process of oxidation.  I start first with the Fine Polish by putting some on my finger and rubbing it in the vulcanite.  I also work it in well around the ‘C’ stamping to clean it more.  After applying, I allow it to stand for some time and then wipe off.  I do the same with the Extra Fine Polish.  After I’ve finished, I still see a deep greenish hue indicating the oxidation is still holding on.  The last picture below tries to capture what I see with the naked eye – it doesn’t do a very good job! One more noninvasive approach to the oxidation I’ll try.  I scrub the stem surface using Magic Eraser.  After working the white sponge over the entire surface, it did do a good job.  More oxidation was removed, but not enough to make me happy!  I still see oxidation especially on the ‘saddle’ of the saddle stem.  The pictures show the progression.Next, I sand the stem starting first with 240 grit paper.  I do not like going through the fine tune buffing with micromesh pads and start seeing oxidation!  So, I sand the entire stem, avoiding the Comoy’s ‘C’ stamping.  I also use at disc to sand against at the stank side of the stem.  The disc helps to guard against shouldering the stem so that the edges are not sharp as the stem joins the shank.  This sanding is primarily for dealing with the oxidation.  In the pictures below, you can see the bit area compressions that are left untouched by the sanding.Before proceeding further with the sanding of the stem, I use the heating method to raise the compressions in the vulcanite in the bit area.  Using a Bic lighter, I paint the bit and button to heat the vulcanite which causes it to expand.  The hope is that this will cause the indentations perhaps to go away or lessen in their impact so that they will then sand out more easily. After painting the bit with the open flame, it helped to minimize some, but it did not erase the dents and compressions on the bit and on the button lips.  I follow with a flat needle file to file the button to refresh and shape the edges.  I follow again with 240 grit paper continuing to sand the dents on the bit.  Using the Bic lighter to raise the dents helps and I’m able to sand out all the dents and compressions from biting. Before proceeding further with the sanding of the stem, I use the heating method to raise the compressions in the vulcanite in the bit area.  Using a Bic lighter, I paint the bit and button to heat the vulcanite which causes it to expand.  The hope is that this will cause the indentations perhaps to go away or lessen in their impact so that they will then sand out more easily. After painting the bit with the open flame, it helped to minimize some, but it did not erase the dents and compressions on the bit and on the button lips.  I follow with a flat needle file to file the button to refresh and shape the edges.  I follow again with 240 grit paper continuing to sand the dents on the bit.  Using the Bic lighter to raise the dents helps and I’m able to sand out all the dents and compressions from biting.  Next, I wet sand the entire stem using 600 grade paper and follow this by buffing with 0000 steel wool. One last thing at this point before turning to the stummel, I give the stem a coat of light paraffin oil to help revitalize it.  I put the stem aside to absorb the oil and dry. With the stummel in hand, I begin the internal cleaning by reaming the light cake build up in the chamber.  I use 3 of the 4 blade heads available from the Pipnet Reaming Kit.  I then use the Savinelli Fitsall Pipe Tool to reach the hard to reach places in the chamber.  I then sand the chamber with 240 grade paper wrapped around a Sharpie Pen followed by wiping the bowl with a cotton pad wetted with alcohol to clean the carbon dust left behind.  Inspection of the chamber reveals some heat fissures on the floor of the chamber.  There also appears to be a small fissure creeping up just above the draft hole.  I take a few pictures that show what I’m seeing.  Are these fissures severe enough to warrant a durable patch or perhaps apply a pipe mud to enhance the growth of a protective cake?  That’s what I’ll be considering.  Continuing the cleaning, I use undiluted Murphy’s Soap on the external briar surface.  To work on the grit lodged in the grooves I use a bristled tooth brush.  I also use a brass wire brush to work around the dome and rim to clear away the old oils. Using a sharp dental probe, I painstakingly clean both dome groves, scraping packed dirt out.  I’m careful not to jump ‘track’ out of the grooves and scratching the briar surface.  The picture shows the cleaning progress. With the externals cleaned up, I turn now to the internal mortise and airway.  Using pipe cleaners and cotton buds dipped in isopropyl 95% I go to work. I quicken the work by scraping the mortise with a dental spatula.  In time, the cotton buds and pipe cleaners were coming out clean.  I’ll continue cleaning later using a kosher salt and alcohol soak.Turning again to the stummel surface, the rim and dome cleaned up well but show the dents and pockets from knocks and drops.  There remains a scorched area at the front of the rim/dome area.  There are small chips in several places around the circumference of the dome grooves.  I believe they’re all too small to patch, but with sanding I’m hoping that most should disappear or be minimized.  The most daunting aspect of the briar landscape is a huge, double fill patch on the right lower side of the stummel.  I take two pictures of the fills to show the position and a super close-up to show the appearance of the fills.  I poked the fills with a dental probe and both fills are rock solid.  Yet, as the close-up picture reveals, there are small air pocket holes in the fills and gaping around the fills.  I’ll leave the fills in place but touch them up with thin, clear CA glue and then sand to blend.  These fills will pretty well drive the boat regarding the finished look of the Comoy’s Bulldog.  The finish needs to be darker in order to mask the fills as much as possible, though even a dark stain will not hide these giants.   Looking again around the dome grooves, on the back-right quadrant there may be at least 2 candidates for a patch before sanding.  I take a picture of this area.  To the top left of the groove chips, there are also a few small holes that I’ll fill with a spot-drop of CA glue.  In this picture there are also two other small fills that seem to be in good shape.Before I begin sanding and patching, I start from the top and work my way down!  Topping the stummel will re-define the rim and address the front quadrant of the rim/dome where the former burn damage has thinned the rim.  I take some pictures to show these issues and mark the start. I put 240 grade paper on the chopping board and rotate the inverted stummel several times, checking as I go to make sure I’m staying level and not leaning into soft spots in the briar. When enough of the top is removed, I then switch the paper to 600 grade paper and turn the stummel a few more rotations. I take pictures to show the progress.  Now to the patching party!  I first wipe the stummel with a cotton pad wetted with alcohol to clean the area. I start with the two large fills by spot dropping a small amount of thin CA glue over the fills and spreading the glue over the entire fill – filling the pockets and gaps.  To move the work along faster, since these are not ‘weight bearing’ patches, I use an accelerator to quicken the curing process.   For the groove patch, I insert a piece of an index card into the groove to create a flow barrier for the CA glue.  I then spot-drop a small amount of CA glue slightly above the chip and draw the glue over the chipped area with a toothpick.  Again, I use an accelerator to solidify the glue.  After a few minutes, I pull the index card away and use a sharp dental probe to make sure the groove is clear of CA glue seepage.  Next, I apply small drops to four other small pits near the grooves and above them – again, I use an accelerator.  I decide also to apply a small drop to the right of the primary groove repair.   The repairs look a mess now, but I’m hopeful that the sanding will prove to reveal a more pleasing surface!Next, I begin the filing and sanding of the two large fill patches down to the surface level.  I use a flat needle file to do this initially when the patch mound is more distinct, then follow with 240 grade paper as the sanding nears the briar surface.  The gaps and pits in the original patch filled nicely, blending better with the surrounding briar.To both clean and sharpen the grooves at the groove patch repair, I insert 240 grade paper into the groove itself.  The groove is only large enough to accommodate a single sheet, so I must flip the paper to sand both the upper and lower edges of the groove.  I use a sawing motion with the paper while in the groove and I flex the paper up to apply a little more sanding action to the groove edge.  This technique does a good job redefining and cleaning up groove edges, especially at the point of the CA glue repair.After filing, sanding the groove patch repairs, and ‘groove sanding’ the groove repair looks great!  The patch has blended, and the groove is cleaner and smarter.Next, I move on to filing and sanding the 4 patches to the left of the groove repair on the dome.  I file the patch mounds down until near the briar surface and then take over with 240 grit paper.  I sand the area of the patches to blend.  It looks good – not pristine, but much less ragged!  The battered stummel is showing some signs of life!I follow by ‘groove sanding’ this area.  I like the results of this technique, so I decide to continue the groove sanding around the entire circumference of the dome for both the upper and lower grooves.  Since I’m able only to do one directional sanding on the grooves, it requires four circuits around the dome to do the job!  I refined the technique as I work – by flexing the paper somewhat I can sand more directly chips encountered on the groove edge as I slowly work around the dome.  The pictures show the groove sanding progress and results – much cleaner and crisper for this Comoy’s Bulldog! I continue preparing the external briar surface by sponge sanding starting first with the coarse sanding sponge.  I then use a medium grade sponge then finish with a light grade sanding sponge.  I avoid totally the upper shank panels with the nomenclature.  Sanding sponges help to clean the surface of the minor nicks and cuts and soften the look without an overly intrusive sanding effect.  The pictures show the results of the 3 sponges. As I sponge sand the dome of the Bulldog, I notice a chip in the inner lip of the rim that became more distinct during the sanding process.  To erase this small divot, I introduce a very gentle inner bevel to the rim using 240 grade paper rolled.  This dispatched the divot quickly. Earlier, I avoided using the sanding sponges on the nomenclature panels in order not to diminish the Comoy’s stampings.   I do want to clean the panels more to rid the old residue finish before applying a fresh stained finish.  To remove the old finish and to clean the panel I apply acetone to a cotton pad and wipe the panels.  This does the job. With the time of my departure for the work day rapidly approaching, I continue the internal cleaning of the mortise and airway using a kosher salt and alcohol soak.  After forming a wick by stretching and twisting a cotton ball, I insert it down the mortise and airway using a stiff wire.  The wick acts to draw out the tars and oils.  I then add kosher salt (no aftertaste) to the chamber and place the stummel in an egg crate for stability.  With a large eyedropper, I add isopropyl 95% to the chamber until is surfaces over the salt.  After a few minutes, after the alcohol has absorbed into the chamber, I top off the alcohol and set the stummel aside to soak for the day.Arriving home several hours later, the soak did the job of finishing the internal cleaning.  I clean the expended salt from the chamber with paper towel and shank brushes as well as blowing through the mortise.  I run an additional pipe cleaner and cotton bud wetted with alcohol to assure the internals were clean.  They are, now moving on!Before proceeding further with the external stummel preparation, I’ve come to a decision point regarding the chamber issues that I saw earlier.  The floor of the chamber has heat fissures which the first picture shows.  The second picture shows the fissure immediately above the draft hole.  The upper chamber shows some heating issues with small, more normal chamber wear.  Earlier, my question had been, do the fissures on the floor of the chamber need a more durable response than simply applying a pipe mud mixture to enhance the growth of a protective cake?  The floor of the chamber has experience overheating issues and I believe at this point would benefit from applying J-B Weld to prevent further damage and to reinforce the resistance of the chamber floor.J-B Weld comes with two components that are mixed together and once mixed harden to form a heat resistant bond.  I’ll mix a small amount and apply it to the floor of the chamber then spread it over the area, including above the draft hole, filling the fissures with the Weld.  After it hardens and cures, I’ll sand the excess. I first wipe the chamber with alcohol and put a pipe cleaner through the airway to block seepage into the draft hole.  After I mix J-B Weld components in equal parts, I apply a small amount on the floor of the chamber and spread it with a dental spatula and my finger. I rotate the pipe cleaner so that it is not stuck but I leave it in place – I don’t want to pull it out while the J-B Weld is wet leaving the mixture in the mortise.  I put the stummel aside for the J-B Weld to cure.  After the repair cured overnight, I take a picture of the sanding process using 240 grade paper wrapped around a Sharpie Pen.  I concentrate on removing the excess J-B Weld so that all that is left of the weld is what has filled the fissures and cracks. The next pictures show a much healthier chamber.  At the floor of the chamber in the first pictures and concentrating on the area immediately above the draft hole in the second picture, you still see what appears to be rough spots, but it is now smooth to the touch in large measure.  The Weld filled the cracks and reinforced the area.  The application of J-B Weld and the additional sanding on the floor and the walls of the chamber cleaned it up nicely.  Putting the stummel aside, I take the stem and wet sand using micromesh pads 1500 to 2400.  I follow by dry sanding with pads 3200 to 4000 and 6000 to 12000.  Between each set of 3 pads I apply Obsidian Oil to revitalize the vulcanite. With the stem waiting in the wings, I continue with the stummel by wet sanding with micromesh pads 1500 to 2400.  I follow this by dry sanding with pads 3200 to 4000 and 6000 to 12000.  I take pictures of both sides of the stummel to show the huge fills on the right side.  If it weren’t for these unavoidable fills, the fantastic recovery the stummel has made would encourage me to leave the original, natural grain finish in place.  The briar surface had many issues, but the results of the micromesh sanding reveal a very attractive grain presentation.  The next step is to apply a dark stain to the Comoy’s Bulldog that will serve to help mask the issues prevalent on the surface.  Without question, my plan is to apply Fiebing’s Dark Brown Leather Dye to the stummel surface.  I assemble all the needed components on the table to apply the stain.  First, using a sharp dental probe I carefully dig out and scrape the dome grooves to make sure the debris is gone.  After wiping the stummel with alcohol to clean and prepare the surface, I fit the stummel with a cork I’ve fashioned as a handle inserted into the mortise.  Next, I heat the stummel with a hot air gun to expand the briar grain.  This aids the briar in absorbing the dye pigment.  Using a folded over pipe cleaner, I apply the dye to the stummel.  After a thorough application, I flame the stummel with a lit candle and the alcohol-based aniline dye combusts and sets the dye in the grain.  After a few minutes, I apply the dye again and flame again to make sure there is an even coverage.  I then set the stummel aside for the dyed stummel to rest. After resting for several hours through the night, it’s time to unwrap the fire-crusted Comoy’s stummel.  Over time, I have developed my own techniques for use with the Dremel since this is my main and only work horse tool on the 10th floor flat of a formerly Communist block apartment building!  My usual method for ‘unwrapping’ has been with the use of a felt buffing wheel, which is more abrasive than cotton, applying Tripoli compound.  I love this technique because the result reveals a more brilliant grain pattern as it lightens the grain veins leaving them in contrast to the softer briar wood which absorbs more of the dye.  However, I have found that using the felt buffing wheel lightens the entire stummel.  With the large dark fills on this stummel in need of remaining masked for better blending, I use a cotton cloth buffing wheel with Tripoli compound to unwrap the flamed crust.  The softer cotton wheel isn’t as abrasive and leaves a darker dyed hue on the briar surface.  After mounting a cotton cloth wheel on the Dremel, I set the speed at the lowest RPM and I apply Tripoli to the stummel. I take a couple staged pictures to show the contrast between the flamed crust and the surface that has been ‘unwrapped’ and buffed with compound.  After completing with the Tripoli, I wet a cotton pad with alcohol to wipe the stummel not so much to lighten but to blend the new stained finish. Next, I rejoin the stem and stummel to apply Blue Diamond compound.  I discover that the junction between the tenon and mortise has loosened through the cleaning process – a common thing in my experience.  To remedy this, I take a drill bit the next size larger than will fit through the tenon airway.  I use a Bic lighter and heat the tenon and after a bit, the vulcanite tenon becomes supple and allows me gradually to insert the drill bit end into the airway.  This expands the tenon and tightens the connection.  This works like a charm!  With the stem now fitting snuggly, I continue to apply Blue Diamond to the stummel and stem.  I mount a cotton cloth buffing wheel to the Dremel and increase the speed to about 40% full power.  I apply Blue Diamond compound to both stem and stummel.Before moving on to applying carnauba wax to the pipe, I have two more projects to do.  The first is to apply white acrylic paint to refresh the Comoy’s ‘C’ stamping on the stem.  The second is to apply pipe mud to the chamber.  I decide to do the latter first.  After the repair done to the chamber, to enhance the healthy development of a protective cake (which should be maintained at about the width of a US dime coin) I use a mixture called pipe mud – a combination of cigar ash and water.  This mixture, once applied to the chamber and dries, hardens to create a starter surface for the cake to develop.  My colleague, Gary, who lives in Plovdiv, Bulgaria, is the cigar man who saves his ash for my use. Thanks, Gary!  I mix some water with ash in a plastic dish and mix it with my pipe nail until it starts to thicken. At this point, I apply it in the chamber with the nail and my finger.  It doesn’t dry quickly so there’s time to spread it evenly over the chamber.  After spread, I insert a pipe cleaner through the draft hole to keep it clear of the mud.  I then put the stummel aside in the egg cart for the mud to cure. Turning now to the Comoy’s ‘C’ stem stamp, I put a drop of white acrylic paint over the ‘C’ and absorb the excess with a cotton pad and ‘dob’ it out so that the paint thins and dries.  I then use a toothpick’s flat edge to gently scrape the excess paint off after it dries.  I have to reapply paint a few times to get it right.  The pictures show the process. After allowing the pipe mud to cure, I rejoin stem and stummel and once more, run the sharp dental probe in the grooves around the circumference of the dome then buff the pipe with a felt cloth clearing away the compound dust before applying wax.  I then mount a cotton cloth buffing wheel to the Dremel, keep the speed at about 40% full power and apply a few coats of carnauba wax to the pipe.  I finish the restoration by using a microfiber cloth to give the pipe a rigorous hand buffing to raise the shine.

I’m pleased with the results of this Comoy’s Made in London, England, Bent Bulldog.  The restoration was fought in the trenches!  The many repairs done to the stummel surface came out well, though the two large fills are still evident, but not as overt. The dark brown dye came out beautifully and the groove patches and repairs have all but disappeared.  I’m glad I also addressed the heat fissure issues in the chamber.  This Comoy’s Bent Bulldog will provide many more years of service to a new steward.  Stephen commissioned this Comoy’s and will have first opportunity to acquire it in the Pipe Steward Store and this pipe benefits the Daughters of Bulgaria – women and girls who have been trafficked and sexually abused.  Thanks for joining me!

 

A Tiny 2 Star BBB 8881 Apple/Globe Provided An Interesting Challenge


Blog by Steve Laug

When I spoke with a fellow here in Vancouver who had a pipe that he wanted me to fix it sounded like a simple repair. He said that it had a very loosely fitting stem. He asked if he could drop by to show it to me and see if I could fix it. From past experience I have learned to never jump to conclusions about what sounded like an easy repair. When he arrived he showed me his GBD Faux Spigot. It turned out to need far more work than just tightening a loose stem. I wrote about that restoration in a previous blog (https://rebornpipes.com/2018/11/03/redoing-a-poorly-restored-ebay-gbd-super-q-9436/). We talked about his GBD for a bit and he made the decision to have me do a restoration on it. Then he reached into his pocket and pulled out a small plastic bag with a little BBB 2 Star apple of globe shaped pipe. It was stamped BBB in a diamond on the left side of the shank with two ** – one on either side of the diamond. ON the right side it was stamped Made in England over the shape number 8881. He said that he had found it at his parents’ house and really no one there knew where it came from.

Here is what I saw. Starting with externals. The pipe was small – kind of a pocket pipe. The grain on the bowl was quite stunning – a mix of flame and birdseye all around the bowl and shank. The rim top was coated with a thick lava coat and it went into the bowl. The inner edge of the bowl was in rough shape having been hacked clean with a knife. There was a crack on the right side of the shank curving to the underside. It looked to me it was made by the poorly made stem being shoved into the shank. The stem was larger in diameter than the shank and had been rounded over with a file. There were deep bite marks on the surface ahead of the button on both sides. Moving to the internals. The end of the tenon was carved with a knife to make it fit the mortise in the small shank. The inside of the shank was dirty but less so than I expected. The inside of the bowl had a light cake but most of that was gone from the knife job that had left a wounded inner edge on the rim. Looking at the pipe I explained what I would have to do to bring it back to life and restore it to use. It would need, cleaning, reshaping on the rim, a band on the cracked shank that would leave the stamping readable, and a reworking of the stem to make it a fitting addition to the lovely briar of the bowl. The pipe was going to be a fun challenge. I took these photos to give you an idea of what I saw. The previous pipeman who had fit a new stem to an old favourite pipe had done a functional job but it looked rough. It was pretty clean on the inside so it was cared for. It must have been a great smoking pipe for him to fit a new stem and not give up on it when the previous one broke or was lost. It was smokable. I took a close up photo of the rim top to show the condition. It is hard to see but the rim top was not smooth. The lava build up was pretty thick and there were some deep nicks and chips in the flat top. The close up photos of the stem reveal the scratches in the vulcanite, the tooth marks and the worn and ill-defined button.  The oversized diameter – prettified to look nice is clear in the photos. I took photos from the side of the pipe to show the stamping on the shank and the prettified stem. In the second photo you can see the crack in the shank curving downward to the underside.I decided to address the cracked shank first. With the crack as large as it was and movable I did not want to further damage it when I worked on the stem and fit of the tenon. I knew that it needed to be banded but that would cover the stamping on the shank so adjustments would have to be made. I used a Dremel and sanding drum to reduce the size of the shank to fit the band I had chosen. I did not take of too much briar and I only damaged the M in Made In England as part of it would end up being covered by the band.I repaired the crack in the shank with super glue and pressure fit the band onto the shank to the point of the end of the sanded portion. I used a Dremel and sanding drum to cut back the band to the width that I wanted. Compare the photos above with the one below to see how much I took off of the band. I topped the band on a topping board with 220 grit sandpaper and smooth out the sharp edge with 1500 grit micromesh. I decided that since I was already working with the Dremel and sanding drum that I would take down the excess diameter on the stem as well. I reduced it to sit snugly against the band giving the pipe a classy look.I cleaned up around the inside edge of the band and edge on the shank with a folded piece of 2220 grit sandpaper to smooth things out and make the fit and transition smooth. I lightly sanded the blade portion of the stem and the area of the tooth marks next to the button with 220 grit sandpaper to remove the oxidation and clean it up. I fit the stem in the shank and took a photo of the pipe at this point in the process. It was beginning to look like a classic BBB to my eye. With the stem roughly fit to the shank it was time to address the bowl top. I topped it on a topping board with 220 grit sandpaper. At that point I called it a night. I had to catch a train down to the southern part of Washington from Vancouver in the morning so I thought I would bag up a couple of pipes I was working on and take them with me.I caught the train south from Vancouver, BC at 6:30am. Once we had our seats we were in for an 8 hour train ride. I figure it would be a good opportunity to work on these two pipes. You can see my work table in the photo below. I used the fold down table. It had a lip around it so I spread out a couple of napkins for the dust and went to work on the pipes.I started working on the BBB by addressing the damage to the inner edge of the rim. It was significant with cuts and burns. My topping worked had helped with the top damage and smoothed that out but I need to work on the rim edge. I used a folded piece of 220 grit sandpaper to smooth out the sharp edges and bring the bowl back to round. Once I had the rim as round as I could get it and smoothed out the damaged edge I polished it with micromesh sanding pads. I polished the bowl and the rim at the same time. I wet sanded with 1500-2400 grit micromesh sanding pads and dry sanded with 3200-12000 grit pads. I wiped the bowl down with a damp napkin after each pad. I touched up the stain around the front of the band and stained the rim top and inner edge with Maple and Cherry stain pens. Together the two stains matched the rest of the bowl.I rubbed down the briar with Before & After Restoration Balm. I worked it into the smooth surface of the briar with my fingertips to clean, enliven and protect it. I let the balm sit for a little wall and then buffed with a cotton cloth to raise the shine. The following photos show the bowl at this point in the restoration process. The rim matches well but still needs to be polished and buffed to raise a shine on it. I used a folded piece of 220 grit sandpaper to reshape the button and also to smooth out the marks left by the Dremel when reducing the diameter of the stem. I sanded the tooth marks near the button on each side of the stem to smooth them out.I polished the stem, tenon and metal work with micromesh sanding pads – wet sanding with 1500-2400 and dry sanding with 3200-12000 grit pads. I wiped the stem down with Obsidian Oil after each sanding pad. I was able to remove the damage on the tenon and polish out the dripping varnish on the metal adornment. The stem looked much better at this point in the process. I the polished stem and bowl with Blue Diamond to polish out the remaining small scratches and raise the shine. I gave the bowl and the stem several coats of carnauba wax and buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The pipe polished up pretty nicely. This turned out to be a beautiful little pocket pipe in terms of shape and finish. The new nickel band adds a touch of class in my opinion and gives the pipe a new elegance. I look forward to hearing what the fellow who dropped it off for repair thinks of it once he has it in hand and is smoking it. The finished pipe is shown in the photos below. The dimensions are Length: 4 inches, Height: 1 3/8 inches, Outside diameter of the bowl: 1 inch, Chamber diameter: 3/4 of an inch. Thanks for walking through the restoration with me.

Resurrecting a Tired and Worn 1937 Dr. Grabow Special 4914 Apple


Blog by Steve Laug

The next pipe on my restoration table is an interesting older pipe that appears to be made out of walnut or some other hard wood. It was tired and worn looking with the remnants of what appeared to be an oxblood stain in the wood. The stamping was dirty and worn but readable nonetheless. On the left side the pipe is stamped Dr. Grabow over Special and on the right side it is stamped with the shape number 4914 near the shank stem junction. That is followed by Pre-Smoked over Reg. US Pat. Off. The rim top was dirty and had some tar ground into it. The bowl had a light cake in it and there was a small nick on the inner right edge of the bowl. It had a hard rubber vulcanite stem with the white Linkman style propeller inset on the top of the stem. The rubber was quite hard and did not show signs of oxidation. There were tooth marks on the top and underside of the stem at the button. I took some photos of the pipe before I started my cleanup. I took some close up photos of the rim top and bowl to show its condition. The tar spots are on the surface. The nick is visible on the right side of the bowl. I also took photos of the stem to show the bite marks and wear on the stem.I took a photo of the stamping on both sides of the shank to show the condition. Interestingly once I cleaned the shank up and removed the stain the stamping was very readable.I looked up information on the Dr. Grabow Special 4914 pipe on Pipedia to see if I could identify the time period that the pipe came from. I had a hunch that it came out during the war years due to the alternative wood that had been used in its manufacture in place of the normal briar (https://pipedia.org/wiki/Dr._Grabow_Models_(Series,Line)_Names_Through_the_Years). Here is what I found out:

SPECIAL (or Special Italian Briar) post-1937, begins with 43, 49, maybe no number at all; DOLLAR DR. GRABOW 1937 or previous, may not be marked as such, begins with 43, 44, 49 Series 43 = Natural Finish (DG), c1937. Series 44 = Dark Finish (DG), c1937. Series 49 = Walnut Finish (DG), c1937.

Thus I knew that the pipe came out post 1937. I still had not confirmed the date of the pipe other than knowing that it was made after 1937. I did some more digging on Pipedia and found the following information that also helped pin down the date (https://pipedia.org/wiki/Dr._Grabow).

The production of the pipes started in 1930/31. In 1937 Linkman began calling his pipes “Pre-Smoked”. An ad dating from 1946 celebrates it as “America’s Most Wanted Pipes” and the text announced that each Dr. Grabow was broken in on the Linkman’s Automatic Smoking Machine with fine Edgeworth tobacco, reducing the need for the new owner to spend time breaking in his pipe. In 1949 the official name read Dr. Grabow Pipe Company Inc. with seat at W. Fullerton Avenue 1150, Chicago 14, Illinois. (Thus the Linkman factory.) Series: Special, De Luxe, Supreme, Tru’ Grain, Select Grain.

That helped to pin down when the first Pre-Smoked Pipes came out on the market. I have included a couple of advertisements from the 1940s on the Pre-Smoked pipes. The advertisements were on Pipedia courtesy of Doug Valitchka. I found a similar pipe for sale on eBay (https://picclick.co.uk/Lovely-Vintage-Dr-Grabow-Special-4914-Smokers-Pipe-372388011756.html). It could very well be a twin of the pipe that I am working on. It is also made from an alternative wood, rather than briar.

I started my restoration on the pipe by wiping down the bowl with acetone on a cotton pad to remove the remnants of the oxblood finish. I took photos of the bowl after the cleanup. I sanded the bowl with 220 grit sandpaper to remove the remaining stain. I sanded the rim top to remove the stain and tars there. I worked over the inner edge of the rim with 220 grit sandpaper to remove the damaged area on the right side. It did not take too much work to remove it. I polished the rim and bowl with micromesh sanding pads – wet sanding with 1200-2400 grit pads. The bowl began to have a rich shine.When I sanded the bowl a small red putty fill showed up on the back right side of the bowl. It was slightly pitted. I filled in the pits with clear super glue to remove the damage. I sanded it with 220 grit sandpaper and then with a 1200 grit micromesh pad.I polished the bowl with red Tripoli on the buffing wheel to smooth out the wood. I heated it and stained it with the “red” tan aniline stain. I flamed it with a lighter and repeated the process until the finish had good coverage. I also gave the bowl a coat of Danish Oil with Cherry stain to highlight the grain. I cleaned out the internals in the stem and the bowl with pipe cleaners, cotton swabs and alcohol. The shank was dirty and the debris and grime that came out made fit of the stem in the shank much tighter.I set the bowl aside and worked on the stem. I sanded the surface of the stem with 220 grit sandpaper to remove the tooth chatter and the lighter tooth marks. I cleaned it up a soft cotton pad to remove the debris. I filled in the deeper tooth marks with clear super glue to repair them. I set the stem aside to let the repairs cure. I sanded the hardened repairs with 220 grit sandpaper to blend them into the surface of the vulcanite.I polished stem with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I wiped the stem down with Obsidian Oil after each pad. When I had finished polishing with the last pad, I gave it a final coat of Obsidian Oil and set it aside to dry. This small war era Dr. Grabow Pre-smoked apple is a unique alternative wood pipe. It has interesting swirled grain around the bowl and cross grain across the shank. The grain really is interesting. The rim top looks much better. The vulcanite stem is high quality and shined up well. I buffed the bowl and the stem with Blue Diamond polish to raise the shine on the briar and the vulcanite. I was careful to not buff the stamping and damage it. I gave the bowl and stem multiple coats of carnauba wax. I buffed the entire pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The finished pipe is shown in the photos below. The rich oxblood stain allows the grain to really stand out while hiding the fill in the bowl side of this little pipe and it works well with the rich black of the vulcanite stem. The dimensions of the pipe are: Length: 5 1/4 inches, Height: 1 1/2 inches, Outside Diameter: 1 inch, Diameter of the chamber: ¾ of an inch. This little Linkman’s Grabow apple fits nicely in the hand and makes a great pocket pipe. Thanks for walking through the restoration with me.

A Hardcastle Bulldog Run Roughshod over: The Original Restoration


Blog by Robert M. Boughton

Copyright © Reborn Pipes and the Author except as cited
https://www.roadrunnerpipes2k.com/
https://www.facebook.com/roadrunnerpipes/

Grace is neither gentleness nor fragility.  Grace is treating yourself, others and even inanimate objects with respect.
— Kamand Kojouri, Iranian-born novelist and poet

INTRODUCTION
A former roommate, one of Stephen King’s Constant Readers, once remarked with ridicule-tainted respect that I have always been attracted to needful things.  He was speaking of someone I met not long before then whose tragic life had left him wounded to the core, one of the results being his over-demanding, often verbally corrosive and manipulative treatment of me.  The roommate, who like almost everyone had plenty of his own flaws if less obvious and abusive, said my other acquaintance was no friend of mine.

“That may be true,” I replied, “but I’m his friend and the only one he seems to have, and I just can’t give up on him because that’s not what friends do.”

The physically and emotionally damaged person I undertook to help ended up becoming and remaining my genuine though stormy friend until he died at home 14 years later from an unusual and excruciating autoimmune disorder for which there is no cure.  He was 46.

My affinity for care-challenged pipes, therefore, should come as no surprise.  I try to avoid those with fatal flaws such as bad cracks or burnouts and for the most part reject any with serious holes in the stem, but as a restorer I prefer estate pipes that need some real attention to rehabilitate as opposed to the few I find ready to sell or to keep in my collection with minimal effort on my part.

I don’t even remember how the Hardcastle Special Selection #7 smooth bulldog came into my custody or why I chose to ignore the obvious void of vulcanite below the lip on the underside of the stem.  Other than that handicap, the pipe was nowhere near as mistreated as I’ve seen but was plagued enough by dings, scratches and other problems to keep me happy.

One final initial note: I repaired this bulldog to almost like-new condition more than a year ago but failed to blog it because of personal distractions that have left me with a large backlog.  I sold it for next to nothing to one of my present housemates who decided he wanted me to refinish it as a black dress pipe.  The same pipe is the subject of Part 2 of my series on that subject, and so I was going to include this original restoration in that blog.  But anyone who reads my harrowing account of the experience that could be called too much of a bad thing will understand why I broke the overall work into two blogs.

Intrigued by the atypical presence of a stinger in the Hardcastle, and an unusual one at that, I searched online for such phenomena with a faint hope of dating the bulldog.  Of course, at the top of the list was one of Steve’s blogs from 2014.  No other road I found led anywhere close to Rome, as it were.  Steve’s pipe is a Dental Briar brandy, bearing the Registered Design Number 857327, with a unique – or bizarre – dental stem, a system-type metal rod in the shank extending to the mortise hole, and a different short stubby little stinger of its own.  Here is the Dental Briar stinger before Steve’s restoration and the pipe after his usual fantastic work.Steve narrowed the date of manufacture to the Family Era and concluded his pipe was created from 1949-1967 using the National Registry link below.  However, looking at the same link, I see in Table 6.5 that designs numbered 548920-861679 were registered between 1909 and 1950 and suspect the 857327 might have been pre-1949 – no disrespect intended to the master!  Besides, he’s right to note that his Dental Briar could have been made at any time between its registration and 1967 when the family lost all control of the brand.  His pipe is also stamped MADE IN LONDON ENGLAND on the right shank.

I am not so fortunate.  The bulldog has no Registered Design Number or even the usual right shank nomenclature (London Made, British Made, Made in London England, Made in England).  This nomenclature is not faded, it’s just not there.  Only the left shank identifies it as a HARDCASTLE/SPECIAL SELECTION/7.  All I know for sure is that I tried it out after a basic sanitization, and it was quite good.

For a great synopsis of Hardcastle’s history, see Steve’s blog below.  Details are in the Pipedia link.

RESTORATION I would have removed the stinger anyway as useless, but it was also bent and more fragile than usual, and so I experienced even less than usual emotional distress heating the pointless thing with a Bic and twisting it out.Considering the appreciable grime, I started by swabbing the stummel first with purified water and then alcohol.  In hindsight, I should have skipped the water method that had little effect.  The blemishes stand out even more after the cleansing with alcohol.  The one shot below showing the minor rim damage, an unevenness being the only bad part, and decent chamber condition was taken with a flash and therefore looks pre-water and -alcohol cleaning.  I’m still having to do the best I can with a cell phone cam.  I used 150-, 220-, 320- and 400-grit papers to start shaping up those areas.After that I re-addressed the chamber and unevenness of the rim with a Senior Reamer and the blade from my Peterson’s Pipe Tool and made them a little better with 150-400-grit paper.I gave the shank a preliminary alcohol cleaning and retorted the pipe with a meerschaum stem that wasn’t crippled by a hole but somehow forgot to snap a pic of the latter.With 220- and 320-grit papers I was able to remove the dings and scratches as well as giving the chamber a semi-final what-fer.For some reason, the band popped off, and I still wasn’t happy with the color.  I decided to go at it once more with the 220.A full micro mesh buff made the old pipe begin to shine as it should.By now I should be somewhat known for fancying two-tones with bulldogs and Rhodesians where the top of the bowl above the two lines curves upward to the rim.  For the most part, at least, I’ve left this area lighter than the rest of the stummel, although on occasion I’ve dabbled in darkening it with, say, maroon stain.  This one screamed at me to lighten the top of the bowl as usual under these circumstances.  And so I stained the stummel below the lines with Lincoln brown leather dye, flamed it and after letting it cool took off the char and a little of the darker color with 8000 and 12000 micro mesh pads.  By the way, I was alarmed when I got a look at the first pic below and noticed what to every appearance seems to be a wicked and poorly repaired crack in the shank.  I assure everyone it’s a trick of the light or whatever, as the other pics prove. Gluing the band on again was a formality after buffing it on the electric wheel.Okeydokey, then.  There could be no more avoiding the chomped and degraded stem with its hole on the underside and other shortcomings. I had already given it an OxiClean soak, and it wanted repair.  Just to get an idea of what the stem would look like when finished, I gave it a quickie micro mesh rub.   I cut a little strip of card stock from the business leftover of someone with whom I didn’t care to do any more business and lubed it and a very small tweezers with a dab of petroleum jelly.  I inserted both into the mouth opening of the stem, with the cleaner behind the paper, until they were firmly in place inside the airway to a point just below the hole.  Finding my trusty old vulcanite stem that was long ago destroyed by another stem abuser, I shaved some fine flakes onto a small piece of paper with one side of a narrow, relatively smooth triangle rasp.

This was where I had to be prepared to act fast: I moved the flakes into a pile and added a few drops of black Super Glue, stirred the two into a gritty paste and scooped up a gob with the part of a three-piece pipe tool made for clearing tobacco from the chamber.  As fast as possible without making a mess, I slapped the goop liberally over the hole and set it aside to dry, removing the card stock and tweezers when the vulcanite mixture was dry on the inside but still a little wet on the outside.It’s a good thing I have an excellent recall of what I did in a particular restoration because the photographs I took of this project were more jumbled and duplicated than those from any other pipe on which I’ve worked.  I had so many of the same thing from alternate angles and differing clarity, for example, that I had to delete quite a few to make sense of it.  I concluded this was because of two things, trying different ways to get a good shot with my poor cell phone camera at the time and lack of sleep during the process.  It’s clear, excuse the pun, that some of the “best” are quite indistinct.  The following photos, as a result, are incomplete, but I always have the words to describe what I did.

For example, after the previous step, I started sanding with 150-grit paper and then smoothed it up with 220-, 320- and 400.  A common, less serious groove resulted, and I added more of the black Super Glue/vulcanite mix and let it dry again.  The mixture settled in well.That’s when I got serious with the sanding, using 150-, 220-, 320- and 400-grit paper and super fine “0000” steel wool.There’s still a small lump visible under the lip that I handled with as little abrasion as possible before the stem was done.  And that was it – for the bottom side.  I still had the top to do.  In every way other than the hole in the bottom, the top was worse, although it only needed a dab of black Super Glue/vulcanite solution to fill a small divot following the same initial OxiClean soak and a more vigorous sanding before filling a small divot with.  Considering again the top of the stem when I received it, close up, notice the wear below the square shank fitting before the rest of the work. The stem never quite fit the shank, which had been given a replacement band somewhere along the way, not to mention the band was damaged. After beginning to re-sand the bottom of the stem, the original hole caved in again.  Accepting defeat, I chose a new bulldog stem I had that needed serious filing at first and then sanding of the 9mm tenon to fit the shank. I bent the stem.  That required heating the stem – with a pipe cleaner inserted through the airhole – at 210° F. for about 15 minutes and bending the nice and pliant material over a complex tool.

Remembering the cell phone photos were atrocious and I had to edit them using every halfway adequate means of adjustment available with my so-called photo editor to show any similarity whatsoever to the actual result, here one last time is the stummel as it in fact looked when it was one step from completion before electric buffing.And these are the final photos of the pipe.  The most offensive discrepancies to me are the obscurity of the two-tone and the lack of shine the pipe had.  The bad twist on the stem in the fifth shot of the rear is all on me!

CONCLUSION
This blog being the occasion of my official announcement in this forum of my new webstore on  my own site, https://www.roadrunnerpipes2k.com/, is unfortunate in that the depictive presentation almost convinced me to give up any idea of writing the blog.  The poor quality and lack of photographs, as well as other stated reasons, were overwhelmingly opposed to the idea of even trying.  Then I thought of the work I put into the briar and the stem alone. In the end, I know how smooth, golden brown and at least hardly blemished the Hardcastle bulldog looked when I was done with it.  Whether anyone else does is of no importance to me.

SOURCES
https://rebornpipes.com/2014/06/27/a-unique-piece-of-pipe-history-almost-lost-a-hardcastles-dental-briar-reg-design-no-857327/
http://www.nationalarchives.gov.uk/help-with-your-research/research-guides/registered-designs-1839-1991/
https://pipedia.org/wiki/Hardcastle

Restoring my Grandfather’s…what the…A Kaywoodie?????


Blog by Paresh Deshpande

Yes!! That is what exactly my thought was, when I looked closely at the small pipe in my hand that I had selected as my next project for restoration. Those who have read my previous write ups on pipe restoration would know that I have inherited a large number of pipes from my grandfather dating between the periods from 1940s to 1970s. I had not come across a single Kaywoodie pipe in the two boxes I had opened, one box still remaining unopened!!!

I have restored two Custom-Bilt pipes from this collection to date, one from 1938-41 era (https://rebornpipes.com/2018/06/02/restoring-my-grandfathers-custom-bilt-pipe/) and second from the Wally Frank era(https://rebornpipes.com/2018/07/20/restoring-a-wally-frank-era-custombilt-sitter-633/), the third Custom-Bilt billiard from 1938-41 era was sent to Mr. Steve of rebornpipes fame to sort out tenon issues and have fallen in love with Custom-Bilt pipes since thereafter!!!! I had picked this pipe assuming it to be a Custom-Bilt and it was only on close scrutiny was it reveled that this was a Kaywoodie!!!!! I deliberately rummaged through the pile again and sure enough, there was another Kaywoodie Bent Billiard with 4 holed stinger in relatively unsmoked condition. It seems my grandfather never took a liking for these Kaywoodie pipes!!!!!

This Kaywoodie Pocket Pipe, now on my work table, has similar large finger like vertical rustications with very thin horizontal lines ensconced within these large vertical rustications. These thick vertical rustications extend upwards and end short of the rim top, giving the rim top a flat smooth surface. These rustications can be seen extending all around the shank on top and bottom, save for smooth surfaces on either sides of the shank. The smooth surface on the left side of the shank bears the stamping “Handmade” over “Super Grain” in cursive hand, over “KAYWOODIE” in block capital letters. The right side of the shank bears the stamp “IMPORTED BRIAR”. All these stampings are thin, worn out but readable under bright light with a magnifying glass. The ¾ bent saddle stem bears the trade mark “Clover leaf” symbol.This pipe comes with a four-holed threaded stinger which screws into the shank. This stinger is stamped with “DRINKLESS”. There is an aluminum spacer ring separating the shank end from the stem end when threaded in. On closer observation, it can be seen that a portion of this spacer, closer to the mortise opening, extends into the mortise and is threaded which matches with the stinger threads.I took all these observation and searched pipedia.com for history of this brand, models and attempt at dating this pipe. This site has detailed information on Kaywoodie pipes, including the history of origin, about the owners of the brand and also various important links to “Collector’s Guide to Kaywoodie Pipes” and “Kaywoodie’s Logos and Markings: Clover variations since 1919”. Here is what was revealed as extracted from pipedia.com:-

Kaywoodie was the name a pipe offered by Kaufman Brothers & Bondy Company (KBB), first appearing in February of 1919. The Dinwoodie pipe, also by KBB, appeared in November of 1919. Sometime before 1924, the Dinwoodie had been discontinued and the Kaywoodie name was beginning to be used on an extensive line of pipes that ultimately would be the name of the company. The origin of the name Kaywoodie is a combination of the K from Kaufman and wood, as in briar. Not much is known of the original KBB company other than it was started in 1851 by the German born Kaufman brothers when they opened a small pipe shop in the Bowery section of New York City. In the back room of this shop, they made their first pipes. From this meager beginning, the Kaywoodie name and organization was to emerge.

When one of the men from the New York office got “gold fever”, he carried a large supply of pipes with him to California that he sold along the way. This early “national distribution” did much to build the reputation of KBB. By the late 1800’s, branches of KBB were opened in Chicago, Atlanta, San Francisco and St. Louis with family and friends acting as agents. The trademarks, for the inlaid cloverleaf and the cloverleaf with the KBB initials inside, were issued in 1881. KBB’s pipes became more popular and were in constant demand by the end of the century. Orders were streaming back east and KBB needed to move to larger manufacturing facilities. By 1915 the move was made to larger facilities in the old Union Hill section of Union City, New Jersey. The salesroom offices were located at 33 East 17th. Street, New York. When the Kaywoodie pipe was first introduced by KBB it came with a hand cut rubber mouthpiece fitted with an aluminum Inbore Tube. This device was to “assure a clean, cool smoke.” Other KBB pipes such as Ambassador, Heatherby and Melrose also had the Inbore tube. The early Drinkless Kaywoodies from 1924 through 1931 had push bit stems. In 1931, after three years of research, the new Drinkless Kaywoodies with the synchro-stem, (threaded drinkless screw-in mouthpiece) were introduced. The drinkless attachment was advertised as cooling the smoke from 850 degrees in the bowl to 82 degrees when it entered the mouth. By the mid 1930’s, all Kaywoodie’s came with the screw mounted Drinkless attachment. (Export Kaywoodies, available briefly from 1950-1955, had push bit stems and were available in all the same shapes and finishes as the drinkless versions.)

Throughout much of the 1940’s, 50’s and 60’s, the Kaywoodie family of pipes consisted of 11 basic grades of briar pipes; though new grades were frequently added to the line and some older grades were discontinued or downgraded. These 11 basic grades of pipes, listed in ascending order of quality, were:

  1. Drinkless
  2. Hand-made Super Grain
  3. Super Grain
  4. Relief Grain
  5. Flame Grain
  6. Silhouette
  7. Oversize Kaywoodies
  8. Meerschaum Inlaid Kaywoodies
  9. Connoisseur
  10. Ninety-fiver
  11. Centennial

Thus from the above, I can safely infer that this pipe was a higher grade Kaywoodie from the 1940s to 1960s.

INITIAL VISUAL INSPECTION
The finish looked a lot like the classic Kaywoodie take on Tracy Mincer’s Custom-Bilt pipes. The carved worm trails seen on the stummel and shank is filled with dust, dirt and grime of years of smoking and thereafter years of uncared for storage. The grime and dirt is so strongly entrenched in to these carved worm trails that it appears black and solidly smooth to the touch. I could see 3-4 small dings and dents on one of the fingers of the raised portion of the stummel. This will need to be addressed. There is a decent layer of cake inside the bowl which is dry and hard to the touch. The smooth rim top is clean and devoid of any apparent damage. The condition of the inner walls of the chamber can be ascertained after the cake has been reamed out. The inner edge of the rim shows minor uneven surface, however, the outer edge of the rim is clean and without dents or dings. The short ¾ bent saddle stem has smooth upper and lower surfaces without any tooth chatter or bite marks. This is unlike any other pipe stem I have seen that had belonged to my grand old man. The four holed stinger is clean, however, the holes appear to be clogged. This was confirmed as air did not flow when I tried to blow through the stem. May be that has been the reason that this pipe was not as extensively used by him. The inlaid white clover leaf is clean and prominent with a tiny portion of the top of the leaf missing!! But it is so tiny chip that it is not immediately visible. The lips are worn out and may need to be reconstructed; again I am not sure about this as there is no damage as such. There is an aluminum spacer between the stem and the shank which breaks the monotony of the pipe. However, it is broken on the right side leaving an ugly gap between the shank and stem. The remaining portion of the aluminum spacer was crumbling and breaks merely to the touch. This needs to be addressed. There is a circular band of white tape or some such material at the end of the stinger where it meets the stem. This is something which is not correct and the reason for it having been placed needs to be checked. THE PROCESS
First and foremost in any restoration of pipe, I start with reaming the chamber with a Kleen Reem pipe reamer. However, in this instance, the cake was dry, tightly packed and very hard. I feared breaking the reamer and resorted to the use of my fabricated knife. After a struggle, I was able to take the cake down to the bare briar. I sanded the inner walls of the chamber with 150, 220 and 600 grit sand paper to completely remove the remaining cake and smooth out the walls. Alas, I observed some superficial gouges on the wall surface due to the use of knife. I would need to address this by coating the chamber walls with pipe mud at a later stage. I cleaned the mortise and internals of the shank with cue tips, pipe cleaners and alcohol. Since the major challenge appreciated in this restoration project was the construction of a new aluminum spacer, I decided that is where I would start!!!! To address this issue, I identified three options, as under, which were available to me:

(a) Coat the entire spacer, including the broken portion, with superglue, building it up in layers and then sanding it to flatten it on a topping board. This coat of superglue will also stabilize the remaining original spacer.

(b) Fabricate an aluminum spacer out of a regular aluminum washer and replace only the broken portion of the spacer.

(c) Replace the entire spacer with the new fabricated aluminum spacer.

I discussed these options with my mentor, Mr. Steve Laug. As is his trademark style of tutoring, his suggestion was, “I would go with the first option”!!!!! He further clarified that the spacer also enters the mortise and has threads for the “synchro-stem” (threaded drinkless screw-in mouthpiece). Thus, I concluded that exercising the third option was best avoided if I wished to avoid ruining the pipe!!! That left me with following either first option or the second option. Any other sane student would have followed the advice of his mentor (which I had been doing up to this point!!!). However, I, for some reason, was convinced that the end result of exercising the second option would result in a better finish and thus embarked on the arduous journey of replacing only the broken portion of the original spacer with the fabricated aluminum washer.

I began the process by shaping the new aluminum washer to match the size, shape and thickness of the original spacer. I was not very meticulous about the size and thickness as the same would, in any case, have to be perfectly matched by sanding it down with needle files. The following pictures will tell the story of the entire process of constructing this spacer. However, what these pictures do not tell you is the long back breaking hours involved, the strain to which eyes were subjected, precise and controlled movements of the needle files and agony experienced whenever the needle file inadvertently scraped the crumbling original spacer, causing it to chip. When I was satisfied with the fit and finish of the new spacer, I applied an even coat of superglue over the entire surface and very painstakingly re-aligned all the broken pieces of the original spacer and also the new fabricated spacer over the coat of the superglue and set it aside to cure overnight. Next day I evenly applied another coat of superglue over the entire spacer and again set it aside to cure so as to stabilize the spacer repairs and even out the surface. Once the glue had sufficiently cured, I topped the surface on a topping board to even out the glue. To further smooth out the surface and ensure a transparent, even and smooth surface, I polished the surface with micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. I frequently wiped the surface with a moist cloth to remove the glue dust. I was able to maintain just sufficient thickness of the coat so as not to disturb the alignment of the stem with the shank while stabilizing and protecting the spacer. I was very satisfied with the results. Now with the spacer taken care of, I start working on the stummel. I thoroughly clean the stummel with undiluted Murphy’s oil soap and a hard bristled tooth brush scrubbing the rustications clean of all the lodged dirt, dust and grime. I had seen a few dents and dings on one of the fingers of the stummel rustication and wanted to address it. I began by sanding the stummel and raised portion of the rustications with a 600 grit sand paper followed by 800 grit sand paper. I had used very light hand so as not to lose too much briar (though at the end I realized that I should have used a bit more force since at the end of the process, these dents and dings were still very much visible!!!!!!). This sanding was followed by polishing with micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. I wiped the bowl down with a moist cloth after each pad to remove all the sanding dust. As I was going through the micromesh pads, I was thinking of adding some twist to the finish and remembered that Mr. Dal Stanton, a gentleman I often turn to for some interesting pipe related conversations and advice, had refurbished a Tom Howard rusticated tomato pipe for me. He had darkened the crevices of the rustications with a dark stain pen and the contrast was eye catching, to say the least. I wanted to have a pair of pipes with this finish and decided to give this Kaywoodie the same treatment. I discussed with Mr. Dal Stanton who wholeheartedly explained the technique of achieving this finish and also gave me some very fine and pragmatic advice which I shall cherish on this journey. I stained the crevices in the rustications with a dark brown stain pen and set it aside for the stain to set in to the crevices. After the stain had set, I rubbed a small quantity of “Before and After” restoration balm in to stummel and set it aside for a few minutes to let the balm work its magic on the briar wood. The balm works to bring back the shine and pours life in to the briar. I buff the stummel with a horse hair shoe brush followed by a nice hand polish with a soft cotton cloth. I liked the way the stummel has finished. To address the superficial gouges in the chamber created by use of knife during reaming, I prepared a mixture of pipe ash and yogurt of putty consistency and applied a coat to the inner walls of the chamber. Once the coating had cured, I gently sand the walls with a 220 grit sand paper to a smooth and even surface. With this, the stummel is all completed. Once the stummel had been finished and set aside, I turned my attention to the stem. There was not much work on this stem since it was sparingly used with only light signs of oxidation and no bite marks or tooth chatter. I start by sanding with micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. I wiped the stem with a cotton swab dipped in alcohol to remove the sand dust and rub a small quantity of Extra Virgin olive oil and allow it to be absorbed in to the stem. The stem is now nice and shiny. The next thing to address was the blocked stem. I tried cleaning the airway in the stem with pipe cleaners dipped in alcohol, but the pipe cleaner would not go in the complete distance. There was gunk and tars which had accumulated inside the airway and in the holes too!!!! Using a straightened paper clip, I probed and cleaned all the holes on the stinger. I tried to blow through the stem, but I realized that it was still blocked. I tried pushing the paper clip through the airway and then there was this small sound of a crack!!!!!! Aargh……..the upper lip now has a chip!!!!! Undaunted by this temporary setback, I continue with the clearing of the blocked stem. Finally, I am able to dislodge the block and now the air flows freely through the stem.To address this chip, I firstly insert a regular pipe cleaner coated with Vaseline in to the air way. This prevents the charcoal and glue mix from dribbling in to the air way blocking it. I mix a small quantity of activated charcoal and CA superglue and spot apply it over the chipped surface. Once I have ensured that the complete surface is coated with the mix, I set it aside to cure overnight. The next evening, I file the filling with a needle file and match it to the surface of the stem. To further match the filling with the rest of the stem surface, I sand the fill with a 220 grit sand paper followed by micromesh polish pads. The stem is now nice and shiny again with a free flow of air through the airway. I finished this restoration by applying a small quantity of Halcyon II wax and rubbed it deeply in to the stummel with my fingers. A few minutes later, I polished it with a soft cotton cloth using muscle power. The stummel now has a nice deep shine to it and the grains on the rim top and raise portion of the rustication can be seen in its full glory. I re-attach the stem and then relies that the stem is off center to the shank!!!! My God, this one was giving me a hard time. I removed the white sticky tape that was stuck around the stinger at the stem end and tried the fit. The fit had improved but it was still off centre. Again, to address this issue, I was presented with two options of either sanding the coating of superglue over the spacer till the off center was corrected or heat the stinger till the glue fixing the stinger in the stem was loosened and turn the stinger in to the mortise till the issue was addressed. I decided to go with the second option as I feared losing the coating of superglue over the spacer and thus exposing the brittle original to further chipping. I heated the stinger with the flame of a Bic lighter so that the glue holding the stinger would loosen a bit and fitted the stem in to the mortise, tightening it till the stem and shank were perfectly aligned. I let the stinger sit in this position till it had cooled down and the glue had hardened again. Now the fit of the stem and the shank is perfectly aligned. Here are the pictures of the finished pipe and hope that this long write up has been an enjoyable read. Thank you for walking with me through this restoration as I attempt to preserve the legacy of my beloved grand old man!!!!!

 

Finishing up a Stanwell de Luxe Regd No. 969-48 Shape 482 for Paresh


Blog by Steve Laug

Not long ago I was speaking with Paresh and Abha on Facetime and they showed me a Stanwell de Luxe 482 that they had been working on. It was cleaned and ready for restoration. Paresh had filled in the multitude of nicks and dents in the briar with super glue and briar dust. He was not happy with the freckled appearance of the briar once he had finished his repairs. The super glue was very runny and had gone all over the bowl leaving darkened patches where ever it ran all around the bowl. Kind of a mess. There were also some fine pin hole nicks in the shank that were around the stamping. He wanted me to pick up where he had left off and finish the pipe for him. The pipe was stamped on the left side of the shank Stanwell over Regd. No. 969-48 over de Luxe. ON the right side it was stamped Fine Briar over the shape number 482. Working on this pipe was truly not a bad deal for me as it was completely cleaned up by Abha and the stem was cleaned and partially finished as well. It would be interesting to see what I could do with it. When the pipe arrived this is what it looked like. I took some close up photos of the rim top and the bowl from various angles to show the freckled appearance that Paresh was speaking about. I carefully wiped the bowl down with acetone on a cotton pad to remove the excess glue that had run and also the stain that remains in the briar without damaging the repairs. The repair spots begin to show clearly. There are still spots on the shank that need to be dealt with. I sanded the surface of the bowl with 220 grit sandpaper to smooth out the repairs and remove the marks from the runny glue. I polished the briar with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-4000 grit pads. I wiped it down after each pad with a damp cloth. I also used the tip of a dental pick to fill in the many tiny sandpits in the sides of the shank. Once the glue cured I sanded them smooth with the tip of a sanding stick and folded sandpaper. Once the fills were blended into the surface of the shank I polish the shank portion again with the micromesh sanding pads. I stained the bowl with Fiebing’s Tan Aniline stain. The stain is a brownish red colour and should help to hide the many repairs to the bowl.Once the stain had dried to touch I wiped the bowl down with a cotton pad and alcohol. I wanted the stain to be transparent and allow the grain to shine through but still be opaque enough to hide the repairs that both Paresh and I had done. I rubbed down the briar with Before & After Restoration Balm. I worked it into the smooth surface of the briar with my fingertips to clean, enliven and protect it. I let the balm sit for a little while and then buffed the bowl with a cotton cloth to raise the shine. The following photos show the bowl at this point in the restoration process. The grain is really starting to stand out. There were still some grooves near the button that needed to be dealt with before I would be happy with the stem. I sanded the grooves out with 220 grit sandpaper until they were smooth.I polished the stem with micromesh sanding pads to remove the scratches. I wet sanded with 1500-2400 grit sanding pads and dry sanded with 3200-12000 grit pads. I wiped the stem down with Obsidian Oil after each sanding pad. I polished stem and bowl with Blue Diamond to polish out the remaining small scratches. I gave the bowl and the stem multiple coats of carnauba wax. I buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The pipe polished up pretty nicely. The rich reds of the tan stain work well to blend in the majority of the fills in the briar. The pin hole nicks in the finish have almost all been repaired and blended in with the stain coat. The grain really stands on the finished bowl and shank. The polished black vulcanite stem works together with the beautiful grain in the briar to give the pipe a rich look. The finished pipe is shown in the photos below. The dimensions are Length: 6 inches, Height: 2 inches, Outside diameter of the bowl: 1 1/4 inches, Chamber diameter: 3/4 inches. The pipe is ready to head back to Paresh in India once I have finished a few more projects for him. Thanks for walking through the restoration with me as I worked over this beautiful little Stanwell.  There were two larger factory fills in the bowl that were rock hard and not workable. I could not pick them out or get the stain to permeate the putty. They are visible in the next two photos. Ah well they will remain in the finished pipe.

The Vintage Notoriety of Tom Howard and his Jumbo Squat Rustified Tomato


Blog by Dal Stanton

I’ve never restored a pipe where the person who made it had more notoriety than the pipe name itself.  The Tom Howard Jumbo Squat Rustified Tomato came to me along with several others from a good friend I worked with in Ukraine several years ago.  Dave Shain is also a fellow pipe man and restores pipes and has a great website, www.ThePipery.com.  In 2017, Dave won the Master of Pipes award from the Chicago Pipe Collectors Club for his work and charitable activities through The Free Pipe Project where Dave spearheads a program to send quality restored pipes to servicemen serving their country.  I visited Dave where he lives near Atlanta, Georgia, and we had a great time renewing our relationship.  He showed me his workshop, pipe and tobacco collections, and of course, we settled down in the ‘Barn’ flanked by a vintage Ford pickup – his Man Cave, to share a bowl or two.  It was a fun reunion!  I left with a tin of his aged Escudo and several pipes he wanted me to restore for the Daughters of Bulgaria, which I was more than happy to do.  Thanks Dave!The Tom Howard is now on my worktable because another pipe man, Paresh, saw it on The Pipe Steward site in my section, For ‘Pipe Dreamers’ Only!  This is where I post pipes that are in my electronic ‘Help Me!’ basket that others can commission to add to their collections.  Like me, through rebornpipes’ Steve Laug’s encouragement and tutelage, Paresh started restoring some of his own pipes in India, where he lives, and publishing his write ups on rebornpipes.  This LINK will take you to his restorations published on rebornpipes – he does a great job!   After seeing some of my restorations online, Paresh visited The Pipe Steward and saw some pipes that chose him – like Harry Potter and the wizard’s wands!  One thing I’ve learned in my growing relationship with Paresh as we’ve communicated back and forth between Bulgaria and India, is that he doesn’t like large pipes – he LOVES large pipes!  And this Tom Howard Jumbo Squat Rustified Tomato got his attention – here are the pictures he saw in For ‘Pipe Dreamers’ Only!The pipe is marked on the left shank with ‘Tom Howard’ in cursive script and ‘Imported Briar’ on the right shank side in the same script.  For a Squat Tomato, I’ve labeled it a ‘Jumbo’ because it has a definite stout presence in the palm.  The dimensions of the bowl give you an understanding of Tom Howard’s presence: Length: 5 5/16 inches, Height: 1 1/2 inches, Bowl width: 2 1/8 inches, Rim width: 1 1/2 inches, Chamber width: 7/8 inches, Chamber depth: 1 1/4 inches.I had never heard of a Tom Howard stamp on a pipe and after I put the name in search tool on Pipedia I was surprised to find what I found.  Tom Howard was a vintage celebrity in America during the 1940s and 50s.  Here’s the Pipedia said about Tom Howard the man:

Tom Howard was a popular comedian and personality in the 1940s/50s, known for vaudeville stage and radio work. But he also was a skilled pipe maker. In a Popular Mechanic article from 1947 he is written up as the “Hobbyist of the Month, Tom Howard.” He made pipes in his workshop outside his home in Red Bank, NJ. starting about 1939 and looks like into the late 1940’s or later. He purchased briar blocks by the bag as well as stem blanks, and in his well-equipped shop he handcrafted his pipes, in about three hours on average. He was a true craftsman, also specializing is intricate model boats, trains and brass canons, all built to scale.

I was intrigued – this vaudeville and stage comedian made pipes and this pipe came from his workshop made by his hands.  How cool is that?  Desiring to find out more about Tom Howard the man, I searched Wikipedia and found a fun and informative article about his professional life and how he hosted a I was intrigued – this vaudeville and stage comedian made pipes and this pipe came from his workshop made by his hands.  How cool is that?  Desiring to find out more about Tom Howard the man, I searched Wikipedia and found a fun and informative article about his professional life and how he hosted a zany Q&A game show that was spoofing the ‘serious’ Q&A game shows.  It was called “It Pays to Be Ignorant”.   Here is what the Wikipedia article said:

It Pays to Be Ignorant was a radio comedy show which maintained its popularity during a nine-year run on three networks for such sponsors as Philip MorrisChrysler, and  DeSoto. The series was a spoof on the authoritative, academic discourse evident on such authoritative panel series as Quiz Kids and Information Please, while the beginning of the program parodied the popular quiz show, Doctor I.Q. With announcers Ken Roberts and Dick Stark, the program was broadcast on Mutual from June 25, 1942 to February 28, 1944, on CBS from February 25, 1944 to September 27, 1950 and finally on NBC from July 4, 1951 to September 26, 1951. The series typically aired as a summer replacement.

Snooping a bit more, I found an online site that had the July 5, 1951 episode of ‘It pays to Be Ignorant’ available for viewing.  I watched it and it was like I was in a time machine!  The video also included period advertising for cars and tobacco and Tom Howard in form, dawning a professorial gown and a gravelly 1950s vaudeville tin can voice.  It’s great! I clipped a picture of the episode.  If you want to see it yourself, here’s the link:  The Internet Archive.

The Pipedia article I included above, referenced one more source to learn a bit more about Tom Howard.  In a 1947 Popular Mechanics edition he was named ‘Hobbyist of the Month’ – but it didn’t say which month!  With a little bit of help from Google, I found Archive.org that housed old editions of many periodicals including Popular Mechanics.  I started in January and started searching – thankfully they had a search tool I utilized for each month.  Finally, I found the article in the Popular Mechanic 1947 June’s edition.   For the absolute nostalgia of it, and for the interesting information it adds about Tom Howard and especially his pipe production, I’m including the pages here for you to read – including the cover page!  I couldn’t pass it up!   With a greater appreciation for the pipe man, Tom Howard, I take another look at the Jumbo Squat Rustified Tomato before me and based upon the articles above the dating of this pipe could range from the late 1930s to the early 50s as Tom Howard died in 1955 at the age of 70 according to Wikipedia.  The chamber has very little cake buildup.  The rim is worn and the rustification on the rim is filled or simply worn down – I’ll need to clean this to see.  The inner lip of the rim is darkened by scorching.  The rustified stummel is attractive – it has scratches and blemishes from use.  The smooth briar around the rustification is nice looking – I think it will look very nice after cleaned and spruced up some.  The stem has some oxidation and the bit shows minor tooth chatter.  I notice too, that Tom Howard but a subtle bend on the saddle stem to give the stem a definite orientation – nice touch and it looks good too.I begin the restoration by cleaning the internal airway of the stem using a pipe cleaner dipped in isopropyl 95% and then adding it to a soak of Before & After Deoxidizer along with other stems of pipes in queue to be restored.  After a few hours I remove the stem from the bath and wipe it down with a cotton pad wetted with light paraffin oil (mineral oil) removing the light oxidation that was raised from the vulcanite.Turning now to the stummel, to remove the light cake in the chamber I use the Pipnet Reaming Kit.  Even though the cake is light, I want to give the chamber a fresh start.  I jump right to the 3rd largest blade head and finish using the largest.  I follow the reaming blades by using the Savinelli Fitsall Pipe Tool to scrape the chamber wall further, then finish by sanding the chamber with 240 grit paper wrapped around a Sharpie Pen.  To clean the carbon dust, I wipe the chamber with a cotton pad wetted with isopropyl 95%.  I inspect the chamber wall and it looks good – no cracks or heat fissures.  The pictures show the process. To clean the external surface of the stummel, I use undiluted Murphy’s Oil Soap and cotton pads.  I also utilize a bristled tooth brush to clean the rustification as well as a brass bristled brush to work on the rim and the dark scorching on the inner lip. Turning to the internals, I use cotton buds and pipe cleaners with isopropyl 95% to clean. I also employ dental spatulas to scrape the mortise walls as well as a drill bit to clean the airway.  I sized a bit just large enough to fit the airway and hand-turn the bit to clean the tars off the walls.  After some time, the cotton buds and pipe cleaners start coming out cleaner.  Later, I will continue the internal cleaning by giving the internals a kosher salt and alcohol soak.Turning to the stem, I use 240 grit paper to sand out the roughness and tooth dent in the bit area – upper and lower.  I follow this by wet sanding the entire stem with 600 grit paper.  I then use 0000 grade steel wool to sand/buff the stem.  The pictures show the progress. While I was sanding, I notice that the draft hole in the button is not shaped well – a bite compression or something.  I use a sharp needle file to even the opening and I repeat the sanding process for the button end – 240, 600 and 0000 steel wool.With my day ending, I continue the cleaning of the stummel internals by utilizing a kosher salt and alcohol soak.  I create a ‘wick’ by pulling and twisting a cotton ball.  I then insert it and stuff it down the mortise into the airway as much as it will allow.  I then fill the chamber with kosher salt – why kosher?  It will not leave a residue taste as iodized salt.  I place the stummel in an egg cart to keep it steady and fill the bowl with alcohol using a large eye dropper until it surfaces over the salt.  After a few minutes I top it off once more – and turn off the lights. The next morning, the kosher salt/alcohol soak had done its job.  The salt and wick are soiled by drawing out more tars and oils.  I throw the used salt in the waste and wipe the bowl with paper towel and blow through the mortise to dislodge any remaining salt.  I then use a few more cotton buds and pipe cleaners dipped in isopropyl 95% to make sure.  All is good – clean – and I move on! Looking at the stummel, I see several scratches on the smooth briar surrounding the rustification.  The rim isn’t even and it is worn.  I decide to freshen the rim by topping the stummel but only lightly – I don’t want to erase the rustification that Tom Howard placed there many years ago!  Using 240 grade paper on a chopping board, I invert the stummel and give it a few rotations and look.  I do this a few times and decide I’ve taken off enough.  It looks good and the rustification remains intact.  I then switch to 600 grade paper on the topping board and give the stummel a few more rotations.  This erases the rougher 240 scratches and smooths the rim surface.  The pictures show the topping process from the start to finish. Darkened briar remains on the inner ring of the rim from scorching (picture above).  To address this, I introduce a gentle internal bevel using 120 grade paper, followed by 240, then 600.  With each paper grade, I roll the piece of sanding paper into a tight roll and rotate it around the circumference of the internal lip by pinching the paper with my thumb.  This allows a uniform beveling to emerge.  The pictures show the progression. Now to the briar surface.  The smooth briar has a lot of small scratches and rough places throughout.  The first picture below also shows an example of Tom Howard’s rustification processes not contained to the rustification areas. I will spot sand these areas. First, I sand out the overrun rustification marks with 240 and 600 paper.  And then, to address the smooth briar of the entire stummel, I use a rough grade sanding sponge to remove the scratches and blemishes.  I then follow with a medium grade sponge then a light grade sponge.  Taking the stummel to the next step, I wet sand it with micromesh pads 1500 to 2400, then dry sand with pads 3200 to 4000 and 6000 to 12000.  All I can say is, ‘Wow!’  I love watching the grain emerge through the micromesh pad regimen.  Each pad teases out the grain a bit more.  The pictures show the progression. I put the stummel aside and pick up the Tom Howard stem and using micromesh pads 1500 to 2400, I wet sand.  Then I dry sand using pads 3200 to 4000 and 6000 to 12000.  Between each set of three pads, I apply a generous coating of Obsidian Oil that revitalizes the vulcanite stem.  The result is the glossy pop we all expect! Looking again at the stummel, there are some pinhead fills on the left shank side that need to be addressed as well as the worn rustification cuts that have fill material visible and generally, is lighter than desired.  I take some pictures of the different things I see.In the Pipedia article of Tom Howard, there were several pictures of his pipes that were provided courtesy of Doug Valitchka, which give an idea of the original motif used when Tom Howard rustified his pipes.  The picture below shows a dark shaded rustification, though it appears that Mr. Howard put a dye on this stummel to give it a more reddish hue.  Using this picture as a guide, I use a walnut dye stick to color and blend the pinhead fills and to redefine the rustification, yet I prefer the natural briar hue of this Tom Howard Squat Tomato and will not stain the stummel. Now, to ‘rough up’ the rustification, I mount the Dremel with a more abrasive felt buffing wheel set at 40% full power and apply Tripoli compound to the rustification.  The effect is that this softens the hue – blends it more so that it doesn’t look painted.  I think it does the job and I like the blending!I buff the stummel with a felt cloth to remove leftover compound and I apply Before & After Restoration Balm to the stummel.  This Balm works well to bring out the deep hues of the natural briar.  I squeeze some Balm on my finger and I work it into the stummel and rustification.  The Balm begins as a light oil texture then thickens as it’s works into the briar.  I let is set for several minutes then I wipe/buff the Balm residue off with a microfiber cloth. I then reunite stem and stummel and mount a cotton cloth buffing wheel to the stummel, maintain a 40% full power speed, and apply Blue Diamond compound to both stem and stummel.  As before, using a felt cloth, I buff the pipe to remove compound dust left behind before waxing.  I then mount another cotton cloth buffing wheel onto the Dremel, maintain the same speed, and apply carnauba wax to the entire pipe.  I finish by giving the pipe a good hand-buffing with a microfiber cloth to raise the shine of the briar even more.

I’m pleased with the results of the Tom Howard Jumbo Rustified Squat Tomato.  I’m pleased with the textured blending of the rustification with the backdrop of beautiful smooth briar.  The contrast between the two is attractive.  I’m thankful to Dave Shain for giving me this Tom Howard to restore for the Daughters.  I’m also thankful for having discovered through the research the story of an interesting man.  Tom Howard was an accomplished comedian and stage person during his time.  But most interesting to me was his pursuits at home – in his workshop making quality pipes – not on a factory production line, but one pipe at a time with his own hands.  His love of pipes and placing them in other’s hands reminds me somewhat of my own worktable – the love of restoration and passing pipes on to others.  Paresh commissioned this Tom Howard and he will have the first opportunity to acquire him in The Pipe Steward Store.  This pipe will also benefit the Daughters of Bulgaria – our work helping women and girls who have been trafficked and sexually exploited.  Thanks for joining me!

Whatever it takes to make a pipe usable – A Creative WWII Trench Repair


Blog by Steve Laug

I was on Facetime recently with Paresh and Abha in India, talking about pipe restoration and what they were currently working on together. Paresh showed me some of the pipes that they were working on as well as several that he wanted to send to me to work on. One of them was a pipe that had come to him from a family friend who told him it came from WW2 and had belonged to a German soldier. He was not sure what to do with this one and almost felt that it was not worth working on. A piece with that kind of story attached is always interesting to me and I wanted to see it and also work on restoring it. Paresh brought the metal box that the pipe came to him in and the assortment of pieces that made up the pipe to the table to show me what was there. It had what looked like two stem options with it. The one that looked right was a Perspex stem. He was able to remove the brass shank extension from the bowl while were talking and thought he had broken it. I did not think so but underneath the brass there was a broken shank. The brass had been slipped over the broken shank as an extension. The pieces could all be combined to make a functional pipe. I was excited to get this pipe and work on it. Here are some photos of the pipe box. It bears the initials CK and a raise pipe on the cover. When the box was opened the pipe parts were scattered in the larger compartment. There was a bent wire in the box as well. I have a theory how that was used and will talk about it shortly. It is obvious that the box was made to fit a pipe in the upper compartment and tobacco and lighting material in the lower portion. There is a fabric piece fixed to the lid that keeps the pipe from moving around the box.Paresh kept the box in India and mailed the pipe parts to me to see what I could do with them. It took a long time for the pipe to arrive in Vancouver from India. I would have forgotten about it if Paresh had not sent me WhatsApp messages to see if it had made it here. Finally there was a parcel notice hanging on my door when I came home from work. The postie had written that a package was at the post office and I could pick it up the next day after 1pm. I picked it up the next day after work and brought it home. I carefully unwrapped the plastic sleeve that enclosed the box. I cut the tape that held the box closed. Inside were the pipes that Paresh wanted me to work on. The “War” pipe was in a plastic bag and wrapped in bubble wrap. I carefully took it out of the wrappings and put it on the desk. I took the following photos to show the condition of all the parts before I started the cleanup and restoration.I examined the pieces carefully to see if I could come to any conclusions about the provenance of the pipe as it now stood. The bowl was in rough condition but I thought it could be cleaned up to at least carry on the trust of a pipeman from the past. The brass was very interesting and had been cut off on one end. Each end had a different diameter. One end was the size to fit on the broken shank and the other fit the wooden extension. The wooden extension appeared to be oak or a like hard wood. The inside appeared to have been burned and was darkened on each end. It had a copper ring around the end where the stem went. The ring had been hammered smooth and worked onto the shank end to keep it from splitting when the stem was inserted. The two stems were interesting. The white one looked like a cigarillo holder to me and probably was the first stem to be used on the pipe. It could possibly fit over the wooden extension prior to the addition of the copper ring. That leaves me to assume that the clear stem was a later addition and the ring was added to make sure that it did not split the wood when inserted. All parts were very dirty but I could see how they went together to make a smokeable pipe. We talked about the background of the pipe on Facetime and also on WhatsApp several other times and he told me the story that had been passed on to him by the friend of his family. I wrote to Paresh and asked if he could give me a summary about the pipe – write down some of what he had told me in our conversations. This is what he wrote to me.

This WWII pipe was handed over to me by one of my best buddies who has a family tradition of serving in the Army. This pipe once belonged to his eldest maternal Uncle who had participated in WW II as a Sepoy (an Indian soldier serving under British or other European orders) and later during the war rose to become a Junior Commissioned Officer. He had participated in the Operations in North Africa as part of a British Indian Division. It was during one of the battles at El Agheila during November – December 1941 that he had picked this up this pipe with its case from one of the overrun German trenches as a souvenir and had been with him since…. – Regards, Paresh

That was the information that I was looking for about this pipe. It is one thing to assume that the pipe was a War Memorabilia but another thing to get the history behind it. Thanks Paresh. Now I knew that I was dealing with a German soldier’s pipe and pipe case that had been left behind either when he was killed or when he abandoned German trenches in haste fleeing the British Indian Division. His friend’s uncle had picked up the case from the trench as a souvenir. It had remained in the family in the case in parts since that time.

This is where my imagination took over and tried to figure out how the pipe had come to its current state. I wonder what was in the mind of the pipeman who put the pieces together. So I took what I could see and imagined the following scenario from the parts.

Somewhere along the journey of the soldier CK and his pipe he had broken the shank on what must have been his only pipe. It was broken and either could be thrown away as garbage along the way or perhaps he could rebuild it. The broken shank was the impetus for repairing the pipe and the way it was done was highly creative.

The remnant of the shank was carefully modified with a knife judging from the way the broken shank end was carved. The pipe man had used his knife to create a ledge around the broken part where it connected to the bowl. A brass shell casing was cut and modified to fit on the shelf that had been carved thus repairing and lengthening the shank. The shell casing was pressed onto the carved shank until it was almost flush with the back side of the bowl. A piece of wood – branch or an oak stick was “drilled out” by heating the bent wire in the box until it was red hot and then inserting it repeatedly down the middle of the wood branch until there was an airway burned into the center. You can still see the burn marks on the inside.

The one end of the shank was drilled out and inserted into the small diameter end of the shell casing. The other end, the shank end of the piece of was carved out with a knife to receive a stem. There was a hammered copper ring that had been crafted and pressed onto the stem end of the shank. The box contained two different stems with the pipe. The first was a cigarette or cigarillo holder that could have been fit over the top of the dowel. Not very pretty and not very functional as it did not fit well. The second stem was a Perspex stem that was quite long. It obviously was the one used with the pipe as the airway was very dirty. There was also some internal burning in the stem itself that is odd. I wonder if the soldier who fashioned the pipe did not put a burning wire up the stem to open it as well and damage the internals of the stem.

I probably will never know the story behind the pipe for sure but what I have imagined is certainly a very real possibility. Whatever the story is the pipe is a fascinating piece of WWII memorabilia.

With the imagination satisfied and combined with the story that came with the pipe I examined the pipe parts to see what I was dealing with. It was obvious that the pipe was smoked a lot. It was probably the soldier’s only pipe and it rarely sat unlit by the looks of it. The bowl was thickly caked and damaged the externals were worn. It appeared that the pipe had been dropped a few times as there were deep gouges in the briar on the heel of the pipe. The finish on the briar was worn out and dark but underneath there were remnants of what looked like nice grain. The rim top was damaged and the inner edge of the bowl was rough. The bowl appeared to have been repeatedly reamed with a knife. The airway entering the bottom of the bowl was also worn from the piece of wire in the pipe case. I would clean up the pipe and leave the character intact. Many would have left the pipe as it was but to me the work that the original pipeman did to keep the pipe useable made me want to carry on his legacy and give Paresh a chance to at least smoke it.

I decided to clean up all of the parts individually. I scraped out the brass shell casing with a small pen knife and then scrubbed the inside with cotton swabs and isopropyl alcohol until the inside was as clean as the shiny brass exterior. The first photo shows the cut edge that the wooden extension inserted into. The second photo shows smooth edge that sat on the carved ledge against the bowl and the other edge was the cut edge. I cleaned the wooden extension next, scraping the grit and tars that had built up on the inside. The end that fit toward the bowl had an airway drilled through from the other end. It looked to me that the airway had been burned through with a hot wire. It was darkened from being inserted into the brass and as it had oxidized it had coloured the wood. The end that held the stem was carved to receive the tenon. It had been banded with a copper ring to stabilize the wood. I used a pen knife to scrape the grime out of the extension and then cleaned it with pipe cleaners, cotton swabs and alcohol. I used the topping board and 220 grit sandpaper to smooth out the insert end and remove some of the damage to the wood.With the brass and wooden shank extensions cleaned it was time to clean the bowl. I took a photo of the bowl to show the thickness of the cake on the walls and the trough that had been carved in the bottom of the bowl to the airway leaving the bowl. It looks to me that the trough has been gouged out over time by cleaning the pipe with the wire that was in the box. The cake on bowl walls was thick and uneven all the way around. It was also quite crumbly and soft. The pipe smelled musty from the years that it had been sitting since the war. Once it was removed there would be work to be done to smooth out the walls of the bowl. There are spots that appear quite thin and there will need to be at least a bowl coating done to protect the bowl.I carefully removed the cake from the bowl with a Savinelli Fitsall Pipe Knife, scraping it from the walls. You can see from the photos how crumbly and soft the carbon chunks were. I wrapped some 220 grit sandpaper around a piece of dowel and sanded the walls to remove the remaining cake.I used a dental spatula to rebuild the inside back edge of the bowl rim with clear super glue and briar dust. This was just the first step in the process that would take a lot more work to bring it back to a useable condition.I lightly topped the bowl on a topping board with a piece of 220 grit sandpaper. I did not want to remove much of the briar, just smooth out the damage. The first photo shows the topping and the second the rim after topping.I filled in the divots in the bottom of the bowl and carefully repaired what looked like a crack in the briar with clear super glue and briar dust. Once the repair had cured I sanded the repair smooth with 220 grit sandpaper to blend it into the surface of the briar. I carefully sanded the bowl and rim with micromesh sanding pads. I set the bowl aside and worked on putting the parts of the shank extension back together. I heated the brass shell casing with a Bic lighter to expand it enough to be pressed on to the wooden shank tube. I scrubbed the tube with Before & After Pipe Balm and lightly sanded the extension with 220 grit sandpaper. I polished the brass and copper band with micromesh sanding pads.I cleaned out the inside of the newly reassembled shank with alcohol, pipe cleaners and cotton swabs. I cleaned out both ends of the new shank.I cleaned out the broken shank on the bowl with pipe cleaners, cotton swabs and alcohol in preparation for gluing on the shank extension. I dried it out and coated the shelf with white all-purpose glue. Once the glue was in place I pressed the shank extension onto the bowl. I wiped away the excess glue. Once the glue had set I took pictures of the pipe at this point in the process. To match the stain remaining on the bowl I used the mislabeled tan aniline stain. It is a reddish-brown almost cordovan coloured. I figured it would match the existing colour very well. I applied the stain with a dauber and flamed it with a lighter to set it in the grain. I repeated the process until the coverage on the bowl was even.I wiped the bowl down with alcohol on a cotton pad to even out the coverage and make the stain more transparent. I wanted the grain to show through the finish. I used a folded piece of 220 grit sandpaper to smooth out the inner edge of the rim and the inside of the bowl.I set the bowl aside and turned my attention to the stem at this point in the process. It was truly a mess. There were tars and oils lining the airway making it almost black and there was damage to the interior of the stem material around the airway. I started the cleaning process using liquid cleanser and pipe cleaners to remove some of the tars. I was able to get a lot of the stuff out of the airway.I used a small round needle file to further clean out the airway. I sanded the interior of the airway to smooth out the surface of the drilled area. I ran alcohol dampened pipe cleaners through after the files to clean out the dust. The stem was finally getting clean. I took some close up photos of the stem to show the airway after filing. The photos also show the internal damage to the stem from what looks like fire. I polished the stem with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I wiped the stem down after each pad with Obsidian Oil. I rubbed down the briar and the oak shank extension with Before & After Restoration Balm. I worked it into the smooth surface of the briar and oak with my fingertips to clean, enliven and protect it. I let the balm sit for a little while and then buffed the bowl with a cotton cloth to raise the shine. The following photos show the bowl at this point in the restoration process. The grain is really starting to stand out. I polished stem and bowl with Blue Diamond to polish out the remaining small scratches. I gave the bowl and the stem multiple coats of carnauba wax. I carefully buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The pipe polished up pretty nicely. The newly stained finish works well when polished to really highlight the variety of grains and mask the damage around the bowl and shank. The polished Perspex stem works together with the beautiful grain in the briar and the brass and oak shank extension to give the pipe a rich look. The finished pipe is shown in the photos below. The shape, finish and flow of the pipe and stem demonstrate the creativity of the German soldier CK who left it in the trenches of North Africa. The dimensions are Length: 7 inches, Height: 1 inch, Outside diameter of the bowl: 1 1/4 inches, Chamber diameter: 3/4 inches. The pipe is ready to head back to Paresh in India once I finish the other ones he sent to me. This pipe has really travelled – from Germany to North Africa to India to Canada and back to India. I wish it could tell its own story. Thanks for walking through the restoration with me as I worked over this interesting piece of memorabilia. 

Tale of Two Somerset Brothers – Part 1


PANELED BILLIARD

Blog by Paresh Deshpande

There are two SOMERSET pipes in my inherited pipe collection; one is a Paneled Billiards and other is a Rhodesian (which is my favorite shape). If there was a pipe/ pipes amongst the large number of inherited pipes that I am not attracted to, this Paneled Billiard ranks right there at the top. The reason for this lack of attraction is primarily two fold; firstly, this eight paneled billiard is a shape which I do not like. I prefer pipes with an even shape either smooth or rusticated or sandblasted, but panels, definitely not my taste. Secondly, the SOMERSET brand, which I had never heard of and neither had I bothered to know more about due to shape!!!!! However, once while discussing pipes on a video call with Mr. Steve, I showed him this pipe and suggested that I would like to discard it as I did not like the shape and also it’s an unknown brand. Mr. Steve, in his wisdom and experience suggested that I should reconsider as SOMERSET is quite possibly a brand of Comoy’s seconds!!!!!! With this suggestion, I decide to work on this pipe.

This square shank, eight paneled billiard has a smallish bowl size with a chamber depth of about 1.1 inches with somewhat thin walls. Beautiful sandblast is seen on the bowl, rim and on three sides of the shank. The bottom surface is smooth, flat without any sandblast and bears the only stampings seen on the pipe. It is stamped on the bottom as “SOMERSET” in a mild arch over “IMPORTED BRIAR” in straight line, all in capital letters. There is no other stamp on either stummel or on the stem. The stummel and shank is stained with a very dark reddish/ maroon hue. The stem is high quality vulcanite without any stampings.I have tried in vain to unearth information on this brand in general and this pipe in particular. Alas!!! I haven’t been able to garner any information from the internet, apart for the input provided by Mr. Steve!!!!! I would love to receive any information that may be available with you on this pipe.

INITIAL VISUAL INSPECTION
This pipe has been well used (and subsequently, I realized ABUSED!!!!!!!) as is evident from the thick cake in the chamber and damage to the inner edge of the rim in 12 ‘O’ clock direction. The sandblast is deeply filled with dust, tars and grime of all the yesteryears of smoking and subsequent disuse for last 35-40 years. The rim top is also sandblasted and there is overflow of lava on to the rim top. As mentioned above, there appears some minor charring to the inner edge of the rim. This needs to be looked into after the bowl has been reamed of all the cake.

The mortise is clogged and air does not flow through it. This condition is consistent with that I have seen on my grand old man’s other pipes!!!! The mortise had clogged, adversely affecting the performance of the pipe and hence had been conveniently set aside and replaced by another one. Such was his habit, it appears.The stem is oxidized but more heavily towards the lips. There is minor tooth chatter with a couple of slightly deeper bite marks on both surfaces of the stem. The fitting of the tenon in to the mortise is very loose and will have to be addressed.THE PROCESS
I start the restoration process by reaming the chamber to get rid of all the cake, using a Kleen Reem pipe tool. I further scrapped the walls of the chamber with a fabricated knife and took the cake down to the bare briar. This is the time when I observed a damage which every restorer of pipes fears the most. With a cringe, I observed a distinct line emanating from a point about mid way of the chamber, above the draught hole extending upwards and downwards. To explore further and also to smooth and remove the last remnants of the cake, I sand the walls of the chamber with a folded piece of 150 followed by a 220 grit sand paper. To my horror, I observed that from the point where I had first observed the crack, there were other cracks which extended around the walls in a circular pattern along the middle of the bowl. I checked the exterior of the stummel and was relieved to find it was solid and that the crack did not extend to the outer surface. Here are the pictures of the process and the damage observed. I was wondering as to how I should address this issue as I did not have J B Weld, when I remembered that Mr. Steve had repaired my inherited Barling Ye Olde Wood by coating the chamber with a mixture of sour cream and activated charcoal. I searched my tool and material box and realized that I was only carrying a few capsules of activated charcoal. The jar of activated charcoal, along with bulk of my pipes, was left behind when I moved to my place of work. I shared the pictures of the damage and predicament with Mr. Steve. He confirmed that this appeared like the beginning of a “burn through” or a “crack”. He also suggested an easier and practical solution; a coating of pipe mud made using pipe ash and water!!! Only a person of his knowledge and experience can share such simple and easy-to-do solutions to complex problems. Thanks again, Sir. The next couple of days were spent in collecting pipe ash!!! Lol…… All readers and first time restorers are advised to collect and keep a jar of pipe ash handy!!!!! Or collect Cigar ash which works just fine.

While collecting ash over the last couple of days, I undertook the restoration of the Somerset Rhodesian and soon realized that this one too had cracks in the bowl. Thus I was now tackling this issue on two pipes simultaneously!!!!! More detailed write up on the Rhodesian will be posted separately. Meanwhile I addressed the stem of the Paneled Billiard. Using a Bic lighter, I flamed the surfaces of the stem to raise the tooth chatter and minor bite marks. I was surprised to find that this process had raised all the bite marks and tooth chatter to the surface. All I was left to do was sand the surfaces with sand paper followed by the micromesh pads. I sanded it with 220, 400 and 800 grit sand paper. I wiped the stem with cotton pad dipped in alcohol to remove the resultant dust. I rubbed some extra virgin olive oil in to the stem and set it aside to be absorbed in to stem. I polished the stem with micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000. I rub a little extra virgin olive oil in to the stem after every three pads. I finish the polishing of the stem by rubbing a small quantity of Paragon wax and giving it a final polish with a soft cotton cloth. The stem is now nice, smooth and shiny. I cleaned the airway in the stem with pipe cleaners and alcohol. The issue of a loose-fit between tenon and mortise was addressed by heating the tenon with a Bic lighter, constantly rotating the stem, till the tenon was slightly pliable. I gently pushed a rounded needle file in to the tenon to enlarge it and set it aside to cool down. Once cooled down, I wiped it clean with a cotton cloth soaked in cold water. I tried the fit, and the stem sat in the shank snugly, making all the right kind of noises. I was very pleased with the fit.I cleaned the internals of the mortise and the airway with hard bristled and regular pipe cleaners and isopropyl alcohol. I scrubbed the mortise with shank brush dipped in alcohol. The internals of the shank are now clean and the pipe smells fresh and new. There are no traces of ghost smells from the stummel.Having addressed the internals, I turn to address the exteriors. I gently scrapped the charred rim down to the bare solid briar. Though this has resulted in a slight undulation to the rim surface, it is very minor and hence, I left it alone. Another reason to let it be was that if I had a Dremel machine, I would have topped the bowl and then carved out very small rustications to match the sandblasted stummel. But I do not have a Dremel machine!!!! That issue settled, I wash the dirty stummel with Murphy’s oil soap and a tooth brush. I thoroughly scrub the sandblast with the hard bristled toothbrush to remove the oils, tars, dirt and grime lodged in the surface. I rinse it under tap water, dried it with paper towels and set it aside to completely dry out. Having collected sufficient quantity of pipe ash, I decided to address the chamber cracks. I cleaned the interiors of the chamber with a cotton ball dipped in isopropyl alcohol. Once cleaned, I inserted a folded pipe cleaner into the shank and up to the draught hole to prevent it from clogging. I made putty like paste of pipe ash and water. This paste was evenly applied to the entire inner surface of the chamber with a thin bamboo frond with shaved end to form a spatula, a bigger one at that, as compared to a regular one. I set it aside to dry out. The climate here being very wet and humid, it will take a long time to dry out.The coating dried completely after about a week and I just gently scrapped the chamber with very light hands to check the layer. Alas, the complete coating just crumbled out leaving a very dry coat of ash through which all the cracks were easily discernible.So, it’s back to square one and all the efforts and waiting has come to a naught!!!! I shared the above pictures with Mr. Steve with a suggestion of using HONEY as a bonding agent rather than water. When he replied that he had never used honey but, uses YOGURT if water mix fails, I dropped the idea and decided to go ahead with yogurt!!!!Fortunately, I had started collecting pipe ash and mixed it with yogurt. Using the same earlier method, I applied an even coat of pipe ash, yogurt and also added two capsules of activated charcoal. I set it aside to dry out, praying that the mixture bonds well and sticks to the walls of the chamber. A few days later, the mixture had completely cured and it did not crumble. The bonding appeared to be strong and durable. With a 400 grit sand paper, I sanded the inner walls very lightly to a smooth surface. Now the internal walls are looking solid and I can’t wait to load my King of England tobacco and enjoy my fruits of labor. Once the stummel had dried out completely, I rubbed a small quantity of “Before and After Restoration Balm” in to the briar and let it rest for a few minutes. The balm almost immediately works its magic and the briar now has a nice vibrant appearance. I further buff it with a horse hair shoe brush. To finish the pipe, I rubbed a small quantity of HALCYON II wax which is used for rusticated/ sandblasted surfaces and set it aside for a few moments. Thereafter I polish it with a horse hair shoe brush and a soft cotton cloth. Though, the pipe feels small in my hands, the chamber is decent sized. Notwithstanding the size, this is a beautiful looking pipe with some great sandblast patterns. The pipe is very well made and of high quality craftsmanship as evidenced by the perfectly aligned and matching edges of the stem and shank as well as the quality of the vulcanite stem. The finished pipe is shown below.

Kathy’s Dad’s Pipes – Restoring a Barontini De Luxe Brandy


Blog by Steve Laug

The next pipe on the work table is also from George Koch’s estate. It is a Barontini De Luxe Brandy shaped pipe with a quarter bend. The pipe was one of many that came to my brother and me in several shipments of pipes from George’s daughter Kathy. When Jeff got each box the pipes were well wrapped and packed. Jeff unwrapped them and took the following photo to give an idea of the volume of the pipes that we purchased. The Barontini came in mixed in a box of pipes much like the one below.In each of the previous blogs that I have written on the restoration of George’s pipes I have told his story. To me it is important to keep the story attached to the pipes that came from his collection. Each pipe I work on I remind myself of the man and in the work give a remembrance to the pipeman who owned these pipes. Having held a large number of his pipes in my hand and having a pretty good feel for the shapes, colour and stems that he liked, I can almost imagine George picking out each pipe in his collection at the Malaga shop in Michigan. I am including Kathy’s brief bio of her father and a photo of her Dad enjoying his “Malagas”. Here is George’s bio written by his daughter.

Dad was born in 1926 and lived almost all his life in Springfield, Illinois. He was the youngest son of German immigrants and started grade school knowing no English. His father was a coal miner who died when Dad was about seven and his sixteen year old brother quit school to go to work to support the family. There was not much money, but that doesn’t ruin a good childhood, and dad had a good one, working many odd jobs, as a newspaper carrier, at a dairy, and at the newspaper printing press among others.

He learned to fly even before he got his automobile driver’s license and carried his love of flying with him through life, recertifying his license in retirement and getting his instrumental license in his seventies and flying until he was grounded by the FAA in his early eighties due to their strict health requirements. (He was never happy with them about that.) He was in the Army Air Corps during World War II, trained to be a bomber, but the war ended before he was sent overseas. He ended service with them as a photographer and then earned his engineering degree from University of Illinois. He worked for Allis Chalmers manufacturing in Springfield until the early sixties, when he took a job at Massey Ferguson in Detroit, Michigan.

We lived in Livonia, and that’s where his love for Malaga pipes began. After a few years he returned to Allis Chalmers and we moved back to Springfield. I remember that when we went back to Michigan to visit friends, Dad had to go to the Malaga store and acquire a few new pipes. Many a year I wrote to Malaga and they picked out a pipe for me to purchase that I could give Dad for a Christmas or birthday present. He was always pleased. His favorites were the straight stemmed medium sized bowl pipes, but he liked them all. 

He had some other pipes, but the Malagas were his favorites. I remember him smoking them sitting in his easy chair after work, with feet up on the ledge by the fire burning in the fireplace.  Growing up it was my job to clean them and he liked the inner bowl and stem coated with Watkins vanilla, leaving a little of that liquid in the bowl to soak in when I put them back on the rack. Dad quit smoking later in life and so they’ve sat on the racks for many years unattended, a part of his area by his easy chair and fireplace. Dad passed when he was 89 years old and it finally is time for the pipes to move on. I’m very happy they are being restored by you and your brother and hope they find homes who enjoy them as much as Dad did. Thank-you for your care and interest. — Kathy, the oldest daughter

Each blog I have posted I thank Kathy for providing this beautiful tribute to her Dad. Jeff and I appreciate your trust in allowing us to clean and restore these pipes. We are also trusting that those of you who are reading this might carry on the legacy of her Dad’s pipes as they will be added to the rebornpipes store once they are finished.

The next the pipe is a nicely shaped Barontini Brandy with an acrylic stem. It has beautiful grain all around the bowl – straight, flame and birdseye that is highlighted by the rich reddish brown stain. The top of the bowl is had some burn marks and some damage. The stamping on the top side of the shank read Barontini over De Luxe. On the underside it has the shape number 702 and Italy at the shank/stem junction. The gold and brown, swirled, pearlized Lucite stem had light tooth dents and chatter on the top and the underside of the stem. The interior of the pipe was caked and had cobwebs. Jeff took these photos before he started the cleanup work on the pipe. Jeff took a close up photo of the bowl and rim to show the condition of the pipe before he started his cleanup work. The rim top had some light lava overflow and some darkening. There appeared to be some rim damage on the inner edge toward the front of the bowl. You can see the wear on the rim top, the cake and remnants of tobacco in the bowl. It also looks like there are some cobwebs in the bowl. The pipe is dirty but in good condition.  He also took photos of the sides and bottom of the bowl and shank from the side to show the grain on this pipe. The finish is very dirty but this is a beautiful pipe. Jeff took some photos to capture the stamping on the top and underside of the shank. The first photo shows the top side of the shank with the stamping Barontini De Luxe and the second shows the shape number 702 on the underside. The third photo shows the ITALY stamping on the underside near the stem. There is also a B stamped on the acrylic stem.The next two photos show the stem surface. There are tooth marks and chatter on both sides near the button. There is also some wear on the sharp edge of the button.I looked up some information on the brand on the Pipephil website to get a quick overview of the history (http://www.pipephil.eu/logos/en/logo-b2.html). I did a screen capture of the listing for the brand. The fascinating thing that I learned in this quick overview was the connection to the entire Barontini family and to other companies like Aldo Velani. It is interesting to see the breadth of the brand in the following screen capture. The  pipe I am working on it stamped like the third photo down – the Classica and the B on the stem is identical to that pipe’s stamping.Pipedia gives further history of the brand (https://pipedia.org/wiki/Barontini,_Ilio) under the listing for Ilio Barontini. I quote that article in full as it has the connection to the De Luxe pipe that I am working on.

Cesare Barontini, who was in charge of the Barontini company since 1955, helped his cousin Ilio Barontini to establish a pipe production of his own.

Ilio started to produce machine-made series pipes of the lower to the middle price categories. Fatly 80% of the pipes went to foreign countries, the bulk being produced for various private label brands. Some of the own lines like “de Luxe”, “Etna” or “Vesuvio” gained a certain popularity. Citation: “Next to excellent craftsmanship Ilio Barontini pipes offer a wood quality, that is almost unrivalled in this price category!”.

The pipes being around still there were some unconfirmed utterances that Ilio Barontini brand has been absorbed by Cesare Barontini or even Savinelli. Who knows?

Now I had some idea of the maker of this Barontini. It appears to be one of the machine made Barontinis in the De Luxe line. Fueled by that information it was time to get working on the pipe itself and see what I had to do with it.

Jeff had reamed the bowl with a PipNet pipe reamer and followed up with a Savinelli Fitsall pipe knife to remove the cake. He scrubbed out the mortise and the airway in the shank and the stem with alcohol, cotton swabs and pipe cleaners. He scrubbed the exterior of the bowl, rim, shank and stem with a tooth brush and Murphy’s Oil Soap to remove the oils and tars on the rim and the grime on the finish of the bowl. He rinsed it under running water. He dried it off with a soft cloth. The rim was thoroughly cleaned and the damaged areas were obvious. Without the grime the finish looked really good. The Lucite stem would need to be worked on but I really like the profile it cast. I took photos of the pipe to show its condition before I started my work on it.   I took close up photos of the bowl and rim top as well as the stem. You can see the condition of the rim top and bowl in the first photo. Jeff was able to remove all of the tar and oils but you can now see the damaged areas on the surface clearly. There are damaged spots on the front inner edge and the back inner edge. There are also some deep dents and nicks in the flat surface of the rim. The acrylic/Lucite stem had tooth chatter and some light tooth marks on the top and underside of the stem just ahead of the button. There was one deeper tooth mark on the underside near the button.I decided to address the damage to the rim top first. I topped the bowl on a topping board using 220 grit sandpaper. I removed the damaged surface of the rim and made it smooth once again.I used a folded piece of 220 grit sandpaper to smooth out the inner edge of the rim. The rim top is looking far better at this point.I polished the rim top with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I wiped the rim off after each sanding pad to remove the dust. The rim really shone once it was polished. Once it was polished the rim was ready to be stained. I started by using stain pens. I used a Maple stain pen to match the colour of the bowl. It was the closest I could get to matching the bowl. Once it cured it was streaked and not quite a match. The first photo below shows the rim after the stain pen.I carefully wiped the rim down with some isopropyl alcohol to smooth out the stain. Once it was smooth I restained it with some Fiebing’s aniline stain. I used a tan coloured stain and flamed it once I had stained the rim. I repeated staining and flaming until the coverage on the rim matched the bowl sides. The second photo below shows the look of the rim after this staining. I rubbed down the briar with Before & After Restoration Balm. I worked it into the smooth surface of the briar with my fingertips to clean, enliven and protect it. I let the balm sit for a little wall and then buffed with a cotton cloth to raise the shine. The following photos show the bowl at this point in the restoration process. The rim matches well but still needs to be polished and buffed to raise a shine on it. There were some tooth marks and chatter on the top and more chatter and a deeper tooth mark on the underside of the acrylic stem at the button. I cleaned off the surface of the stem with alcohol and filled in the deep tooth mark with clear super glue. Once it cured, I sanded both sides smooth with 220 grit sandpaper to blend the tooth chatter and the repair into the surface of the stem. It did not take too much sanding to remove the marks and smooth out the stem surface. When it was sanded it was smooth and the marks were gone. I polished the acrylic stem with micromesh sanding pads – wet sanding with 1500-2400 grit sanding pads and dry sanding it with 3200-12000 grit sanding pads. I wiped it down after each sanding pad with a damp cloth. I the polished stem and bowl with Blue Diamond to polish out the remaining small scratches and raise the shine. I gave the bowl and the stem several coats of carnauba wax and buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The pipe polished up pretty nicely. This turned out to be a beautiful pipe in terms of shape and finish. This is the thirteenth pipe that I am restoring from Kathy’s Dad’s collection. I am looking forward once again to hearing what Kathy thinks once she sees the finished pipe on the blog. The finished pipe is shown in the photos below. The dimensions are Length: 6 inches, Height: 2 inches, Outside diameter of the bowl: 1 3/8 inches, Chamber diameter: ¾ of an inch. Thanks for walking through the restoration with me as I worked over this Barontini Brandy from George’s estate. More will follow in a variety of brands, shapes and sizes. I will be adding it to the rebornpipes store shortly so if you are interested in adding it to your collection and carrying on the trust from her father send me an email or a message on Facebook. Thanks for looking.