Tag Archives: fitting a stem

Farida’s Dad’s Pipes #7 – Restoring a Charatan’s Make Belvedere 48DC Pot


Blog by Steve Laug

I am back working on one of the two pipes that are left in the lot that came from the estate of an elderly gentleman here in Vancouver. I met with his daughter Farida almost a year ago and we looked at his pipes and talked about them then. Over the Christmas 2017 holiday she brought them by for me to work on, restore and then sell for her. There are 10 pipes in all – 7 Dunhills (one of them, a Shell Bulldog, has a burned out bowl), 2 Charatan Makes, and a Savinelli Autograph. I have restored all but three of them – a Dunhill Shell and the two Charatan’s Makes. His pipes are worn and dirty and for some folks they have a lot of damage and wear that reduce their value. To me each one tells a story. I only wish they could speak and talk about the travels they have had with Farida’s Dad.

The pipe I am working on is a Charatan’s Make Belvedere. Whenever I see that stamping I am taken back to a US sitcom that I used to watch in the 80s called Mr. Belvedere. It was about a butler, Lynn Aloysius Belvedere who worked for an American family called Owens. Throughout the series, Mr. Belvedere serves as a mentor of sorts to Wesley as well as to the other children. Being a cultured man with many skills and achievements (having even once worked for Winston Churchill), he also comes to serve as some sort of “counselor” to the Owens clan, helping them solve their dilemmas and stay out of mischief (https://en.wikipedia.org/wiki/Mr._Belvedere).

The stocky and solid look of this cultured Charatan’s Make Belvedere is built almost as solidly as Lynn Aloysius Belvedere. When it came to me it was worn and tired looking. I have already caused a lot of discussion on the cleanup of this pipe on the Facebook Tobacco Pipe Restorers Group. The ongoing debate of Restoration vs. Preservation filled a lot of airtime on the group. I do not care to relive or recount that as I am only following the directives of the daughter of the original deceased pipeman. She wanted them restored to usable condition so others can carry on her father’s love of these pipes. She is quite happy with the finished results and others of his pipes are now all over the world being enjoyed by the next generation of pipemen.

When first looked at the pipe here is what I saw. The bowl on the pipe was thickly caked and the cake had flowed over onto the smooth finish on the rim top forming hard lava that made the top uneven. It was hard to know if there was damage to the inner and outer edges of the rim and I would not know until I removed some of the grime. It looked like there was some burn damage on the top toward the front of the bowl but it was hard to know. The outer edge looked far better than any of the other pipes in this collection when I started. The finish was invisible under the thick coat of oils and grime that covered the bowl and shank. In fact at this point I had no idea what the stamping looked like because it was covered. I have wondered as I cleaned the other pipes in this lot if the oily build up was a combo of the life lived in the Antarctic. The stem was oxidized and very dirty but otherwise in good condition. There was a thick sticky, oily substance on the surface of the stem that I could scrape with my fingernail. There were tooth marks and chatter on both sides in front of the button. The stem would not seat properly in the tenon do to the tars in the shank. I took photos of the pipe to show what it looked like before I started the cleanup work. I took close up photos of the bowl and rim top as well as the stem. You can see the condition of the rim top and bowl in the first photo. The outer edge appears to be in decent condition under the grime and lava. The inner edge looks ok but there looks like some damage on the front. I won’t really know the full story until I remove the thick lava overflow on the surface. The stem had tooth chatter and some bite marks on the top and the underside of the stem just ahead of the button.It has been a while since I have worked on the remaining pipes that belonged to Farida’s Dad. I thought it might be helpful to remind us all of the background story of these pipes. Here is the material that I quoted in previous blogs. I have included both the written material and the photo that Farida included of her Dad.

When I wrote the blog on the Classic Series Dunhill and thinking about its travels, Farida sent me an email with a short write up on her Dad. She remembered that I had asked her for it so that I could have a sense of the stories of her Dad’s pipes. Here is what she wrote: My dad, John Barber, loved his pipes. He was a huge fan of Dunhill and his favourite smoke was St. Bruno. No one ever complained of the smell of St. Bruno, we all loved it. I see the bowls and they’re large because he had big hands. When he was finished with his couple of puffs, he would grasp the bowl in the palm of his hand, holding the warmth as the embers faded. The rough bowled pipes were for daytime and especially if he was fixing something. The smooth bowled pipes were for an evening with a glass of brandy and a good movie. In his 20s, he was an adventurer travelling the world on ships as their radio operator. He spent a year in the Antarctic, a year in the Arctic and stopped in most ports in all the other continents. He immigrated to Canada in the mid-fifties, working on the BC Ferries earning money to pay for his education. He graduated from UBC as an engineer and spent the rest of his working life as a consultant, mostly to the mining companies. Whatever he was doing though, his pipe was always close by.

She sent along this photo of him with his sled dogs in the Antarctic sometime in 1953-1954. It is a fascinating photo showing him with a pipe in his mouth. He is happily rough housing with his dogs. As a true pipeman the cold does not seem to bother him. Thank again Farida for sending the photo and the story of your Dad for me to use. I find that it explains a lot about their condition and gives me a sense of who Dad was. If your Dad was rarely without a pipe I can certainly tell which pipes were his favourites.As I looked over the pipes I noted that each of them had rim damage and some had deeply burned gouges in the rim tops. The bowls seemed to have been reamed not too long ago because they did not show the amount of cake I would have expected. The stems were all covered with deep tooth marks and chatter and were oxidized and dirty. The internals of the mortise, the airway in the shank and stem were filled with tars and oils. These were nice looking pipes when her Dad bought them and they would be nice looking one more when I finished.

Here are the links to the previous six blogs that I wrote on the five pipes that I have finished. The first was a Dunhill Shell oval shank pot (https://rebornpipes.com/2018/02/04/restoring-a-1983-dunhill-shell-41009-oval-shank-pot/). The second was a Dunhill Classic Series Shell Billiard (https://rebornpipes.com/2018/02/08/faridas-dads-pipes-2-restoring-a-1990-lbs-classic-series-dunhill-shell-billiard/). The third pipe was a Savinelli Autograph (https://rebornpipes.com/2018/02/15/faridas-dads-pipes-3-restoring-a-savinelli-autograph-4/).The fourth pipe was a Dunhill Red Bark Pot that was in rough shape (https://rebornpipes.com/2018/03/10/faridas-dads-pipes-4-restoring-a-dunhill-red-bark-pot-43061/). The fifth pipe was a Dunhill Root Briar Bent Billiard (https://rebornpipes.com/2018/07/07/faridas-dads-pipes-5-restoring-a-dunhill-root-briar-56-bent-billiard/). The sixth pipe was a Charatan’s Make Distinction https://rebornpipes.com/2018/08/22/faridas-dads-pipes-6-restoring-a-charatan-make-distinction/

Today, I went back to the remaining two pipes in the collection today and chose to work on the Charatan’s Make – a pot shaped pipe. It was dirty so it took a bit of cleaning on the shank to read the stamping. On the left side of the shank it is stamped Charatan’s Make, over London, England over Belvedere. Under that at the bowl shank junction is a cursive L in a circle denoting a Lane era pipe. To the right of the stamping near the shank stem junction it is stamped with the shape number 48DC. The DC refers to the Double Comfort style stem. The smooth finish was sticky with oils and thick grime. The bowl felt oily to touch.

To try to figure out the era of the Charatan’s pipe I was working on I turned to the pipephil website, Logos and Stampings. There is some really helpful information on each of the lines of Charatan’s Make pipes that entered the market. Here is the link to the section of the site that I turned to, http://www.pipephil.eu/logos/en/logo-charatan.html. There is an alphabetical listing of the lines but the Belvedere they showed had a stem made for a 9mm filter while the one I have is a nonfiltered pipe. The site did give a short history of the brand. I quote the portion that is most pertinent.

The brand was founded in 1863 by Frederik Charatan. When his father retired in 1910, Reuben Charatan took over the family business. All the pipes were handmade until 1973. The brand name has been overtaken by Dunhill in 1978 and sold in 1988 to James B. Russell Inc.(NJ, USA). During the period 1988-2002 Charatans were crafted by Butz Choquin in St Claude (France). Dunhill re-purchased Charatan brand name in 2002 and Colin Fromm (Invicta Briars, Castleford) followed up on freehand production.

I turned to Pipedia to see if I could find more information on the brand and possibly a link to the Distinction line (https://pipedia.org/wiki/Charatan) but once again in the general article it was not listed.  It did give a little more historical information. I quote the pertinent parts and have highlighted in bold the sections that give information on this particular pipe.

In 1863 Frederick Charatan, a Russian/Jewish immigrant, opened a shop in Mansell Street, located in the borough of Tower Hamlets, London E1, where he began to carve Meerschaum pipes. These pipes got very popular soon, and thus Charatan moved to a bigger workshop in Prescot Street, just around the corner. Here he began to make briar pipes which should make the name famous the world over. Charatan was the first brand to make entirely hand-made briars from the rough block to the finished pipe including the stems. The nomenclature “Charatan’s Make” refers to this method of production and was meant to differ Charatan from other brands who “assembled” pipes from pre-drilled bowls and delivered mouthpieces.

Being the undisputed No. 1 in English pipemaking, Charatan was approached by Alfred Dunhill who was unsatisfied with the quality of the pipes he imported from France. During 1908 – 1910 Dunhill bought pipes from Charatan paying exorbitant prices to ensure he had some of the very best pipes for sale in England. In 1910 he lured away Joel Sasieni, one of Charatan’s best carvers, and opened his own small pipe workshop on 28 Duke Street. On the retirement of his father in 1910 Reuben Charatan took over the family business…

…The pre-Lane period (prior to 1955) and the Lane era pipes (1955 to until sometime between 1979 – 1984) are of primary interest the collector. The Lane era is often quoted as beginning about 1950… Charatan records are almost non-existent before Lane due to a factory fire, making it difficult to date pre-Lane pipes. Charatan used 4 basic grades prior to 1950: Supreme, Selected, Executive, and Belvedere. After 1950 Herman Lane’s influence began, and the grades started to expand. In 1955 Lane took over sole distributorship of Charatan in the US. In 1957 he introduced the Supreme S. Most of his other introductions were from the 60’s and early 70’s…

The section called Miscellaneous Notes had some interesting information.

Charatan records indicate the DC (Double Comfort) bit was introduced in the 50’s, but some report seeing them in earlier production. Still others indicate they were introduced by Lane in 1960. Regardless, the DC bit is not an accurate way to date a pipe because many Charatan’s were made with regular and saddle type bits throughout the “Lane Era”…

…The Lane Trademark serif and circled L indicates the pipe is from the “Lane Era” (approx. 1955 to 1979 -1984?), however it appears that both the English factory or Lane themselves sometimes, or perhaps even often forget to stamp the L on a pipe. The Charatan factory was known for inconsistencies, especially in stampings. Therefore, although an L on the pipe definitely defines it as a Lane Era pipe, the lack of it could simply mean the pipe missed receiving the stamp from the factory. The lack of the trademark could also mean the pipe was destined for the European market.

I continue digging further into the dating of the pipe, but what I had found was a good start for me. If some of you would like to try your hand at dating it more accurately as to the time period it came out you might want to check out the article on Pipedia on Dating Charatans (https://pipedia.org/wiki/Dating_of_Charatans). I had enough for me to start working on the pipe itself and see what lay beneath the heavy tars and oils.

Like most work the refurbisher does this one walks a fine line between restoration and preservation. The deciding feature with this pipe was the wishes of the family. They wanted the pipe to be cleaned and smoked by someone who could carry on the pipe man’s legacy of their Dad. I understand that it meant changing the current state of the pipe to bring it back closer to the way it was when their father bought it. I reamed the bowl with a PipNet reamer. I used two of the four cutting heads to clean out the cake. The bowl was thickly caked I started with the smaller of the two and worked my way up to the second which was about the same size as the bowl. I cleaned the remnants with a Savinelli Fitsall Pipe Knife and scraped it back to bare briar. I finished by sanding the inside of the bowl with a dowel wrapped in sandpaper. I scraped the top of the rim with the edge of the Savinelli Fitsall Pipe Knife to remove the lava. I scrubbed the exterior of the bowl and shank with a tooth brush and Murphy’s Oil Soap to break through all the grime. I rinsed the bowl under running water to remove the grime and grit. I repeated the process until I had the bowl clean. I took photos of the cleaned exterior of the bowl to show where things stood at this point in the process. I topped the bowl on a topping board with 220 grit sandpaper to remove the damage to the top surface of the rim and clean up the damage to the edges. I did not have to remove a lot and repeatedly checked it to make sure that I had removed enough but not too much. I wanted to take the rim top down until the burn damaged area was smooth and minimized. The second photo shows the remaining burn mark at the front of the bowl. I used a folded piece of 180 and 220 grit sandpaper to bevel the inner edge of the rim until I had removed most of the damage on the back inner edge.With the externals clean it was time to clean out the mortise and shank and airway into the bowl and the airway in the stem with alcohol, cotton swabs and pipe cleaners. I scraped the mortise with a dental spatula and a pen knife to loosen the tars before cleaning. I worked on the bowl and stem until the insides were clean. I wiped down the exterior of the bowl with alcohol on a cotton pad to remove any remaining oils and grimes from my cleaning of the bowl and rim. Once the alcohol evaporated the briar was very dry but also very clean. I restained the bowl with a Maple stain pen to match the colour that was original on this pipe. The rim top matched the rest of the bowl. When the stain dried I wiped the bowl down with alcohol to even out the stain on the sides and top of the bowl. I rubbed down the briar with Before & After Restoration Balm. I worked it into the smooth finish to clean, enliven and protect the new finish. It also evened out the stain coat and gave the stain a dimensional feel. I let the balm sit for a little wall and then buffed it with a horsehair shoe brush. I buffed the bowl with a cotton cloth to raise the shine. I buffed the bowl with Blue Diamond on the buffing wheel to raise the shine and smooth out the finish. I took photos of the pipe at this point to show the condition. I was still not happy with the burned edge toward the front of the bowl and figured I would give it a light bevel to smooth it out and make it less noticeable. The next series of photos tells the story on this. Though I know some will find this damaging to the bowl to me it removes the significant char on the front edge of the bowl and gives it a refined look.  I polished the rim top with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I wiped the rim down with a damp cloth after each pad. The rim was really looking better. I gave it a light coat of a walnut stain to blend it in with the rest of the bowl colour. The photos below tell the story. I set the bowl aside and turned my attention to the stem. I sanded out the tooth chatter on both sides with a folded piece of 220 grit sandpaper. I polished the stem with micromesh sanding pads – wet sanding with 1500-2400 grit micromesh sanding pads and dry sanding it with 3200-12000 grit pads. I rubbed the stem down with Obsidian Oil after each pad. When I finished I gave it a final rub down with the oil and set it aside to dry.  With the stem polished I put it back on the pipe and lightly buffed the bowl with Blue Diamond. I buffed the stem with a more aggressive buff of Blue Diamond. I gave the bowl several coats of Conservator’s Wax and the stem several coats of carnauba wax and buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The pipe polished up pretty nicely. The finished pipe is shown in the photos below. This is the seventh of Farida’s Dad’s pipes that I am restoring from his collection. I am looking forward to hearing what Farida thinks once she sees the finished pipe on the blog. This Charatan’s Make Belvedere Pot shaped pipe will soon be on the rebornpipes store if you want to add it to your rack. The dimensions are Length: 5 ¼ inches, Height: 1 3/4 inches, Outside diameter of the bowl: 1 1/2 inches, Chamber diameter: 7/8 inches. Thanks for walking through the restoration with me as I worked over another of her Dad’s pipes. I have one more of his pipes to work on –a Dunhill Shell Billiard with a saddle stem.

Refreshing a Comoy’s Made in London, England Bent Bulldog


Blog by Dal Stanton

I saw this Comoy’s Bent Bulldog as a charity listing on eBay for the Akron Art Museum, in Akron, Ohio.  The seller, like me, was providing pipes for a good cause and I like that.  I also liked the Bulldog I saw in the pictures the seller provided and by the description, it seemed the seller was a pipe person.  The nuts and bolts description:

A classic bulldog! About 5 1/4” long, bowl is 1 1/2” tall, 1 5/8” wide tapering to 1 1/8” at rim. ID 13/16”, depth 1 5/16”. Marked on one side of shank COMOY’S, other side MADE IN LONDON ENGLAND in circular fashion 4097, beneath shank a capital H. A capital C stamped on side of bit. No other marks detected.

Diamond saddle bit is well-seated push fit, cleaned and polished, showing some bite wear but no holes through. Some oxidation as well. Stummel is well hand worn and smoothed, some dings and scratches, scorch on rim, light cake in bowl. Though the pipe is smokable as is, this one has the possibility of being a real beauty with some TLC!

I took the gambit dangled in the last sentence regarding this Bulldog’s possible condition with some TLC.  My bid on the auction block was sufficient, I supported the Akron Art Museum, and now this Comoy’s Bent Bulldog is on the worktable here in Sofia, Bulgaria, on track to benefit the Daughters of Bulgaria, my favorite cause.  This was the second pipe that Stephen commissioned along with a Custom-Bilt Rusticated Panel.  Here’s the picture I saw on eBay which got Stephen’s attention in the For ‘Pipe Dreamers’ Only! collection:Now on my worktable, I take more pictures to get a closer look at the condition of this Comoy’s Bent Bulldog. The nomenclature on the Bulldog’s diamond shank is clear.  On the upper left shank is stamped ‘Comoy’s’.  The right upper shank has encircled, ‘MADE’ with ‘IN’ in the center and ‘LONDON’ on the bottom.  Underneath the circle is ‘ENGLAND’ in straight script.  To the right is shape number ‘409 7’.  Underneath this on the lower right shank panel is stamped ‘H’.  All indicators of the nomenclature point to a Cadogan era pipe which began in 1979 with the merger absorbing Comoy’s.  The simple ‘C’ stem stamp confirms this without the classic 3 piece inlaid ‘C’.  The shape number of 409 has historically indicated a Bulldog on earlier shape charts with a slight quarter bend.  The addition of the ‘7’ on this Bulldog I’m not clear on this, except that during the Cadogan era they added a 4th number to the shapes according to the Pipepedia article on shapes. I would say that this Comoy’s Bent Bulldog has been lovingly enjoyed over the years.  He’s got quite a few scrapes and bruises for the wear, mainly on his dome and circling the double grooves.  I took quite a few pictures of these above.  I’ll need to do some repairs especially on the back side of the dome where there are several small concentrated dents.  The front of the rim has been scorched from lighting practices it appears.  The dome grooves need to be cleaned and I detect a few chips of briar on the back-right side along the grooves.  Also, of interest are two huge fills on the right side of the bowl as it tapers down.  I’ll need to take a good long look at these.  The stem has oxidation and typical tooth chatter and compression dents on the button lip and just before the button.  The former steward was a clencher.

I begin the restoration of this Comoy’s Bulldog by placing the stem in a soak of Before & After Deoxidizer along with other pipes and stems in the queue.  Whoops, I include the original seller’s pictures – I forgot to take pictures of the original stem’s condition before putting the stem into the soak. After some hours of soaking, I remove the Bulldog stem and using a cotton cloth wetted with alcohol, I wipe down the stem removing the raised oxidation.  I follow this by wetting a cotton pad with light paraffin oil (mineral oil) and continue to wipe off the oxidation and the oil helps rejuvenate the vulcanite.After the soak wiping and the stem dries, I can still detect oxidation on the stem which requires more attention.  Before I start sanding the stem, I use Before & After Fine and Extra Fine Polishes to work on the oxidation.  It is advertised to continue the raising process of oxidation.  I start first with the Fine Polish by putting some on my finger and rubbing it in the vulcanite.  I also work it in well around the ‘C’ stamping to clean it more.  After applying, I allow it to stand for some time and then wipe off.  I do the same with the Extra Fine Polish.  After I’ve finished, I still see a deep greenish hue indicating the oxidation is still holding on.  The last picture below tries to capture what I see with the naked eye – it doesn’t do a very good job! One more noninvasive approach to the oxidation I’ll try.  I scrub the stem surface using Magic Eraser.  After working the white sponge over the entire surface, it did do a good job.  More oxidation was removed, but not enough to make me happy!  I still see oxidation especially on the ‘saddle’ of the saddle stem.  The pictures show the progression.Next, I sand the stem starting first with 240 grit paper.  I do not like going through the fine tune buffing with micromesh pads and start seeing oxidation!  So, I sand the entire stem, avoiding the Comoy’s ‘C’ stamping.  I also use at disc to sand against at the stank side of the stem.  The disc helps to guard against shouldering the stem so that the edges are not sharp as the stem joins the shank.  This sanding is primarily for dealing with the oxidation.  In the pictures below, you can see the bit area compressions that are left untouched by the sanding.Before proceeding further with the sanding of the stem, I use the heating method to raise the compressions in the vulcanite in the bit area.  Using a Bic lighter, I paint the bit and button to heat the vulcanite which causes it to expand.  The hope is that this will cause the indentations perhaps to go away or lessen in their impact so that they will then sand out more easily. After painting the bit with the open flame, it helped to minimize some, but it did not erase the dents and compressions on the bit and on the button lips.  I follow with a flat needle file to file the button to refresh and shape the edges.  I follow again with 240 grit paper continuing to sand the dents on the bit.  Using the Bic lighter to raise the dents helps and I’m able to sand out all the dents and compressions from biting. Before proceeding further with the sanding of the stem, I use the heating method to raise the compressions in the vulcanite in the bit area.  Using a Bic lighter, I paint the bit and button to heat the vulcanite which causes it to expand.  The hope is that this will cause the indentations perhaps to go away or lessen in their impact so that they will then sand out more easily. After painting the bit with the open flame, it helped to minimize some, but it did not erase the dents and compressions on the bit and on the button lips.  I follow with a flat needle file to file the button to refresh and shape the edges.  I follow again with 240 grit paper continuing to sand the dents on the bit.  Using the Bic lighter to raise the dents helps and I’m able to sand out all the dents and compressions from biting.  Next, I wet sand the entire stem using 600 grade paper and follow this by buffing with 0000 steel wool. One last thing at this point before turning to the stummel, I give the stem a coat of light paraffin oil to help revitalize it.  I put the stem aside to absorb the oil and dry. With the stummel in hand, I begin the internal cleaning by reaming the light cake build up in the chamber.  I use 3 of the 4 blade heads available from the Pipnet Reaming Kit.  I then use the Savinelli Fitsall Pipe Tool to reach the hard to reach places in the chamber.  I then sand the chamber with 240 grade paper wrapped around a Sharpie Pen followed by wiping the bowl with a cotton pad wetted with alcohol to clean the carbon dust left behind.  Inspection of the chamber reveals some heat fissures on the floor of the chamber.  There also appears to be a small fissure creeping up just above the draft hole.  I take a few pictures that show what I’m seeing.  Are these fissures severe enough to warrant a durable patch or perhaps apply a pipe mud to enhance the growth of a protective cake?  That’s what I’ll be considering.  Continuing the cleaning, I use undiluted Murphy’s Soap on the external briar surface.  To work on the grit lodged in the grooves I use a bristled tooth brush.  I also use a brass wire brush to work around the dome and rim to clear away the old oils. Using a sharp dental probe, I painstakingly clean both dome groves, scraping packed dirt out.  I’m careful not to jump ‘track’ out of the grooves and scratching the briar surface.  The picture shows the cleaning progress. With the externals cleaned up, I turn now to the internal mortise and airway.  Using pipe cleaners and cotton buds dipped in isopropyl 95% I go to work. I quicken the work by scraping the mortise with a dental spatula.  In time, the cotton buds and pipe cleaners were coming out clean.  I’ll continue cleaning later using a kosher salt and alcohol soak.Turning again to the stummel surface, the rim and dome cleaned up well but show the dents and pockets from knocks and drops.  There remains a scorched area at the front of the rim/dome area.  There are small chips in several places around the circumference of the dome grooves.  I believe they’re all too small to patch, but with sanding I’m hoping that most should disappear or be minimized.  The most daunting aspect of the briar landscape is a huge, double fill patch on the right lower side of the stummel.  I take two pictures of the fills to show the position and a super close-up to show the appearance of the fills.  I poked the fills with a dental probe and both fills are rock solid.  Yet, as the close-up picture reveals, there are small air pocket holes in the fills and gaping around the fills.  I’ll leave the fills in place but touch them up with thin, clear CA glue and then sand to blend.  These fills will pretty well drive the boat regarding the finished look of the Comoy’s Bulldog.  The finish needs to be darker in order to mask the fills as much as possible, though even a dark stain will not hide these giants.   Looking again around the dome grooves, on the back-right quadrant there may be at least 2 candidates for a patch before sanding.  I take a picture of this area.  To the top left of the groove chips, there are also a few small holes that I’ll fill with a spot-drop of CA glue.  In this picture there are also two other small fills that seem to be in good shape.Before I begin sanding and patching, I start from the top and work my way down!  Topping the stummel will re-define the rim and address the front quadrant of the rim/dome where the former burn damage has thinned the rim.  I take some pictures to show these issues and mark the start. I put 240 grade paper on the chopping board and rotate the inverted stummel several times, checking as I go to make sure I’m staying level and not leaning into soft spots in the briar. When enough of the top is removed, I then switch the paper to 600 grade paper and turn the stummel a few more rotations. I take pictures to show the progress.  Now to the patching party!  I first wipe the stummel with a cotton pad wetted with alcohol to clean the area. I start with the two large fills by spot dropping a small amount of thin CA glue over the fills and spreading the glue over the entire fill – filling the pockets and gaps.  To move the work along faster, since these are not ‘weight bearing’ patches, I use an accelerator to quicken the curing process.   For the groove patch, I insert a piece of an index card into the groove to create a flow barrier for the CA glue.  I then spot-drop a small amount of CA glue slightly above the chip and draw the glue over the chipped area with a toothpick.  Again, I use an accelerator to solidify the glue.  After a few minutes, I pull the index card away and use a sharp dental probe to make sure the groove is clear of CA glue seepage.  Next, I apply small drops to four other small pits near the grooves and above them – again, I use an accelerator.  I decide also to apply a small drop to the right of the primary groove repair.   The repairs look a mess now, but I’m hopeful that the sanding will prove to reveal a more pleasing surface!Next, I begin the filing and sanding of the two large fill patches down to the surface level.  I use a flat needle file to do this initially when the patch mound is more distinct, then follow with 240 grade paper as the sanding nears the briar surface.  The gaps and pits in the original patch filled nicely, blending better with the surrounding briar.To both clean and sharpen the grooves at the groove patch repair, I insert 240 grade paper into the groove itself.  The groove is only large enough to accommodate a single sheet, so I must flip the paper to sand both the upper and lower edges of the groove.  I use a sawing motion with the paper while in the groove and I flex the paper up to apply a little more sanding action to the groove edge.  This technique does a good job redefining and cleaning up groove edges, especially at the point of the CA glue repair.After filing, sanding the groove patch repairs, and ‘groove sanding’ the groove repair looks great!  The patch has blended, and the groove is cleaner and smarter.Next, I move on to filing and sanding the 4 patches to the left of the groove repair on the dome.  I file the patch mounds down until near the briar surface and then take over with 240 grit paper.  I sand the area of the patches to blend.  It looks good – not pristine, but much less ragged!  The battered stummel is showing some signs of life!I follow by ‘groove sanding’ this area.  I like the results of this technique, so I decide to continue the groove sanding around the entire circumference of the dome for both the upper and lower grooves.  Since I’m able only to do one directional sanding on the grooves, it requires four circuits around the dome to do the job!  I refined the technique as I work – by flexing the paper somewhat I can sand more directly chips encountered on the groove edge as I slowly work around the dome.  The pictures show the groove sanding progress and results – much cleaner and crisper for this Comoy’s Bulldog! I continue preparing the external briar surface by sponge sanding starting first with the coarse sanding sponge.  I then use a medium grade sponge then finish with a light grade sanding sponge.  I avoid totally the upper shank panels with the nomenclature.  Sanding sponges help to clean the surface of the minor nicks and cuts and soften the look without an overly intrusive sanding effect.  The pictures show the results of the 3 sponges. As I sponge sand the dome of the Bulldog, I notice a chip in the inner lip of the rim that became more distinct during the sanding process.  To erase this small divot, I introduce a very gentle inner bevel to the rim using 240 grade paper rolled.  This dispatched the divot quickly. Earlier, I avoided using the sanding sponges on the nomenclature panels in order not to diminish the Comoy’s stampings.   I do want to clean the panels more to rid the old residue finish before applying a fresh stained finish.  To remove the old finish and to clean the panel I apply acetone to a cotton pad and wipe the panels.  This does the job. With the time of my departure for the work day rapidly approaching, I continue the internal cleaning of the mortise and airway using a kosher salt and alcohol soak.  After forming a wick by stretching and twisting a cotton ball, I insert it down the mortise and airway using a stiff wire.  The wick acts to draw out the tars and oils.  I then add kosher salt (no aftertaste) to the chamber and place the stummel in an egg crate for stability.  With a large eyedropper, I add isopropyl 95% to the chamber until is surfaces over the salt.  After a few minutes, after the alcohol has absorbed into the chamber, I top off the alcohol and set the stummel aside to soak for the day.Arriving home several hours later, the soak did the job of finishing the internal cleaning.  I clean the expended salt from the chamber with paper towel and shank brushes as well as blowing through the mortise.  I run an additional pipe cleaner and cotton bud wetted with alcohol to assure the internals were clean.  They are, now moving on!Before proceeding further with the external stummel preparation, I’ve come to a decision point regarding the chamber issues that I saw earlier.  The floor of the chamber has heat fissures which the first picture shows.  The second picture shows the fissure immediately above the draft hole.  The upper chamber shows some heating issues with small, more normal chamber wear.  Earlier, my question had been, do the fissures on the floor of the chamber need a more durable response than simply applying a pipe mud mixture to enhance the growth of a protective cake?  The floor of the chamber has experience overheating issues and I believe at this point would benefit from applying J-B Weld to prevent further damage and to reinforce the resistance of the chamber floor.J-B Weld comes with two components that are mixed together and once mixed harden to form a heat resistant bond.  I’ll mix a small amount and apply it to the floor of the chamber then spread it over the area, including above the draft hole, filling the fissures with the Weld.  After it hardens and cures, I’ll sand the excess. I first wipe the chamber with alcohol and put a pipe cleaner through the airway to block seepage into the draft hole.  After I mix J-B Weld components in equal parts, I apply a small amount on the floor of the chamber and spread it with a dental spatula and my finger. I rotate the pipe cleaner so that it is not stuck but I leave it in place – I don’t want to pull it out while the J-B Weld is wet leaving the mixture in the mortise.  I put the stummel aside for the J-B Weld to cure.  After the repair cured overnight, I take a picture of the sanding process using 240 grade paper wrapped around a Sharpie Pen.  I concentrate on removing the excess J-B Weld so that all that is left of the weld is what has filled the fissures and cracks. The next pictures show a much healthier chamber.  At the floor of the chamber in the first pictures and concentrating on the area immediately above the draft hole in the second picture, you still see what appears to be rough spots, but it is now smooth to the touch in large measure.  The Weld filled the cracks and reinforced the area.  The application of J-B Weld and the additional sanding on the floor and the walls of the chamber cleaned it up nicely.  Putting the stummel aside, I take the stem and wet sand using micromesh pads 1500 to 2400.  I follow by dry sanding with pads 3200 to 4000 and 6000 to 12000.  Between each set of 3 pads I apply Obsidian Oil to revitalize the vulcanite. With the stem waiting in the wings, I continue with the stummel by wet sanding with micromesh pads 1500 to 2400.  I follow this by dry sanding with pads 3200 to 4000 and 6000 to 12000.  I take pictures of both sides of the stummel to show the huge fills on the right side.  If it weren’t for these unavoidable fills, the fantastic recovery the stummel has made would encourage me to leave the original, natural grain finish in place.  The briar surface had many issues, but the results of the micromesh sanding reveal a very attractive grain presentation.  The next step is to apply a dark stain to the Comoy’s Bulldog that will serve to help mask the issues prevalent on the surface.  Without question, my plan is to apply Fiebing’s Dark Brown Leather Dye to the stummel surface.  I assemble all the needed components on the table to apply the stain.  First, using a sharp dental probe I carefully dig out and scrape the dome grooves to make sure the debris is gone.  After wiping the stummel with alcohol to clean and prepare the surface, I fit the stummel with a cork I’ve fashioned as a handle inserted into the mortise.  Next, I heat the stummel with a hot air gun to expand the briar grain.  This aids the briar in absorbing the dye pigment.  Using a folded over pipe cleaner, I apply the dye to the stummel.  After a thorough application, I flame the stummel with a lit candle and the alcohol-based aniline dye combusts and sets the dye in the grain.  After a few minutes, I apply the dye again and flame again to make sure there is an even coverage.  I then set the stummel aside for the dyed stummel to rest. After resting for several hours through the night, it’s time to unwrap the fire-crusted Comoy’s stummel.  Over time, I have developed my own techniques for use with the Dremel since this is my main and only work horse tool on the 10th floor flat of a formerly Communist block apartment building!  My usual method for ‘unwrapping’ has been with the use of a felt buffing wheel, which is more abrasive than cotton, applying Tripoli compound.  I love this technique because the result reveals a more brilliant grain pattern as it lightens the grain veins leaving them in contrast to the softer briar wood which absorbs more of the dye.  However, I have found that using the felt buffing wheel lightens the entire stummel.  With the large dark fills on this stummel in need of remaining masked for better blending, I use a cotton cloth buffing wheel with Tripoli compound to unwrap the flamed crust.  The softer cotton wheel isn’t as abrasive and leaves a darker dyed hue on the briar surface.  After mounting a cotton cloth wheel on the Dremel, I set the speed at the lowest RPM and I apply Tripoli to the stummel. I take a couple staged pictures to show the contrast between the flamed crust and the surface that has been ‘unwrapped’ and buffed with compound.  After completing with the Tripoli, I wet a cotton pad with alcohol to wipe the stummel not so much to lighten but to blend the new stained finish. Next, I rejoin the stem and stummel to apply Blue Diamond compound.  I discover that the junction between the tenon and mortise has loosened through the cleaning process – a common thing in my experience.  To remedy this, I take a drill bit the next size larger than will fit through the tenon airway.  I use a Bic lighter and heat the tenon and after a bit, the vulcanite tenon becomes supple and allows me gradually to insert the drill bit end into the airway.  This expands the tenon and tightens the connection.  This works like a charm!  With the stem now fitting snuggly, I continue to apply Blue Diamond to the stummel and stem.  I mount a cotton cloth buffing wheel to the Dremel and increase the speed to about 40% full power.  I apply Blue Diamond compound to both stem and stummel.Before moving on to applying carnauba wax to the pipe, I have two more projects to do.  The first is to apply white acrylic paint to refresh the Comoy’s ‘C’ stamping on the stem.  The second is to apply pipe mud to the chamber.  I decide to do the latter first.  After the repair done to the chamber, to enhance the healthy development of a protective cake (which should be maintained at about the width of a US dime coin) I use a mixture called pipe mud – a combination of cigar ash and water.  This mixture, once applied to the chamber and dries, hardens to create a starter surface for the cake to develop.  My colleague, Gary, who lives in Plovdiv, Bulgaria, is the cigar man who saves his ash for my use. Thanks, Gary!  I mix some water with ash in a plastic dish and mix it with my pipe nail until it starts to thicken. At this point, I apply it in the chamber with the nail and my finger.  It doesn’t dry quickly so there’s time to spread it evenly over the chamber.  After spread, I insert a pipe cleaner through the draft hole to keep it clear of the mud.  I then put the stummel aside in the egg cart for the mud to cure. Turning now to the Comoy’s ‘C’ stem stamp, I put a drop of white acrylic paint over the ‘C’ and absorb the excess with a cotton pad and ‘dob’ it out so that the paint thins and dries.  I then use a toothpick’s flat edge to gently scrape the excess paint off after it dries.  I have to reapply paint a few times to get it right.  The pictures show the process. After allowing the pipe mud to cure, I rejoin stem and stummel and once more, run the sharp dental probe in the grooves around the circumference of the dome then buff the pipe with a felt cloth clearing away the compound dust before applying wax.  I then mount a cotton cloth buffing wheel to the Dremel, keep the speed at about 40% full power and apply a few coats of carnauba wax to the pipe.  I finish the restoration by using a microfiber cloth to give the pipe a rigorous hand buffing to raise the shine.

I’m pleased with the results of this Comoy’s Made in London, England, Bent Bulldog.  The restoration was fought in the trenches!  The many repairs done to the stummel surface came out well, though the two large fills are still evident, but not as overt. The dark brown dye came out beautifully and the groove patches and repairs have all but disappeared.  I’m glad I also addressed the heat fissure issues in the chamber.  This Comoy’s Bent Bulldog will provide many more years of service to a new steward.  Stephen commissioned this Comoy’s and will have first opportunity to acquire it in the Pipe Steward Store and this pipe benefits the Daughters of Bulgaria – women and girls who have been trafficked and sexually abused.  Thanks for joining me!

 

Rescue of a Stately Stanwell Henley Special, Made in Denmark, Oval Shank Billiard


Blog by Dal Stanton

I have been looking forward to this project ever since I landed three Stanwell Henley Special pipes on the eBay block from a seller in Maryland.  The seller provided helpful information that only helped urged me to place a bid:

This auction is for three vintage Stanwell, Henley Line estate pipes from the 1950’s-60’s era. All are in good pre-owned condition. The stems are primarily free from teeth marks. The stems do have some fading. All of the stems fit snug and the wooden bowls are free from outstanding blemishes. As seen from top to bottom, the first pipe reads Henley Special #57, the second and third read Henley Special without any numbers seen. All of the pipes read Made in Denmark.

Since I started collecting and restoring pipes, I’ve grown in my appreciation for Danish made pipes.  They tend to be stout, well made pipes.  The stems are also interesting – the ‘pinched saddle’ fish tail is unique.  When I saw the 3 Henley Specials, I was attracted to the line-up but had never heard of ‘Henley’.  When I read the sellers description I was sold – I was especially drawn to the ‘Chimney’ on the top of the group below, sporting a pinched saddle fishtail stem.  The Stanwell Henley on my workbench now is the classic Oval Shank Billiard in the center.  Along with a Comoy’s Moorgate, Jim saw the Henley Special in the For ‘Pipe Dreamers’ Only! collection and commissioned him.  He saw what I also see in these classic Danish pipes.  As with frosting on the cake, this pipe benefits the Daughters of Bulgaria, our work here in Bulgaria helping women and girls who have been trafficked and sexually exploited.  The pictures show what I saw on eBay. Unfortunately, I cannot find much online regarding the Henley line.  Pipedia’s article on Stanwell pipes simply places the Henley Special line in the list of Stanwell second brands.  Pipephil.eu provided more information with a Henley much like the slightly bent, Chimney above with the characteristic bulging midsection, but with a blasted finish.  It also show a ‘H’ stem stamp.  If the Henley on my worktable had one, it is now long gone.The only information I found that gave any reference to dating is spurious at best. I found the following picture on Google images but the link to pipesmokersforum.com is now a dead end.  “Who made this pipe?”  I would have loved to read the thread that discussed the dating of the discontinued Stanwell second, Henley Special.  The picture puts a question mark in the late 50s.  Looking at all the 3 Henley Specials I acquired, the look and feel of them lends toward this dating, but…. This picture and the eBay seller’s description placing the pipes in the 50s or 60s are anecdotal, but seem to me to be accurate.  Oh, for the return of the now defunct, Chris’ Pages website, to look through the old catalogs! One very interesting find was a Stanwell Henley Special for sale in the listings of SmokingPipes.com in restored state – very nice.  It gives me an idea of what might be under the older, tired finish of all three Henleys in my collection.Taking a closer look at the Henley Special Oval Shank Billiard on my worktable, I take these pictures for a closer look. The nomenclature is found on the upper side of the oval shank.  A very thin, worn ‘Henley’ (in cursive script) [over] offset ‘SPECIAL’.  On the underside is the COM, ‘MADE IN DENMARK’. As with the other two Stanwell Henley pipes I acquired at the same time, the finish is extremely dark from years of grime and oil build up.  The uniformity of the darkened state of the pipes lends to a common period of manufacturing, which I’m guessing to be in the 1950s or 60s.  Even though I know it’s not an exact science, the feel of the pipes seems older.  I need first to clean the briar surface before I can see what is going on with the briar – the condition or even the look of the grain.  The oval saddle stem has oxidation, tooth chatter and dents which need attention.  The cake in the chamber is thick and will be removed to give the briar a fresh start.  The rim has significant lava flow and I detect a divot on the internal lip of the rim which needs attention.

To begin the restoration of this vintage Stanwell Henley Special Oval Shank Billiard, I run a pipe cleaner dipped in isopropyl 95% through the airway to clean it up.  I then add the oval saddle stem to a soak of Before & After Deoxidizer with other pipes and stems in the queue.  I leave it in the soak for several hours and fish it out, letting the Deoxidizer drain off the stem.  I then wipe the raised oxidation with cotton pads wetted with alcohol.  I follow the alcohol by wiping the stem with a pad wetted with light paraffin oil. Turning now to the bowl, I begin by reaming the chamber.  There is heavy cake in the chamber tightens as it descends in the chamber.  Using the Pipnet Reaming Kit, I start with the smallest of the 4 available blade heads.  After putting some paper towel on the table, I go to work.  I use 3 blade heads of the 4 and then transition to the Savinelli Fitsall Pipe Tool. With the Fitsall tool I continue scraping the chamber wall and fine-tuning the reaming and reaching to the difficult angles.  Then, wrapping 240 grade paper around a Sharpie Pen, I sand the chamber removing more carbon and revealing fresh briar.  To complete the chamber cleanup, I wipe it with a cotton pad and alcohol to clear the carbon dust.  With the carbon cake cleared, an inspection of the chamber reveals no problems with cracks or heat fissures. The pictures show the progress. Turning now to the external surface, I use undiluted Murphy’s Soap on cotton pads.  I’m anxious to see what the Murphy’s Soap does on this very dark, aged briar surface. As I use the cotton pad, I very quickly begin to see what beauty was waiting underneath.  I called my wife to take some pictures as I scrubbed the ancient layer of oils and tars that have cocooned the briar underneath.  I also use a bristled tooth brush and a brass wire brush on the rim.  My, oh my!  I’ve never seen a pipe clean up to such a pristine condition.  I rinse the bowl with tap water and literally marvel at what is in my hand.  The rim is still darkened a bit from lava flow, but the flame grain that dominates the bowl’s external surface is striking.  I take two pictures after the cleaning to mark the progress.  As I look at the stummel, I decide to hydrate the briar using light paraffin oil (mineral oil) which also gives me a sneak peek at a finished stummel.  The before and after pictures tell the story. Turning now to the internals of the stummel, I use cotton buds and pipe cleaners dipped in isopropyl 95% to clean the mortise and airway. I also utilize long shank brushes to save on pipe cleaners.  To loosen up the tars and oils, I employ a dental spatula to scrape the mortise wall and reach into the airway.  A drill bit effectively excavates crud out of the airway. To do this, I use a bit the size of the airway and hand turn the bit so that it proceeds down the airway.  The bit grabs the buildup and removes it.  After some time excavating and scraping, pipe cleaners and cotton buds start coming out clean.  The pictures show the tools and the progress.I continue the internal cleaning with a kosher salt and alcohol soak.  After twisting and stretching a cotton ball to form a wick, I stuff it down the mortise/airway to draw the oils and tars.  Following this, I fill the bowl with kosher salt (kosher salt has no residual after-taste as does iodized salt) and set it in an egg crate.  Using a large eye dropper, the bowl fills with isopropyl 95% until the alcohol surfaces over the salt.  After a few minutes the alcohol is absorbed, and I top off the alcohol and set the stummel aside for the night. The next morning, the soak did the work.  I toss the expended salt in the waste and wipe the bowl with paper towel to remove the salt.  I also use a shank brush in the chamber and down the mortise to remove any remaining salt.  Finally, I blow through the mortise.  To make sure all is clean, I finish by wetting a pipe cleaner and cotton bud with isopropyl 95% and running them through the mortise.  I declare the stummel to be cleaned. With the pipe cleaned, I look again at the stummel surface which almost appears to have been protected by the layer cocooning it.  My task will be to preserve the patina of the briar’s finish by not introducing sanding that will be too invasive and remove the aged surface.  I sent a note off to Steve of rebornpipes, just to make sure my plan received his concurrence before moving further with the Henley.  My plan is to first repair the divot on the inside of the rim lip, shown at the 2 o’clock position on the first picture below.  I could introduce an internal bevel to mask the divot, but I would rather salvage the rim real estate with this vintage pipe.  I make a patch of briar dust and thick CA glue and mix a small amount of putty with it.  After wiping the area with alcohol to clean it, I mix the CA glue and briar dust until it reaches the viscosity of molasses and apply the putty to the divot using a toothpick.  It takes very little.  I put the stummel aside to allow the patch to cure. With the patch curing, I look at the stem and take some close ups of the bit area.  The chatter is light with some bites.  I begin by using the flame method to raise the indentations in the vulcanite.  With a Bic lighter, I paint the button area.  The physics of vulcanite – a compound rubber, expands when heated.  The heating causes the bites and chatter to lessen in the intensity.  As I heat, it does lessen but is not fully removed.  I next use 240 grit paper and sand out the chatter and dents remaining.  I also use the flat needle file to redefine the button lips – upper and lower.  The pictures show the progress. Following the 240 paper and filing, I use 600 grade paper and wet sand the entire stem.  I follow this using 0000 steel wool to sand/buff the stem.  The pictures show the progress.Next, using micromesh pads 1500 to 2400, I wet sand the stem.  I follow by dry sanding using pads 3200 to 4000 and 6000 to 12000.  Between each set of 3 pads, I apply a coat of Obsidian Oil to the stem to revitalize the vulcanite.  The pictures show the progress of restoring that glossy pop.  I like it! With the stem drying, I look again to the stummel.  The briar dust patch is cured, and time to be file and sand the patch mound.  I use both a flat and a half-rounded needle file to gently and patiently file the patch mound on the top of the rim and on the inside lip.  I’m careful not to impact the surrounding rim briar.  After some time filing, I use a piece of 240 tightly rolled to finish the sanding, bringing the patch flush with the briar on the top and inside.  I chronicle the progress. Next, I gently clean the whole rim surface by lightly sanding it starting with micromesh pad 1500 and completing with pad 3600.  The rim looks good.To preserve the patina in the old finish, I’m willing to allow some scratches and dents to pass as badges of this Stanwell Henley’s past walk in life.  I did want to try raising some in an area where I identified a concentration of these.  I take a picture to show a closeup of the area.  I then take my wife’s iron (she always raises her eyebrows when I ask for permission and my response to her question regarding what use HER iron will be to the art of pipe restoration! 😊) and wet a rag with tap water and place the rag over the briar area to be addressed.  After the iron is heated, I place the iron over the rag which heats both water and wood creating a steaming effect on the dents and scratches.  The effect of the heating and moisture causes the briar to absorb the moisture and expand, helping to close the wounds.  This technique helped, but there remain some badges of the past for the Henley Special! Following this heating technique, I apply Before & After Restoration Balm to the entire briar surface working it in well.  I apply some to my fingers and massage the Balm into the briar.  The Balm begins with the texture of a light oil but thickens into a heavy wax as it is worked into the briar.  After the Balm absorbs for a few minutes I wipe it off the stummel surface with a microfiber cloth.  As I wipe, the Balm-treated surface loosens, and it becomes more of a buffing.  I like what the Before & After Restoration Balm does to bring out and enrich the briar. The water spot (above) disappeared as the Balm did its job.At this point, I rejoin the stummel and stem and often I find that the cleaning process has loosened the connection.  To remedy this, I choose a drill bit that is the next size larger than the bit easily fitting down the airway of the mortise. I heat the vulcanite of the tenon by painting it with a lit Bic lighter.  As the vulcanite heats, it becomes supple allowing me to work the drill bit into the tenon thus expanding the tenon’s diameter microscopically and securing a tighter fit for the tenon in the mortise.  The expansion worked so well, that I needed to loosen the tenon a bit using 470 and 600 grade papers and then 0000 steel wool.  The fit now is good. With the tenon now fitting the mortise snugly, I mount the Dremel with a cotton cloth buffing wheel, set the speed at about 40% full power and apply Blue Diamond to the entire pipe.  With this compound being the only abrasive, I’m applying to the bowl, I spend extra time working the compound over the briar.  The compound doesn’t remove the ‘badges’ I’ve left behind, but it buffs out the very fine lines in the briar surface creating that natural briar shine.   When I add wax to this natural shine, it’s like frosting on a cake!  After applying the Blue Diamond is complete, I hand buff the entire pipe with a felt cloth to remove the excess compound dust left behind before applying carnauba.I now mount another cotton cloth buffing wheel to the Dremel, maintaining the same speed, and apply a few coats of carnauba wax to the stem and stummel.  I finish the restoration by giving the pipe a rigorous hand buffing with a micromesh cloth which raises the gloss even more.

Oh my!  When Jim commissioned this Stanwell Henley from the For ‘Pipe Dreamers’ Only! collection, could he have possibly seen what was hidden in this stately Oval Shank Billiard, Made in Denmark?  The grain and patina are beautiful.  I called the pipe, ‘stately’.  It’s remarkable, how so much beauty is hidden underneath the surface appearance and neglect of years.  Yet, as the vertical, flame grain cascades upwardly to the rim, if one looks closely at the rim, revealed there are the small bird’s eye grains formed by the cut cross-sections of the vertical grain.  I’m pleased with the small, seemingly insignificant internal lip patch to the rim – it blends well and joins the ensemble without notice.  With the bowl’s striking grain revealed, the oval shank now compliments well as it flows to the saddle stem.  I fear I’m waxing too much at this point!  Jim has the first opportunity to acquire this 1950s or 60’s Stanwell Henley Special from The Pipe Steward Store and this benefits the work we do here in Bulgaria with the Daughters of Bulgaria – women and girls who have been trafficked and sexually exploited.  Lest we forget, I begin with a ‘before’ picture for the striking contrast. Thanks for joining me!

 

Restoring Life to a Early 20th Century Gitana Depose Apple


Blog by Steve Laug

I was going through boxes of old pipes here, sorting and getting them ready to sell as grab bags. In the process I came across this pipe. It is stamped Gitana in an oval with an L on the left of the oval and G on the right side of the oval. Underneath the oval stamp is the word Depose. There is a polished aluminum band on the end of the shank. The briar is quite nice with birdseye around the bowl. The stem is horn and has a lot of tooth damage next to the button on both sides. There are deep troughs carved by the teeth in the horn material on both sides. The rim had a lot of damage from burn marks and the inner edge had been damaged by reaming with a knife. There was a white waxy substance on the inside of the bowl from the edge down about a ½ inch. There was a light cake in the bowl and some light lava on the bowl top. I took a close up photo of the rim top to show the damage to the inner edge of the bowl from the reaming job. The cake on the bowl sides and the tarry oil on the rim top are also visible. The briar at the top is quite damaged and will take some work to remove the knife cuts and deep gouges in the briar. The stem is also shown with the chewed damage on both sides.  I removed the stem from the shank and was a bit surprised by the aluminum system that was inside. The tenon was aluminum and had a bullet shaped cap on the end of it. The cap had a hole in the top that allowed the smoke to be drawn through the airway in the stem. The previous own had wrapped the aluminum portion of the tenon with what looked like aluminum foil to build it up to fit tightly in the shank. The photos below show the tenon and the system. I was unfamiliar with the brand and was surprised by the tenon system. I did some searching online and could find nothing on the Gitana brand or the Gitana Depose brand. I did happen across a similar pipe on Smokingpipes.com. The writer who described the pipe for the site wrote the following which contained some really helpful information. I quote:

We were able to ascertain a little information about La Gitana, which was a French brand created by Chapel Frés…but this relic from the early 20th century still sports its original horn stem, coupled with a novel aluminum tenon arrangement that we can only assume is meant to trap moisture. Although we aren’t sure how well it achieves this, it does do quite well at looking like an old-school James Bond accessory. It fits securely within a cork-lined mortise, which many briars of this period tended to have. https://www.smokingpipes.com/pipes/estate/france/moreinfo.cfm?product_id=196840

From that I learned that the brand was called La Gitana. It was a French made pipe from a company called Chapel Frés. It was made in the early 20th century and the author had described the tenon system like the one I had.  I also learned that the mortise had originally been cork lined to facilitate holding the tenon snuggly in the shank. This was what was missing in the pipe I had and it had been replaced with the foil mess that is seen in the above photos.

Armed with the name Chapel Frés I looked on Pipedia under French Pipe Companies and found the brand there. It stated that it came from that factory and the brand had been founded in 1904 in Saint-Claude, France. Here is the link https://pipedia.org/wiki/Chapel_Fr%C3%A9s.

Armed with that information I started my cleanup of the stem. I scraped away the foil that was wrapped around the tenon. I examined the bullet shaped cap on the tenon and figured out that it unscrewed from the tenon. I cleaned the metal underneath alcohol, cotton swabs, pipe cleaners and steel wool. I cleaned out the airway in the shank at the same time. The tube in the end of the tenon looked clean. I used alcohol, cotton swabs and pipe cleaners to clean out the inside of the bullet cap. I cleaned out the walls in the shank with pipe cleaners, cotton swabs and alcohol. It was a very dirty pipe that once it was clean had an interesting look to it. I cleaned up the inside of the bowl with a Savinelli Fitsall Pipe Knife. I scraped the walls clean of the carbon build up. I sanded the walls of the bowl with a piece of dowel wrapped with 220 grit sandpaper.To remove the damage on the rim top I topped the bowl until the damaged areas were removed and the rim top was clean. I used a folded piece of sandpaper to smooth out the inner edge of the rim and bring it back to round as much as I could. I washed down the exterior of the bowl with acetone on a cotton pad to remove the finish and the grim on the briar. The pipe looked really good at this point. I needed to round down the outer edges to bring it back to the shape it was when I started but for now it was clean. I took a photo of the stamping on the left side of the shank. The stamping is quite readable and clear.The tenon had some sticky substance for the glue on the foil on the tenon end. The tenon and threads still needed more cleaning to remove the oils.I filled in the tooth marks and troughs in the surface of the horn with clear super glue. I set the stem aside to dry.I decided to try to fit a cork in the shank to line it as suggested above. I cut away some of the excess cork from a wine cork I had. I trimmed it down with a Dremel and sanding drum until the diameter was close to the inside of the shank. I drilled it out with a series of drill bits starting small and working my way up to one that was close to the size of the tenon. I sanded down the cork exterior until it was a fit in the shank. I pressed it in place in the shank.I used a needle file to thin down the inner walls of the cork lining. It needed to be very thin to allow the tenon to fit in the shank. I tried to put the tenon in the shank. The fit was still not right. The cork was too thick to allow a fit. I pulled it out of the shank and slid it over the tenon. I sanded it down with sandpaper and files until it was a good fit. I glued the cork on the tenon and let it dry. When it cured I rubbed the cork down with Vaseline to soften it and allow it to slide into the shank. The fit was very good. I took some photos to show what the pipe looked like at this point in the restoration (I had also started the shaping on the bowl top). I polished the briar with micromesh sanding pads – wet sanding it with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I wiped it down with a clean cloth after each pad. The grain began to pop and really stand out. Once the glue repairs cured I sanded them with 220 grit sandpaper to smooth out the repairs. I sanded them to blend them into the surface of the horn. I polished the stem with micromesh sanding pads – wet sanding with 1500-2400 and dry sanding them with 3200-12000 grit pads. I wiped the stem down with Obsidian Oil after each pad. I gave it a final coat and let it dry. The following photos show both sides of the stem. I worked Before & After Restoration Balm into the briar and the horn stem with my fingertips to clean, enliven and protect the wood and the horn. I let the balm sit for about 20 minutes and buffed it off with a soft cotton cloth. I took photos of the pipe at this point in the process to show what the bowl and stem looked like. I am happy with the look of the pipe. I polished the bowl and stem with Blue Diamond to polish out the scratches in the briar and horn. I gave the bowl and the stem multiple coats of carnauba wax. I buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The pipe polished up pretty nicely. The original patina on the bowl came alive with the buffing and worked well with the polished striated horn stem. The pipe has a rich look. The finished pipe is shown in the photos below. The shape, finish and flow of the pipe and stem work give the pipe a very classic look. The dimensions of the pipe are Length: 5 1/2 inches, Height: 1 1/2 inches, Outside diameter of the bowl: 1 1/2 inches, Chamber diameter: 3/4 of an inch. Thanks for reading this while I worked on it. It was interesting and unusual piece to restore and I really enjoyed the work.

A Challenging Restoration of Vintage Era First Choquin “A Metz”


Blog by Paresh Deshpande

I had been on a short leave to my home town last month and that is where this happened!!!!! Even though there are still a number of pipes from the two of the three inherited boxes of pipes waiting their turn for restoration, curiosity got the better of me and I could not resist the temptations of opening the third box. What happened thereafter is that I had to unpack all the pipes earmarked to accompany me to my work place for restoration in my free time which in turn invited the wrath of my wife who had helped in packing in the first place, and repack the newly selected pipes from the third box!!!!!! In addition to the regular collection of Barling’s, Charatan’s, Comoy’s and other assorted collection, I came across two pipes which caught my fancy!!!!!The pipe on the left bears a football stamp that reads “CHOQUIN” over “A METZ” and the one on the right side simply reads “GBD”  (there are other stampings on the silver ferrule, details of which will be highlighted when it comes up for restoration). Both these pipes looked vintage and unique enough that I immediately Facetimed with Mr. Steve of rebornpipes. His admission that he is willing for a trade with me for these two pipes was an indication enough for me to know and understand their uniqueness!!! Thus these two pipes moved to the top of my unorganized and chaotic list of restoration.

The pipe first on my work table is the CHOQUIN. It is a huge pipe with a humongous acorn shaped smooth briar bowl with a steeply raking shank, the end of which is adorned by a fixed sterling silver ornamented ferrule. This similarly designed sterling silver also masks the tenon of the horn stem.The shank and the horn stem are connected by a push-fit type bone extension. The huge acorn bowl shows beautiful, large and loosely packed birdseye grain on the right side while mixed grain adorns the left side. The stummel on the front, back and the shank displays densely packed straight grains. The only stamping that is seen on this pipe is the football stamp on the left side of the shank and reads “CHOQUIN” over “A METZ”. For its age, the stamping is crisp and clear.This time around, before commencing the restoration process, I posted the pictures of this pipe on the Tobacco Pipe Restorers group on Facebook as my next project. In addition to input from my mentor, Mr. Steve, I collected a lot of valuable information from all the knowledgeable stalwarts. From all the input that I have gathered, the flat bottom bowl, the stamping, the sterling silver adornments, the bone shank extension and horn stem, I can safely place this piece as being one of the first A Metz pipes from the 1858 era!!!!!

INITIAL VISUAL INSPECTION
Well, even before I could start my initial visual inspection, I faced the first of the many numerous hurdles that I had to overcome during the restoration of this pipe. The shank extension and the stem would not budge even a millimeter to separate from the shank and the bone extension respectively. I remembered Mr. Steve referring to the technique of freezing the stuck parts in the freezer for a couple of hours for easy separation. I followed his advice and had to put the complete pipe in the freezer for a couple of hours as it could not be dismantled. True enough, the horn stem separated from the shank extension with the application of a little force, but the extension would not budge from the shank!!!! So I went back to Mr. Steve to tap in to his wealth of knowledge and experience. He suggested that I should apply the method of “Hot and Cold” shock treatment in which you gently and carefully heat the stuck part using a heat gun and then get it back in to the freezer. This process may need to be repeated a number of times before the parts separate. Well, I did exactly that, albeit heating with a hair dryer as I did not have a heat gun, and after 3/4 attempts, the extension finally separated from the shank!!!!The first thing that I noticed was that the shank extension and the mortise were completely filled with oils, tars and grime. The shank extension was filled to an extent that a pipe cleaner would not pass through!!!! How very much typical of my Old Man!!!!!!! Through all this muck, just a swipe of the bone extension with a cotton swab dipped in isopropyl alcohol revealed no apparent damage to the shank extension. Cleaning this would need to be a very careful, meticulous, time consuming and a tedious process given the delicate structure of such a vintage bone. Likewise, the tenon also was filled with oils and grime. Air flow through the stem was laborious to say the least!!! Both the upper and lower surface of the horn stem shows significant damage. The lower surface is peppered with 3-4 worm holes with one significantly larger than the other. Thankfully, it had not migrated through the upper surface!!!! The tenon is completely and permanently encased in the sterling silver ornament. The condition of the stummel was an equally horrendous story. Firstly, the rim top is heavily covered in overflowing lava. The overflow is so heavy that it has accumulated over the rim surface in blobs of dried tar and tobacco oil which can be seen in the subsequent pictures. This overflow had not restricted itself to accumulation on the rim top, but has spilled on to the stummel surface covering the stummel in sticky grime which has attracted more dirt and dust giving the stummel a dull and lackluster appearance. The overflowing lava has even accumulated in the junction where the shank and bowl are joined.  Some dents and dings are seen on the surface through the overflow and I do not envisage any major issue like the ones I faced while working on an Imperial Yello-Bole Carburetor that I had I restored. However through all this dirt, tar, oil, grime and damage, lovely grains can be seen on the sides and the shank. It will be a challenge to address these issues and make the grains to reveal themselves in all glory. The chamber is no different story!!! There is a thick build up of cake in the chamber. The inner edge of the rim is covered under the thick cake and as such, its condition can be commented upon only after the cake has been scrapped. The outer edge of the rim, however, shows significant damage in the form of dents, dings and deep scratches to the front in 12 o’clock direction. The cause for this damage is….. Oh, forget it, let’s not even go there!!!! The condition of the inner walls of the chamber can be ascertained only after the chamber has been completely reamed devoid of any cake, but I do not foresee any major damages here as the stummel feels solid to the touch and this huge solid piece of briar can sustain some serious damage. You have to feel the stummel in your hand to understand what I am trying to write. It is one heavy and handful of a pipe!!!!The sterling silver ferrule and tenon ornament was black as is typically seen in heavily oxidized silver. However through all this discoloration, delicate, intricate decorative design can be appreciated. This is another pointer towards the vintage of this pipe.THE PROCESS
I started the process of restoration by polishing the sterling silver ornaments at the shank end and tenon with pipe ash as suggested by Mr. Steve. This was followed by reaming the chamber with size two of the PipNet reamer head and progressing through to size four. Yes Sirs, there is no typo error!!! It is indeed PipNet and not a Kleen Reem reamer as you have gotten used to reading in my write ups !!!!!! Mr. Steve has sent me a set along with some beautiful pipes that I had got from him. I followed up the reaming with scrapping the remnants of the cake from the walls, flat bottom of the chamber and the rim top surface with my fabricated knife (Oh, how I long for a Sav Fitsall reaming knife!!! Hope you are reading this Steve Sir). The cake was so hard, that I invariably ended up scratching the flat bottom surface while scraping. Once the cake was reamed back to the bare briar, I used a 150 grit sand paper followed by 220 grit sand paper to remove all the traces of remaining cake and also to smooth the inner walls of the chamber surface. Finally, to remove the carbon dust, I wipe the chamber with a cotton pad wetted with isopropyl 99%. I gently scrapped the rim top surface with a sharp knife. Removing all the cake from the chamber and rim top revealed that firstly, the rim was out of round and secondly was a web of fissures along the internal walls. There was one crack, which showed prominently after a cleanup with Murphy’s oil soap, bothered me and can be seen in the pictures below which has been highlighted by a red circle. I shared these images with Mr. Steve and Mr. Dal Stanton for their opinion as to the extent of damage and further repairs. They too expressed fears that the crack may have migrated through the stummel. Mr. Steve suggested picking the crack on the top of the rim using a toothpick and filling it with CA superglue. I decided that I would address this issue later after further investigations. I cleaned the internals of the shank, shank extension and the stem using hard bristled and regular pipe cleaners, q-tips, shank brushes, all generously dipped in isopropyl alcohol. I had never used such drastic measures like initially cleaning the bone shank extension by carefully inserting a round needle file for creating an opening through which pipe cleaners could pass through for subsequent cleaning. The heap of pipe cleaners and q-tips that are seen in these pictures are just the proverbial tip of the iceberg. I must have gone through an entire packet of 50 of both types of pipe cleaners, in addition to the q-tips and brush cleaning!!!!! To further deep clean and refresh the internals, I used cotton and alcohol soaks. Using a cotton ball to create a wick, I inserted it through the mortise and into the airway. I then stuffed the bowl with tightly packed cotton balls and placed it in bowl filled with rice grains to provide stability. Similarly I made a tight cotton wick and inserted it through the bone shank extension to further remove all the oils, tars and smells. With a large eye dropper, I then filled the bowl and the bone shank extension with isopropyl 99% until it surfaced over the cotton. I refilled the alcohol in a few minutes after it was absorbed into the cotton balls. I put the stummel and the bone shank extension aside for several hours to soak. After some time, the cotton and the wick were soiled. I discarded the expended cotton and wiped the bowl and the bone shank extension with paper towel. To make sure all was clean, I used a cotton bud and pipe cleaner dipped in isopropyl 99% and they came out clean. I cleaned the stummel with undiluted Murphy’s oil soap and Scotch- Brite pad and rinsed the stummel under running tap water. This cleaning helps in bringing to the fore any other damage which could be hidden under all the dirt and grime. Fortunately, there were no major dents, dings or gouges to the stummel. There were a few minor ones which I think would be addressed when I would sand the stummel surface and subsequent micromesh polish. I dried the bowl with a paper towel and soft cotton cloth. Initially I had decided that I would not be topping the rim top and maintain its original profile. However, in order to ascertain if the crack had migrated through the stummel, I decided to top the rim surface. This would also help to address the numerous dents, dings and scratches on the rim’s top surface and also to remove traces of lava overflow. I topped the rim surface on a 220 grit sand paper. Though it is recommended to have a wooden board with the 220 grit sand paper firmly fixed over it, I just keep the sand paper on a flat table top, holding it firmly with my left hand and rotating the stummel rim top over it with my right hand. I have come to realize that this set up gives me lot more freedom of movement, better control and convenience of storage. Fortunately, it was revealed that the supposed crack was superficial and had not migrated through. Staying with the rim, the next issue that I addressed was the inner rim edge. With a folded piece of 180 grit sand paper pinched between my thumb and fore finger, I created a light bevel on the inner edge. This addressed the issue of uneven and out of round inner edge. The damage to the outer edge was addressed to a great extent when I had topped the rim top surface. Whatever little dents and nicks that remained on the outer edge were very minor, though visible, and I decided to let them be.I sand the stummel surface with a 220, 320, 600 and 1000 grit sand paper, in that order, to remove the minor scratches and marks on the rim and stummel surface. I frequently wiped the sanded surface with a moist cloth to remove the briar dust and also to check the progress of my work. Once I was satisfied with the match, I followed it up by micromesh polishing pads, wet sanding with 1500 to 2400 grit pads. Again, I wiped the bowl with a moist cotton cloth after each pad. I used the 3200 to 12000 grit pads to dry sand the stummel to a nice shine. I was disappointed when after all my efforts up to this stage; there were some very minute chips that were visible in pictures. But overall, at this stage of restoration, the entire bowl, rim top surface and shank is looking fresh and clean. Even though some of the dents and chips could not be completely addressed and are visible only on very close visual scrutiny, in my view, they lend this pipe a battle scarred warrior like a character. I rubbed a small quantity of “Before and After Restoration Balm” with my fingers deep in to the stummel surface. What this balm does is it revitalizes the briar wood and breathes a new life in to the briar. It’s amazing to see the transformation as the balm works its magic on the briar wood. I further buff it with a horse hair shoe brush. Turning my attention to the horn stem, I cleaned the stem surface, including the worm holes, with q-tips dipped in isopropyl alcohol to remove all the dirt and dust before the fill. I filled the worm hole on the bottom and top surface with clear CA superglue and set it aside to cure.  Once the superglue had cured, I sanded the fills with a flat head needle file. To further match the fills with the surface of the stem, I sanded it with 220, 320, 600 and 1000 grit sand paper. I wiped the stem with cotton pad dipped in alcohol to remove the resultant dust. I rubbed some extra virgin olive oil in to the stem and set it aside to be absorbed in to stem. A few minutes later, I polished the stem and also the bone shank extension with micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000. I rubbed a little extra virgin olive oil in to both after every three pads. The stem is now nice, smooth and shiny while the extension though smooth and shiny, still had the golden brownish hues of the tobacco oils and tars. I was wondering as to next course of action, Mr. David Goostree, an experienced member from The Tobacco Pipe Restorer group on FB, provided valuable information that the bone is similar to a Meer and absorbs oils from the tobacco and colours just like a meerschaum. Another issue taken care of!!! To finish the restoration, I mounted a cotton cloth buffing wheel to the Dremel (actually it is not the brand machine, but a local machine which is similar).  I set the speed at about 40% full power and applied White Diamond compound to the entire pipe.  Afterwards, I wiped/ buffed the pipe with a soft cotton cloth to clear it of any leftover compound dust. I then mounted another cotton cloth wheel to the polishing machine, maintaining 40% speed and applied several coats of carnauba wax.  I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further. In my excitement mixed with apprehension in using the polishing and waxes for the first time, I completely missed out on taking any pictures. The completed pipe looks lovely, fresh and vibrant. Thank you for having the patience to reach this far while reading the write up. Your comments are of utmost importance to me for improving my skills in restoration process as well as writing about it. Cheers!!!!!

PS: – During this journey of restoring this beauty, I had, on occasions felt low and demoralized as issues kept cropping up like the supposed crack to the stummel, the shank extension not supposedly cleaning up as I had incorrectly anticipated and the 2/3 occasions when the my polishing machine slipped on the surface and caused very minor scratches on the stummel. However, my Guru and mentor, Mr. Steve was always around with his words of wisdom and encouragement to egg me on towards completing this project. Thank you once again, Mr. Steve. I would like to thank all the esteemed members of “The Tobacco Pipe Restorer” group on FB for their interest and valuable inputs, which made this project interesting.

Converting a Zettervig Freehand into a Churchwarden


Blog by Steve Laug

Sometime pipes come back to you. I had restored and restemmed this pipe for a fellow here in Vancouver not too long ago and made a freehand stem for it. I had also worked on converting a broken shanked Brigham into a churchwarden. The other night he dropped by and we sat and chatted for a bit. He pulled four pipes out of his bag for me to look at. One was a new find from a junk store. The other three were pipes that I had already done for him. The first two were churchwardens and he decided that they just were not for him. He also took the freehand stem out of the Zettervig and put it in the Brigham and said that he had been smoking it that way and really liked it a lot. We talked about options – restemming all three, using the stem from the Zettervig on the Brigham, restemming the churchwardens with shorter stems or just selling the pipes. The one churchwarden would be just a cleanup. The other was a little more involved. It meant fitting the existing churchwarden stem on the Zettervig pipe and seeing if that would move it. We chose the last option selling the two pipes as churchwardens to someone who really wanted them.

Here are some pictures of the Zettervig as it was when I sent it home with him. I thought they would give us a base for the change. The pictures give a clear picture of the beauty of the pipe. The stamping on the pipe is on the underside of the shank and reads Zettervig over Copenhagen over Handmade. Under that it is stamped with the shape number 351 followed by Denmark. As a reminder I quote from the blog on the Zettervig to summarize the history of the brand for you all. Here is the link to the blog: https://rebornpipes.com/2018/07/28/restoring-and-restemming-a-zettervig-handmade-351-freehand/

In the 1960’s and into the early 1970’s Ole Zettervig had a shop in Copenhagen, Denmark where he was carving high quality pipes equal to Stanwell, Larsen, Anne Julie, Thurmann, Bang and others. These early pipes were marked “Copenhagen” and are very collectible. He sold his shop at some point in the 70’s and moved to Kolding and continued to produce pipes as a hobby, but the quality of briar and workmanship is said to not equal the early production. The later pipes he now marked as Kobenhaven rather than Copenhagen, and these were sold by Ole at flea markets throughout Europe.

http://www.pipephil.eu/logos/en/logo-z.html

I took the churchwarden stem from the Brigham and reworked it for the Zettervig. I needed to trim the tenon down slightly and reshape the shank end of the stem. I worked on it until the fit was perfect in the shank. I rounded the area above the tenon to fit into the angled plateau on the end of the shank. I used 220 grit sandpaper to shape the tenon and stem. Unfortunately I was on a roll and forgot to take pictures of that part of the process.

I lit a votive candle and used it to heat the stem. I inserted a long pipe cleaner in the stem and turned it over and over until the vulcanite was pliable. I checked the pliability repeatedly and when it was finally bendable I bent it over a round jar to give it an even bend that matched the flow of the bowl and shank. I held it in place until the bend was set. The stem was used by the Vancouver fellow so I needed to remove the light tooth chatter on the top and underside near the button and also clean it to remove the light tars. I cleaned the stem with alcohol and long pipe cleaners. Once the cleaners came out clean that part was finished.I polished the vulcanite with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I wiped down the stem with Obsidian Oil after each pad to protect and polish it. I gave it a final polish with Before & After Pipe Stem Polish – both Fine and Extra Fine. I gave it a final coat of Obsidian Oil and set it aside to dry. The Zettervig bowl had been smoked more than the churchwarden stem from the Brigham. It was dirt in the shank and airway. It also had a light buildup of carbon in the bowl and it was dirty. The finish was also dull so that would need to be address. I cleaned out the shank and airway with pipe cleaners, cotton swabs and alcohol until they were clean. I cleaned out the carbon on the bowl walls with a Savinelli Fitsall Pipe Knife to smooth out the interior of the bowl. I rubbed down the smooth briar with Before & After Restoration Balm. I worked it into the smooth surface of the briar on the sides and the bottom of the bowl and shank with my fingertips. I worked it into the plateau on the rim top and shank end with my finger tips and worked it in with a horsehair shoe brush. I wanted to make sure that the balm got deep into the briar to do its work. The balm works to clean, enliven and protect the briar. I let it sit for a little while and then buffed with a cotton cloth to raise the shine. The following photos show the bowl at this point in the restoration process. The rim looks much better than when I started but still needs to be polished and buffed to raise a shine on it. I the buffed stem and the bowl with Blue Diamond on the buffing wheel to polish out the remaining small scratches and raise the shine. I carefully avoided the stamping on the underside of the shank. I gave both the bowl and the stem multiple coats of carnauba wax and buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The pipe polished up pretty nicely. This turned out to be a beautiful pipe in terms of shape and finish. The combination of the Danish Zettervig bowl and the vulcanite churchwarden stem looks very good. The finished pipe is shown in the photos below. The dimensions are Length: 11 inches, Height: 2 inches, Outside diameter of the bowl: 1 3/8 inches, Chamber diameter: ¾ of an inch. Thanks for walking through the conversion of this bowl to a churchwarden with me.

Recommissioning a Comoy’s Moorgate 102 of Italy


Blog by Dal Stanton

I saw this attractive Comoy’s Moorgate on the eBay auction block last year and fortunately provided enough of a bid to bring it home to Bulgaria.  What attracted me to this Comoy’s was the interesting finish which is a darkened, orange hue with nice feathered grain.  This Comoy’s Moorgate also got Jim’s attention after he saw it posted on my website in the For ‘Pipe Dreamers’ Only! collection I list online for pipe men and women to commission.  I enjoyed communicating with Jim via email very much.  Jim not only commissioned the Comoy’s, but he also commissioned a very interesting, older Stanwell Henley Special which I acquired along with 2 brother Stanwell Henleys – 3 pipes I’ve been looking forward to restoring and learning more about.  Along with these 2 pipes that Jim commissioned, were his encouraging words of appreciation for the work we’re doing with the Daughters of Bulgaria – women and girls who have been trafficked and sexually exploited.  Jim was glad that the pipes he was commissioning benefited these efforts.  Thanks, Jim!  Here are a few pictures of the pipes – the Comoy’s and the Stanwell Henley Special – Jim’s is the Saddle Stem Billiard in the middle.  When Jim commissioned these pipes, I’m grateful that he also agreed to be patient as the pipes gradually made it to the top of the queue.  I take some additional pictures to take a closer look at the Comoy’s Moorgate on my worktable here in Sofia, Bulgaria, on the 10th floor of a formerly Communist block apartment building. The nomenclature identifies this Comoy’s as a post-Cadogan era pipe which dates it no older than the early 1980’s when the Cadogan merger took place.  On the left side of the shank is ‘COMOY’S’ [over] ‘MOORGATE’.  The right side of the shank is stamped with the shape number, ‘102’.   The upper side of the stem has the well-known ‘C’ Comoy’s stamp and the underside is stamped, ‘ITALY’. All the stampings point to a post-merger Comoy’s pipe.  The COM being Italy and not ‘Made in London England’ confirms this as Cadogan farmed out the manufacturing.  Interesting also is the shape number, ‘102’.  Pipedia provides a Comoy’s Shape Number Chart that identifies the 102 as being an army mounted, large, straight Pot which does not correspond to the Half Bent Billiard on my table.  The chart most likely pointing to earlier shape numbers.Pipephil.eu provides a Comoy’s Moorgate that matches up with what I’m seeing before me – nomenclature and stampings.  It references a Comoy’s second brand with the name ‘Moorgate’.  I look up the reference and it is a different line altogether – nomenclature and stem stamps and COM as ‘Made in England’.Looking at the condition of the Comoy’s Moorgate on my worktable, it is generally in good condition.  I take a few more pictures to look at some trouble areas.  The chamber has moderate cake build up and some significant lava flow caked on the rim.  The bowl surface has some dents which I’ll try to lift with the hot iron method to preserve the finish.  The stem has moderate oxidation and tooth chatter – no huge problems detected there. To begin, I run a pipe cleaner wetted with alcohol through the draft way and then put the stem in a bath of Before & After Deoxidizer along with several other pipes in the queue.  After several hours soaking, I fish out the Comoy’s stem and allow the Deoxidizer fluid to drain off.  I then take a cotton cloth wetted with alcohol and wipe off the raised oxidation. I continue wiping off oxidation and conditioning the stem by wetting the cotton pad with light paraffin oil.  The Deoxidizer seems to have done a good job. Next, I address the chamber cleaning by reaming it with the Pipnet Reaming Kit. To help with the cleanup, I put down some paper towel to catch the dislodged carbon.  Beginning with the smallest of four blade heads, I ream the chamber. I only use 2 of the 4 blades available.  I follow this by using the Savinelli Fitsall Pipe Tool to fine tune the reaming.  I also use the Fitsall Tool to scrape gently an internal rim bevel that emerges from underneath the carbon cake.  I also use my thumbnail to scratch the carbon off the rim.  Following this, I wrap a piece of 240 grit paper around a Sharpie Pen and sand the chamber.  Finally, to remove the carbon dust, I wipe the chamber with a cotton pad wetted with isopropyl 95%.  With the chamber cleaned, I inspect the chamber walls and I find no issues with heat fissures or cracking. Turning now to the external briar surface, I use undiluted Murphy’s Soap on a cotton pad and clean.  I take my time on the rim to remove the lava.  After cleaning the surface, I use cool tap water to rinse the bowl.Turning now to the internals of the bowl, I use cotton buds and pipe cleaners with alcohol to clean. I also use a dental spatula to scrape the mortise walls more quickly removing the built-up tars and oils.  In time the buds and pipe cleaners start coming out cleaner.  Good for now.  I move on!To achieve a deeper cleaning and refreshing of the internals, I use a kosher salt and alcohol soak.  Using a cotton ball to create a wick, I stretch and twist it and then insert it through the mortise and into the airway.  I then fill the bowl with kosher salt and place it in an egg carton to provide stability.  With a large eye dropper, I then fill the bowl with isopropyl 95% until it surfaces over the salt.  I top the alcohol in a few minutes after it’s absorbed into the salt.  I put the stummel aside for several hours to soak.  After some time, the salt and the wick were soiled.  I tossed the expended salt, wipe the bowl with paper towel, and blow through the mortise to remove salt crystals.  To make sure all was clean, I use a cotton bud and pipe cleaner dipped in isopropyl 95% and they are clean.Putting the cleaned bowl aside, I take the flat needle file and work on the button.  I file the button lips, upper and lower to redefine them.  To erase the scratches of the file, I follow by sanding the bit area, upper and lower with 240 grade sanding paper.  I also sand the entire stem to remove further residual oxidation.  I’m careful to avoid the stem stampings while sanding.  To remove the scratches left by the 240 grade paper, I wet sand using 600 grade paper followed by applying 0000 steel wool buffing to the entire stem.In order to further enrich the vulcanite, I use Before & After Fine and Extra Fine Polish in that order.  I put some Fine polish on my fingers and work the polish in.  After some minutes, I wipe it off.  I follow with the same process with the Extra Fine Polish, giving it some minutes and wiping it off and buffing up the stem.  The stem is cleaning up very nicely.Turning again to the stummel, there are 2 significant dents that I want to see if I can minimize using the heating method with an iron.  I take pictures of the two places I have in mind.  I heat the iron and dampen a cotton handkerchief with water.  I place the cloth over the dent and press the hot iron against the cloth over the dent in the briar.  The heat and moisture are supposed to expand the dent and in this case it does. Interestingly, taking a picture of the two dents afterwards, what emerged is a roughness caused by the heat. Hmmm, not sure why that happened.  The pictures show what I see before and after heating. To remove the roughness caused by the heating and to remove the normal wear nicks, I wet sand the stummel using micromesh pads 1500 to 2400.  I then dry sand with pads 3200 to 4000 and 6000 to 12000.  The grain on this Comoy’s Moorgate is unique as it emerges through the micromesh process.  It looks great! To enrich the natural grain of the bowl, I apply Before & After Restoration Balm.  I apply some Balm on my fingers and work it into the briar surface.  The Balm starts with a thinner oil-like viscosity then gradually thickens to a waxy consistency.  After I apply the Balm thoroughly, I let the bowl stand for several minutes while the Balm absorbs.  I then wipe off the Balm using a microfiber cloth and gradually, as the Balm is removed, I transition to buffing with the cloth. I take a picture while the Balm is doing its thing and after. I’m liking it a lot!Returning to the stem, I now continue with the micromesh sanding phase.  I begin by wet sanding using pads 1500 to 2400, then dry sanding using pads 3200 to 4000 and 6000 to 12000.  Between each set of 3 micromesh pads, I apply Obsidian Oil to continue revitalizing the vulcanite.  The rubber has that glossy pop!  I put the stem aside to dry. Next, I want to refresh the stem stamping, ‘ITALY’.  To do this I place a drop of white acrylic paint over the lettering.  I then use a cotton pad to blotter the excess paint, thinning it so that it dries rapidly. With the flat edge of a toothpick, I then gently scrape the excess paint off the stem.  The pictures show the progress. I now reunite the stem and the bowl and mount a cotton cloth buffing wheel to the Dremel.  I set the speed at about 40% full power and apply Blue Diamond compound to the entire pipe.  Afterwards, I wipe/buff the pipe with a felt cloth to clear it of leftover compound dust.  While I was buffing with the felt cloth, I note that the stem fitting is a little loose for my liking.  This sometimes happens after cleaning the pipe well and scraping the mortise.  To remedy this, I fit a drill bit just larger than the airway diameter and heat the tenon with a Bic lighter.  As the vulcanite tenon heats, it becomes supple allowing me to insert the bit into the airway and it expands the tenon slightly.  I test the fit and it works perfectly, and I am satisfied.  After rejoining stem and stummel, I then mount another cotton cloth wheel to the Dremel, maintaining 40% speed and apply several coats of carnauba wax.  I finish the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further.I’m pleased with the results of this Comoy’s Moorgate.  The briar is spectacular with its diversion of colors and swirls of grain.  Patches of orange settle in the grain knots and from there the colors are an eye catching kaleidoscopes. It is a unique piece of briar and the half-bent Billiard nicely rests in the palm.  Jim commissioned this Comoy’s from the For ‘Pipe Dreamers’ Only! collection and he will have the first opportunity to acquire it from The Pipe Steward Store.  This pipe benefits the Daughters of Bulgaria – women and girls who have been trafficked and sexually exploited.  Thanks for joining me!

A Tiny 2 Star BBB 8881 Apple/Globe Provided An Interesting Challenge


Blog by Steve Laug

When I spoke with a fellow here in Vancouver who had a pipe that he wanted me to fix it sounded like a simple repair. He said that it had a very loosely fitting stem. He asked if he could drop by to show it to me and see if I could fix it. From past experience I have learned to never jump to conclusions about what sounded like an easy repair. When he arrived he showed me his GBD Faux Spigot. It turned out to need far more work than just tightening a loose stem. I wrote about that restoration in a previous blog (https://rebornpipes.com/2018/11/03/redoing-a-poorly-restored-ebay-gbd-super-q-9436/). We talked about his GBD for a bit and he made the decision to have me do a restoration on it. Then he reached into his pocket and pulled out a small plastic bag with a little BBB 2 Star apple of globe shaped pipe. It was stamped BBB in a diamond on the left side of the shank with two ** – one on either side of the diamond. ON the right side it was stamped Made in England over the shape number 8881. He said that he had found it at his parents’ house and really no one there knew where it came from.

Here is what I saw. Starting with externals. The pipe was small – kind of a pocket pipe. The grain on the bowl was quite stunning – a mix of flame and birdseye all around the bowl and shank. The rim top was coated with a thick lava coat and it went into the bowl. The inner edge of the bowl was in rough shape having been hacked clean with a knife. There was a crack on the right side of the shank curving to the underside. It looked to me it was made by the poorly made stem being shoved into the shank. The stem was larger in diameter than the shank and had been rounded over with a file. There were deep bite marks on the surface ahead of the button on both sides. Moving to the internals. The end of the tenon was carved with a knife to make it fit the mortise in the small shank. The inside of the shank was dirty but less so than I expected. The inside of the bowl had a light cake but most of that was gone from the knife job that had left a wounded inner edge on the rim. Looking at the pipe I explained what I would have to do to bring it back to life and restore it to use. It would need, cleaning, reshaping on the rim, a band on the cracked shank that would leave the stamping readable, and a reworking of the stem to make it a fitting addition to the lovely briar of the bowl. The pipe was going to be a fun challenge. I took these photos to give you an idea of what I saw. The previous pipeman who had fit a new stem to an old favourite pipe had done a functional job but it looked rough. It was pretty clean on the inside so it was cared for. It must have been a great smoking pipe for him to fit a new stem and not give up on it when the previous one broke or was lost. It was smokable. I took a close up photo of the rim top to show the condition. It is hard to see but the rim top was not smooth. The lava build up was pretty thick and there were some deep nicks and chips in the flat top. The close up photos of the stem reveal the scratches in the vulcanite, the tooth marks and the worn and ill-defined button.  The oversized diameter – prettified to look nice is clear in the photos. I took photos from the side of the pipe to show the stamping on the shank and the prettified stem. In the second photo you can see the crack in the shank curving downward to the underside.I decided to address the cracked shank first. With the crack as large as it was and movable I did not want to further damage it when I worked on the stem and fit of the tenon. I knew that it needed to be banded but that would cover the stamping on the shank so adjustments would have to be made. I used a Dremel and sanding drum to reduce the size of the shank to fit the band I had chosen. I did not take of too much briar and I only damaged the M in Made In England as part of it would end up being covered by the band.I repaired the crack in the shank with super glue and pressure fit the band onto the shank to the point of the end of the sanded portion. I used a Dremel and sanding drum to cut back the band to the width that I wanted. Compare the photos above with the one below to see how much I took off of the band. I topped the band on a topping board with 220 grit sandpaper and smooth out the sharp edge with 1500 grit micromesh. I decided that since I was already working with the Dremel and sanding drum that I would take down the excess diameter on the stem as well. I reduced it to sit snugly against the band giving the pipe a classy look.I cleaned up around the inside edge of the band and edge on the shank with a folded piece of 2220 grit sandpaper to smooth things out and make the fit and transition smooth. I lightly sanded the blade portion of the stem and the area of the tooth marks next to the button with 220 grit sandpaper to remove the oxidation and clean it up. I fit the stem in the shank and took a photo of the pipe at this point in the process. It was beginning to look like a classic BBB to my eye. With the stem roughly fit to the shank it was time to address the bowl top. I topped it on a topping board with 220 grit sandpaper. At that point I called it a night. I had to catch a train down to the southern part of Washington from Vancouver in the morning so I thought I would bag up a couple of pipes I was working on and take them with me.I caught the train south from Vancouver, BC at 6:30am. Once we had our seats we were in for an 8 hour train ride. I figure it would be a good opportunity to work on these two pipes. You can see my work table in the photo below. I used the fold down table. It had a lip around it so I spread out a couple of napkins for the dust and went to work on the pipes.I started working on the BBB by addressing the damage to the inner edge of the rim. It was significant with cuts and burns. My topping worked had helped with the top damage and smoothed that out but I need to work on the rim edge. I used a folded piece of 220 grit sandpaper to smooth out the sharp edges and bring the bowl back to round. Once I had the rim as round as I could get it and smoothed out the damaged edge I polished it with micromesh sanding pads. I polished the bowl and the rim at the same time. I wet sanded with 1500-2400 grit micromesh sanding pads and dry sanded with 3200-12000 grit pads. I wiped the bowl down with a damp napkin after each pad. I touched up the stain around the front of the band and stained the rim top and inner edge with Maple and Cherry stain pens. Together the two stains matched the rest of the bowl.I rubbed down the briar with Before & After Restoration Balm. I worked it into the smooth surface of the briar with my fingertips to clean, enliven and protect it. I let the balm sit for a little wall and then buffed with a cotton cloth to raise the shine. The following photos show the bowl at this point in the restoration process. The rim matches well but still needs to be polished and buffed to raise a shine on it. I used a folded piece of 220 grit sandpaper to reshape the button and also to smooth out the marks left by the Dremel when reducing the diameter of the stem. I sanded the tooth marks near the button on each side of the stem to smooth them out.I polished the stem, tenon and metal work with micromesh sanding pads – wet sanding with 1500-2400 and dry sanding with 3200-12000 grit pads. I wiped the stem down with Obsidian Oil after each sanding pad. I was able to remove the damage on the tenon and polish out the dripping varnish on the metal adornment. The stem looked much better at this point in the process. I the polished stem and bowl with Blue Diamond to polish out the remaining small scratches and raise the shine. I gave the bowl and the stem several coats of carnauba wax and buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The pipe polished up pretty nicely. This turned out to be a beautiful little pocket pipe in terms of shape and finish. The new nickel band adds a touch of class in my opinion and gives the pipe a new elegance. I look forward to hearing what the fellow who dropped it off for repair thinks of it once he has it in hand and is smoking it. The finished pipe is shown in the photos below. The dimensions are Length: 4 inches, Height: 1 3/8 inches, Outside diameter of the bowl: 1 inch, Chamber diameter: 3/4 of an inch. Thanks for walking through the restoration with me.

Salvaging a ‘Really’ Poor Richard’s of Italy Giant Billiard


Blog by Dal Stanton

Let’s be honest. When I saw this Poor Richard’s on the eBay auction block I thought the name was a joke by the seller.  He WAS huge (L: 6 3/4”, H: 2 1/8”, Rim W: 1 1/2″, Chamber W: 7/8”, Chamber D: 1 7/8”, Weight: 74gr), no doubt, but his condition could qualify him for the title: King of the Basket Pipe Realm.  His condition was indeed poor and adding to the ‘joke’ was that he was displayed on satiny royal purple material.  But the clincher was coming. Adding insult to injury, the seller’s byline description under Poor Richard’s picture was: Poor Richard’s Classic Bulldog Large Estate Pipe Beautiful !!!  Nice  !!!  Bulldog?  I felt sorry for him.  I placed a bid and when the auction ended, it was no surprise that mine was the only bid seeking a new life for Poor Richard’s.  My wife’s response when she first saw Poor Richard’s was that Poor Richard’s dog got a hold of him!  Here are the pictures I saw. After bringing Poor Richard’s back to Bulgaria, I put him on my website in the For ‘Pipe Dreamers’ Only! section where my friend and fellow Pipe Dreamer from India, Paresh, saw him.  Poor Richard’s became the fourth pipe Paresh commissioned – all of them on the larger side and each one of them advancing our work here in Bulgaria benefiting the Daughters of Bulgaria, helping women and girls who have been trafficked and sexually exploited.

Taking more pictures on my worktable on the 10th floor of a formerly Communist ‘Block’ apartment building, the nomenclature on the left shank is ‘PoorRichard’s’ in what I call an ‘Old World’ script.  There are no other markings on the shank.  The stem is stamped with an interlocking ‘PR’.  The bottom of the stem is stamped with the COM, Italy.When I began doing the research on this Poor Richard’s, I recalled that rebornpipes’ contributor, Al Jones (aka: Upshallfan), had recently posted a restoration of a Poor Richards 9438 Cordovan Rhodesian shape.  Reading Al’s write-up was helpful because it clued me into the ‘mystery’ surrounding the origins of the Poor Richard’s name.  I noticed that our pipes shared the ‘Old World’ script nomenclature as well as the interlocking ‘PR’ stem stamp.  The obvious difference was the COMs – his, London, England and mine, Italy and his included a shape number, and mine, without.As I’ve done in the past with much benefit, I wrote to Al asking about the differences between our Poor Richard’s and what to make of the differing COMs?  His response was helpful:

Dal

Unfortunately, there is nothing but speculation about these Poor Richard pipes.  The one shop here, with that name, can’t even conclusively determine if they had shop pipes.

I suspect it was a shop pipe, made by various makers for this shop.  But a shop in Montana having shop pipes doesn’t exactly make sense either.  Usually shops with their own pipes were larger, and in metro areas, not out in the wilderness of Montana.

Poor Richard pipes are not listed in “Who Made That PIpe”, so my guess is still a shop pipe.  Perhaps that Montana shop was bigger than I presumed. 

I suspect Italian companies, like GBD made shop pipes as well.  Perhaps that one was made by Savinelli or other?  Without a shape number, it’s impossible to determine.

Have fun restoring it!

Al

Al referenced the pipe shop in Montana that in a subsequent email he referenced that Steve had also worked on a Poor Richard’s attributed to the ‘Poor Richard’s’ pipe and tobacco shop in Bozeman, Montana. However, Al said that Steve’s Poor Richard’s pipe had a totally different nomenclature with Montana stamped on the pipe.  I found this write up on Rebornpipes and what a write up!  It was one of Steve’s and Charles Lemon’s classic collaborations including a pinning tutorial.  When these two masters get together, its fun to see the wonders happen!  (See this post which is worth the read:  A Humpty Dumpty Cross Canada Project – Could this Poor Richards Select Square Shank Billiard 9489 ever be whole again?)  Steve’s research on the Montana shop is good and saved me time and steps.  Since Steve’s write up in 2016, the website had changed and a description of Poor Richard’s history beginning in 1962 can be found here: History.  The following pictures show the shop early on and what it is today.Even with the mystery and the discrepancies with the nomenclatures, in researching different pipe shop pipes in the past (L. J. Peretti, Pipe Pub), I found that it’s common to have pipes manufactured in various places.  Another indicator that the Poor Richard’s nomenclature refers to a shop is simply because it is possessive – Richard’s, pointing to something else.  Whether there’s another Poor Richard’s shop other than the one in Bozeman, I don’t know.  This question has been lost to history.

The condition of the giant Poor Richard’s before me now is poor. I take more pictures to take a closer look. The chamber has moderate cake build up that needs to be removed to inspect the condition of the chamber.  The lava flow on the rim is thick.  The stummel surface reminds one of a moonscape with all the craters in need of attention!  Along with the pits and holes there are dents and scrapes.  The oxidation on the stem is joined by bites and compressions on the lower and upper bit.  With a better understanding of the Poor Richard’s name, I begin the salvage of the giant Billiard by running pipe cleaners dipped in isopropyl 95% through the stem and then adding it to a soak of Before & After Deoxidizer along with several other commissioned pipes in the queue.  The Poor Richard’s stummel and stem are first on the left.  After letting it soak overnight, I fish out the Poor Richard’s stem and let the fluid drain off.  I then push a pipe cleaner through it to help remove the Deoxidizer.  I then wipe the stem with cotton pads wetted with isopropyl 95% to remove the raised oxidation from the vulcanite stem.  After wiping off with the alcohol, I then wipe again using a cotton pad and light paraffin oil (mineral oil) to clean and condition the stem further.  Finally, I run another pipe cleaner through the stem dipped in isopropyl 95%.  The pictures show the process. Taking the stummel, I use the Pipnet Reaming Kit to clean the chamber.  After putting paper towel down on the table for easier clean up, I start reaming using the third largest blade head since the chamber is so large.  I also use the fourth and largest blade to ream.  Following the reaming, I use the Savinelli Fitsall Pipe Tool to scrape the chamber walls removing additional carbon cake – especially down in the floor of the chamber with the difficult angles.  Then, after wrapping 240 grit paper around a Sharpie Pen, I sand the chamber walls removing additional carbon and smoothing the chamber surface.  I clean the chamber next using a cotton pad wetted with isopropyl 95%.  While inspecting the chamber, I do see some hairline heat cracks that are very small, but not serious enough to warrant repair.  Next, using undiluted Murphy’s Oil Soap I work on the external briar surface using a cotton pad.  I also use a brass wire brush on the rim to remove the lava and follow by carefully scraping the rim surface with a flat knife edge.  After scrubbing, I rinse the stummel in the sink with cool tap water.Turning to the internals, I use pipe cleaners and cotton buds dipped in isopropyl 95% to clean the mortise and airway. I also use a small dental spatula tool to scrape tars and oils off the mortise walls.  The cleaning wasn’t too bad. Later, I’ll continue cleaning the internals with a kosher salt and alcohol soak.With the internals cleaned, I now look at the stummel surface.  I have several fills to dig out and to fill.  My main tool in doing this is a sharp dental probe.  The goal is to only have a solid base in the holes – either old filler material or briar.  It takes quite a bit of time, but I move from fill to fill doing the needed excavation work. With the holes excavated, I prepare a batch of briar dust and CA glue patch to apply to the problem areas.  I scoop briar dust in a small mound on an index card and put a glob of thick CA glue next to the briar dust.  Using a dental spatula, I mix briar dust into the CA glue until I reach a thicker consistency, like molasses.  I then trowel the patch mixture into each of the holes leaving excess to be sanded down after cured.  The pictures show the process. With the Briar Dust patches curing, I turn to the stem.  After the soak in the Before & After Deoxidizer, much of the oxidation was removed.  But looking more closely, there remains oxidation but it’s much subdued. I decide to place the stem in another soak – this time with OxiClean.  I put a pipe cleaner through the stem and put it in the OxiClean to let it soak overnight.With the day ending, I continue the cleaning and refreshing of the stummel internals.  To do this I employ a kosher salt and alcohol soak.  First, I form a wick by stretching and twisting a cotton ball and with a stiff piece of wire, I stuff it down the mortise and airway.  It will serve to draw out tars and oils.  Then I fill the bowl with kosher salt and place the stummel in an egg crate to keep it stable.  With a large eyedropper, I fill the bowl with isopropyl 95% until it surfaces over the salt.  After a few minutes, I top off the alcohol as it is absorbed and turn out the lights.The next morning, there isn’t too much discoloration of the salt which means I didn’t put in enough alcohol or that the internals are clean.  The wick is darker.  I toss the expended salt into the waste, wipe the bowl with paper towel and blow through the mortise to remove remaining salt crystal.  I then use a shank brush on both the bowl and the mortise – blowing again.  Finally, to make sure all is clean and ready to go, I wet a cotton bud and pipe cleaner with isopropyl 95% and run them through the mortise and airway.  They come out clean and it’s time to move on. I put the stem in an OxiClean soak through the night and it’s time to fish it out.  I take a picture of the additional oxidation that has been raised and I take the stem to the sink and wet sand the stem with 600 grade paper to remove the oxidation.  It looks cleaner now after sanding.Looking more closely now at the bit area, there are good sized compressions.  The button also has some bite marks.  The first step is to use the heating method to see if it will expand the vulcanite reducing the severity of the compressions.  I use a Bic lighter and paint the upper- and lower-bit areas. The areas were lessoned, but not erased by heating the vulcanite. I then use 240 grade paper and sand the upper- and lower-bit areas as well as redefine the button with a flat needle file.  I take pictures of each step. First, the upper bit progress:After heating:After 240 sanding and filing:Progression of the lower bit area:After heating:After 240 sanding and filing: I’ve sanded out as much as will sand and now I will patch the areas that did not sand out.  I first wipe the stem with alcohol to clean the area.  I then apply black CA glue to the areas.  And I wait, and wait, and wait….  Well, I just discovered that Black CA glue can go flat and lose its ability to bond.  Reading the directions, is says to refrigerate to prolong shelf life.  Well, the shelf life must have been reached.  I wipe the old CA glue off and thankfully, I had purchased another bottle of Hyper Bond Black Rubber Reinforced CA glue.  I discover that the bottle mouth is larger than the squirt spouts that I have so I end up troweling a small bit of the glue on the end of a pointed dental spatula and apply it to the spot.  It works!  To advance the curing time I spray the upper and lower patches with an accelerator which does the trick.  The first picture, upper that didn’t cure and the new glue on the lower.  New bottle of glue is heading for the fridge! Next, taking a flat needle file I start filing the black CA patches staying on top of the glue mounds.  I then follow by using 240 grade sanding paper to bring the excess CA glue to flush with the vulcanite surface.  First, pictures showing the upper bit: The next step with the stem is to wet sand it with 600 grade paper then I follow by buffing the stem with 0000 steel wool to prepare the vulcanite surface for the micromesh pad phase of sanding.  The patches on the bit blended very nicely.I put the stem aside because I’m anxious to get started on the Poor Richard’s stummel.  I decide to start from the top and work down.  I will establish fresh lines for the rim and remove the surface scratches by topping the stummel.  I first use 240 grade paper on the chopping board and invert the stummel and rotate the stummel over the paper. After the 240 paper, I use 600 grade paper for another few rotations.  It looks good. To dress this Poor Richard’s up a bit, I create an internal bevel.  To me, an internal bevel softens the rim lines and is a classy touch.  I cut the bevel initially using a rolled piece of coarse 120 grade paper then follow with 240 and 600.  I simply pinch the rolls of sand paper under my thumb and rotate around the internal circumference of the rim.  I like it. Now, time to work on filing and sanding all the briar dust putty patches all over the stummel surface.  I use the flat needle file to work the mounds down to near the briar surface then I finish off with 240 grit paper, bringing the patch flush with the surface.  The pictures show the process.  Lots of filing and sanding! With the patches all repaired, I use sanding sponges to sand the entire stummel to remove additional nicks and scratches and to blend the patch areas.  I start with a coarse sponge, follow with a medium then light sponges. I like the way sponge sanding cleans up a rough bowl.Moving on to the micromesh stage, I wet sand the stummel with pads 1500 to 2400 then dry sand with pads 3200 to 4000 and 6000 to 12000.  I love the way the micromesh process teases out the briar grain. This Poor Richard’s is looking good! To mask the plethora of fills scattered on this Italian Poor Richard’s stummel, I will give him a dark stain.  I use Fiebing’s Dark Brown Leather Dye to do the job.  With it being an aniline based dye, later I can wipe the bowl with alcohol to blend and lighten as I choose.  I assemble the components used in applying dye on my worktable.  I mount a cork in the mortise to act as a handle and I pour the dye into a shot glass.  I use a folded pipe cleaner to apply the dye and a lit candle to flame the aniline dye.  I begin by wiping the stummel with alcohol to clean the surface.  I then warm the stummel using a hot air grain. This expands the briar grain aiding in it being more receptive to the dye.  Using the pipe cleaner, I then apply dye liberally to the entire stummel making sure to cover the rim well.  I then ‘flame’ the stummel with the lit candle and the alcohol immediately combusts leaving the pigment sealed in the grain.  After letting the stummel ‘rest’ a few minutes, I repeat the process of applying dye and flaming.  I then put the stummel aside to rest for several hours helping to assure that the dye is set and will not rub off later on hands when the pipe is put back into service.  The pictures show the process. With the flamed stummel resting, I turn again to the stem.  Using micromesh pads 1500 to 2400, I wet sand the stummel.  Following this, I dry sand using pads 3200 to 4000 and 6000 to 1200.  After each set of three micromesh pads, I apply a coat of Obsidian Oil to the stem to revitalize the vulcanite.  The stem is looking good. The stained stummel has rested for about 24 hours and it’s time to unwrap the flame crust. After mounting a 1 inch felt buffing wheel on the Dremel, I set the speed to the lowest RPM and apply the more abrasive compound, Tripoli, to remove the crust revealing the newly stained briar surface.  As I have refined my technique using the Dremel during the compound phases, I’ve learned that using a felt buffing wheel and Tripoli allows me to have more control over the degree of opaqueness allowed through the stain, especially when using darker stains like with this Poor Richard’s.  When I begin removing the crust with the felt wheel and the coarser Tripoli compound, the initial pass of the buffing process removes the top crusty layer, but thick, ‘blotched’ stain remains.  These blotches, or darker patches of stain hide the grain underneath.  After this first pass, my practice is to purge the wheel quickly on the side of the chopping board that is on my lap, providing the work platform for all the buffing.  After I purge the wheel of the thick stain residue from the flaming, I load more Tripoli to the felt wheel and then begin additional passes over the same area – frequently purging and reloading the felt wheel with Tripoli.  Through this process I can determine how the grain is presented.  More Tripoli buffing, the lighter hues are raised in the grain, giving more definition.  When I’m working an area where a patch is located, I tend to allow it to remain darker to enhance the masking.  After staining, I would say that this phase applying the Tripoli is the most critical for the finished look of the grain.  Why?  The coarse Tripoli combined with the coarser felt wheel does the heavy lifting by increasing the opaqueness of the stain when desired which sets the stage for the finished look.  The following less coarse compounds, such as Blue Diamond, and using the cotton wheel, provides more buffing of what is there rather than remove it.  The pictures below give a hint of what I’m describing.  For those who use a Dremel, I hope this is helpful. To blend the stained finish, I lightly wipe the stummel with a cotton pad wetted with alcohol.  I don’t need to lighten the stummel, only blend.After wiping down the stummel with the cotton pad, the Tripoli with felt wheel had lightened more than I wanted in order to provide a darker shading to blend and to mask the fills.  I decide to stain the stummel again, but the second time around, I use a cotton cloth buffing wheel and Tripoli instead of the more aggressive felt wheel.  Saving on pictures repeating the same process, here is the stummel after the second staining and flaming.  Again, I wait several hours allowing the stain to rest.Following the Tripoli compound, I mount another cotton cloth buffing wheel in the Dremel, increase the speed to about 40% full power, and apply Blue Diamond compound to both the stem and stummel which I reunite.  After completing the application of Blue Diamond, I wipe/buff the pipe with a felt cloth to remove the residual compound dust in preparation for the wax application.Before applying wax, I refresh the Poor Richard’s stem stamping, the interlocking ‘PR’ and the country of manufacturing stamp, ‘Italy’.  Using white acrylic paint, I use a pointed cotton tip to apply paint to the stamps.  While still wet I lightly wipe the excess paint off leaving the stamps filled.  It works well, and the Poor Richard’s is shaping up well! To finish the buffing stage, I mount another cotton cloth wheel to the Dremel, leaving the speed at 40%, and I apply carnauba wax to stem and stummel.  I follow by giving the pipe a rigorous hand buffing with a microfiber cloth.

I’m pleased with the transformation of the Poor Richard’s.  The dark brown dye helped to mask the repairs done to the stummel and it looks great.  This straight Billiard is a classic shape and as large as this Poor Richard’s is, I believe it will serve its new steward well.  Paresh commissioned him from the For ‘Pipe Dreamers’ Only! section on The Pipe Steward site.  He will have first opportunity to acquire the Poor Richard’s from the The Pipe Steward Store which benefits the Daughters of Bulgaria – helping women and girls who have been trafficked and sexually exploited.  Thanks for joining me!

Recommissioning a Hefty Ben Wade Bent Billiard Made in London England


Blog by Dal Stanton

I saw this large Ben Wade Bent Billiard on the eBay auction block a few years ago and secured it with the winning bid.  This was the first time I had acquired a Ben Wade, so my initial thought was to add it to my own collection.  I noticed that Ben Wade stamped pipes usually attracted more than usual bidding attention and so I was looking forward to restoring it and learning more about the name.  In the end, I put him in the For ‘Pipe Dreamers’ Only! section on the Pipe Steward site and this is where Paresh saw it and commissioned it to add to his collection and this benefits the Daughters of Bulgaria.  The Ben Wade, without question, fits the profile of being a ‘hefty’ pipe fitting well in the hand.  Here are some of the pictures that got Paresh’s attention: I take some additional pictures on my work table in Sofia, Bulgaria, looking at the stamping.  On the left shank is ‘Ben Wade’ in cursive script over MADE IN [over] LONDON ENGLAND.  The right shank side has 79 stamped – I’m assuming a shape number. The stem also has a BEN WADE stamp. Pipedia’s article on Ben Wade is interesting and very helpful in explaining the history.  The ‘Family Era” (1860 to 1962) is described as the ‘hay day’ of the British pipe maker:

The company was founded by Benjamin Wade in 1860 in Leeds, Yorkshire, where it was located for over a century. Ben Wade started as a pipe trader, but yet in the 1860’s he established a workshop to produce briar pipes. The pipes were made in very many standard shapes – always extensively classic and “very British”. Many models tended to be of smaller dimensions. Ben Wade offered a very high standard of craftsmanship and quality without any fills. Thus, the pipes were considered to be high grade and a major competitor to other famous English brands.

Along with most pipe manufacturers, the Second World War was a difficult time for Ben Wade.  German air raids destroyed the factory in Leeds, but the Ben Wade Co., quickly rebuilt after the war.  The Pipedia article gives several examples of the Ben Wade based in Leeds nomenclature during the Family Era (courtesy of Doug Valitchka):The ’Family Era’ ended when the business was sold in 1962:

…the owner family decided to leave pipe business and sell off the firm. The family went into negotiations with Herman G. Lane, president of Lane Ltd. in New York at about the same time as the Charatan family. Lane Ltd. bought both firms in 1962. Herman G. Lane had been Charatan’s US sole distributor since 1955 and Charatan always remained his pet child. But Ben Wade was treated in another way by its new owner. The fabrication of pipes was reduced and the factory in Leeds was closed in 1965 finally.  So this was the end of Ben Wade pipes stamped “Made in Leeds, England”.

The ‘Lane Era’ is described as a time when the historic quality of Ben Wade declined to a ‘second’ with reference to the production of standard shapes:

Alas the “new” Ben Wades were quite usual series pipes, copies of well-known standard shapes. The pipes often showed hardly masqued fillings and were processed quite coarsely with hardly polished pre-moulded Ebonite stems. Therewith Ben Wade degenerated definitively to a second brand.

According to the Pipedia article, after the death of Herman G. Lane, the business was sold to Dunhill Pipes Limited in 1978 and the new owner had no need to produce ‘seconds’ coming from the acquisition.  The Ben Wade Bent Billiard on my work table comes from the ‘Lane Era’ produced between 1965 and 1978 matching the nomenclature during this period.  “Made in London England” or just “London” replaced “Leeds” with the characteristic cursive script and ‘Ben Wade’ stem stamp (again courtesy of Doug Valitchka):I had one other question regarding the name ‘Ben Wade’ – the Danish connection? In 1971, the young, Danish pipe maker, Preben Holm, came to Lane with financial difficulties and in need of a new US distributer of his pipes made in Denmark.   The new partnership put the Ben Wade name on the Freehand production coming from the Danish factory into the burgeoning US ‘Freehand’ market with a commitment to quality rather than quantity.  The market grew through the 70s until 1985, when the market for these pipes fell resulting in the downsizing of the factory in 1986 but the production of Danish Ben Wade pipes came to an end in 1989 after the death of Preben Holm.  The Pipedia article concludes by describing the status of the Ben Wade name.  Duncan Briars purchased rights to the Ben Wade name from Dunhill Pipes in 1998 and continues to produce pipes at the same factory where Dunhill pipes are made:

The bowls are carved at the world famous 32 St. Andrews Road, Walthamstowe pipe factory, in London, England. The same factory where Dunhills are made. Every pipe is drilled spot on and exhibits a good blast and all have high quality German Vulcanite mouthpieces. Every pipe is stamped “Ben Wade, Made in London, England”. The craftsmanship and smokability have always been superb.

With a greater appreciation for the Ben Wade name, I take another look at the Ben Wade Bent Billiard on my worktable.  Even though the Pipedia article gave more of a negative view of traditional shapes of Ben Wades produced in the Lane Era, the pipe I’m looking at doesn’t reflect this.  The grain is beautiful, and I see no fills on the surface.  The chamber appears to have been cleaned and the briar surface is clean as well showing normal nicks and scratches.  The stem does have some minor oxidation and tooth dents on the button.  I also detect that there is a gap between the shank and stem – I’ll see if cleaning might correct this.  I take some close ups of these issues. To begin the cleanup of the Ben Wade, I run a pipe cleaner dipped in isopropyl 95% through the stem.  Then, along with other pipes in the queue, I put the stem in a soak of Before & After Deoxidizer to remove the oxidation.  After a few hours, I remove the stem and wipe off the raised oxidation using cotton pads and light paraffin oil – mineral oil.  I also run another pipe cleaner through the airway to remove Deoxidizer. Turning to the stummel, I remove the very light cake in the chamber. With the chamber so large, I jump to the largest blade head from the Pipnet Reaming kit.  I follow this by using the Savinelli Fitsall Pipe Tool and scraping the chamber walls further.  I finish by sanding the chamber wall using 240 grit paper wrapped around a Sharpie Pen.  To remove the carbon dust residue, I wipe the chamber with a cotton pad wetted with isopropyl 95%.  The pictures show the progress. One of the purposes of removing the old cake to bring the chamber down to the briar, is not only for a fresh start.  When the carbon is removed the chamber can be inspected for problems usually pertaining to heat fissures and potential burn throughs.  Inspecting the Ben Wade, I detect on the forward part of the chamber a sloping indentation that is a little to pronounced to ignore.  Using the Savinelli Fitsall Tool again, I scrape carbon out of the indentation to make sure I’m getting down to the briar.  This reveals the full extent of the abnormal burning.  I take pictures to show what I see, but the picture doesn’t do too well.  Changing the aperture, the picture is lightened, and I outline the perimeter of the indentation in the final picture below.  I need to address this budding burn through later after cleaning the stummel.  Next, I clean the external stummel surface using undiluted Murphy’s Oil Soap and a cotton pad.  The stummel cleans up well but reveals a tired, lackluster, thin finish. I then clean the internals of the stummel using cotton buds and pipe cleaners dipped in isopropyl 95%.  The grunge is thick, so I also employ a dental spatula to scrape the mortise walls as well as a drill bit to hand turn down the airway to excavate the old tars and oils.  To save on pipe cleaners I also utilize a long shank brush to scrub the airway.  Eventually, the tide begins to turn, and the buds and pipe cleaners are emerging less soiled.   I take a picture of the tools I use.To continue cleaning the internals, I use a kosher salt and alcohol soak.  I like to do this additional step in cleaning to further clean the tars and oils out of the internal briar and to freshen the pipe.  I use kosher salt because it doesn’t leave an aftertaste.  I stretch and twist a cotton ball to form a wick that I then insert down the mortise and airway pushing it with a straight, stiff wire.  I then fill the bowl with kosher salt and place the stummel in an egg crate to keep it stable.  With a large eyedropper, I fill the bowl with isopropyl 95% until it surfaces over the salt.  I put the stummel aside to soak for several hours.Again, I look closely at the stem that had already soaked in the Before & After Deoxidizer and I see that there remains deeper oxidation.  Instead of going directly to sanding out the oxidation, I decide to put the stem in the OxiClean bath to let it soak overnight – to see if more oxidation would be raised.  I put a small bit of petroleum jelly over the Ben Wade stem stamping and I put the stem in the OxiClean and turned out the lights.  Another day is finished.The next morning the soak had done the job. After tossing the expended salt in the waste, I wipe the chamber with paper towel and blow through the mortise to clear any residual salt crystals. I also use a long shank brush down the mortise.  To make sure the internals are clean, I finish by using a cotton bud and pipe cleaner dipped in isopropyl 95% down the mortise and airway.  They come out clean.Next, I fish the stem out of the OxiClean where it has been soaking through the night.  More oxidation has surfaced.  I begin sanding the entire stem using 240 grit paper careful to protect the Ben Wade stamping and shouldering the stem.  I focus on the bit area removing the minor tooth chatter.  Using a flat needle file, I freshen the button edges.  I follow by wet sanding with 600 grit paper and then 0000 steel wool.  The oxidation appears to be removed for the larger part except for some around the Ben Wade stamping which I won’t sand for the sake of preserving the stamp. Taking it one step further, using Before & After Fine and Extra Fine Polish, I rub each into the vulcanite in succession.  Putting some on my finger, I work the polishes into the vulcanite and let the stem sit for a time to absorb the polish.  The polishes are advertised not only to revitalize vulcanite but also to continue to remove the oxidation.  After each polish is absorbed, I then wipe the stem down with a cotton pad.  The pictures show the progress.Putting the stem aside for now, I work on the budding burn through in the chamber.  Previously, I dug out any remaining charring in the indentation.  To make sure the area is fully clear, I sand the area again and wiped the chamber with a cotton pad wetted with isopropyl 95% to clean the chamber.  As far as chamber burn throughs go, this one is minimal.  It has not progressed far and the size and the thickness of the bowl means that there was never any imminent danger.  Yet, for the long-term view and use of this beautiful Ben Wade Bent Billiard, I repair the problem where it is before it grows and becomes a worse problem.  I mix a small batch of J-B Kwik Weld on an index card.  After combining the two components, ‘Steel’ and ‘Hardener’, I have about 4 minutes to apply the mixture before it starts setting. I use a flat dental spatula as a trowel and apply the J-B Weld to the indentation in the chamber.  I put the stummel aside to allow the J-B Weld to thoroughly cure. After it cures, I use a sanding drum mounted on the Dremel to sand the excess.  I follow this using the Sharpie Pen wrapped with 240 grit paper to leave the chamber smooth and shaped. I’m pleased with the results and glad I went the extra mile to arrest the potential burn through.  Later, I’ll apply a coat of activated charcoal and sour cream mixture to the chamber wall to improve the aesthetics and to aid formation of a new protective cake. Before continuing, I reunite the stem and stummel to examine the shank junction.  Earlier I saw a gap between the shank and the stem.  Often, after cleaning these problems are resolved.  I find that this indeed was the case as the stem is now seated as it should be.  Pictures are before and after.With the stem now properly seating, I turn again to the stem and using micromesh pads 1500 to 2400 I wet sand the stem.  Following this, I dry sand using pads 3200 to 4000 and 6000 to 12000.  Following each set of three pads, I apply a coat of Obsidian Oil to revitalize the stem.  I love the glassy pop of a micromeshed stem! Turning now to the external surface of the stummel, I take a closer look at the condition of the briar.  I identify some very small fills which are solid except for one, which is pitted.  Along with normal dents and scratches from wear, there is a small skin mark on the forward outer lip of the rim.  For the pitted fill, I dig out more of the old fill with a sharp dental probe.  Since I will put clear CA glue on the pitted fill, I color the fill with a walnut dye stick to aid in blending.  I then spot drop CA glue on the area and set the stummel aside allowing the glue to cure. After a full work day, the CA glue patch I applied this morning is fully cured.  I remove the CA glue mound starting with a flat needle file.  The key is to stay on the mound and gradually bring it down close to the briar surface.  I don’t want to impact any surrounding briar.  I follow the filing by using a tightly rolled piece of 240 grit paper to bring the glue down until it’s flush with the briar surface.  My rule of thumb is to sand until I can feel no roughness.  The patch looks good – blending well with the briar.To address the rim nicks, I decide to give the rim a very light topping.  Using a chopping board as my topping board, I place a sheet of 240 grade paper on the board.  Inverting the stummel, I rotate the stummel a few times on the board to freshen the rim lines and remove the nicks.  I follow with a few rotations on 600 grade paper.  The pictures show the progress. Next, to address the briar surface, I use in succession rough, medium and light grade sanding sponges to work out the cuts and nicks in preparation for the micromesh pads.  I find that using sanding sponges on smooth briars helps clean the surface of the old, tired finish without being greatly invasive.  The sponges also smooth and soften the rim lines after the topping.  I enjoy watching the grain begin to take center stage through the process.Next, using micromesh pads 1500 to 2400 I wet sand the stummel.  I follow by dry sanding with pads 3200 to 4000 and 6000 to 12000.  I forgot to take a picture of the first set of 3 pads.  The grain is coming through nicely. Rejoining stem and stummel, I mount a 1-inch cotton cloth buffing wheel to the Dremel set at about 40% full power and apply Blue Diamond compound to the entire pipe.Before applying carnauba wax to the stem and stummel, I need to touch up the Ben Wade stem stamping with the hope there’s enough tread left in the ‘Wade’ portion of the stamp to hold the paint.  Using white acrylic paint, I apply paint over the stamping and sponge off the excess while still wet and allow the paint to dry. After dry, I gently scrape the excess with the flat edge of a toothpick.  I’m less than satisfied.  I try reapplying more paint and wiping while still wet.  After working with it for some time, I’ve come to the best I can do.  The ‘Wade’ part of the stamping simply does not have enough depth left to fully hold paint.  The picture shows my less than hoped for results. One more project to finish before the final waxing.  After completing the chamber repair using J-B Weld and sanding, to aid the aesthetics and to provide a starter layer for developing a protective cake, I mix together sour cream or natural yogurt with activated charcoal to form an application to cover the walls of the chamber.  When I first heard about this mixture from Steve on rebornpipes, I was a bit doubtful then, but no longer.  I have used this application many times and after applying and drying, the result is a very sturdy layer.  After the pipe goes into service, the only caution is when cleaning out the bowl after use do not scrape the chamber with a pipe tool.  I simply use a folded bristled pipe cleaner to scrape the wall after dumping the ash.  This has worked well for me.  I place a pipe cleaner in the draft hole to keep the airway open.  Here in Bulgaria, yogurt is very plentiful, so I scoop some natural yogurt in a small bowl and add some activated charcoal powder and mix it.  After it mixes and thickens enough so it won’t be runny, I trowel the mixture into the chamber with a pipe nail tool and spread it evenly.  After it’s distributed well, I set the stummel aside for a time to allow the charcoal/yogurt mixture to cure. After the Charcoal/Yogurt coating sets, I reunite stem and stummel.  Using the Dremel, I mount another cotton cloth wheel, leaving the speed at about 40% and apply carnauba wax.  After a few coats of wax, I give the pipe a rigorous hand buffing with a microfiber cloth to raise the shine.

This hefty Ben Wade Made in London England Bent Billiard turned out very well.  The horizontal grain on the huge stummel flows in a striking picture and is joined by large bird’s eye pools. The bowl rests very nicely in the palm and will provide its new steward with much enjoyment. Paresh commissioned this Ben Wade and will have the first opportunity to acquire it from The Pipe Steward Store.  This pipe benefits the Daughters of Bulgaria – helping women and girls who have been trafficked and sexually exploited.  Thanks for joining me!