Tag Archives: Stem repairs

Renewing and restemming a La Strada Staccato Bent Pot


Blog by Steve Laug

This tired old La Strada came to me for repairs. It was in rough shape. The stem had been gnawed, broken and gnawed again. The finish was shot and covered in oils and grease to the point that it was hard to see the rope rustication around the bowl. The bowl had a thick crumbling cake and smelled heavily or aromatics. The lava from the bowl had flowed over the top of the rim and darkened the finish there. The outer edge of the rim was heavily damaged on the front left side and looked as if the bowl had been dropped. There were dents on the underside of the bowl as well from a similar event. The shank was so dirty that the stem would not fit into the mortise. I was able to get it in but the fit was not tight against the shank. The shank is slightly off round so the stem was slightly different.la1 la2The next photo is out of focus but the road rash on the bowl bottom is visible.la3I took a series of close up photos of the bowl and rim and the stem to show the condition of the pipe when I started. In the first photo you can see the thick crumbly cake and the damage to the rim surface and edges. It was hard to tell if the inner edge of the bowl was damaged and only after reaming would I be able to know for certain. The stem was a write off as the damage was too extensive to repair. The fit against the shank also warranted a new stem.la4 la5I reamed the bowl with a PipNet reamer and went through the various cutting heads. I cleaned up the remaining cake in the bowl bottom with the Savinelli Pipe Knife. I took the cake completely out of the bowl and reamed it back to bare briar.la6I wiped down the surface of the bowl with acetone on cotton pads to remove the finish. It came off with a bit of scrubbing but there were places where it did not come off with the acetone. It would take some sanding to remove the totality of the finish.la7 la8The damage to the bowl top and outer edges required that I top the bowl. I gently topped it on the topping board so as not to remove too much and remove the smooth portion above the rope rustication on the top edge.la9I sanded the bowl and rim top with a medium and a fine grit sanding sponge and took the following photos.la10 la11I cleaned out the internals of the shank and the replacement stem that I fit to the shank with alcohol, pipe cleaners and cotton swabs. It took a lot of scrubbing to get the mortise and the airway clean in the shank. The stem was in decent shape so it did not take too much work on it.la12I took some photos of the pipe at this point to get a feel for the look with the new stem in place.la13 la14I wrapped some sandpaper around a dowel and sanded the walls and bottom of the bowl. There was a ring at the bowl bottom that was grooved and needed to be smoothed out. It did not take a lot of sanding before the inside walls were smooth.la15I restained the bowl with a dark brown aniline stain mixed 50/50 with isopropyl alcohol to approximate the original colour of the pipe and to highlight the grain on the pipe. I flamed the stain and repeated the process until the coverage was even around the bowl and rim.la16I buffed the bowl with White Diamond on the buffing wheel to even out the new finish and give it a bit of a shine. I took photos of the bowl at this point to give a clear picture of the new look.la17 la18Now all that remained was to finish the fit and polishing of the stem. I sanded it with 220 grit sandpaper until it fit the shank well. It took some adjusting of the diameter of the stem to match the slightly out of round shank. In the end it fit well. I polished the stem with micromesh sanding pads – wet sanding it with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads to give it a deep shine.la19 la20 la21I buffed the bowl and stem with Blue Diamond on the buffing wheel to polish the minute scratches on the vulcanite and on the briar. I buffed them both until the stem and briar glowed. I gave the bowl and stem multiple coats of carnauba wax. I buffed the bowl and stem with a clean buffing pad to raise the shine. I hand buffed it with a microfibre cloth to deepen the shine. The finished pipe is shown in the photos below. It is ready to go back to the pipe man who sent it to me for restemming and refurbishing. I think he will enjoy it and it will deliver a life time of good smokes to him. la22 la23 la24 la25 la26 la27 la28 la29 la30

Repairing a broken Peterson stem


Blog by Joe Mansueto

Joe Mansueto sent me this link to a helpful tutorial on how he repairs broken stems. I thought it would be helpful to post it after I just posted Dal Stanton’s stem repair piece on the blog today. Here is the original link to the Dr. Grabow Web Forum if you want to have a look at the original post and the responses there. http://drgrabows.myfreeforum.org/ftopic9615-0-asc-0.php. Here is Joe’s article.

A new friend snapped his Pete stem… glued it… dropped it… lost some pieces… This is what it looked like when it arrived for me to work on.pete1I drilled some small holes into each face to create ‘roots’ for the patch material…pete2Once the repair dried I sanded it until it was smooth. The photo below shows the stem after sanding. It came out smooth.  A bit of a buff is all that’ needed…pete3Back in service… The next photo shows the finished repair. The pipe was ready to go back to its owner for many more years of service.pete4After completing the repair I received a lot of responses and questions about how it was done and if I would make a tutorial for the above repair. The tools/supplies I used (prior to buffing) include 91% isopropyl, a Dremel (with a scribing bit), activated charcoal, and high-quality CA (cyanoacrylate). I say ‘high-quality’ because I get it from a professional wood-turner… and after using his product… the strength and speed of adhesion seems better than anything else I’ve used.

Here is the step by step process:

  1. ‘Rough up’ the faces / areas being joined. I used the scribing tool on a Dremel. This provides a rough surface for the patch material to adhere to.
  2. If you want to use the “roots” process that I’ve used, you simply use a tiny drill bit…or a tiny scribing tool to push some holes into the face…making sure you don’t drill in and back “out” again…lol.

Here is an image showing where I might drill holes. With these ‘roots’…the holes do NOT need to be directly across from the roots being drilled on the face of the other broken piece.  If I were inserting some very thin gauge wire into these roots (which would lend even more strength)…you’d have to make sure these holes lined up perfectly across from each other…and that’s a whole ‘nother tutorial! pete-jpgScrub clean the 2 faces being joined…I used the 91% iso and a toothbrush…and let it dry well.

  1. I used a pipe cleaner as you can see, to keep the 2 faces lined up. Critical to that detail is covering the pipe cleaner in ‘shiny’ scotch / packing tape…because if the patch material gets to the pipe cleaner (and it will), it won’t stick to the shiny tape. The pipe cleaner not only kept these 2 pieces lined up, but also is essentially what “held them together” in place, while the patch dried.
  2. The patch material is made from the CA and activated charcoal. I used medium viscosity CA. The mix is “close to” 50/50 between the 2…the consistency is more like molasses than honey…very thick.
  3. To begin with…I used a sharp ended toothpick to jam the patch down into each root. Then covered both faces…held onto the pipe cleaner at one end…and pushed the broken tip down onto the rest of the stem.  I made sure that they were sitting at the correct angle…then I smeared enough of the patch to be sure it was all filled / covered.
  4. Once hard (I let it sit 30 min), I filed off the excess back down near the surface of the surrounding stem…and had to add a 2nd small patch to a spot where it had caved in just slightly.
  5. Dried again…filed it down with multiple needle files.
  6. Wet sand (360, 500, 800, 1000).
  7. Buffed with Tripoli, followed by white diamond.

It is a bit of work just to save a stem…but it’s been a while, I needed the practice….and I preferred doing this instead of refitting the pipe with an aftermarket stem.

A Christmas Gift in need of a stem splice – L J Peretti Squared Shank Billiard


Blog by Dal Stanton

After a wonderful time in the US, sharing Christmas and New Year with our family, and catching up on ‘grandpa time’ with our two grandsons, my wife and I returned to Sofia, Bulgaria, to find as much snow as we left in Denver!  Two memorable ‘piping events’ transpired while in Denver.  First, the inaugural smoke of the restored 1907 McLardy Gourd Calabash (See: Link) which was filled with a tasty bowl of Dark Star recommended by Steve for the special occasion.  It was a wonderful, cool smoke.  The McLardy did admirably. per1The second ‘piping event’ was a pipe-picking expedition several of my family members (guess who this trip was for?) did to Denver’s huge Brass Armadillo Antique Mall!  We had a great time in search but unfortunately, I found no treasures to bring home.  Yet secretly, my youngest son stowed away his Christmas gift for me which I discovered under the tree a few days later!  He got a great deal and I can see why!  He knew I would have fun trying to breathe new life into the L J Peretti now before me on my work table in Sofia.  I am anxious to get back to work on a pipe and this Peretti is a great starting block for 2017!per2 per3 per4 per6 per7 per8With the obvious need to solve the issue of the broken and missing stem piece, I can easily see what attracted my son to this stummel.  The briar swirls stunningly into fire grain and very distinct and tight bird’s eye knots.  There are a few lightened fills that will need attention and the bowl has significant cake and will need to be reamed down to the fresh briar.  The rim shows some thick lava flow and has minor dents.  Unfortunately, the center swatch of the L J Peretti – Imported Briar marking on the squared shank is worn off – over achieving buffing or wear?  The Peretti ‘P’ is visible on the surviving legacy of the original saddle stem.  I’ve grown to appreciate the enduring marks of a pipe’s provenance and for this reason, this surviving piece of this pipes history needs to be protected and restored!  I’ve been thinking for some days – actually, starting with the opened gift (!) about how to splice a new piece of stem to the survivor?  I haven’t done this particular maneuver before, but I’m sure it can be done!

When I began my research on L J Peretti, I was surprised to discover that it is not an Italian pipe as one might expect with such a name!  In fact, I discovered the genesis of a significant story of Americana pipe history with the establishment of the L. J. Peretti Company of Boston in 1870 (Pipedia citing: Pipes, Artisans and Trademarks, by José Manuel Lopes), the second oldest tobacco shop in the US, second only to Iwan Ries & Co. of Chicago established in 1857 (See: Link). per9Going directly to L J Peretti’s website, now president, Stephen L. Willett provides this historical summary of this Boston icon (Link: http://www.ljperetti.com):

In 1870, Libero Joseph Peretti arrived in Boston from Lugano, Switzerland. Filled with an entrepreneurial spirit and a love for fine tobacco, L.J. established the “Peretti Cuban Cigar Co.” in Boston’s historic North End. In the first two decades of business, the company provided a number of contributions to the tobacco industry and began to blend “house cigars”.

1892 marks the establishment of the Peretti Cigar Factory in Park Square, Boston. For over forty years, the company employed fifty rollers who produced some of the finest cigars in New England. Not only did Peretti’s manufacture blended cigars, but they also created Clear Havana Vitolas such as the legendary La Mirendella.

L.J.’s son, Joseph, aka “The Major”, followed his father into the family business. His primary love was pipes and pipe tobacco. Among his notable accomplishments was the creation of the first “English” blend, called British, in the United States; as well as securing the exclusive import rights to Peterson pipes and Sullivan & Powell tobaccos.

After World War II the third generation Peretti’s, Robert, entered the firm. The original store had moved from the North End to the centre of Boston on Massachusetts Avenue and there were additional stores throughout the financial district of Boston. Robert became a tobacco legend in United States and throughout the world. Most of the more than eighty house blends of pipe tobacco were created by Robert Peretti. His reputation as a blender led politicians, actors, celebrities and gentlemen of all callings to seek his tobacco advice.

I enjoyed reading several comments after the interview of Stephen Willett on The Pipes Magazine Radio Show (See: Pipes Magazine Radio Interview) extolling the fact that tobaccos are mixed in house and one could take his pipe to their shop on 2 1/2 Park Square today, and be guided by experienced tobacconists and test several selections before making a decision to purchase.  My son and daughter-in-law, formerly of Boston, also had the opportunity to explore this historic tobacco shop!

I was still curious about the name, “Peretti”, and its Swiss (not Italian) origins with the patriarch Libero Joseph Peretti’s arrival in the US in 1870 from Lugano, Switzerland.  It did not take long to figure it out when looking at the location of Lugano on a map of Europe thanks to Google Maps.  The Italian influence would be inescapable as Lugano is situated in a slender finger of Swiss land on the southern edge of the Alps with greater topographical access to the Italian planes falling away to its south than to Switzerland proper to the north – through the Alps.  Curiosity satisfied.per10One other question hounds me – the question for each pipe: Where was this particular L J Peretti pipe made?  In Boston?  Per L J Peretti’s website, today pipes with the Peretti stamping are made exclusively by Briar Works in Nashville, TN.  This Peretti, however, predates this association.  Briar Works began operations in 2012.   One possible clue came at the close of Stephen Willett’s interview on the Pipes Magazine Radio Show in April of 2016 referenced above.  Willet was asked about relating a ‘favorite pipe story’.  Willett commented on being in London smoking pipes with a John Redman, who used to make pipes for L. J. Perretti Co.  So, a possible source.  The John Redman Ltd. and British Empire Pipe Co. is cited in Pipephil.eu listing the names produced (Aristocrat, Buckingham, Buckingham Palace, Canberra, Captain Fortune, Dr John, Golden Square, Redonian, Richmond, Smokewell, Twin Bore) but no reference to a L. J. Peretti association.  I sent an email to the L. J. Peretti Tobacconists shop in Boston regarding the provenance of this particular Peretti names-sake before me.  We’ll see if we can learn more.

I was gratified when an email arrived from the L. J. Perretti Co. Tobacconists shop in Boston a few days later.  Here is what I found:

Hello Dal,

We have been sourcing our proprietary pipes from a number of different manufacturers. That said, it is most likely that Arlington Briars made the pipe you have in your possession. Photos would help us identify the pipe further. I will have to look through some of our old content and see what I can find. Hope this helps,

Tom

LJP

Thankful to Tom for his response, I sent on photos.  Per Pipedia,

Arlington Briar Pipes Corporation was founded in 1919 in Brooklyn, New York, and produced the Arlington, Briarlee, Firethorn, Krona and Olde London brands among dozens of others, primarily acting as a subcontractor making pipes to be sold under other brand names. Among others, in the 1950’s, Arlington turned pipes for the famed Wilke Pipe Shop in New York City. The corporation was dissolved by the State of New York as inactive on December 6, 1978. 

With a greater appreciation for the pipe before me and the rich heritage of the L. J. Peretti name and company, I take another long, hard look at the surviving stem piece.  My goal is to splice the stem by cannibalizing another saddle stem.  My original idea was to see if I could find a piece of stainless steel tubing small enough to insert into the airways of both the survivor stem piece and the new cannibalized piece and connect them – providing a firm connection point and reinforcement for the splice.  Before returning to Bulgaria, I went to a specialized store in Denver with hope of finding such a tube.  They were not able to help me and indicated that I could probably find tubing like I wanted in a medical equipment context….  So, with this idea put aside, my goal is a clean bond using only superglue.  I take another picture of the surviving stem piece and the stem candidate. I want to remove the stinger and after it refuses to budge I heat it with a lighter loosening the vulcanite grip.  It joins the other retired stingers in the bottle. Using a straight edge, block and sharpie pen, I draw a line across the original stem.  It will act as a guide as I cut the vulcanite using the Dremel with a cutting blade.  Well, after starting with a cutting blade, I discovered that it was difficult to maintain control over the blade movement.  I switched to the sanding drum and that worked much better. I’ll fine tune the cut after cutting the second stem. The pictures show the progress.per11 per12 per13 per14 per15I want to cut the donor stem very close to the saddle expansion where the stem is thickest.  This hopefully will give me more wiggle room as I fashion the two stems together.  I use the Dremel blade to do a rough cut to remove the shank side of the stem.  I’ll save this piece to fabricate a breather insert later – waste not want not!  Key to this stem splice working is a proper aligning of the airways while working on shaping the external stem appearance.  Hopefully to accomplish this, to keep the airway stationary, I form a temporary insert stabilizer by cutting off the ends of a Q-tip and wrap the center plastic Q-tip tubing with scotch tape.  I do this to enlarge the circumference of the left-over Q-tip to form a tight fit as each end is inserted into the airways of the adjacent stem pieces.  It took me a few test Q-tips to get the size right.  Now I can gradually shape the external stem and keep things lined up.  In the final picture of the set below, you can see the aligning tube. The pictures show my plan materializing.  I have hope that it will work!per16 per17 per18 per19 per20Now to fine-tune the trueness of the cut stem ends.  I start with the survivor by standing it and eye-balling it next to a straight edge – not perfect!  The first picture shows the leaning tower of Pisa!  Working out of our 10th floor flat, I don’t have all the tools available to me to automate procedures so I must improvise.  I have a miter box that might do the trick.  I take a strip of 240 grit sanding paper and use the miter’s perpendicular position to create a sanding mechanism that should produce a flat, true end.  Moving the sanding paper back and forth while I manually pinch it against the triangle seems to do the job.  After patient, easy back-and-forth motion, the end of the survivor stem piece looks good!  A comparison shot to the leaning Tower of Pisa shot shows the progress.per21 per22 per23 per24The new extension also needed some fine-tuning.  Since there is a taper in the stem and therefore it’s uneven, I cannot use the miter box like before.  I use the topping board with 240 grit paper to bring the angle into proper alignment – I discover that it is not an easy slam dunk to get things right.  It takes several spins on the board following each spin by refitting the extension with the original stem and looking for the gaps between the two pieces.  I need the junction to be as true, tight, and flat as possible for a good bond and a straight stem. After several cycles, I have it about as good as its going to get.  The pictures show the process.per25 per28 per27 per26I replace the temporary Q-tip stabilizing insert with a pipe cleaner inserted through both pieces and linking them up.  The pipe cleaner will serve to keep the airway lined up during gluing as well as guard against glue possibly clogging the airway. I use a narrower, less fuzzy bristled pipe cleaner.  After testing I found that a non-bristled pipe cleaner had too much fuzz and inhibited a tight junction between the pieces.  I apply a little petroleum jelly to the section of the pipe cleaner that may meet the superglue.  This will (hopefully!) keep the pipe cleaner from sticking to the glue.  I wipe off excess jelly because I don’t want it interfering with the glue bonding.  I then apply Starbond Black Medium KE-150 glue to the original stem piece, not too thick and spread it over the junction surface with a toothpick.  My main concern is to allow the bond to settle ‘naturally’ around the airway alignment and have the stem straight.  If gaps appear I can add additional glue later as a fill.  Pulling the pipe cleaner from the shank side I draw the pieces together, align and compress for a few minutes.  I set the spliced stem aside allowing the KE-150 glue to cure.  The pictures show the progress.per29 per30 per31Turning now to the stummel, I take another close-up of the rim and chamber before starting.  I use the Pipnet reaming kit and clean out the moderately thick carbon cake formed in the chamber.  I use 3 of the 4 blades available to me to remove the harder than usual cake.  After the Pipnet blades, I fine tune the chamber surface with the Savinelli pipe knife and then, using my finger and a dowel rod, I sand the internal chamber wall with 240 grit paper.  Finally, I wipe the bowl out with a cotton pad dampened with isopropyl 95%.  The chamber wall looks good – no problems there.per32 per33 per34per35Before cleaning the rim and stummel externals, I take Q-tips and pipe cleaners with isopropyl 95% to clean the internals of the stummel.  Following this, I use Murphy’s Oil Soap undiluted with cotton pads and scrub the rim and surface.  The lava build up on the rim proved to be resistant so I added use of the brass brush to the cleaning job.  The inner rim appears to have burn marks on the front and back of the bowl.  I’ll remove this damage by cutting an inner rim bevel later.  The pictures show the cleaning progress.per36 per37After rejoining the curing spliced stem to the stummel to avoid creating shank shoulders, I take a medium grade sanding sponge and sand the entire stummel surface and rim, avoiding the shank panel containing the L J Peretti stamping.  I follow this with the same regimen using a light grade sanding sponge.  With the sanding sponges, I’m removing small pitting and imperfections from the briar surface.  To clean up the rim further, I cut an initial bevel on the inner rim first using a tightly rolled piece of 120 grade paper.  I follow this using 240 grit then 600.  I closely examine the surface and the sponge sanding did the job so that I did not need to use any super glue for fills. I did use the stain marker and darken fills that had lightened.  The pictures show the initial stummel prep.per38 per40 per39 per41I’m anxious to return to the stem repair to begin the ‘sculpting’ process.  I’m sure that the donor stem that I’m using isn’t the best candidate for a match, but it is the only other saddle stem I have that isn’t already claimed by a stummel here in Bulgaria.  Oh my – it reminds me that I just saw lots of 100 stems being auctioned on eBay!  If only….  I take a few pictures of the spliced stem before I begin. To do the sculpting I use my Dremel high-speed rotary tool and mount the drum sanding tool.  With the Dremel speed set on 2 of 5 (1 being the slowest RPMs) I gently and patiently begin removing vulcanite and shape the stem to give it a uniform look.  The pictures show the progress until…per42 per43…You’ve heard me say before, “As they say, it was going so well until it wasn’t.”  The new superglue bond between the two stem parts simply gave way.  I sat back in my chair looking at the divide and contemplated a visit to my favorite adult beverage.  Before starting this project, I researched through the blogs looking for different approaches and techniques to this specific genre of stem repair – splicing.  Steve has a very helpful Reborn essay, What are the options for repairing a damaged stem?  I could not find anything with the specifics I was facing.  Now with the two pieces before me, I decide to shoot an ‘SOS’ to Steve, even though I know he’s somewhere in the world traveling with his work.  I press the send button, turn off the light,  and head to bed!per44Gratefully, Steve’s reply arrived the next morning referencing another Reborn Pipes contributor, Jacek A. Rochacki, from Poland.  Steve’s email described Jacek’s technique of creating a simple interlocking step between the two stem pieces by filing 90 degree angles out of the upper half of one piece and a corresponding 90 degree angle out of the lower half of the other piece.  Essentially creating a juxtaposed and flipped ‘L’ on each stem piece.  The step will provide more area for the glue to bond as well as distribute the stummel’s weight across the stem rather than at one tension point.  The science behind the technique sounds good, now I need to bring the theory into physical reality!  I decide to use the width of a flat needle file to determine the steps’ widths.  Starting with surviving stem, I score a line to provide a guide for the edge of the step (first picture).  After this, I wedge the stem piece in the miter box and invert the flat needle file and use it as a saw to cut a straight vertical incision half-way into the stem.  Pictures 2 and 3 show this in progress.  I use the Dremel to gradually remove the vulcanite and finish the fine-tuning with the needle file.  The pictures show the progress.per45 per46 per47 per48The other stem piece follows the same protocol.  The whole process took quite a bit of time filing, eye-balling, test fitting and filing again.  The junction I have is not a perfect fit.  Dealing with the odd matching stem pieces presents its own challenges.  The key as before, is to align the airway holes to have as much as possible a seamless airflow.  The final picture in the set below shows the pipe cleaner inserted through the pieces and mimics the natural alignment before bonding with superglue.  In this position, to test the freedom of the pipe cleaner to move, I compressed the pieces at the ‘step junction’ and then pulled the pipe cleaner back and forth to assure as much as possible a good alignment.  The pictures tell the story.per49 per50 per51 per52As before, I use a bristled pipe cleaner with less fuzz, apply petroleum jelly to the pipe cleaner to avoid sticking to the glue, and apply Black KE-150 Glue to the step surfaces. I pull the pipe cleaner from the shank-side to draw the stem pieces together to allow a natural placement favoring a clear airway.  Once the steps fully engage, I compress the steps together to form the bond.  While I apply this pressure, I also give a little pull on the pipe cleaner to assure that it is still moving freely and not crimped at the splice junction.  After curing for 24 hours, I inspect the junction lines and apply additional KE-150 glue where needed to seal the joint.per53-copy per54With the stem splice curing, I turn my attention to the stummel.  Staying clear of the L J Peretti nomenclature on the left shank panel, using micromesh pads 1500 to 2400 I wet sand the stummel.  Following this, I dry sand the stummel using micromesh pads 3200 to 4000 then again with pads 6000 to 12000.  The depth of the briar grain looks good.  The pictures show the progress.per55per56per57I like very much the lighter brown, butterscotch tones of the briar.  I decide to apply a very light stain made up of one part Fiebing’s Light Brown Leather Dye to 4 parts isopropyl 95%.  My desire is to blend the fills on the bowl even though I had already applied stain sticks to these areas.  Using a pipe cleaner folded I apply a generous coat of the dye mixture, making sure to cover the entire stummel.  After applying the dye, while still wet I fire the dye with a lit candle.  This sets the hue of the dye well in the grain.  After a few minutes, I repeat the process concluding with firing the wet dye.  The alcohol in the dye burns off quickly and normally this does not burn the wood.  I did scorch the wood of the rim of a restoration not long ago.  I concluded that the problem was the cork that I had inserted in the bowl to manipulate the stummel while staining – the cork itself was saturated with the alcohol and kept ‘firing’ and scorched the thin wood of the rim…. Ever learning!  Now, I hold the stummel by inserting a couple twisted pipe cleaners in the shank acting as a handle.  The picture shows the final state after the second application of stain.per58I set the stummel aside to allow it to ‘rest’ through the night.  The next day, I’m looking at the stummel and the spliced stem.  I decide to jump into the stem work.  Honestly, as I look at the stem, the word that comes to mind is ‘Frankenstem’.  The stem that I cannibalized was not the best match to begin with.  Changing the positioning of the stem pieces to give the ‘step splice technique’ a chance of working, left a spliced stem with a definite limp.  Yet, I’m not finished and I’ve discovered along the way, there is a lot of forgiveness and flexibility in working with vulcanite.  As the old Timex commercial assured, “Takes a lick’n and keeps on tick’n!”  That will be my mindset as I approach the Frankenstem!  I take some pictures to show the challenges.  The first picture, perspective from the top looking down, shows the greatest challenges.  The stem addition is offset revealing the original stem’s protrusion underneath.  There is also more taper in the stem addition than in the original stem.  My approach as I look at the stem will be to try to create a higher (toward the shank) taper on the original stem (on the lower side in the picture).  This hopefully will blend the mismatch.per59I decide to chronicle the approach I take.  I first work on the ‘straight’ side of the stem (lower) by using a rounded needle file to create a ‘dimple’ that would represent the deepest part of the tapered curve.  It was adjacent to the protrusion on the right side (above in the picture below).  After creating the dimple, I then gradually fan out the dimple with 240 grit sanding paper until I achieve a smooth taper joining the saddle with the button.  I’m pleased with the results of phase 1.per60Phase 2 is creating another dimple on the other side – right at the point of the protrusion sticking out from underneath from the original stem step (pictured better above).  Again, after the dimple is formed with the rounded needle file I use 240 grit sanding paper to fan the taper evenly throughout the stem.  While the stem still is off center a bit, the tapering gives the allusion of a straighter stem.  It seems to me the stem is resembling a fishtail style reminiscent of Stanwell pipes.per61Next, I sanded the upper and lower stem with 240 grit paper to smooth and blend the splice repair.  This is helpful because it enables me to see that there are gaps in the seams of the patch.  In the pictures below you can see the vulcanite dust from sanding lodged in the gaps.  I decide to apply a bit of the Black Medium KE-150 glue to fill the gaps.  Before I do, I wash the stem with water and a bit of dish soap.  I apply the KE-150 then spray the joint with an accelerator that I just brought back to Bulgaria from my time in the US for Christmas. per62per63Putting the stem on the sidelines to cure a bit, I’m anxious to ‘unwrap’ the stummel and look at the briar underneath the fired dye crust.  I take the Dremel and mount a felt wheel and using Tripoli compound, I apply the compound using the slowest speed available on the Dremel.  For detailed ‘how tos’ in using a Dremel for this process, see my essay on Dremel Polishing Technique.  After I finish the cycle with the Tripoli compound, I wipe the bowl lightly with a cotton pad and isopropyl 95% to blend the stain.  After the Tripoli, I change to the Blue Diamond compound felt wheel at the same RPMs and apply Blue Diamond.  Then I take a clean cotton cloth and give the stummel a rubdown removing the excess compound residues which is like powder.  The stummel is looking great even before the carnauba wax application, but I decide to delay the wax application and again turn back to the stem.

To see the big picture, I unite the spliced stem with the stummel.  I like the proportions.  I was concerned that the stem might end up being too short and the L J Perretti becoming a nose warmer.  This is not the case as the picture shows!per64Accelerator is God’s gift to the impatient!  My first time to use it and it is nice – though I understand the downside of using an accelerator is the potential of a weaker bond, at least as I have read. The Black K-150 glue looks good.  I return to sanding the stem to blend the patch and finish the shaping.  With 240 grit paper, I smooth out the superglue fill and even though I can still see the lines, the touch test is the goal.  I can feel no ridge at the junction seams.  Success!  With all this rigorous sanding, the verdict is in – the step splice technique is holding!  I continue sanding moving down the stem removing the sand marks left by the Dremel drum sanding wheel.  I finally arrive at the button and to lower lip is out of line.  I straighten this with a flat needle file and I freshen the button lines while I’m at it.  I use 240 grit paper again to remove the effects of the needle file use in the button area.  Finished with the 240 grit paper, I use 600 grit paper to smooth the stem more and to reveal nicks or gouges that may have been missed.  The last two pictures below show the finished shaping project.  I’m very pleased with the results – the splice is holding well and the newly shaped stem is passable.  Even though the splice seams are visible, they are smooth to the touch and I’m hopeful that as the stem polishing and waxing is completed, the seams will blend more.  I think Frankenstem has been transformed well.  Before bringing out the micromesh pads on the stem, I drop the newly spliced stem into the Oxi-Clean bath to raise the heavy oxidation left in the original stem piece.  Another day is finished. per65 per66 per67The next morning I fish the soaking stem out of the Oxi-Clean bath.  The oxidation has surfaced, and as expected, especially on the original stem piece.  Initially I use 600 grit paper and wet sand the stem removing the top layer of oxidation.  I use a topping board with 600 grit paper to make quick work of 3 of the 4 panels of the saddle stem block (not sure if there is a special name for this part of the stem).  I am careful to protect the Perretti ‘P’ on the other panel by putting my thumb over it as I sanded around it.  I repeated the process using 0000 steel wool.  As always, the most difficult part to rid of oxidation were the vertical ‘rise panels’ above and below the stem.  I’m satisfied with the progress the pictures show.per68 per69 per71 per72With the new day, I’m in the home-stretch!  With so much focus on the stem repair, I only now recall that I have not cleaned the internals of the now spliced stem.  Using pipe cleaners dipped in isopropyl 95% I work on cleaning the internals. After running 2 pipe cleaners through the airway, for a nice change, I discover that all is clean!per73I turn now to the micromesh cycles with the stem.  Beginning with pads 1500 to 2400 I wet sand the stem and follow the set with an application of Obsidian Oil over the stem.  Next, I dry sand using pads 3200 to 4000 followed by 6000 to 12000, following each set with a fresh application of Obsidian Oil. I’m generally pleased with the technique of this splice, but the fine polishing of the two pieces of vulcanite have revealed that not all vulcanite is the same.  I assume the original survivor piece was of better quality than the donor piece.  The polishing reveals that the original is a darker hue of black and it wasn’t evident only until now.  So, we do the best we can with what we have!  The pictures reveal this with a close look.  The stem still looks good and what I’ve been through with it make it even look better!  The pictures show the progress. per74per75per76Before rejoining stummel and stem to apply carnauba wax, I want to re-establish the Perretti ‘P’ stamping on the stem.  Checking with the L. J. Perretti Co. stampings on Pipephil.eu, most stem marks are set with white lettering.  I want to do the same to emulate how this Perretti most likely was commissioned.  Taking white acrylic paint, I dab a bit over the ‘P’ on the stem.  After an hour or so, after dried, I gently scrape the top layer of paint off with a pointed Q-tip which I picked up in the US at Hobby Lobby.  Pictures show the result.per77 per78 per79Rejoining stem and stummel, I apply several coats of carnauba wax to both.  I use a cotton cloth wheel mounted on the Dremel, increase the speed to a setting of 2 and apply the wax moving the wheel in a circular motion over the surface.  After completing the carnauba wax application, I mount a clean cotton cloth wheel on the Dremel and clean buff the stummel and stem.  Following this, I give the entire pipe a hand buffing with microfiber cloth to bring out the luster and depth of the grain even more.

The briar of this L J Perretti is unbelievable – a beautiful display of fire grain and very clear and distinct bird’s eye.  The stem isn’t a perfect rendition mainly because of the unmatched vulcanite creating the splice.  Yet, the ‘step’ technique Jacek provided (via Steve!) is working very well.  The squared shank transitioning into the tapered fishtail-like stem I think is very nice. It works.  I’m thankful to my son for gifting me with this L J Perretti!  I would have enjoyed my inaugural smoke to have been a bowl of a special hand blended mixture from the L. J. Perretti Co. Tobacconists in Boston!  Yet, after taking the presentation pictures following, I settled for a bowl of my favorite Cavendish blend – Lane BCA. Report?  The L J Perretti smoked very well, indeed.  Thanks for joining me!per80 per81 per82 per83 per84 per85 per86 per87 per88

Great Grain – a Triangle Shank Grabow Westbrook Billiard


Blog by Steve Laug

Wikus asked me in a comment on the blog I wrote on the KBB Yello-Bole Churchwarden why I don’t give the pipe a coat of either varnish or shellac after I have refinished them. I wrote a response in which I said I don’t like that finish and want the pipe to be able to breathe. I have found that the varnished bowls get hot when smoked so that is another reason. But probably the biggest reason is that I really like a more matte finish instead of the high gloss that some like. I have to be honest – to me the matte finish that lets the grain pop and hides nothing behind the shine really is my preference. It does not mean I don’t like a shine but rather that I like the shine of a good wax and buff over the other options.

The pipe I worked on next is a prime example of what lies beneath the varnish coat. This one is a unique (at least to me as I have not seen one before) triangular shank billiard made by Dr. Grabow. It is stamped on the left side of the shank WESTBROOK over Dr. Grabow (the bottom edge of the lower stamp is faint as it is very close to the ridge on the angle of the side). It is stamped on the right side Imported Briar (faint stamp) over Adjustomatic in script. Underneath both lines it reads PAT.2461905. My brother picked this one up because the grain and shape caught his attention. He took the following photos before he cleaned it up.grab1 grab1aFrom the above photos you can get a general idea of the shape and condition of the pipe. It is sound and has no cracks or burns on the surface. The finish is pretty well shot – the varnish is crackled and checked looking on the sides of the bowl and shank. The overall look is cloudy and muddied by the varnish going. There is a pretty thick cake in the bowl and it overflows onto the rim top. The bowl however appears to still be in round both on the inner and outer edges as far as can be seen in the slightly out of focus third photo. The stem looks good at this point with light oxidation and some tooth chatter and marks on the topside near the button. The orange Grabow spade logo is in place on the left side of the stem. More will be revealed through his close up photos.

The first photo shows the rim condition up close. My initial observation about the edges need to be modified somewhat. The inner edge looks good but it will be better determined once the thick and uneven cake is removed from the bowl (good news is that this one must have been a good smoker to have developed this kind of cake). The outer edge looks good other than some slight damage to the front right side where there appears to be a chip and some wearing.grab2The next close up photos show the stamping and stem logo. I have recorded the condition and content of the stamping above. I include these for you to see the overall condition of them and the finish on the shank and stem.grab3The last photos he included show the condition of the stem. There is a visible line that covers the separates the first inch of the stem from the rest which looks to me that the stem had a Softee bit on it for most of its life. There is tooth chatter on both sides of the stem and on the top side (second photo below) there are visible tooth marks that need to be dealt with. This is why I think the bit protector came after the initial tooth marks or they would have been far worse. On the underside of the stem there is a small tooth mark that is quite deep. Both sides will need some work to smooth out the damage.grab4I did a US Patent search to see what I could find out about the patent number on the side of the shank. I was able to find out that the patent was filed on Jan. 25, 1946 but was not issues until February 15, 1949. I learned that the inventor of the Adjustomatic system for Grabow was D.P. Lavietes. I know nothing about him but I do know that Dr. Grabow used the mechanism in their pipes. With this information I know that the pipe was made after 1949 because the patent stamp says that the mechanism is patented not patent applied for. I have included the entire patent below for those who may be interested. I enjoy the descriptions, rationale and drawings that the inventor includes in these old patents. They are a pleasure for me to read through them. If you want you can skip over the next four photos and read about the pipe’s restoration.grab5 grab6 grab7 grab8My brother did his usual thorough cleaning of the pipe. He reamed the bowl and cleaned the internals of the shank, mortise and stem with alcohol, cotton swabs and pipe cleaners. He scrubbed the rim and was able to remove all of the tars and oils that had built up there. He cleaned the exterior of the bowl and stem with Murphy’s Oil Soap to remove the grime and build up in those areas. When I received the pipe in Vancouver it was clean. The only thing that he had not been able to do was remove the stinger from the threaded tenon to clean behind it. The next four photos give a clear picture of what the pipe looked like when it arrived.grab9 grab10The close up photo below shows how well the rim and bowl cleaned up. The inner rim was in pretty decent shape other than a little burn on the front edge almost in line with the chip on the outer edge.grab11The stem was in better condition than I expected as in the cleaning process a lot of the chatter seems to have been removed with the calcification.grab12I took photos of the condition of the stinger apparatus because it was looking really good. In the past when I got these they were black and looked awful. They were bad enough that if I did not like stingers before, the general grime and grit would have sealed the deal. This one however was sparkling.grab13I heated the stinger with a Bic lighter and the tars that held in the tenon released it. With the stinger removed I was able to clean out the buildup behind it in the stem. I used pipe cleaners, cotton swabs and alcohol to clean out that area of the stem. I cleaned out any remaining debris in the mortise at the same time.grab14I sanded the tooth marks and the rest of the stem to deal with the oxidation using a folded piece of 220 grit sandpaper. The tooth marks came out of the top side of the stem with no problem. There was still one small almost pin hole tooth mark on the underside that I would need to deal with and repair. I cleaned the surface of the stem with alcohol and filled in the mark with clear super glue. Once it dried I sanded it with 220 grit sandpaper to blend it in with the rest of the stem surface.grab15 grab15aI buffed the stem with Red Tripoli on the buffing wheel and brought it back to the work table to polish it with micromesh sanding pads. I wet sanded it with 1500-2400 grit pads and dry sanded it with 3200-12000 grit pads. After each set of three pads I rubbed it down with Obsidian Oil. After the last pad I gave it a final coat of oil and set it aside to dry.grab15b grab15cAfter polishing with the 1500-2400 grit pads I wiped down the tenon with an alcohol wet cotton pad to remove some of the darkening in the threads. In doing so I got some alcohol on the end of the stem and it brought out a bit more oxidation to the surface. This is one of those frustrations but also a good thing as I was able to then back track and sand the stem again with 1500-4000 grit pads and then buff it with some Blue Diamond on the wheel and I removed the rest of the oxidation. I then went back to polishing the stem with 6000-12000 grit pads to bring the shine to the surface.grab15dWith the stem polishing done I set it aside and turned to the bowl. I examined it and decided that the best way to deal with the crackling varnish coat was to remove it. My choice for removing varnish coats is to scrub the finish with acetone on a cotton pad until it is gone. The first wipes will leave the surface gummy and rough. You have to scrub the surface until it is smooth to touch. The next four photos show the bowl with the crackled finish.grab16 grab17It took four cotton pads and acetone to remove this crackled varnish finish. Underneath the cloudy varnish coat there was some really stunning grain.grab18 grab19Once the finish was gone and I had wiped the pipe with a paper towel with a little bit of olive oil I took photos of the pipe. There was some scratching in the briar that would need to be polished and there were some nicks that would need to be lifted if they did not polish out but the overall appearance of the pipe was stunning.grab20 grab21I worked on the bevel of the inner edge to smooth out and remove the damage on the front side. I used 180 grit and 220 grit sandpaper to bevel the rim a little to accommodate the edge damage. I polished the briar on the rim with 2400 grit micromesh sanding pads to remove the scratching left behind by the beveling. I polished the bowl and rim with 3200-12000 grit micromesh sanding pads to raise a shine in the briar and make the grain stand out.grab22 grab23I put the stem and bowl back together again and buffed the pipe with Blue Diamond on the wheel to further polish it. I gave the bowl and stem multiple coats of carnauba wax to protect it and buffed it with a clean buffing pad to raise the shine. I hand buffed it with a microfibre cloth to deepen the shine. The finished pipe is shown in the photos below. It has come a long way from the worn and tired pipe that came to my brother in Idaho. The depth of the shine, the look of the grain and the flow of the pipe all work together to make this a beautiful Dr. Grabow pipe. It is one of the earliest pipes of the RJ Reynolds era. It was a fun pipe to work on and the results just multiplied as each step I took in the cleaning and polishing process brought more of the beauty of this piece of briar alive. Thanks for looking.grab24 grab25 grab26 grab27 grab28 grab29 grab30 grab31

Restoring Another Unique Windy Perpetual Drysmoker


Blog by Steve Laug

Today I have been working on the second Windy Perpetual Dry Smoker that has come across my work table. The first was a gift from Troy who writes here on rebornpipes. I have written the description of the restoration on a previous blog. You can read about the cleanup and restoration on that blog: https://rebornpipes.com/tag/windy-perpetual-drysmoker-pipe/ . In that blog I did some research on the brand, as prior to the first pipe I was gifted I had never heard of or seen one of these pipes. I decided to repeat a portion of that first blog here to give some background on the brand.

Here is the link to one of my favourite informational sites on metal and unique system style wooden pipes. The link will take you to the article as a whole and some photos that show the pipe quite well: http://www.smokingmetal.co.uk/pipe.php?page=508

“WINDY PERPETUAL DRYSMOKER by Stan Wolcott”

“In my travels I recently came across this intriguing pipe on which very little information appears online by Google search. The left side (?) is stamped “Windy Perpetual Drysmoker” and on the right side (?) “Imported Briar/Italy”. The stem has a small round gold medallion on the left side bearing an “R”. Although several similar pipes are pictured online here in the USA and UK, no explanatory information is included with those images. Floyd Norwood of Tennessee, who restored the pipe for me, also had no idea how the pipe was to be smoked. Tony Pringle of the UK, who has one pictured on his website, believes there may be other pieces which are missing from the four present in the images—flat cap, rounded cap with five vent holes (presumably the wind cap) and the pipe bowl and stem. As can be seen from the images, the flat cap has female threads and screws into the bottom (?) onto male threads on the bowl. The wind cap has male threads and screws into the top (?) of the bowl. I have placed the question marks in parentheses following the terms top, bottom, right and left, since I’m not even sure whether the flat cap is intended to be the bottom. Can someone out there enlighten me and the NASPC readership about this “mystery pipe”, its manufacturer and the proper way of smoking it?”

“The “Perpetual” part of the name seems to come from the ability to actually load more tobacco from the bottom of the pipe whilst still alight and of course the dottle etc. gets burnt as the smoking progresses. Rather ingenious. There are at least two possible for makers from the logo, REGIS and EMPIRE STATE and nothing seems to be known of these either.

Tony Pringle of smokingmetal then includes the following photos of the pipe. There is no doubt that it is the same pipe that I have. There are a few variations between the two but the overall design is the same. He shows photos of the pipe as a whole, taken apart and of the stamping.dry1I have only included the first photos as the pipe I have is virtually identical to this one. Mine also has the gold circle R on the logo on the side of the stem. The only difference is that mine is has a brass spacer on the stem that forms a thin band between the shank and stem. Mine is also in better condition than the one in the photos with no cracks or breaks in the bowl, caps or threads. I believe along with Tony from smokingmetal that the pipe was crafted in the late 1940s. Many things about the briar quality, the rubber that is used in the stem etc. point to manufacture of the pipe occurring during or after the conclusion of World War II.

The stamping on the one above and the one I have is simply WINDY over PERPETUAL over DRYSMOKER in caps on what is the left side of the shank. On the right side of shank it is stamped Imported Briar over Italy. The pipe is meant to be smoked with the perforated, rounded cape pointing downward. That is why the stamping is the way it is. If the pipe is held otherwise the stamping is upside down. If the pipe is inverted it can be set upright on a desk or table on the flat top cap and act as a sitter pipe. The pipe is 5 ¼ inches from the front of the bowl to end of bit. The diameter of the outer bowl is 1 3/8 inches. The chamber diameter is just over 5/8 inch and depth is over 1 ¼ inches with both the top and bottom cap removed. The pipe is lit from the bottom and the wind cap cover is screwed in place. I think that more tobacco can be fed in from the top of the bowl with the flat cap removed thus making the pipe a PERPETUAL DRYSMOKER.

The pipe my brother Jeff picked up is shown in the next photos that he took of it before cleaning it and sending it to me in Vancouver. You can see some darkening in the finish around the flat cap on the bowl and some general wear and tear to the finish as a whole. The bowl has quite a few fills in the shank, the left and right front sides and the crowned perforated bottom cap. The stem was oxidized quite heavily and the diameter of the shank and the diameter of the stem did not match.dry2Jeff took some great photos of the bowl taken apart. Contrary to what Tony and Stan mention in the quote article from the website all the parts are present with the pipe. There are no additional pieces needed to make the pipe functional. The first two photos show the rounded bottom cap and the flat top cap removed from the bowl. You can see the wooden threads on the inside of the bowl in the first photo where the bottom cap screwed into it. The second photo shows the threads on the outside of the bowl where the flat top cap screwed onto it. The completed pipe resembled a salt or pepper shaker to my mind – a unique and interesting smoking device. Both caps were darkened by smoking but appeared to be clean. There was a small crack in the rounded bottom cap but it did no effect the fit in the bowl.dry3He also took some photos with the parts laid out together to give an overall idea of what the pipe looked like.dry4My brother also included some close up photos of the sides of the bowl to show the condition of the finish and what would need to be done to clean it up. He included a photo of the flat top cap to show the remarkable grain underneath the staining and grime.dry5 dry6The next two photos show the stamping on both sides of the shank. The third photo shows the brass circle R logo on the stem and also the brass spacer in between the stem and the shank.dry7 dry8The final two photos Jeff included showed me the condition of the stem. It looked really good other than the oxidation. There was no tooth chatter or tooth marks in the surface. The only issue I would need to address was the mismatched diameter of the shank and the stem.dry9My brother did a really thorough job cleaning up this old pipe. When it arrived in Canada the inside of the bowl and both caps was really clean. He had scraped out the light cake in the bowl and cleaned out the mortise and airway in the stem and shank with alcohol, cotton swabs and pipe cleaners. He cleaned off the exterior of the bowl and was able to remove much of the grime on the surface. The brass space was oxidized but would clean up easily when I worked on the diameter of the stem. I took the next four photos to show the condition I found the pipe in when I unpacked it here in Vancouver.dry10 dry11I took the pipe apart and took photos of the parts of the bowl – the centre core, the rounded bottom cap and the flat top cap. In the photos the core is flat side up in the first one and rounded side up in the second one. The bowl and caps were very clean and you could see raw briar inside all of the parts which led me to think that the pipe had not been smoked often.dry12I took some close up photos of the stem to record its condition as well.dry13The fit of the crowned bottom cap to the edge of the core part of the pipe had some damage to it that did not allow the cap to seat tightly against the edge of the core. I topped it with 220 grit sandpaper on the topping board until the cap fit snugly.dry14I put the cap back in place and wiped the bowl down with acetone on cotton pads to remove the finish. The fills on the bowl were dimpled so they would need to be repaired with briar dust and super glue.dry15 dry16With the finish removed I could better assess the darkened areas around the sides and bottom of the flat cap. I could also see areas that needed to be sanded around the edges of the rounded bottom cap also. I sanded the entire pipe with 220 grit sandpaper to remove the damaged areas and smooth out the transitions between the core and the caps. I also smoothed out the edges of the fills to prepare them for repair later in the process.dry17 dry18With that part finished I needed to rework the shank/stem diameter. The right side of the shank was narrower than the right side of the stem. With the stem removed it was easy to see why. That side of the briar shank was thinner in terms of the thickness of the walls of the shank than the left side. The red circle shows the side that needed to be taken down.dry19I used the Dremel with a sanding drum to take down the excess vulcanite and brass of the spacer.dry20I cleaned out the areas around the fills and removed any of the loose debris around them. I rebuilt the areas around the fills with a mixture of clear super glue and briar dust. I overfilled the repairs to allow for shrinkage. I sanded the repairs smooth to match the surface of the bowl.dry21I sanded the repairs smooth and then polished the areas with micromesh sanding pads. I wet sanded the repaired areas with 1500-2400 grit sanding pads and dry sanded them with 3200-12000 grit pads. I wiped the bowl down with a damp cloth. I stained the bowl and the caps with dark brown aniline stain and flamed it to set it. I repeated the process until the coverage was even.dry22 dry23I buffed the bowl with Blue Diamond polish on the buffing pen. I gave it several coats of carnauba wax and buffed it to a shine.dry24 dry25I sanded the stem with 220 grit sandpaper to smooth out the scratch marks on the vulcanite. I polished it with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I rubbed the stem down with Obsidian Oil after each set of three pads. After the final coat of oil I set it aside to dry.dry26 dry27 dry28I buffed the pipe with Blue Diamond once more and then gave the bowl and stem multiple coats of carnauba wax. I buffed it with a clean buffing pad to polish it and then by hand with a microfibre cloth to deepen the shine. The finished pipe is shown in the photos below. Some of the character marks of the pipe that came to me still show and I am sure could tell a story if they were able to speak. I like the finished look – the marks and all give the pipe a sense of history and time. It is not a bad looking old pipe considering that it has traveled from the 1940s into 2016 and who knows how much longer. Thanks for looking.dry29 dry30 dry31 dry32 dry33 dry34 dry35 dry36

Refreshing Another Giant – a KBB Yello-Bole Imperial 3068C Bent Billiard


Blog by Steve Laug

When I cleaned up a previous KBB Yello-Bole Imperial 3068C for a reader of the blog my brother immediately was struck by the beauty of the old pipe. He decided he would find one for me that matched the one I cleaned up for the reader. If you want to read about the cleanup of that one here is the link: https://rebornpipes.com/2016/11/10/breathing-life-into-a-huge-kbb-yello-bole-3068c-bent-billiard/. The 3068C is a large pipe. It is reminiscent of the WDC Wellington in many ways but to me there is a simple elegance to the lines of the 3068C that are more smooth and beautiful. This is another giant pipe. The dimensions are: length 10 inches, height 2 ¼ inches, outer diameter of the bowl 1 ½ inches, inner bowl diameter 7/8 inches. I took a photo of the pipe in hand to give an idea of the size of this old giant.imp1As opposed to the other 3068C I cleaned up this one was in remarkably good shape. The shiny varnish coat actually was perfect with no peeling or nicks in it. The grain shone through and was a great mixture of birds-eye and cross grain. The Yello-Bole Honey Cured coating still showed on the bevel of the inner rim and in parts of the bowl. The rim surface had some very small dents or scratches in it but they did not seem to break the finish on the bowl. There was a light cake in the bowl. The nickel ferrule was oxidized and lightly scratches but otherwise undamaged. The stem had the classic older Yello-Bole circle on the top of the stem just behind the saddle and was lightly oxidized with minimal tooth chatter on the top and underside of the stem at the button.imp2 imp3My brother took the above photos and the ones that follow to show the overall condition of the pipe. The next two close up photos show the rim top and inner rim bevel. The Yello-Bole Honey Cured coating can be seen on the edge of the bowl and going down into the bowl. You can also see the small dents in the rim and the light grime that had built up on the surface of the rim.imp4The next two photos give a good idea of the grain that shone through on this old pipe. The front and back of the bowl has some amazing birds-eye grain and the sides, rim and bottom show some really nice cross grain.imp5The stamping on the shank was sharp and readable. The left side bore the KBB cloverleaf logo with Yello-Bole over stamping that read Reg.U.S.Pat.Off. Beneath that was the line stamping in script Imperial. Finally underneath all of that was stamped Cured with Real Honey. On the aluminum ferrule cap there was a remnant of the KB&B cloverleaf. It is interesting to me that while all Yello-Bole pipes are stamped with KBB (minus the ampersand &) in a cloverleaf on the shank both this pipe and the previous one had the KB&B cloverleaf on the ferrule. I wonder if the company made one size fits all with the ferrules and used them on both Yello-Boles and KB&B pipes. The right side of the shank is stamped Real Bruyere over the shape number 3068C.imp6The final two photos that my brother included show the tooth marks and chatter on the top and underside of the vulcanite stem at the button. The mild oxidation is also visible in the photos.imp7My brother did the necessary cleaning on the pipe – reaming and cleaning out the mortise and the airway in the stem and shank. I cleaned off the grime on the finish and wiped down the stem. When I received the pipe it looked be in excellent condition and would not take a lot of work to refresh it. I took the next four photos to show what it looked like when it arrived in Vancouver.imp8 imp9I took some close up photos of the rim and the stem to show the condition. The rim was in excellent shape and Jeff was able to clean up the inner bevel on the rim to reveal the Yello-Bole Honey Coating. The stem photos show the oxidation and the small tooth marks and chatter on both sides of the stem near the button.imp10 imp11I sanded the oxidation on the stem with 220 grit sandpaper to remove the brown topcoat that it had and also worked over the tooth chatter and tooth marks on both sides.imp12I used drops of medium viscosity black super glue to fill in the small tooth marks on both sides of the stem. They are shown in the photos below. The small black spots are the super glue repairs to the stem surface. You will note that there were more issues on the underside of the stem than the top side.imp13Once the repairs were dry I sanded them back to the surface of the stem with 220 grit sandpaper.imp14I polished the sanded spots by wet sanding with 1500-2400 grit micromesh sanding pads.imp15I wet sanded the entire stem and continued to sand the repaired areas with 1500-2400 grit micromesh sanding pads. I rubbed the stem down with Obsidian Oil and then dry sanded it with 3200-12000 grit pads. I rubbed it down with oil after each set of three pads and after the final set I gave it a last coat of Obsidian Oil and set it aside to dry.imp16 imp17 imp18The nickel ferrule had a lot of tiny scratches in the surface of the metal. I sanded it with micromesh sanding pads to polish out the scratches and raise a shine in the nickel.imp19I polished the briar with 3200-12000 grit micromesh sanding pads to raise the shine and smooth out the small scratches on the sides and bottom of the bowl as well as the rim.imp20 imp21 imp22I buffed the bowl and stem with Blue Diamond on the buffing wheel to further polish the briar and vulcanite. I gave the stem multiple coats of carnauba wax and buffed the bowl and stem with a clean buffing pad to polish and raise the shine. I hand buffed it with a microfibre cloth to deepen the shine. The finished pipe is shown in the photos below. It turned out to be a very beautiful pipe that needed just a few touches of TLC to bring it to its fullest. It is another large pipe that would make a great reading or house pipe. It is comfortable in hand and the grain is interesting enough to give hours of observation pleasure. Thanks for looking.imp23 imp24 imp25 imp26 imp27 imp28 imp29 imp30

An Estate Sale Find – A Castello Sea Rock SC 54P Bulldog


Blog by Steve Laug

My brother Jeff is truly the king of estate sale, junque store and antique store pipe finds. He seems to have not only developed an eye for a good pipe but seems to have an uncanny ability to find them. A few months back now he messaged me from an estate sale he had gone to near Boise, Idaho. He had driven to the town the evening before so he was first in line for the sale. He found some great pipes in that sale and on that trip. I wrote about the finds he came home with on that trip in a previous blog (https://rebornpipes.com/2016/10/31/sometimes-you-just-get-lucky-an-amazing-pipe-hunt/). This little Castello Sea Rock 54P Bulldog came home with him on that trip. From his description and the photos that he sent along the pipe showed lots of promise. The Sea Rock Finish was dirty and the crevices had dust in them. The rim was tarred with overflow of cake from the heavily smoked bowl. The pipe seemed to sport an after factory band as there were no Castello marks on the silver. The stem was in good shape though it had tooth marks on the top and bottom sides next to the button. It had the diamond logo on the side of the saddle stem which I knew meant it was made for the United States market.castello1My brother took some close up photos of the rim top and the cake in the bowl to show what it looked like when he found it. You can see how thick the cake is and how much of the rim rustication has filled in with the overflow.castello2Other than being dirty, the finish was in very good shape. There were no chips of dings in the surface of the rim or on the bowl or the shank.castello3The silver band was tarnished and seemed to have some flaking on the surface. I am not sure if the silver plate is peeling or if it is just left over remnants of the sticky tag that had been there with the price. The stamping was very clear on a smooth patch on the left underside of the diamond shank and read Castello over SC Sea Rock Briar. Underneath that and to the left it read 54P (which is the shape number) and Made in Cantu over Italy. The underside of the left side of the Lucite stem also had stamping that read Hand Made over Castello and the number 5. The stamping of Hand is faint though it can be seen with a magnifying glass.castello4The fit of the stem against the shank was off – it looked as if the mortise was filled with oils and had pushed the stem out. It did not fit snugly against the shank. The faux diamond circle on the saddle portion of the stem is also visible in the photo below. The second photo below shows the debris on the silver band and the grime in the rustication of the shank.castello5The last two photos that my brother sent show the condition of the stem. It is hard to see the tooth marks near the button on both sides of the stem but you can see the chatter on the underside and the “gunk” (technical term) that had built up in the corners of the slot in the button.castello6Before I worked on the pipe I wanted to do a bit of research to see if I could shed some more light on the pipe I had in hand. I learned from the pipephil website that the rhinestone logo was originally on pipes for the US market. There was no hint as to why that was done only that it was and that it is occasionally still used http://www.pipephil.eu/logos/en/logo-castello.html

I have an older article called PCCA’s Castello Grade & Style Guide. It was written by Robert C. Hamlin (c) 1988, 1992, 1994. Robert gathered some remarkable information on the Castello lines and I have often used his guide in the past to give me pertinent data. There I found more information regarding the shiny logo on the side of the stem.

“American logo’d Castello pipes use a small round “Diamond” (referred to and looking like, but it is NOT actually a diamond) inlaid into the mouthpiece. This was originally done so that the standard Castello white bar logo did not conflict with another brand and logo that was sold by Wally Frank called the “White Bar Pipe” (in the 1950’s).”

The above quote and the remainder of those following come from the same article by Robert Hamlin. You can read the full article at the following link: http://www.pipes.org/BURST/FORMATTED/196.016.html

I read further in the article to help me understand the stamping on the underside of the shank. My knowledge of Castello pipes is pretty limited so when I get one to restore I resort to this article and others to try to make heads or tails of the stamping. First of all I had no idea what the SC stamped ahead of the Sea Rock Briar stamping meant. I had seen Castello’s with the signature of Carlo Scotti on them but not this stamping. Robert gave me the information I needed.

“Older Castello pipes will usually include the “REG No.” and have the letters “SC” stamped as a part of the nomenclature. The SC stamp was for Scotti, Carlo (in Italy all names are listed last, first). Today the full name of Carlo Scotti, contained in a small oval, has replaced the SC stamp.”

I learned that the Sea Rock Briar stamp also signified something and told me more about the pipe. Robert pointed out:

“SEA ROCK [Carved Black or dark brown]: This is the lowest grade of the Castello line and is the most common in the USA. Sea Rocks are produced by taking a smooth bowl that has not been “final finished” and surface carving the finish with tools. This “carved” finish is then evened out using a steel wire brush, stained and then waxed. The Natural Vergin carved finish is left unstained and unwaxed as a rule, although we have seen waxed and partially waxed “Vergins”.” 

The remaining mystery for me was the meaning of the stamping on the stem. I of course understood the Hand Made and the Castello stamping but the number 5 was a mystery to me. I was not sure what it referred to. So once again Robert’s article gave me the information I needed to understand that last piece of the mystery.

“#2: All Castello standard shaped pipes have a number (3, 4, 5 or 6) stamped on the mouthpiece or sometimes on the lucite ferrule. What does this number mean? Not much really, it is the number of the size for the proper straw tube or reed that fits the shank and stem of the pipe. These straw tubes are rarely used in the United States. The Castello reed is considered superfluous and useless to most, but with this number you will always know which one fits (the different numbers have to do with length, not diameter).”

When the pipe arrived in Vancouver it was inside of a Castello suede bag missing only the drawstrings at the top. It bore the classic Castello Castle logo and reading Pipa Castello di Carl Scotti Cantu (Italy) stamped on the front in brown paint/ink. castello7I tipped the pipe out of the bag to see what my brother had done with it. He had written and warned me that he had done a minimal clean up on the pipe as he did not want to damage it. I was not sure what I would see when I removed it from the bag. The four photos below show the state of the pipe when it arrived.castello8 castello9Examining the pipe closely I could see that he had reamed the bowl and cleaned up the rim to remove the tars and oils that had overflowed onto the top of the rim. He had also cleaned the finish on the pipe quite nicely. The internals were cleaner but would need some more work but the pipe looked pretty good.castello10I took some photos of the stem to show the tooth marks on the top and underside near the button. In the first photo of the top, you can see the tooth mark neat the button and the one on the top edge of the button. In the second photo you can see the damage to the underside of the stem near the button and on the top of the button there as well.castello11I used a brass bristle tire brush to clean up the small particles that still remained in the grooves on the rim of the bowl. It did not take too much to remove what was left and leave the rim clean.castello12I wiped off the sticky spots on the silver band with a little alcohol on a cotton pad. I could see that the band had been stamping diagonally in several places with letters from the word silver but that none of them spelled it out completely. I was pretty certain from Robert’s article above that the silver band was after market and may be part of a repair to a cracked shank. Cleaning the pipe further would either confirm or deny that assumption on my part. I polished the band with micromesh sanding pads from 1500-12000 grit pads. The polished band is shown in the photo below.castello13I sanded the tooth marks out on both sides of the stem at the button using 220 grit sandpaper and also sanded the damage to the button surface itself. There was also slight damage to the slot itself on the end of the button. I sanded the slot and cleaned up the damaged areas there. castello14I used micromesh sanding pads to polish the newly sanded areas on the Lucite stem surface. I wet sanded with 1500-2400 grit pads and wiped the stem down with a damp cotton pad. I dry sanded it with 3200-12000 grit pads and wiped it down with the damp pad several times throughout the process. In doing so I was able to remove all signs of the damage to stem in those spots along the edge and top of the button.castello15 castello16 castello17With stem exterior finished other than buffing I ran a pipe cleaner with alcohol through to remove any sanding debris from my clean up and sanding of the surface and the slot. It was remarkably clean.castello18I cleaned out the shank with alcohol, pipe cleaners and cotton swabs to remove the tars and oils that kept the stem from properly seating against the end of the tenon. It was pretty thickly tarred and took some scrubbing to remove the grime. While I was cleaning the interior of the grime I found what I had surmised was under the band. The end and inside of the mortise revealed a small crack underneath the grime. It looked like it had been repaired somewhere along its life. The end of the crack on the shank end was the worst part of the damage. The hairline crack on the exterior of the shank – almost an underline of the word Cantu showed signs of having been glued and clamped until it sealed. That settled my question regarding the purpose of the aftermarket silver band on the shank.castello19 castello20With the internals cleaned and the crack examined with a lens and deemed solid I polished the silver band with a jeweler’s cloth to further remove any remnants of tarnish and give it a deeper shine and protection. I hand waxed the bowl with some Conservator’s Wax and buffed it with a shoe brush to raise the initial shine on the briar. The photos below show the bowl after the waxing and polishing.castello21 castello22I put the stem in place in the shank. The fit was perfect and it sat snuggly against the end of the mortise as it did when it left Cantu. I buffed the stem with Blue Diamond polish on the buffing wheel avoiding the silver band and the briar. I waxed the stem with carnauba wax on the wheel and buffed the entire pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfibre cloth to deepen the shine. The finished pipe is shown in the photos below. It is truly a beautiful little bulldog. The shape and the rustication make it a pleasure to hold in the hand. It fits snuggly with my thumb curled around the back of the bowl and the rest of the fingers holding the bowl. The finish is extremely tactile and should be interesting in hand as the bowl heats up during smoking. For me there is absolutely nothing lacking in the design and form of this old Sea Rock Briar and I think it will be one I hang onto. Thanks for walking with me through the restoration process.castello23 castello24 castello25 castello26 castello27 castello28 castello29 castello30 castello31

A Gold Banded Stanwell Copenhagen Calabash


Blog by Steve Laug

The next pipe on the work table is a striking Stanwell Calabash pipe with sandblasted body and smooth capped rim. The sandblast has exposed some wonderful ring grain around the bowl. The smooth wide rim typical of the calabash shape is wonderful birds-eye grain. The brass collar ring contrasts nicely with the dark stain of the sandblast shank. The gold crown S logo on the left side of the saddle stem combines with the other parts of the pipe to give this one a classic look. My brother Jeff found this Stanwell in an antique shop in Astoria, Oregon. It was on consignment by a widow who was selling her pipe collector husband’s collection. He bought a few of the pipes from her consignment and this is the second one that I have worked on. The first one was also a Stanwell – it was a shape 180 that was designed by Tom Eltang that I wrote about in an earlier blog (https://rebornpipes.com/2016/12/14/a-shape-you-gotta-love-a-stanwell-majestic-180/).cope1The finish on the sandblast portion was in great shape – just dirty with grit and grime. The rim cap however was another story. It had the overflow onto the top of the thick cake that was in the bowl. There was also some darkening of the inner edge of the rim. The brass band and the brass crown S logo on the stem were also dull and lifeless due to tarnishing. The stem was oxidized and had a buildup of calcification on both sides near the button. There were tooth marks and chatter on both sides of the stem and on the button. The slot in the button was nearly closed off with a thick tar.cope2My brother took two close up photos of the rim cap to show the condition of the inside of the bowl and the cap itself. There was a thick coat of tars and oils that is visible flowing over the back side of the cap. There were also several dings and dents in the cape itself though there was some nice birds-eye grain showing through the grime.cope3He also took a photo of the bowl bottom side up. The lovely bell shape of the pipe is visible from this view from the front.cope4The side view of the band and the shank/stem union shows that the connection is tight and clean. There is nothing wrong that a little polishing on the band and some elbow grease to remove the oxidation on the stem won’t take care of. The second photo below shows the stamping on the underside of the shank. It is very sharp and readable. It has the Stanwell stamp over Copenhagen over Calabash in script (it appears to have been double stamped). Beneath that it reads Made in Denmark (it is upside down in orientation to the rest of the stamping).cope5The next photos show the condition of the stem. You can see the tooth marks on the stem itself and the damage marks against the button on both sides. The calcification on the stem may have come for a Softee bit that the original owner had on the stem to protect it from more bite marks.cope6My brother Jeff again did a magnificent job cleaning up the pipe. He was able to get the grim out of the grooves and the majority of the buildup off the rim. He reamed and cleaned the interior of the pipe and stem with alcohol, cotton swabs and pipe cleaners. I took the following photos to show the condition of the pipe when I received. It was on its way to being clean.cope7 cope8I took a close up photo of the rim to show how much of the tars and oils he removed. It is pretty clean. There was some darkening on the inner edge of the rim on the back side that would need to be dealt with.cope9He also removed much of the calcification on the stem and some of the debris on the surface of both sides. The photos also show the tooth marks and chatter that was on the stem.cope10I sanded the stem to remove the rest of the debris and calcification and then wiped the stem down with alcohol on a cotton pad. I cleaned out the tooth marks with cotton swabs and alcohol and then filled them in with black super glue. I set the stem aside to let the repairs dry.cope11I sanded the inner edge of the bowl with 220 grit sandpaper to remove the darkening and then worked over the rim with 1500-1800 micromesh sanding pads to clean up the inner edge and begin polishing the rim cap. You can see the grain on the cap begin to pop and reveal the beautiful birds-eye grain.cope12When the glue had cured I sanded the patches smooth, blending them in with the surface of the stem using 220 grit sandpaper. I sanded the entire stem to work on more of the oxidation that was present on the surface. The photos below tell the story of the repairs and sanding to this point in the process.cope13I polished the bowl rim with 3200-12000 grit micromesh sanding pads and gave the sandblast bowl several coats of Conservator’s Wax. I buffed it with the shoe brush to raise the shine. The photos below show the bowl at this point.cope14 cope15I touched up the stain on the rim with a dark brown stain pen. I buffed it with a microfibre cloth and then polished it with micromesh sanding pads using 1500-12000 grit pads to polish and raise a shine.cope16 cope17I probably should have done this earlier in the process but my brother has been doing such a good job in his cleaning that I honestly forgot. I decided to give the internals of the stem and the mortise and shank a quick cleanup with pipe cleaners, cotton swabs and alcohol.cope18I polished the stem with micromesh sanding pads – wet sanding it with 1500-2400 grit pads and dry sanding it with 3200-15000 grit pads. I rubbed the stem down with Obsidian Oil after each set of three pads. I gave it the last coat of oil and set it aside to dry.cope19 cope20 cope21I polished the pipe and stem with Blue Diamond on the buffing wheel avoiding the sandblast portions of the bowl. I did not want to get the polishing compound in the grooves of the sandblast. It would be hard to get out of the grooves. I gave the sandblast portion several coats of Conservator’s Wax and buffed it with a shoe brush. I gave the stem and rim several coats of carnauba wax and buffed the entire pipe a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth. The finished pipe is shown in the photos below. It has come a long way from the pipe I started on in the first photos above. It is a classic looking calabash pipe with a great contrast between the smooth briar, the sandblast briar, the gold band and the vulcanite stem. (The brass is so shiny now that it is hard to get the vulcanite not to reflect the brass colour. In person the oxidation is gone and the stem is shiny black.) Thanks for walking through the process with me.cope22 cope23 cope24 cope25 cope26 cope27 cope28 cope29

 

Replacing a Stem on a Stanwell Antique 156 Bulldog


Blog by Steve Laug

The next pipe I brought to my work table is another Stanwell Antique. This one is stamped on the underside of the shank with the words Stanwell over the script Antique and over the top of them both is the number 156 which is the shape number. This one came in the same lot as the two victims of Jaws that I have already written about on the blog – the Estella and the GBD Midnight (https://rebornpipes.com/2016/12/06/jaws-and-an-estella-non-pareil-%c2%bc-bent-9606-stack-by-savinelli/ and https://rebornpipes.com/2016/12/09/another-jaws-victim-a-gbd-midnight-788-oval-shank-apple/). This Stanwell Antique Bulldog had a poorly fit replacement stem – a diamond shaped stem from a classic bulldog shape. The stem had many deep tooth marks on both the top and the underside of the stem. anti1The finish on the bowl was in decent shape though the rim had some tarry buildup and there was a thick cake in the bowl. The first photo shows the mixture of sandblast and smooth on this pipe was a nice contrast. The front of the pipe was smooth and joined the smooth rim. The second photo shows that the front outer edge had nicks and dents in it as did the surface of the rim. The close up photo of the rim shows the condition of the pipe when my brother received it.anti2The Lucite shank extension is amber coloured. The thickness of the extension makes it hard for the light to shine through it. The mortise had been damaged – it is my thought that whoever put the new stem in place redrilled the mortise and damaged the inner edge and the bottom of the mortise. anti3The stamping on the underside of the shank is better than the stamping on the previous Antique I just finished. The shape number is very clear and sharp. The Stanwell logo is lighter on the left side and the Antique stamping is also very clear and sharp.anti4The next photo shows the transition from the smooth front of the bowl to the sandblast on the rest of the bowl. You can see some of the grit in the grooves and crevices of the blast and the grime on the smooth portion.anti5The last photo that my brother sent me shows the bite marks on the diamond stem. They are identical in pattern to the ones on the previous two “Jaws” pipes.anti6My brother cleaned up the pipe with his usual thoroughness. When the pipe arrived in Vancouver the finish was clean and the grooves and crevices clean. The rim was better though it show the damage to the front edge and the dents to the top of the rim. He had reamed and cleaned the mortise and the airway in the replacement stem so the pipe was very clean and ready for me to work on.

I cleaned up the shank extension end and used clear super glue to rebuild the damage portion of the Lucite. I sanded it with 180 grit sandpaper and also with 220 grit sandpaper to smooth out the repairs. I cleaned out the shank with a cotton swab and warm water to remove the debris in the shank. I took photos of the bowl after I cleaned it up and scrubbed it with Murphy’s Oil Soap.anti7 anti8The rim shows some damage to the top and the back edge in the photo below.anti9The stem was an obvious replacement so I put it in my can of stems and looked for a stem that would be a good candidate for a replacement. I had one in a lot of stems that my brother sent me. It was a Danish looking freehand stem that had a long tenon and a step up toward the ring in the middle. I forgot to take a photo of the stem before I worked on it but I had another example of one that was similarly shaped that is shown in the next photo.anti10I sanded the stem with a Dremel and sanding drum to shorten and remove the step down area. I wanted to have a smooth transition from the tenon end to the mid ring. I also wanted to make the slope to the ring more abrupt that it was in the one above. The stem was in pretty rough shape. There was deep tooth mark on the topside of the stem from the damaged button forward. There was also some tooth damage on the underside of the stem in the middle and on one side. The button was also damaged on the underside. There was a missing chunk of vulcanite on the button edge. I filled in the damaged areas with black superglue to build them up. I let the glue dry and once it was dry I sanded it smooth to match the surface of the rest of the stem. I filled in the damaged button and built up the edge on the top and bottom sides. I sanded the button as well once it had cured and reshaped it.anti11I sanded the diameter of the tenon area on the new stem until the fit in the mortise was correct. The stem still looked a little long but I would take care of that shortly. I put it in the mortise and took photos of the pipe with the new stem.anti12 anti13I sanded the stem with 180 grit and 220 grit sandpaper to smooth out the repairs and reshape the stem to match the rest of the stem.anti14I polished the stem with micromesh sanding pads – wet sanding with 1500-2400 grit sanding pads and rubbed it down with Obsidian Oil and dry sanding with 3200-12000 grit sanding pads and rubbing it down with the oil after each set of three pads. After the final set I gave it a final coat of the oil and set the stem aside to dry.anti15 anti16 anti17To remove the damage to the front edge and the top of the rim I topped the bowl with 220 grit sandpaper on the topping board. I sanded it with 1500-6000 grit micromesh sanding pads to sand out the scratches in the rim surface. I restained the rim to match the front of the bowl using a dark brown stain pen. I buffed it lightly with a microfibre cloth.anti18I sanded the smooth portions of the bowl face and the rim with 1500-6000 grit micromesh sanding pads to polish them.anti19 anti20I buffed the rim and smooth part of the bowl and the stem with Blue Diamond polish on the wheel. I gave the stem multiple coats of carnauba wax and gave the bowl several coats of Conservator’s Wax. I buffed the pipe with a clean buffing pad and hand buffed it with a microfibre cloth to deepen the shine. The finished pipe is shown in the photos below. The repairs on the stem show under the bright lights of the flash but in person they are pretty well blended into the surface of the stem. Thanks for walking through the restoration with me.anti21 anti22 anti23 anti24 anti25 anti26 anti27 anti28

Another Jaws Victim – A GBD Midnight 788 Oval Shank Apple


Blog by Steve Laug

I love old GBD pipes no matter what era they come from. I gave my brother a list of pipes to keep an eye open for in his treasure hunts as he travels and on his eBay forays as well. GBD has been at the top of that list. He found a newer generation GBD recently and sent it my way. It is a nicely grained apple that is stamped GBD in the oval over MIDNIGHT on the top of the shank. On the underside it is stamped London England over 788 which is the shape number for an oval shank apple. The stem is a green swirled Lucite saddle shape with the GBD Oval stamped on the top of the saddle portion. The pipe was in decent shape. The finish was dirty and there was a buildup of cake in the bowl that had overflowed onto the rim. There were some dents in the outer edge of the rim on the back left side and some nicks and scratches on the left side of the bowl. The stem was another one that Jaws had gotten a hold of just like the Estella Non Pareil that I just finished and wrote about (https://rebornpipes.com/2016/12/06/jaws-and-an-estella-non-pareil-%c2%bc-bent-9606-stack-by-savinelli/). The top side had some deep dents and the underside had them as well. There were better situated in that they were in the blacker portion of the stem so blending in the repairs would be simpler.jaws1The photos my brother Jeff sent me really show the grain on the pipe. It has some stunning swirls of grain on the sides and some stunning birdseye on the top and the bottom of the shank and bowl.jaws2 jaws3The next photos show some close ups of the rim and the bowl bottom. The top of the rim was thickly coated with the overflowing cake in the bowl. The birdseye on the bowl bottom is stunning.jaws4The stamping on the shank and the stem was clear though lighter to the right edge on the topside of the shank. The fit of the stem to the shank was messy due to the build up of tars and oils in the shank and the mortise. I was pretty certain that once the pipe was cleaned up the fit would be back to normal.jaws5The next two photos show the work of Jaws on the Lucite. I can only say that I am thankful that the stem was not vulcanite or it would have been destroyed!jaws6My brother did his usual thorough clean up and was able to remove all of the tars and oils from the rim and the cake from the bowl. He scrubbed the grime and oils from the finish with Murphy’s Oil Soap and cleaned out the internals with alcohol, cotton swabs and pipe cleaners. The next four photos show the pipe when it arrived on my work table in Vancouver. I am getting spoiled by him doing all the grunt work of reaming and scrubbing. The pipes I get are all cleaned and reamed and ready to be restored. It is a great arrangement!jaws7 jaws8I took a close up photo of the bowl and rim to show how clean it was when it got to me.jaws9The tooth dents in the stem are shown in the next two photos. After the stem had been cleaned up they did not look as daunting as the ones in the Estella. The button had been worn down some as well by the chomper.jaws10I “painted” the dents in the stem with the flame from a Bic lighter. I was able to raise them quite a bit on this stem. On the top side only one deep tooth mark remained and on the underside there were three left.jaws11I sanded the dented areas with 220 grit sandpaper to smooth out the surface around the dents. I washed it down with alcohol on a cotton swab to make sure I did not leave any of the white sanding dust in the tooth marks. I decided to use black superglue to fill in the tooth dents as they were in the darker portion of the stem. I filled them in and let the glue dry.jaws12Once the glue had dried I sanded the patches smooth with 220 grit sandpaper to blend them into the surface of the stem. The patch on the topside disappeared into the dark green/black of the rest of the stem. The ones on the underside were a little more temperamental and showed some light areas on some small parts of the patches.jaws13I polished the stem with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I wiped the stem down with a damp cotton pad after each set of three pads.jaws14 jaws15 jaws16I set the stem aside and worked on the bowl. I used 1500-2400 grit micromesh sanding pads to work over the nicks in the rim and on the left side of the bowl. I was able to minimise them so that they blended into the briar better. I stained the bowl with a dark brown aniline stain cut 50/50 with isopropyl alcohol and flamed it with a lighter. I repeated the process until the coverage was even on all sides of the bowl.jaws17I buffed the bowl and stem with Blue Diamond on the buffing wheel and gave the pipe multiple coats of carnauba wax to protect it. I buffed it with a clean buffing pad to polish the carnauba and give it a shine. I hand buffed the pipe with a microfibre cloth to deepen the shine. The finished pipe is shown in the photos below. The rich brown of the stain is a great contrast to the green of the Lucite stem. The overall look of the pipe is rich and the feel in the hand is perfect. This one will be available on the store in the days ahead. Thanks for journeying with me in this refurb.jaws18 jaws19 jaws20 jaws21 jaws22 jaws23 jaws24 jaws25