Tag Archives: removing tooth marks

Farida’s Dad’s Pipes #6 – Restoring a Charatan Make Distinction


Blog by Steve Laug

I am back working on one of the pipes that came from the estate of an elderly gentleman here in Vancouver. I met with his daughter Farida a year ago and we looked at his pipes and talked about them then. Over the Christmas 2017 holiday she brought them by for me to work on, restore and then sell for her. There are 10 pipes in all – 7 Dunhills (one of them, a Shell Bulldog, has a burned out bowl), 2 Charatan Makes, and a Savinelli Autograph. I have restored all but three of them – a Dunhill Shell and the two Charatan’s Makes. His pipes are worn and dirty and for some folks they have a lot of damage and wear that reduce their value. To me each one tells a story. I only wish they could speak and talk about the travels they have had with Farida’s Dad.

The bowl was thickly caked and the cake had flowed over onto the smooth finish on the rim top forming hard lava that made the top uneven. The inner and outer edges of the rim were both damaged. On the right front of the bowl the rim had a burned area – it was not a deep burn but it had darkened. On the back of the bowl there was damage on the inner edge of the bowl and it looked like it might be slightly out of round. The stem was oxidized but otherwise in good condition. There was a thick sticky, oily substance on the surface of the stem that I could scrape with my fingernail. There were tooth marks and chatter on both sides in front of the button. I took photos of the pipe to show what it looked like before I started the cleanup work. I took close up photos of the bowl and rim top as well as the stem. You can see the condition of the rim top and bowl in the first photo. The outer edge has damage on the front right – burn damage and wear that comes from lighting a pipe repeatedly in the same spot. The inner edge at the back middle also shows damage but I won’t know until I remove the thick lava overflow on the surface. The stem had tooth chatter and some bite marks on the top and the underside of the stem just ahead of the button.I took a photo of the left side shank stamping – it is readable but faint on the left side.It has been a while since I have worked on the remaining pipes that belonged to Farida’s Dad. I thought it might be helpful to remind us all of the background story of these pipes. Here is the material that I quoted in previous blogs. I have included both the written material and the photo that Farida included of her Dad.

When I wrote the blog on the Classic Series Dunhill and thinking about its travels, Farida sent me an email with a short write up on her Dad. She remembered that I had asked her for it so that I could have a sense of the stories of her Dad’s pipes. Here is what she wrote: My dad, John Barber, loved his pipes. He was a huge fan of Dunhill and his favourite smoke was St. Bruno. No one ever complained of the smell of St. Bruno, we all loved it. I see the bowls and they’re large because he had big hands. When he was finished with his couple of puffs, he would grasp the bowl in the palm of his hand, holding the warmth as the embers faded. The rough bowled pipes were for daytime and especially if he was fixing something. The smooth bowled pipes were for an evening with a glass of brandy and a good movie. In his 20s, he was an adventurer travelling the world on ships as their radio operator. He spent a year in the Antarctic, a year in the Arctic and stopped in most ports in all the other continents. He immigrated to Canada in the mid-fifties, working on the BC Ferries earning money to pay for his education. He graduated from UBC as an engineer and spent the rest of his working life as a consultant, mostly to the mining companies. Whatever he was doing though, his pipe was always close by. 

She sent along this photo of him with his sled dogs in the Antarctic sometime in 1953-1954. It is a fascinating photo showing him with a pipe in his mouth. He is happily rough housing with his dogs. As a true pipeman the cold does not seem to bother him at all. Thank you Farida for sending the photo and the background story on your Dad for me to use on the blog. I find that it really explains a lot about their condition and gives me a sense of who Dad was. If your Dad was rarely without a pipe I can certainly tell which pipes were his favourites.As I looked over the pipes I noted that each of them had extensive rim damage and some had deeply burned gouges in the rim tops. The bowls seemed to have been reamed not too long ago because they did not show the amount of cake I would have expected. The stems were all covered with deep tooth marks and chatter and were oxidized and dirty. The internals of the mortise, the airway in the shank and stem were filled with tars and oils. These were nice looking pipes when her Dad bought them and they would be nice looking one more when I finished.

Here are the links to the previous five blogs that I wrote on the five pipes that I have finished. The first was a Dunhill Shell oval shank pot (https://rebornpipes.com/2018/02/04/restoring-a-1983-dunhill-shell-41009-oval-shank-pot/). The second was a Dunhill Classic Series Shell Billiard (https://rebornpipes.com/2018/02/08/faridas-dads-pipes-2-restoring-a-1990-lbs-classic-series-dunhill-shell-billiard/). The third pipe was a Savinelli Autograph (https://rebornpipes.com/2018/02/15/faridas-dads-pipes-3-restoring-a-savinelli-autograph-4/). The fourth pipe was a Dunhill Red Bark Pot that was in rough shape (https://rebornpipes.com/2018/03/10/faridas-dads-pipes-4-restoring-a-dunhill-red-bark-pot-43061/). The fifth pipe was a Dunhill Root Briar Bent Billiard https://rebornpipes.com/2018/07/07/faridas-dads-pipes-5-restoring-a-dunhill-root-briar-56-bent-billiard/

Today, I went back to the remaining three pipes in the collection today and chose to work on one of the Charatans – a triangular shank Dublin. It was dirty but I was able to read the stamping. On the top left side of the triangular shank it is stamped Charatan’s Make, over London, England over Distinction. On the right side it was stamped Made By Hand in the City of London. I cannot see any shape number on the shank as it is pretty worn. The smooth finish was sticky with oils and thick grime. The bowl felt oily to touch.

To try and figure out the era of the Charatan’s pipe I was working on I turned to the pipephil website on Logos and Stampings. There is some really helpful information on each of the lines of Charatan’s Make pipes that entered the market. Here is the link to the section of the site that I turned to, http://www.pipephil.eu/logos/en/logo-charatan.html. There is an alphabetical listing of the lines but unfortunately they did not list the Distinction. The site did give a short history of the brand. I quote the portion that is most pertinent.

The brand was founded in 1863 by Frederik Charatan. When his father retired in 1910, Reuben Charatan took over the family business. All the pipes were handmade until 1973. The brand name has been overtaken by Dunhill in 1978 and sold in 1988 to James B. Russell Inc.(NJ, USA). During the period 1988-2002 Charatans were crafted by Butz Choquin in St Claude (France). Dunhill re-purchased Charatan brand name in 2002 and Colin Fromm (Invicta Briars, Castleford) followed up on freehand production.

I turned to Pipedia to see if I could find more information on the brand and possibly a link to the Distinction line (https://pipedia.org/wiki/Charatan) but once again in the general article it was not listed.  It did give a little more historical information. I quote the pertinent parts and have highlighted in bold the sections that give information on this particular pipe.

In 1863 Frederick Charatan, a Russian/Jewish immigrant, opened a shop in Mansell Street, located in the borough of Tower Hamlets, London E1, where he began to carve Meerschaum pipes. These pipes got very popular soon, and thus Charatan moved to a bigger workshop in Prescot Street, just around the corner. Here he began to make briar pipes which should make the name famous the world over. Charatan was the first brand to make entirely hand-made briars from the rough block to the finished pipe including the stems. The nomenclature “Charatan’s Make” refers to this method of production and was meant to differ Charatan from other brands who “assembled” pipes from pre-drilled bowls and delivered mouthpieces.

Being the undisputed No. 1 in English pipemaking, Charatan was approached by Alfred Dunhill who was unsatisfied with the quality of the pipes he imported from France. During 1908 – 1910 Dunhill bought pipes from Charatan paying exorbitant prices to ensure he had some of the very best pipes for sale in England. In 1910 he lured away Joel Sasieni, one of Charatan’s best carvers, and opened his own small pipe workshop on 28 Duke Street. On the retirement of his father in 1910 Reuben Charatan took over the family business…

…The pre-Lane period (prior to 1955) and the Lane era pipes (1955 to until sometime between 1979 – 1984) are of primary interest the collector. The Lane era is often quoted as beginning about 1950… Charatan records are almost non-existent before Lane due to a factory fire, making it difficult to date pre-Lane pipes. Charatan used 4 basic grades prior to 1950: Supreme, Selected, Executive, and Belvedere. After 1950 Herman Lane’s influence began, and the grades started to expand. In 1955 Lane took over sole distributorship of Charatan in the US. In 1957 he introduced the Supreme S. Most of his other introductions were from the 60’s and early 70’s…

The section called Miscellaneous Notes had some interesting information.

Charatan records indicate the DC (Double Comfort) bit was introduced in the 50’s, but some report seeing them in earlier production. Still others indicate they were introduced by Lane in 1960. Regardless, the DC bit is not an accurate way to date a pipe because many Charatan’s were made with regular and saddle type bits throughout the “Lane Era”…

…The Lane Trademark serif and circled L indicates the pipe is from the “Lane Era” (approx. 1955 to 1979 -1984?), however it appears that both the English factory or Lane themselves sometimes, or perhaps even often forget to stamp the L on a pipe. The Charatan factory was known for inconsistencies, especially in stampings. Therefore, although an L on the pipe definitely defines it as a Lane Era pipe, the lack of it could simply mean the pipe missed receiving the stamp from the factory. The lack of the trademark could also mean the pipe was destined for the European market.

…Generally, when the pipe is stamped with the BLOCK letters “MADE BY HAND” it means the pipe was probably made between 1958 and 1965”

Generally, block letters “MADE BY HAND” and some of the other nomenclature in script (i.e. City of London or Extra Large next to the MADE BY HAND) means the pipe was made sometime between 1965 and the mid 1970’s. The total script nomenclature “Made by Hand in City of London” evolved over this period of time, so many pipes had variants, such as Made By Hand in block letters and City of London in script, or some other variation of the terms or stampings. The Charatan Logo (CP) on the pipe bit was changed over the years.

I found an interesting Russian site on the various lines of Charatan. Here is the link to that site – http://brbpipe.ru/wp-content/uploads/2012/06/T-shop_1-2011-12_56-69_3.pdf. I did a google translation of the section on the DISTINCTION line.

The first of two medium sized factories. Neutral flame grain under contrast stain. Sometimes, however, there is a completely fantastic, almost perfectly smooth cross cut, sometimes – inclined to the side of the smoker flame. The most important thing: in this and the next grade begins a serious predominance of freehand over cataloged shapes.

The reason for this predominance lies in the strategy of educating carvers. Both medium grades are the launch pad for those who sought the right to work with top grades. Where the freaks have become the rule. The master had to work out a sufficient number of freehands and show a personal fantasy, so that he was allowed to work with the best, selective locks. And if at this “school of life” you could make extra profits … well, you remember that in this regard, there was a little iron Hermann.

I also found a description of the Distinction on VKpipes. Here is the link to that site, https://www.vkpipes.com/pipeline/charatans-make-distinction. I quote from that site.

Distinction was one of the most successful and valued lines of Charatan’s pipes from the “first Lane era” (1961-95). These years the old good Charatan’s family manufactory turned into the brightest star of the pipe making by means of new investments, a successful management and a creative approach of the Charatan’s artisans. There’s no shape number on the pipe: it was made by one of the leading carvers at this factory regardless any catalogues…

I also found a list of the various lines of Charatan’s Make Pipes that helps to place the Distinction in the hierarchy of pipes. Here is the link to the list https://www.reddit.com/r/PipeTobacco/comments/z9knr/charatan_models_shape_information_for_the/. I will be posting it as a separate blog shortly. The Distinction line is just below the Executive line and just ahead of the After Hours line – both Charatan’s Make Freehand Straight Grains.

From all of the historical data I could work through this Charatan’s Make Distinction was one of the higher grade pipe from the mid 1970’s Lane era. I continue digging further into the dating of the pipe, but what I had found was a good start for me. If some of you would like to try your hand at dating it more accurately as to the time period it came out you might want to check out the article on Pipedia on Dating Charatans (https://pipedia.org/wiki/Dating_of_Charatans). I had enough for me to start working on the pipe itself and see what lay beneath the heavy tars and oils.

I began working on the pipe by reaming the bowl with a PipNet reamer. I used two of the four cutting heads to clean out the cake. The bowl was thickly caked so I started with the smaller of the two and worked my way up to the second one which was about the same size as the bowl diameter. I cleaned up what remained in the bowl with a Savinelli Fitsall Pipe Knife and scraped it back to bare briar. I finished by sanding the inside of the bowl with a dowel wrapped in sandpaper. I worked on the top of the rim with the edge of the Savinelli Fitsall Pipe Knife. I scraped the heavy buildup that was there. I topped the bowl on a topping board with 220 grit sandpaper to remove the damage to the top surface of the rim and clean up the damage to the edges. I did not have to remove a lot and repeatedly checked it to make sure that I had removed enough but not too much. I wanted to take the rim top down until the burn damaged area was smooth and minimized. The second photo shows the burned and damaged areas clearly. I continued to top the bowl until I had removed the damage. I wiped down the rim top with alcohol and cotton pads to remove the sanding dust. I scrubbed the exterior of the bowl and shank with a tooth brush and Murphy’s Oil Soap to break through all the grime. I rinsed the bowl under running water to remove the grime and grit. I repeated the process until I had the bowl clean. I took photos of the cleaned exterior of the bowl to show where things stood at this point in the process. I used a folded piece of 180 and 220 grit sandpaper to bevel the inner edge of the rim until I had removed most of the damage on the back inner edge.With the externals clean it was time to clean out the mortise and shank and airway into the bowl and the airway in the stem with alcohol, cotton swabs and pipe cleaners. I scraped the mortise with a dental spatula and a pen knife to loosen the tars before cleaning. I worked on the bowl and stem until the insides were clean. I wiped down the exterior of the bowl with alcohol on a cotton pad to remove any remaining oils and grimes from my cleaning of the bowl and rim. Once the alcohol evaporated the briar was very dry but also very clean. I rubbed down the briar with Before & After Restoration Balm. I worked it into the smooth finish to clean, enliven and protect the new finish. It also evened out the stain coat and gave the stain a dimensional feel. I let the balm sit for a little wall and then buffed it with a horsehair shoe brush. I buffed the bowl with a cotton cloth to raise the shine. There was some darkening on the rim top on the right front and around the inner edge of the bowl but the briar was solid all around the bowl. The bowl looked really good at this point in the process. I set it aside and turned my attention to the stem. I sanded out the tooth chatter on both sides with a folded piece of 220 grit sandpaper. I cleaned the surface of the stem with alcohol on a cotton pad and filled in the tooth marks with black super glue and set the stem aside to let the repair cure.While the stem repair was curing I stuffed the bowl with cotton balls and put a folded pipe cleaner in the shank. I filled the bowl with alcohol to leech out the oils and tars in the bowl. I set the bowl in an old ice cube tray and let it sit throughout the day while I was at work. I find that cotton balls work as well as kosher salt and the folded pipe cleaner leeches tars out of the shank as well. The first photo shows the pipe when I set it up early in the morning. The second shows it after it sat all day. The cotton balls were dark brown with the oils that had wicked out of the briar. The pipe smells fresh and new now!When the repair had cured I used a needle fill to clean up the sharp edge of the button. I sanded the repairs on the stem with 220 grit sandpaper to blend them into the rest of the surface of the vulcanite.I polished the stem with micromesh sanding pads – wet sanding with 1500-2400 grit micromesh sanding pads and dry sanding it with 3200-12000 grit pads. I rubbed the stem down with Obsidian Oil after each pad. I polished it further with Before & After Pipe Polish, using both the Fine and Extra Fine polishes to further protect and polish out the scratches. When I finished with those I gave it a final rub down with the oil and set it aside to dry.  With the stem polished I put it back on the pipe and lightly buffed the bowl with Blue Diamond. I buffed the stem with a more aggressive buff of Blue Diamond. I gave the bowl several coats of Conservator’s Wax and the stem several coats of carnauba wax and buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The pipe polished up pretty nicely. The finished pipe is shown in the photos below. This is the sixth of Farida’s Dad’s pipes that I am restoring from his collection. I am looking forward to hearing what Farida thinks once she sees the finished pipe on the blog. This Charatan Distinction will soon be on the rebornpipes store if you want to add it to your rack. The dimensions are Length: 6 inches, Height: 1 3/4 inches, Outside diameter of the bowl: 1 1/2 inches, Chamber diameter: 7/8 inches. Thanks for walking through the restoration with me as I worked over another of the her Dad’s pipes. I have two more of his pipes to work on – one more Dunhill and one Charatan’s Make.

New Life for a Karl Erik Made in Denmark 5A Freehand


Blog by Steve Laug

The next pipe on the work table was a beautifully grained Freehand. The bowl and shank had a smooth finish with mixed grain. The top of the bowl and the end of the shank was plateau. The shape of the bowl top was oval. The walls of the bowl are scooped on the sides and front of the bowl. Toward the back of each side there is a ridge running from the top to the bottom of the bowl. The bottom of the bowl is shaped almost like a spade. The shank is quite thick and the underside is stamped toward the shank end. It reads Karl Erik over Hand Made in Denmark over 5 over A. The bowl had a dull and dirty finish. There was a thin cake in the bowl and lava overflow and grime in the plateau on both the top and the end of the shank. The stem was oxidized but the Karl Erik KE logo was in perfect condition on top. There was tooth chatter on the top side and some deep tooth marks and chatter on the underside. I took photos of the pipe before I cleaned it up. I took a close up photo of the bowl and rim to show the condition of the pipe before I started to work on it. The plateau rim top was dirty and cake with lava overflow. The bowl had a thin cake but looked to be solid. The finish of the bowl was dull and looked tired. The second photo shows both the plateau top and the shank end. I reread the blog that Robert M. Boughton did for us on his “Grade O” Karl Erik to refresh my memory on the brand and the grading system (https://rebornpipes.com/2018/07/28/a-three-card-draw-for-an-inside-straight-with-an-old-karl-erik-hand-made-grade-o-freehand/). It was enlightening and from there I went on and looked up the brand on both Pipephil’s site and Pipedia to add some details to my knowledge.

Photo courtesy of Pipedia

From the Pipephil site I got a quick overview of the history of the brand. I quote: Brand created in 1965-66 by Karl Erik Ottendahl (1942 – 2004 †). In the best years he employed up to 15 craftsmen among which Bent Nielsen (see Benner) and Peder Christian Jeppesen. Former grading (ascending): from 4 to 1, and “Ekstravagant” (entirely handmade).  http://www.pipephil.eu/logos/en/logo-k1.html

From Pipedia here is a bit more detailed history of the brand.

Karl Erik Ottendahl (1942 – 2004) was born in Aalborg (Jutland), just a few miles from the very northernmost tip of Denmark. He began smoking a pipe when he was 14 and upon leaving school he started an apprenticeship…as a lithographer at the age of 16.

While working as an apprentice he began hand carving pipes as a hobby. Many were given as gifts to his more senior colleagues. Upon completion of his apprenticeship he moved to Nairobi, Kenya to work as a lithographer during the 1962 war. While in that war torn country, he was unable to procure pipes for himself. In the face of such a predicament, he chose to continue to make pipes for his own use rather than go without.

Returning to Denmark after three years he couldn’t find a well paid… job, and so he began making a few pipes on the side to boost his income choosing his prenames “Karl Erik” – logo “KE” – for his label. When he managed to find some major Copenhagen pipe stores willing to sell his pieces his reputation grew little by little and he was finally able to purchase more and better machinery and began working full time as a pipe maker. https://pipedia.org/wiki/Karl_Erik

Pipedia also included a short description of the grading system that was used. From what I can discern the numbers ascended (6-1) and the letters ascended as well.

KE’s new grading used numbers ascending from D to A. The unique “Ekstravagant” pipes C, B, A, AA to AAA. These superb pieces of remarkable quality were, almost certainly, the least expensive high- quality hand made pipes coming from Denmark today! https://pipedia.org/wiki/Karl_Erik

I used a brass bristle brush to clean up the plateau on the rim top and shank end. I scrubbed it dry to remove the buildup of grime and tars on both surface. The bristles are hard enough to remove the grime and soft enough not to scratch the surface. It is a tool I always have close at hand when working on Freehand pipes.Once the buildup was gone from the top and shank end I scrubbed the entire exterior with a tooth brush and Murphy’s Oil Soap to remove the dirt on the surface of the briar and the remaining dust in the plateau. I rinsed it under running water to remove the soap and debris from the pipe. I dried it off with paper towels and twisted the paper towels into the bowl to remove the light cake that was there. The pipe was starting to look really good. The grain stood out and the contrast was nice. I took a photo of the underside of the shank to show the stamping. You can read the stamp easily and the grade markings though more faint are still readable.I scrubbed out the shank – working on the mortise with pipe cleaners, cotton swabs and alcohol until it was clean. I cleaned the airway in the shank and stem with alcohol and pipe cleaners as well. I always use 99% isopropyl alcohol because of the low percentage of water in it and the quick evaporation rate.With the interior and exterior of the pipe clean I rubbed down the briar with Before & After Restoration Balm. I worked it into the plateau on the rim top and shank end as well as into the smooth briar on the rest of the bowl and shank. The Balm works to clean, enliven and protect the briar. I worked it into the briar with my fingertips and the help of a horsehair shoe brush. I let the balm sit for a little wall and then buffed with a cotton cloth to raise the shine. The briar came alive with the balm. I took the following photos to give a picture of the pipe at this point in the process. With the bowl finished at this point (other than the final buffing and waxing) I set it aside and turned my attention to the stem. I painted the deep tooth mark on the underside of the stem with the flame of a Bic lighter to raise the dent. It worked better than I expected and reduced the size of the bite mark significantly. (The first photo below is the stem prior to heating with the flame).The KE logo on the stem was in perfect condition so I worked around that so as not to damage it. I lightly sanded the stem down with 220 grit sandpaper to remove the oxidation and cleaned out the debris from the tooth marks with a cotton swab and alcohol. Once the stem was cleaned up I filled in the tooth mark with black super glue and set the stem aside to let the glue cure. Later in the afternoon when the glue had hardened I sanded the repair smooth with 180 and 220 grit sandpaper to blend it into the rest of the stem surface.I polished the stem with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I wiped the stem down after each pad with Obsidian Oil to preserve and protect the rubber. After the final pad I gave it a final coat and set it aside to dry. I the polished the bowl and stem on the buffing wheel with Blue Diamond to remove the remaining small scratches and raise the shine. I gave the bowl and stem multiple coats of carnauba wax and buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The pipe polished up pretty nicely. This turned out to be a beautiful pipe in terms of shape and finish. The finished pipe is shown in the photos below. The dimensions are Length: 6 inches, Height: 3 inches, Outside diameter of the bowl: 2 1/4 inches, Chamber diameter: 7/8 of an inch. Thanks for walking through the restoration with me as I worked over another beautiful Karl Erik Freehand. I will be adding it to the rebornpipes store shortly so if you are interested in adding it to your collection send me an email or a message on Facebook. Thanks for looking.

Bringing a Butz Choquin Simour 1507 Back to Life


Blog by Steve Laug

With this blog I worked on another of the pipes from Kathy’s Dad’s estate. This is the twelfth of the pipes from collection. For a reminder to myself and those of you who are reading this blog I will retell the story of the estate. Last fall I received a contact email on rebornpipes from Kathy asking if I would be interested in purchasing her late Father, George Koch’s estate pipes. He was a lover of “Malaga” pipes as well as others and she wanted to move them out as she cleaned up the estate. We emailed back and forth and I had my brother Jeff follow up with her as he also lives in the US and would make it simpler to carry out this transaction. The long and short of it is that we purchased her Dad’s pipes – Malagas and others. Included in the lot was this interesting Butz-Choquin Classic Pot shaped pipe with an inset of what looks like copper on the left side toward the rear of the bowl. The condition of all them varied from having almost pristine stems to gnawed and damaged stems that need to be replaced. These were some well used and obviously well-loved pipes. Cleaning and restoring them will be a tribute to this pipeman. Jeff took these photos of the Butz-Choquin before he cleaned it. Jeff took photos of the rim top and bowl to show the thick cake and what looked like potential damage to the inner edge of the rim at the right front and the middle at the back. He also took photos of the bowl from various angles to show the condition of the finish and the copper insert I spoke of above.  The stamping on the left side of the shank clearly reads Butz-Choquin and underneath it is a bit more faint but looks to read Simour. On the right side it is stamped St. Claude over France and a shape number 1507 beneath that.The stem was in better condition than most of the others in the collection. There was light tooth chatter on both sides near the button and the sharp edge of the button had some tooth damage. As I look at it I wonder if it is not an acrylic stem. We shall see.Those of you who have followed me for a while know how much I love getting to know about the pipeman who held the pipes in trust before me. That information always gives another dimension to the restoration work. This is certainly true with this lot of pipes. I can almost imagine George picking out each pipe in his collection at the Malaga shop in Michigan. Once again, I am including that information with this restoration so you can know a bit about the pipeman who held these pipes in trust before they are passed on to some of you. I include part of Kathy’s correspondence with my brother as well…. I may well be alone in this, but when I know about the person it is almost as if he is with me while I work on his pipes. In this case Kathy sent us not only information but also a photo of her Dad with a pipe in his mouth.

Jeff…Here is a little about my dad, George P. Koch…I am sending a picture of him with a pipe also in a separate email.

Dad was born in 1926 and lived almost all his life in Springfield, Illinois. He was the youngest son of German immigrants and started grade school knowing no English. His father was a coal miner who died when Dad was about seven and his sixteen year old brother quit school to go to work to support the family. There was not much money, but that doesn’t ruin a good childhood, and dad had a good one, working many odd jobs, as a newspaper carrier, at a dairy, and at the newspaper printing press among others. He learned to fly even before he got his automobile driver’s license and carried his love of flying with him through life, recertifying his license in retirement and getting his instrumental license in his seventies and flying until he was grounded by the FAA in his early eighties due to their strict health requirements. (He was never happy with them about that.) He was in the Army Air Corps during World War II, trained to be a bomber, but the war ended before he was sent overseas. He ended service with them as a photographer and then earned his engineering degree from University of Illinois. He worked for Allis Chalmers manufacturing in Springfield until the early sixties, when he took a job at Massey Ferguson in Detroit, Michigan. We lived in Livonia, and that’s where his love for Malaga pipes began. After a few years he returned to Allis Chalmers and we moved back to Springfield. I remember that when we went back to Michigan to visit friends, Dad had to go to the Malaga store and acquire a few new pipes. Many a year I wrote to Malaga and they picked out a pipe for me to purchase that I could give Dad for a Christmas or birthday present. He was always pleased. His favorites were the straight stemmed medium sized bowl pipes, but he liked them all.  He had some other pipes, but the Malagas were his favorites. I remember him smoking them sitting in his easy chair after work, with feet up on the ledge by the fire burning in the fireplace.  Growing up it was my job to clean them and he liked the inner bowl and stem coated with Watkins vanilla, leaving a little of that liquid in the bowl to soak in when I put them back on the rack. Dad quit smoking later in life and so they’ve sat on the racks for many years unattended, a part of his area by his easy chair and fireplace. Dad passed when he was 89 years old and it finally is time for the pipes to move on. I’m very happy they are being restored by you and your brother and hope they find homes who enjoy them as much as Dad did. Thank-you for your care and interest. — Kathy, the oldest daughter

Kathy, once again I thank you for providing this beautiful tribute to your Dad. We so appreciate your trust in allowing us to clean and restore these pipes. I am also trusting that those of you who are reading this might carry on the legacy of her Dad’s pipes as they will be added to the rebornpipes store once they are finished.

Jeff cleaned this one up before he sent it my way. He is really good at the cleanup work. He had reamed the bowl with a PipNet pipe reamer and followed up with a Savinelli Fitsall pipe knife to remove the cake. He scrubbed out the mortise and the airway in the shank and the stem with alcohol, cotton swabs and pipe cleaners. He scrubbed the exterior of the bowl, rim, shank and stem with a tooth brush and Murphy’s Oil Soap to remove the oils and tars on the bowl, plateau rim and shank. He rinsed it under running water. He dried it off with a soft cloth. The lava mess on the rim was thoroughly removed without harming the finish underneath it. It revealed the burned areas on the inside edge of the rim that I was wondering about. However, without the grime the finish looked really good.  The feather or leaf carvings in the briar of the bowl and shank look good and the inset of what I thought looked like copper was flat. The acrylic stem would need to be worked on but I really like the shape. I took photos of the pipe to show its condition before I started my work on it. I took some close up photos of the rim and bowl to show the damage to the rim top and edge. Jeff did a great job on the cleanup but boy did it reveal some damaged spots. I have circled the damaged areas in red in the first photo below. I have also included some photos of the stem to show the condition before I polished it.The pipe has some stunning grain and then it has this copper coloured insert in the side of the bowl (It may well be a piece of copper, I will know more once I polish it). I am still trying to figure this out. I wrote an email to Butz-Choquin to see if they can give me information on the line. We shall see. The next photo shows the inset.The next photo shows the leaf or feather carvings on the shank and the grain pattern. This is a pretty piece of briar.I had an interesting challenge ahead of me – to try to remove some of the damage to the rim edge without damaging the carved feather/leaf on the rim top. I needed to reduce the burned area on the rim top so that I could bevel the edge inward to hide the darkening in those spots. I progressed slowly on the topping board, checking every couple of rotations to make sure I was not making things worse.Once I had the burn damage removed I worked on the darkening on the top surface of the rim toward the front and at the back side of the bowl. I was able to minimize the damage on the top. I sanded those areas with a folded piece of 220 grit sandpaper to blend it in better. I beveled the rim inward with a folded piece of 180 and 220 grit sandpaper. I was happy with the finished look of the rim edge. A good blend of stains will blend in the edge even more.I stained the rim top with a Maple stain pen first to blend it into the rest of the bowl. I worked on the inner bevel with Cherry and Walnut stain pens to darken the edge of the rim. I feathered the stain toward the out edge of the rim top and buffed it by hand to smooth out the transitions between the pens.I rubbed down the briar with Before & After Restoration Balm. I worked it into the carved feather/leaf patterns around the bowl, rim and shank. I rubbed it into the smooth portions to clean, enliven and protect the briar. I worked it into the briar with my fingertips and the help of a horsehair shoe brush. I let the balm sit for a little wall and then buffed with a cotton cloth to raise the shine. Here is where things are after the balm. I polished the briar with micromesh sanding pads – dry sanding with 1500-12000 grit pads. As I polished the briar the inset metal began to stand out. I was pretty certain that it was a piece of copper. It really began to shine and flash on the side of the bowl. It was an interesting touch to add that kind of adornment to a pipe. I set the bowl aside at this point and turned to work on the stem. I used 220 grit sandpaper to sand out the tooth chatter on both sides of the stem at the button. I also worked on the edge of the button to reshape it at the same time.I polished the acrylic stem with micromesh sanding pads – wet sanding with 1500-2400 grit sanding pads and dry sanding it with 3200-12000 grit sanding pads. I wiped it down after each sanding pad with a damp cloth.

 

Restoring a STANWELL # 89


Blog by Paresh Deshpande

This pipe, because of its interesting Dublin shape with a round rim, beautiful grain and it being a STANWELL, had been attracting my attention for some time now. However, I was always relegating its restoration since the condition was far worse and would require a ton of work as well as time to complete it.

After I had finished the pair of KRISWILLS, I could not think of working on any other pipe but this STANWELL!!!!!! And so, here I am with this pipe, admiring the shape, feel of the pipe in my hand and the beautiful grain that could be seen through all the dirt, oils, tars and grime.

A medium sized fancy Dublin with an oval shank, this pipe has beautiful densely packed birdseye grain on either side of the bowl with lovely cross grain extending from the front of the bowl right down the bottom to the shank end. Similarly, the grain extends from the back of the bowl up to the shank end!!!!! The flattish surface of the shank further accentuates the dense grain. No wonder then that this Stanwell is stamped as “SELECTED BRIAR”!!!!!!!! This beauty is stamped “STANWELL” in an inverted arch over “REGD No. 969- 48” over “HANDMADE” on top of the shank while on the bottom of the shank it is stamped “SELECTED BRIAR” over “89” over “MADE IN DENMARK”. The stem is stamped on the top of the saddle with a crown over “S” and on the bottom of the saddle with “HANDCUT”.All the stampings are crisp and easily readable.

I searched the net for information on this brand in general and this pipe in particular. The first site I always visit is Pipedia. I gathered a lot of information about the brand and some important snippets of information are reproduced below:

Stanwell Article from smokingpipes.com

When pipe smokers talk about pipes that are consistently great smokers, exhibit the creative and beautiful designs that exemplify Danish pipemaking and offer the best value in factory produced pipes, they are talking about Stanwell. We hear time and time again, from customers and top pipe makers from around the world, that Stanwell is the best factory produced pipe in the world. Stanwell maintains the most modern pipe making facility in the world and for many years has enjoyed some unique relationships with many legendary Danish pipe makers. In fact, Stanwell occupies a pivotal place in the history of the world-wide popularity of Danish-made pipes.

At the end of the war, briar became available again, so Nielsen began importing his own briar and started making briar pipes to compete with the English manufacturers. It must be remembered that in 1948, England was the single great center for pipe making. Therefore, Nielsen changed the name of his pipes to “Stanwell”, which sounded much more like a proper English name than “Nielsen”. He also created the horse drawn carriage logo for its English connotations. He later changed his own last name from Nielsen to Stanwell, a testament to his devotion to the pipes he made. Stanwell’s relationships with Danish pipe makers goes back to Sixten Ivarsson, who is considered the originator of modern Danish pipe making. Ivarsson was commissioned to design Stanwell shapes. In 1969, the factory was moved a town called Borup, just outside of Copenhagen to be closer to Ivarsson.

Essentially the goal of Stanwell is, and always has been, to produce high quality pipes at a price that is truly within the reach of the common man. In this they have succeeded admirably, offering perhaps more pipe for the money than any other pipe manufacturer in their price range. Stanwell pipe offers exceptional quality at a remarkably affordable price. Today it often seems that there are few options in between low cost, very low quality pipes and the handmade pipes that fetch hundreds of dollars. Stanwell manages to fill this void commendably by offering pipes close to the quality of the handmade with prices that are only slightly higher than drug store pipes.

Stanwell pipes are a must for any pipe collection. The Stanwell name is a cornerstone of Danish pipe making. In owning a Stanwell, you will not only enjoy beautifully styled, great smoking pipe at a great price, you will own a piece of pipe making history.

Now that I have some historical information about the brand, I went ahead with my attempt at dating this pipe. I had read that Mr. Basil Stevens is generally considered an authority on Stanwell pipes and so that was logical start point for me. I gathered some information from a site, https://www.scribd.com/document/45022903/Stanwell-Dating-Pricing-Information-by-Basil-D-Stevens, which I have reproduced from the above site:-

Dating Information:

1) Regd. No. stamping discontinued in late 1960s to very early 1970s. This is the Stanwell trade mark registration. The “48” indicates that the registration was made in 1948. (info rec’d from Jorgen Grundtvig, Managing Director, Stanwell A/S)

3) Up until the early 1960s only the top pipes, e.g. “Hand Cut” had the stem/mouth pieces stamped with the Stanwell logo of a crown over “S”.

6) “Handcut” stamped on black vulcanite stems have not been done since at least the 1970s and possibly earlier. (info from J.G.).

STANWELL SHAPES
Shape “89”
Two versions of this shape number
a) Freehand, oval stem, short oval saddle mouthpiece, by Sixten Ivarsson.
b) Large pot, thin, long saddle mouthpiece.

From the above information that I have gathered and highlighted in blue, I feel that this particular pipe was from the 1960s and is a freehand made by Sixten Ivarsson. Any variation or additional information or any incorrect assessment on my part may please be conveyed through your comments on rebornpipes.com

Armed with this information, I carried out my detailed initial visual inspection of the entire pipe. This assessment helps me in identifying the issues that are seen as well as understand likely issues that may present themselves subsequently while making a mental map of the entire restoration process.

INITIAL VISUAL INSPECTION
The stummel is covered in oils, tars and grime to such an extent that the bowl is very dull to look at with all the grains hidden and sticky to the touch. This will need thorough cleaning. Whether to sand the bowl with micromesh pads to bring to fore the lovely grain will be decided later. The bowl is heavily caked and has large amounts of lava overflow on top of the rim. The internal condition of the bowl and rim will be ascertained only after the cake has been completely reamed out. There is always the fear of possibility of charred rim edges or burn fissures or charred briar inside the chamber of pipes in this condition. However, the entire stummel appears solid to touch from the outside reducing the probability of any of the above possibilities being present.The short oval saddle stem is heavily oxidized with a number of light tooth chatter on both surfaces. The lips on both sides have been chewed off. I had masked both the stampings on the stem with a whitener pen, you could of course use acrylic paint or any other stuff, but I found the whitener pen to be the best option as it helps to fill the letters at a later stage. As expected, the airway is clogged and a test draw was rewarded with debris and carbon dust. This will have to be cleaned.THE PROCESS
The first step that I usually follow is the reaming of the bowl. Using a Kleen Reem pipe tool and my trusty and effective fabricated knife, Abha, my wife, cleaned out the cake from the chamber. To smooth out the inner surface of the chamber and completely remove the last traces of remaining cake, she sanded the inner surface with a 220 grit sand paper. With a sharp knife, very gently scraped the surface of the rim top and removed the accumulated tars, oils and grime.She cleaned the bowl and rim using undiluted Murphy’s Oil soap and a toothbrush. Thereafter, the bowl was washed under running tap water and immediately dried out using paper towels and a soft cotton cloth.

The stummel is now clean and fresh. Inspection of the rim and chamber revealed an intact inner edge and a perfect condition of the inner walls of the chamber. What a relief this was!!!!! The only issue was that the rim top is still blackened and an eye sore. I addressed this issue by sanding the rim and the entire stummel with micromesh pads. I very lightly and briefly wet sanded with 1500 to 2400 pads, gently wiping with a moist soft cloth to remove the dust left behind due to sanding.I dry sanded the rim and stummel using 3200 to 12000 grit micromesh pads. At the end of the dry sanding, I rubbed a small quantity of “Before and After Restoration Balm” with my fingers into the briar. The immediate and incredible transformation that takes place is a worthy reward for all the efforts!!! The bowl now looks fresh and attractive with the grains popping out any which way you look at the briar; it feels somewhat like DIWALI, festival of lights celebrated here in India. I polished off the balm with a soft cloth to a lovely shine. I AM ABSOLUTELY IN LOVE WITH THIS PIPE!!!!!Turning my attention to the stem, I started by sanding the stem with a 220 grit sand paper. I was especially careful around the edges and the stampings. Using the crisp edge of the folded sand paper, I reshaped the buttons and sanded it to even out the surface. Thereafter, I sanded the stem with 320 and 440 grit sand paper. To finish the stem I went through the complete set of micromesh pads, wet sanding with 1500 to 2400 pads and dry sanding with 3200 to 12000 grit pads. I wiped the stem with moist cloth after each pad and rubbed olive oil into the stem after every three pads. I carefully removed excess whitener from the stampings. The stem is now looking nice and shiny with crisp stampings. Having addressed the “appearance” aspects of this beauty, I turned my attention to the “performance” aspect to ensure that this beauty smokes as well as it looks. I thoroughly cleaned the shank internals using shank brush, pipe cleaners, cue tips and isopropyl alcohol. The stem airway was cleaned using regular pipe cleaners and also bristled ones dipped in alcohol. The airway is now clean and the draw is full and open.

To complete the restoration, I rubbed a minute quantity of PARAGON WAX on the stummel and the stem. After a few seconds, using muscle power and a microfiber cloth, I polished the entire pipe to a lovely shine. Can’t wait to load and fire up this stunning piece of briar!!!! The finished pipe is shown below and yes… for the curious reader, the prop is not Beer filled mug, but a Beer mug filled with GREEN TEA!!!!! Thank you for your valuable time spent in reading my amateurish chronicle.

Restoring a Kriswill “Golden Clipper”


Blog by Paresh Deshpande

“………. and now make me handsome and desirable too!!!!!” This is what the sibling of the Kriswill “CHIEF”, the “GOLDEN CLIPPER” appeared to be demanding of me and who am I to refuse this lovely pipe. So here I am with all my enthusiasm to work on this beautiful pipe with mixed grains.

This was one of the pair of Kriswill pipes which was dug out by my younger daughter from the large pile of pipes, the other being Kriswill “CHIEF”. Both these beauties had an issue with their stems. The stem of the “CHIEF” did not sit flush with the shank and appeared smaller in diameter compared to the shank, while the stem of the “GOLDEN CLIPPER” sat flushed with the shank but was larger in diameter than the shank. I addressed this issue in an ingenious way and completed the restoration of the “CHIEF”. For those interested in knowing the issue of stem in detail, process to address it and the complete restoration, please follow the link https://rebornpipes.com/2018/08/04/breathing-new-life-into-a-kriswill-chief-20/. I am sure you will find it an interesting read.

My joys knew no bounds when the “CHIEF’S” stem fit perfectly like a glove in the shank of the “CLIPPER” (the time-consuming, cautious, accurate and nerve-wracking but enjoyable work of matching the stem and shank of the “CHIEF” still fresh in my mind!!!!!!). Here are the pictures of a perfectly matching stem and shank on the CLIPPER.This KRISWILL “GOLDEN CLIPPER” has a medium sized bowl with mixed grain. It is stamped “KRISWILL” over “GOLDEN CLIPPER” over “HANDMADE IN DENMARK” on the left side of the shank. At the bottom of the shank and close to the edge of the shank where it takes the stem, is stamped with number “54”.As I had determined the dating of this pipe, while searching information for the “CHIEF”, from 1970s (the snowflakes stamp on the stem and block letters on the shank were adopted post 1970), I proceeded to carry out a visual inspection of the condition of the pipe in my hand. This helps me map the road to restoring the pipe by identifying the issues involved and identify methods/ options to address the same.

INITIAL VISUAL INSPECTION

The bowl is covered in dust, oils, tars and grime of yesteryear. It is filled with a thick cake and the lava has overflowed on to the rim. I would still say that this bowl is not as heavily caked as I have gotten used to with my grand old man’s pipes. The cake has completely dried out.The rim surface is pock-marked with few minor dents and dings of being banged around. Exact extent of damage, there appears to be some, to the inner edge will be known after the bowl has been reamed down to its bare briar. The outer edge of the rim appears to be in decent condition.The interchanging of stem with the CHIEF ensured a perfect fit of the stem on this pipe and required no matching the fit to the shank end. The stem is, again comparatively to what I have dealt with before, lightly oxidized with light tooth chatter. The lip has been bitten off at one place and will need to be rebuilt and reshaped. There is some calcification seen around the lip on either surface. As I have come to expect, the airway in the stem is blocked and the mortise is clogged with gunk, debris and tars. I will need to clean both to ensure an open draw.The stummel needs to be cleaned. I will have to decide if I should retain the stain finish or polish it to its natural look and match it to its bigger sibling, the “CHIEF”.
THE PROCESS
Abha, my wife, dealt with the cake by reaming the chamber with a Kleen Reem pipe tool and a British Buttner pipe tool. Using the fabricated pipe knife, she further scraped the cake from the bottom of the bowl and also the walls of the chamber. She was especially very careful while reaming with the knife so as not to damage the inner edge of the rim. Once the solid briar was exposed, she further smoothed the walls and removed remaining cake by sanding with a 180 followed by 220 and 600 grit sand paper. Another advantage of this process is the elimination of traces of ghosting to a great extent. She gently scraped the rim top with the sharp edge of the knife and removed the accumulated overflow of lava. Abha followed this by scrubbing the chamber walls with cotton swab dipped in isopropyl alcohol. This removed the fine cake dust, leaving the chamber clean, fresh and smooth. As can be seen from the picture, after the cleaning, the dents and dings are more pronounced and will need to be addressed. Further, if observed closely, there is a small chip to the inner edge which can be seen on the right side in the 3 o’clock direction. I had the following two courses of action to choose from to address these issues:-
(a)        Create a slight bevel on the inner edge to eliminate the inner edge chip.
(b)        Topping the rim on a topping board.

Abha suggested proceeding with the second option since the “CHIEF” was without a bevel and as these were together, she wanted to maintain the similarities as far as possible. I concurred with her since topping will also address the minor dents and dings seen on the rim top. I gently topped the stummel on a 220 grit sand paper, frequently checking the progress.  This is very important since you do not want to lose too much briar and there is always a fear of distorting the proportions of the pipe due to excessive sanding. How much sanding is sufficient, is a question to which the answer can never be quantified. For me the mantra is, topping or sanding should be kept to the minimum and preserve maximum briar even at the cost of very minute dents/ chips being visible.

I topped the bowl just enough to address the dents and dings on the rim surface. The small nick to the inner edge of the rim has also been addressed to a great extent, but not completely. It is barely perceptible in person and acceptable to me. Hence, I left it at that!!I cleaned out the internals of the shank/ mortise and airway using pipe cleaners, cue tips and isopropyl alcohol. Thereafter using undiluted Murphy’s oil soap and tooth brush, I cleaned all the tars, oils, dust and grime from the bowl and washed it under running water. I wiped it down with paper towels and a soft cotton cloth.

Using a brown stain pen (Yes!!! I finally have them, thanks to my guru, Mr. Steve who had diligently packed them with the pipes that he had sent me after repairs, when he learnt that I was unable lay my hands on them), I stained the rim to match the rest of the bowl and set it aside to dry out. In my haste to finish the restoration, I forgot to click pictures of the above mentioned process and the look of the pipe at this stage.

While the stummel was kept aside for drying, I turned my attention to the stem. Starting with the use of Bic lighter, I painted the surface with its flame to raise the tooth chatter and bite marks as much as possible. I scrubbed the stem with a piece of moist Mr. Magic Clean sponge to clean the stem of the calcification. Minor tooth chatter was addressed to a great extent, however, some stubborn and deep bite marks and the bitten off lip stood out like sore thumb!!! Having learnt my lessons and working around the handicap of glue, I spot applied clear CA superglue with a tooth pick and set it aside to cure over night. The next morning, I applied another layer of the superglue and set it aside to cure. The reason I decided to adopt this technique is because the glue I have and available to me is of very thin consistency and hence the layering technique. After 24 hours, I checked the fills and proceeded to sand down the fills and reshape the edge of the button with a flat head needle file to match the surface of the stem. Using a 220 grit sand paper followed by wet 320 grit sand paper, I evened out the fill and removed oxidation from the stem surface. Thereafter, I used micromesh pads, wet sanding with 1500 to 2400 pads and dry sanding with 3200 to 12000 pads. I deeply rubbed a very small quantity of Extra Virgin Olive oil after every three pads. I am pleased with the way the stem has turned out. It is now smooth and shiny.Using normal and bristled pipe cleaners dipped in alcohol, I completely cleaned out the airway in the stem till the pipe cleaners came out nice and clean from the other end. However, when I checked the draw, I found it to be constricted and laborious. It was not a free flowing and open draw. I checked the alignment of the airway in the stem and shank and realized that the airway was not aligned. With a rounded needle file, I file down the tenon hole and the mortise opening in the shank to the point where there are perfectly aligned. Now the draw is full and open.

By this time, the stain on the rim top has dried out and I applied a small quantity of Before and After Restoration balm to the entire surface of the stummel, including the rim top. This product is absolutely fantastic as it freshens up the briar and makes the grain to pop out. Using a horse hair shoe brush, I buffed the bowl. Later, with a soft cotton cloth, I polished it to a nice shine. As a final touch, I rubbed a very small quantity of PARAGON wax on to the stem and the stummel. A few seconds later, using muscle power and a microfiber cloth, I polished the entire pipe to a lovely shine. Here are the pictures of the finished pipe. Hope you enjoyed reading the write up and yes, my apologies for the lack of pictures since I had to catch a flight late in the evening to rejoin my duty station, I forgot to take pictures at this stage as completing the restoration was priority task.

This Petite Bari De Luxe Freehand Speaks to me…


Blog by Steve Laug

I was emailing back and forth with John, a pipeman in Edmonton who wanted to sell of his pipes. He was cleaning up things and thought he would see if I was interested in them. He said that he had several Bari’s that were in the lot and he wanted to move those out. He sent me photos of the pipes he had and we soon struck a deal. Since we were both in Canada it did not take long for the package to make its way to me. I opened it and went through his pipes to see what I had to work on. There were some pipe racks and accessories in the box as well. I went through the pipes and set them aside. Today I decided it was time to start working on them. I chose a little Bari De Luxe as the first of those Bari’s that I would work on. I have included two of the photos of the pipe that he sent to me before I purchased the lot.You can see that it was a well-loved pipe and one that he smoked often. The finish was in good condition but dirty. The plateau on the shank end and the rim top was dusty and dirty. The rim top had a lot of tars and lava on the surface filling in some of the roughness of the finish. Under the grime the pipe looked to be in good condition. The stain highlighted the beautiful grain on the briar and the plateau was stained black in stark contrast to the reddish brown of the bowl. The bowl was caked and would need to be reamed but otherwise good condition. The stem had a sticky oily substance on it that almost smelled nutty. There was some oxidation under the oil but there were not any tooth marks or chatter on the surface. I took the following photos of the pipe before I began the cleanup. (The pipe came in an original Bari pipe sock. I have included it in the photos to give you an idea of the small, petite size of the pipe.) I took a photo of the pipe with the stem removed to give a look at the style of the fancy stem.I took photos of the stamping on both sides of the shank. On the left it was stamped Bari over De Luxe and on the right side it was stamped Hand Made in Denmark. The stamping was faint toward the bowl on both sides of the shank but was still readable.I went to Pipedia and refreshed my memory on Bari pipes. I was pretty sure that they were connected to Viggo Nielson but wanted a reminder. Here is the link to the article on Pipedia: https://pipedia.org/wiki/Bari. I summarized the material that I found there as it gives a clear picture of the brand. I have been working on several pipes by Viggo Nielsen recently so it was a good reminder.

Pipedia states that Bari Piber was founded by Viggo Nielsen in Kolding, Denmark around the turn of 1950/51. His sons Kai and Jørgen both grew into their father’s business from a very young age and worked there till 1975. Both have become successful pipe makers.

Bari successfully adapted the new Danish design that had been started mainly by Stanwell for its own models. Bari was sold in 1978 to Van Eicken Tobaccos in Hamburg, Germany though the pipes were still made in Denmark. From 1978 to 1993 Åge Bogelund and Helmer Thomsen headed Bari’s pipe production.

Helmer Thomson bought the company in 1993 re-naming it to “Bari Piber Helmer Thomsen”. The workshop moved to more convenient buildings in Vejen. Bogelund, who created very respectable freehands of his own during the time at Bari got lost somehow after 1993. Bari’s basic conception fundamentally stayed the same for decades: series pipes pre-worked by machines and carefully finished by hand – thus no spectacular highgrades but solid, reliable every day’s companions were what they turned out. The most famous series are the smooth “Classic Diamond” and the blasted “Wiking”.

I started my cleanup of this pipe by working on the internals. I scraped out the remaining cake in the bowl with a Savinelli Fitsall Pipe Knife (I totally forgot to take photos of that part of the process). I cleaned out the airway in the shank and the stem with pipe cleaners and alcohol. I cleaned out the mortise in the shank with cotton swabs and alcohol. It was dirty but I was surprised it was as clean as it was. I rubbed some Before & After Restoration Balm into the surface of the briar to enliven, clean and preserve it. I rubbed it in with my fingertips working it into the briar. I worked it into the nooks and crannies in the plateau on the rim and the shank end using a cotton swab. I brushed those areas with a shoe brush to work it in more deeply and spread it out. I set it aside for a little while to let the balm do its work. I buffed it off with a cotton cloth and then buffed it with a microfiber cloth. The photos below show the pipe at this point in the restoration process. I set the bowl aside and turned my attention to the stem. I wiped the oily, sticky stuff off of the surface of the stem with alcohol on a cotton pad. The smell of the stuff was almost nutty, like peanuts or something similar. It needed to go so that I could work on the stem.I sanded the light tooth chatter out of the surface of the stem and also worked over the oxidation that was prevalent in the grooves and spindles of the stem using 220 grit sandpaper. I forgot to take photos of that part of the process. I polished the stem using micromesh sanding pads – wet sanding with 1500-2400 grit pads and then buffing on the wheel with red Tripoli. I dry sanded the stem with 3200-12000 grit pads to further polish it. After each pad I wiped it down with Obsidian Oil to protect and enliven the stem. When I finished the last pad I gave it a final coat of oil and set it aside to dry. This small Bari De Luxe Freehand is a real beauty with straight and flame grain all around the bowl. The shank end and bowl rim are both beautiful plateau that is deep and craggy. The brown of the bowl and the black of the plateau look really good with the black of the turned vulcanite stem. I buffed the bowl and the stem with Blue Diamond polish to raise the shine on the briar and the vulcanite. I lightly buffed the rim top and shank end as well. I was careful to not buff the stamping and damage it. I gave the bowl and stem multiple coats of carnauba wax. I buffed the entire pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The finished pipe is shown in the photos below. The dimensions of the pipe are: Length: 5 1/4 inches, Height: 1 3/4 inches, Outside Diameter: 1 1/2 inches, Diameter of the chamber: ¾ of an inch. This is the first Bari De Luxe that I have worked on and the petite size and rugged looking plateau make it a pipe that I may hang on to for a while and enjoy. I am looking forward to enjoying my first bowl in it. Thanks for walking through the restoration with me.

 

 

 

The Last of Boston’s Peretti Oom Paul Sitter Recommissioned


Blog by Dal Stanton

I’ve enjoyed restoring a Lot of 10 Peretti pipes and recommissioning them for new stewards.  All the Oom Pauls in the picture below, except for one which I added to my collection, are in the hands of new stewards except for the one on my worktable now.  I have been pleased to hear back from stewards who have these Oom Pauls and often I’ve heard that they have become favorites in their rotation lineups! I like Perettis myself and have a healthy collection of them.  They are great smokers in my experience and my Peretti Oom Paul is a favorite for me too – he hangs on the chin perfectly, like a good lap dog!  When I began my research on the L J Peretti name, I was surprised to discover that it is not an Italian pipe as one might expect with such a name!  In fact, I discovered the genesis of a significant story of Americana pipe history with the establishment of the L. J. Peretti Company of Boston in 1870 (Pipedia citing: Pipes, Artisans and Trademarks, by José Manuel Lopes), the second oldest tobacco shop in the US, second only to Iwan Ries & Co. of Chicago established in 1857 (See: Link).  The Peretti family originally comes from Switzerland, but the Italian name is explained by the fact that they originated from the southern slopes of the Swiss Alps which flows south toward Italy more easily than to the north – the heart of Switzerland.  The Calabash (upper left) and the Goliath Billiard (bottom) are waiting to be restored to be added to my collection of Perettis.  The hefty Egg in the middle is already in my lineup!Brian commissioned two pipes (See: For ‘Pipe Dreamers’ Only), a nice looking Jobey Hand Rubbed Dublin (next on the worktable) and the Oom Paul Sitter before me – both pipes benefit the Daughters of Bulgaria – helping women and girls who have been trafficked and sexually exploited.  Thanks Brian!  For a close-up look at the Oom Paul Sitter, I take several pictures on my worktable.  The nomenclature is the simple L.J. PERETTI stamp on the left shank.  This Oom Paul shares every single challenge that his former brothers had – the former steward seemed to have a scorched earth policy.  The chamber is heavily caked, and the rim scorched.  The rim challenges are the most daunting for this restoration.  The stummel has a build up of grime and minor nicks from usual wear.  The stem has significant oxidation and bit clenching and chewing which needs addressing.  To begin the restoration of this, the last Peretti Oom Paul Sitter in need of a new steward, after cleaning the internal airway with a pipe cleaner dipped in isopropyl 95%, I put the stem in a soak with Before & After Deoxidizer along with 5 other stems.  After some hours soaking, I fish out the Peretti stem and wipe off the raised oxidation with a cotton pad wetted with light paraffin oil (mineral oil in Bulgaria).  The Deoxidizer seems to have done an adequate job. Next, I attack the chamber carbon cake build up using the Pipnet Reaming Tool.  Putting paper towel down to minimize clean up, starting with the smallest blade head, I use 3 of the 4 blades available to me. I follow the blade heads by using the Savinelli Fitsall Tool to reach down into the chamber to scrape more carbon off the wall.  Then, to clean the chamber and to bring out fresher briar, I sand the chamber using a piece of 240 grit paper wrapped around a Sharpie Pen.  To remove the thick carbon dust left behind, I wipe the chamber with cotton pads wetted with alcohol.  After clearing the cake away, a look into the chamber reveals no problems – no heat cracks or fissures.  Good! Now to scrub the stummel surface and the rim with its thick lava I start with undiluted Murphy’s Oil Soap and cotton pads.  I also use a brass brush on the rim to break up the lava crust.  To scrape the rim, I use a pin knife as well as the straight edge of the Savinelli Fitsall tool.  As I scrape the crust off, I also remove the scorched charcoal that is on the inside of the rim mainly on the left side of the stummel – the area where the former steward damaged all his pipes.  The result is that the left side of the rim is narrower after the cleaning.  The stummel is in great condition – the rim is the challenge. Before moving on with the rim repairs I continue with the internal cleaning of the stummel.  Using pipe cleaners and cotton buds dipped in isopropyl 95% I go to work. I also employ a dental scalpel to scrape the internal wall.  I’m pleased that there wasn’t too much resistance.  At the end of my work day I’ll continue the cleaning process by giving the stummel a kosher salt and alcohol soak.Turning now to the stem, I begin addressing the tooth dents and chatter on the bit.  With his brother Oom Pauls, there usually was some button damage too, but this guy’s in better shape in that regard.  I first use the heat method to raise the vulcanite dents to make them less severe.  By heating the vulcanite, it expands, and the dented vulcanite naturally seeks its original positioning.  I use a Bic lighter and paint the upper and lower bit and after heating several passes, I do see a lessening of the severity of the dents as the vulcanite expands.  As a result, I can sand the remaining dents out with both the upper and lower bit.  Before the heating:After the heating:I sand out the damage using 240 grit paper.I move on to using 600 grit paper by wet sanding the entire stem.  I follow this with 0000 steel wool sanding/buffing the entire stem.Moving forward with the stem, I wet sand using micromesh pads 1500 to 2400 followed by dry sanding with pads 3200 to 4000 and 6000 to 12000.  To revitalize the vulcanite, I apply a coat of Obsidian Oil after each set of 3 pads.  I love the glossy pop! Looking now to the stummel, I see a few very small, nicely camouflaged fills which are in good shape, but I see one significant cut into the briar that needs attention.  To address it, using a toothpick, I lay a line of thick CA glue over the cut.  I set the stummel aside to allow the patch to cure.After a while, the patch has set enough for me to work on the rim.  The bad news is that the loss of briar on the left side of the internal rim from scorching is gone – it can’t be replaced.  The good news is that the aesthetic imbalance of the rim as a result can be mitigated somewhat by creating a bevel around the entire rim.  The bad news – there is additional loss of briar.  In restoring a pipe there’s always this tension between loss and gain.  With this Peretti, as with all his Oom Paul brothers, I did the same thing and they turned out well.  I start the process by taking the stummel to the topping board to remove the damaged wood on the top. Topping an Oom Paul can be a challenge because the shank extends beyond the plane of the rim.  So, to top the rim, the shank needs to hang off the side, so it isn’t unintentionally topped!  I take a picture to mark the start. I turn some rotations on the board and check out the progress.  I also utilize a small sanding block which allow me to focus on a certain area of the rim.  After the 240 paper, I put 600 grit paper on the board and do a few more rotations.  The pictures show this progress. Now, using a tightly rolled piece of coarse 120 grit paper, I begin beveling the internal rim edge – hoping to bring more balance to it.  I take a bird’s eye picture first to mark the progress.  I pinch the paper under my thumb as I move it in the areas of the rim to be reduced.  While I work on equalizing the rim diameter, I’m also sanding down the chamber to taper the walls as they move downwardly.  I’m looking for greater aesthetic balance.  I come to the point where I’ve done all I can do.  I think it looks much better.  I do another bird’s eye shot for comparison. I take the stummel one more time to the topping board using 600 grade paper.  I do this simply to reestablish the lines after the sanding. One more thing I want to do with the rim.  I’ve worked on the inside balance, now I also introduce a very gentle bevel on the outside of the rim.  I do this to soften the edge which is sharp after the topping.  I use 120 grit paper then 240 and finish with 600 – each rolled tightly.  With the rim repair done, I take the flat needle file and begin to file down the patch on the side of the stummel.  When I bring the patch down close to the surface, I switch to using 240 grit paper to remove the excess patch to the briar surface, making the patch area flush with the surface.  I then finish the sanding with 600 grit paper.  The patch will blend well later.My day has ended and I will continue the cleaning process of the stummel with a kosher salt and alcohol soak.  This freshens the briar and draws out more latent tars and oils from the briar.  I fashion a wick from a cotton ball by pulling and twisting it.  I insert it down the mortise and airway.  I then fill the bowl with kosher salt, which has no aftertaste, and then put isopropyl 95% into the bowl until it surfaces over the salt.  I wait a few minutes and top off the alcohol and turn out the lights. The next morning the soak has done the job through the night.  The salt and wick show soiling from the tars and oils.  I clean the stummel of residue salt with paper towel, blowing through the stummel, and to be on the safe side, I run a cotton bud with alcohol through the mortise to clean up any leftover remnants – after a couple of cotton buds I move on. The next step is to address the external briar surface of the Peretti Oom Paul Sitter.  I filled the one cut I saw on the surface that stood out.  There are other nicks and scratches that are normal from use.  To address these, I use micromesh pads.  I first wet sand using pads 1500 to 2400, then dry sanding 3200 to 4000 and 6000 to 12000.  The grain looks good as the micromesh pads coaxed it out.  The one bummer is the darkened wood from the scorching damage around the inner edge of the rim.  That will not go away because it would sacrifice too much briar to accomplish it. Since the rim had been topped and sanded, it is a shade lighter than the rest of the stummel.  To remedy this, I apply a maple color dye stick around the rim.  I forgot to take a starting picture for comparison but here is the aftermath.  It looks good and matches well.As I’ve done with all the other Peretti Oom Pauls (and one Bent Billiard!) I restored, I kept the color true to the original as much as possible.  To do this I used Before & After Restoration Balm on the briar and it does a great job deepening and enriching the color already there.  I do the same with this Sitter.  I squeeze some of the Balm on my fingers and work it into the surface.  The Balm starts with the consistency of light oil but as it is worked into the briar it gradually thickens to a wax-like feel.  After applying it fully and working it in, I set the stummel aside for a while, about 30 minutes to allow the Balm to do its thing and take a picture.After about 30 minutes I use a clean cloth to wipe and buff off the Balm.  I’m pleased with the results.  Turning now to the application of Blue Diamond compound, I rejoin stem and stummel, mount a cotton cloth wheel onto the Dremel, set the speed at 40%, and methodically apply the compound.  After finished, I wipe the pipe with a felt cloth to remove compound dust in preparation for the wax.  I mount a different cotton cloth wheel to the Dremel dedicated to applying carnauba wax, leave the speed at 40% and again, methodically apply a few coats of wax to stem and stummel.  I finish the restoration of the Oom Paul Sitter by giving the pipe a rigorous hand buffing with a microfiber cloth to raise the shine.

I am very pleased with the restoration of this, my last for now, Peretti Oom Paul Sitter.  The grain is rich on the huge, ample bowl which is the reason many pipe men and women desire an Oom Paul in their collections. The added benefit to this Oom Paul is that it is a Sitter.  He can comfortably join his steward at a table playing cards or board games!  Brian commissioned (see For ‘Pipe Dreamers’ Only) this Peretti Oom Paul Sitter and will have the first opportunity to acquire it in The Pipe Steward Store.  This pipe benefits the Daughters of Bulgaria – women and girls who have been trafficked and sexually exploited.  Thanks for joining me!

Repairing a Chipped Button on a ≠ Ago Hand Made In Italy


Blog by Steve Laug

I received an email from Dave, a reader of rebornpipes about a pipe he had purchased recently. It seemed that he had dropped it after just a few smokes and chipped the top edge of the button. I told him I would have a look at the pipe and see what I could do with the chip in the button edge. It would be hard to know until I received the pipe to have a plan of repair but it was worth a shot. When the pipe arrived it was actually a beautiful pipe – well made, beautiful grain, handmade with a black Lucite stem that fit snuggly on the shank. The chip was small but very visible and had sharp edges. I have circled it in red in the second photo. This was the first ≠Ago pipe that I worked on. It was quite impressive. I can see why Dave wanted me to repair it for him. I took some close up photos of the rim top and the stem. The rim top and the bottom of the bowl had some beautiful birdseye grain. The bottom is stamped ≠Ago over Hand Made over Italy. The Lucite stem is well made. The ≠ logo is inset on the top side of the stem. The topside of the button has a chip out of it. I have circled it in red as is shown in the second photo below.I tried to take a close up photo of the chip in the topside of the button. It came out a little blurry but the chipped area is still visible.Once I had looked the pipe over and examined the chipped area I wrote Dave back to let him know that I would be glad to give the repair a try. I also asked him about the brand as it was a new brand to me. He wrote back the following email…

Steve:

Thanks so much. It is a terrific pipe.‎ The guy who makes them — actually he and his staff — is Gianmarco Ago. You won’t find his pipes in any stores. He’s made his name via the Internet, specifically Facebook. If you go online on Facebook, he has 2 pages:

* Gianmarco Ago‎
* Pipe ≠ Ago Hand Made In Italy Lifetime Guarantee

Go to either — or both — and click on “photos” so you can see a couple of years’ worth of his pipes. I have several and they are all very good smokers.

I can’t begin to tell you how much I appreciate your doing your “Lucite” thing and fixing the stem… Again, my thanks.

Best regards, Dave

I went to the Pipe≠Ago page on Facebook to get some background and history on the brand. Here is the link to the page: https://www.facebook.com/pg/gianmarcoagopipe/about/?ref=page_internal. I have included a section from the page that they entitled “Our Story”. I quote:

Pipe ≠ Ago, came into being due to a lucky meeting between Gianmarco Ago and skillful craftsmen. From this meeting ≠ Ago was born, a unique line, devoted and reserved, consisting of few refined items.

The ≠ Ago line has not wished to participate in an already saturated market, but desires to be an emblem, a philosophy of this article is limited to the requirements of friends who embrace the art of pipe smoking and have become enamoured of these small masterpieces reaching out with their shapes, colours and materials to one’s inner depths.

Pipe ≠ Ago is a hymn to the skill of the craftsmen who produce them. The aim of ≠ Ago is to make these works of art a moment of thought and aggregation for all, an area of research and of an opportunity to share… the symbol “different from” is intended as a synonym of a search for values in a congenial essence in becoming, an expression of diversity in the sense, as it were of a spiritual and intellectual enrichment.

Now that I knew some background on the pipe and the philosophy of the ≠Ago Company it was time to work on the repair and see what I could do with it. I used the sharp end of a sanding stick to start layering the black super glue onto the chipped area. I knew that this would be a process of building layers up until the chipped area had disappeared into the surface of the button area. It took time to build it up because I let the repair cure between each layer. As they cured I would add another layer of the glue.When the repair hardened I shaped the sharp edge of the button with a needle fill to clean up the edge and remove the overflow of glue on the surface. The second photo shows the repair at this point in the process. I still needed to fill in a few spots and to reshape the slot to accommodate the repair.I sanded out the file marks in the surface of the Lucite stem with 220 grit sandpaper to blend it into the surface of the stem. I still need to shape the button a bit more. I started the process with a round and a knife blade needle file.I filled in the damaged areas a bit more with the glue and continued shaping the button with the needle files. I reshaped the repaired areas on the top and underside of the button.I continued to work on the shape of the slot. It was getting close and certainly looking better than when I started the repair.I polished the stem with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads to polish out the scratches from the sandpaper. I wiped it down with a damp cotton pad after each sanding pad. I continued shaping the slot with files and folded sandpaper. The repair is smooth with the face of the button. The edge is clean on the inside of the slot.I put the stem back on the bowl and buffed the pipe with Blue Diamond on the buffing wheel. I gave the bowl and stem several coats of carnauba wax and buffed the pipe with a clean buffing wheel. I hand buffed it with a microfiber cloth to deepen the shine. The finished pipe is shown in the photos below. Soon I will pack it up and ship it back to Dave. Thanks for reading the blog. It was an interesting challenge.

 

An email from France brought me another SINA pipe – a Horn Stemmed Chubby Billiard


Blog by Steve Laug

A couple of weeks ago I received an email from Jean Paul in France asking if I was interested in purchasing an old pipe he had. It was stamped SINA on the left side of the shank and on the stem. I asked him to send me some photos of the pipe to show me what he was offering. He sent me the following photos – a left side view, a top view and a photo of the pipe taken apart. The pipe was definitely an old one. The stamping on the left side of the thick shank and on the horn stem had remnants of gold stamping and reads SINA. The rim top was dirty and had a thick looking overflow but it was hard to see what the cake looked like. The inner and outer edges of the bowl looked to be in good condition. The horn stem was in excellent condition with some light tooth chatter on both sides of the stem at the button. There was an inner tube that ran from the tenon end into the bowl. It was heavily lacquered with tobacco oils and tars but otherwise in good condition. I sent another email and a payment via Paypal and the pipe was mine. The pipe was soon on its way across the Atlantic. The SINA brand was not uncommon to me as I have previously worked on another older SINA – a Rhodesian with a hard rubber stem. If you are interested in reading about the restoration of that old pipe the link will take you to the blog (https://rebornpipes.com/2014/08/28/giving-new-life-to-a-sina-rhodesian/). I have included two photos of the other SINA pipe in my collection. It is also an old timer from the same time period. When I worked on that pipe I did a bit of research to find out about the maker of the SINA pipe. I have included the information I found for that blog below. I figured it would be good to have it here as well as in the earlier blog. I quote:

I looked on Pipephil’s site and was able to find out that there was indeed a connection to GBD. The connection was with the French branch of GBD.From the screen capture above you can see the two links under the photo on the left. The first connects the pipe to the Marechal Ruchon & Co. factory that made GBD pipes. They eventually sold out to the Oppenheimer group. The French brand was also connected to C.J. Verguet Freres and to Sina & Cie which were sold to Oppenheimer in 1903-1904. In 1905-1906 Oppenheimer merged the two companies. The accompanying chart gives an overview of the twisted trail of the GBD brand and its mergers and sales. The chart also comes from the Pipephil site and was the second link under the above photo. Once I had refreshed my memory on the SINA brand I knew that this second pipe was made before the 1905-1906 mergers as well. It fits well with the thick horn stem and the shape of the button and narrow slot opening. The thick shank also fits well with the period. I really like the shape and style of this era of pipe history so this one would be a pleasure to clean up. I took the following photos of the pipe when I took it out of the box. It was really dirty as I had guessed from the presale photos. It was in good condition underneath it looked like but it was a mess. The outside of the bowl was very dirty grime and tars covering the front and right side of the bowl. The rim top had a thick coat of lava and tars and there was a thick cake in the bowl. The stem looked pretty decent other than tooth marks on the top and underside near the button. I took close up photos of the rim top and both sides of the stem to show its condition. You can see from the photo the thick cake in the bowl and the overflow on the rim top. The second and third photos show the tooth marks chatter on both sides of the stem at the button. The final photo shows the SINA in a logo stamped on the left side of the shank.I took photos of the bowl from a variety of angles to show the ground in grime and dirt in the briar on the exterior. I reamed the bowl with a PipNet pipe reamer starting with the smallest cutting head and working up to the third cutting head. I took the cake back to the walls of the bowl. I cleaned it up with a Savinelli Fitsall Pipe Knife to remove the cake that remained behind on the walls and on the bottom of the bowl. I sanded the inside of the bowl smooth with 180 grit sandpaper wrapped around a piece of dowel. I scraped the rim top with the Savinelli Fitsall Knife to remove the thick lava that had overflowed onto the rim. I wiped it down with acetone on cotton pads to remove the residual grime on the rim and around the bowl and shank.I took photos of the bowl after I had wiped it down with the acetone. The bowl looked quite good. There was some deep pits and nicks on the rim top and bowl edges as well as some burn marks toward the front of the bowl. I lightly topped the bowl with 220 grit sandpaper on a topping board. I worked over the inner edge of the bowl with a folded piece of 220 grit sandpaper.I polished the rim top and the rest of the bowl with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I wiped the bowl down after each sanding pad with a damp cloth. I touched up the stain on the rim top with an Oak coloured stain pen to match the rest of the bowl. I would blend in the stain later in the process.I rubbed some Before & After Restoration Balm into the surface of the briar to enliven, clean and preserve it. I rubbed it in with my fingertips working it into the briar. I set it aside for a little while to let the balm do its work. I buffed it off with a cotton cloth and then buffed it with a microfiber cloth. The photos below show the pipe at this point in the restoration process. I touched up the gold leaf in the oval SINA logo on the left side of the shank using Rub’n Buff Antique Gold. I rubbed it into the stamping on the shank side and pressed it into the stamp with the sharp point of a sanding stick. Once the gold had dried I buffed it off with a cotton cloth. The second photo shows the stamp after the touch up. It does not look too bad for a pipe made before 1905-06.I scraped out the inside of the shank with a dental spatula to remove the lacquered tars and oils that had hardened in the mortise. I don’t think this pipe had been cleaned since it was first smoked in the early 1900’s.I turned the inner tube in the metal tenon in the stem to remove it. It was pressure fit and the tars and oils had it held tightly in place. With it removed and the shank scraped clean the pipe was ready to be cleaned up.I cleaned out the inside of the mortise and the airway in the shank and stem with pipe cleaners, cotton swabs and alcohol.I used clear super glue to repair the tooth marks on the stem. I sanded the stem surface with 220 grit sandpaper to smooth out the chatter and wiped it down with alcohol on a cotton swab. I filled in the tooth marks with clear glue and set it aside to cure.When the repair had cured, I sanded the surface of the repairs on the stem with 220 grit sandpaper to smooth out the repairs and blend them into the surface of the horn stem. I forgot to take photos of this part of the process as I was anxious to see what the stem looked like polished. I quickly move on to polish the stem with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I wiped the stem down after each sanding pad with Obsidian Oil and after the final sanding pad I gave it a final coat of oil and set it aside to dry. The horn stem was beginning to look really good for a pipe of this age. I put the cleaned inner tube in the tenon and aligned the angle of the spear end so that it would sit on the bottom of the bowl when inserted in the shank. I took photos of stem at this point to show the inner tube.I used the sharp point of a sanding stick to apply Rub’n Buff Antique Gold to the stamping on the left side of the stem. I worked it into the grooves. I let the gold dry and then buffed it off with a soft cloth.This SINA, GBD predecessor is a beautiful pipe with mixed grain all around the bowl sides, top and bottom. The grain really is quite stunning. The rim top looks much better. The horn stem repaired easily and shined up well. I buffed the bowl and the stem with Blue Diamond polish to raise the shine on the briar and the vulcanite. I was careful to not buff the stamping and damage it. I gave the bowl and stem multiple coats of carnauba wax. I buffed the entire pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The finished pipe is shown in the photos below. The rich patina of the original finish allows the grain to really stand out on this pipe and it works well with the rich lustre of the polished horn stem. The dimensions of the pipe are: Length: 5 1/4 inches, Height: 2 inches, Outside Diameter: 1 3/8 inches, Diameter of the chamber: 3/4 of an inch. This old and beautiful SINA Chubby Billiard will sit next to the other SINA pipe in my personal collection. I am looking forward to enjoying my first bowl in it soon. Thanks for walking through the restoration with me.

Resurrecting a Badly Damaged BBB ** Billiard


Blog by Victor C. Naddeo

I have been following the Pipe Club of Brasil Group on Facebook for quite a while now and have enjoyed the posted that Victor Naddeo has made about his restoration work. He is the administrator of the Facebook Group and we have chatted back and forth. When he posted this restoration I was intrigued by his solution to the crack in the bowl. He sent me photos on Messenger and we talked about the repair and BBB pipes in general. Seems we are both devotees to BBB pipes. I asked him to write up this repair on an old BBB ** that was in very rough shape before he started. He gladly did so. I am hoping this is just the first of many blogs on rebornpipes by Victor. Welcome to rebornpipes! Now in Victor’s own words.

A few years ago i had my first experience with restorations. As a young man just into adulthood, I had little money to invest in good pipes, and on one fateful day I met an old Bent Apple BBB ** for sale at an antique dealer. The pipe had a very rusty stem, there were beat marks all over the edge of the bowl, and a cake that looked more like the shell of a turtle. Already for some time I followed the blog rebornpipes and the work of Steve, and inspired by him I decided to get involved in this project. Two months later (and after many mistakes made) I finally managed to bring the old warrior back into action. On that day I gained two new passions: Restoration and old BBB’s. This restoration I will show you below began months ago when in an auction I bought this BBB billiard from a not very honest auctioneer who had not reported that the bowl was cracked. After some time waiting in a drawer, I finally decided to do something to bring another warrior to this army of BBBs, I hope you like it!

As you can see, looking from the side he was just an old billiard that needed a bit of polishing and cleaning. Good shapes, harmonious proportions, these are typical features of an old BBB and the main reasons that made me fall in love with the brand. What I did not expect was that his former owner somehow managed to create a large crack in the front of the bowl with about 3cm.The interior of the ducts was also completely clogged with a mass of tar residues derived from years of non-cleaning use. The cake was also quite thick, which led me to believe that the pipe had never been reamed, and if it was, that was many decades ago. To remove the cake, I had to use some chisels first, because as the passage was very narrow, it was impossible to insert my Senior Reamer into the chamber. It took me some time (and I also got some blisters on my hand). In the picture you can see the amount of carbonized material being removed from inside the bowl. After using the chisels and also the senior reamer, I also use a series of sandpaper inside the bowl, starting from grit 220 through 400, 600 and ending with 800, so that the inside of the bowl has a uniform surface.After a 30 minute bath in a solution of Oxyclean and water, I washed the inside of the stem using bristle pipe cleaners and running water. With a Dremel and felt disks, used blue polishing compound to polish the inner tube. I finished cleaning the inside of the stem using cotton pipe cleaner soaked in grain alcohol, removing what was left of residues and possible bacteria. The Oxyclean bath brings the oxidation back to the surface of the stem, which facilitates the polishing and removal of the oxidized material. Returning to the subject of the dreaded crack in the bowl. I decided to use a briar insert to cover it. To prevent cracking from increasing over time and to facilitate insertion of the insert, I used a cutting blade attached to the Dremel to cut the broken part and make a V shape instead of the crack. I used this same disk to also cut out a briar block, an insert of a similar size and I used sanding paper to leave it the perfect size to fit into space. To glue the insert, I used a mixture of briar dust, pigments and super glue. I settled the insert and held it for a few minutes until the glue dried. I waited a few hours to make sure that all the glue was dry and insert was firmly in place. I cut the burrs and used sandpaper to level the insert with the rest of the bowl. I also used brown and black dye to match the colors. I used 220, 400, 600, 800, 1000 and 1200 grit sanding sticks to remake the shapes of the bowl edge that were completely destroyed by the beat marks. As you can see, after reshaping the top of the bowl, you can already see the ancient times of glory of this pipe that once was the faithful companion of some gentlemen.

After dying, it was time for the first polish. I used two different compounds, red and brown, on denim disks and jeans disks, such as a high spin, to remove sediments and dirt that were stuck to the outside of the bowl and excess dyeing of the insert and the new bowl top . I used the same process on the stem to remove the oxidized material, but finalizing with flannel discs using the blue compound and white diamond to give a mirrored sheen.