Tag Archives: bite marks

Challenges of a Bakelite Stem Rebuild – A Meerschaum Carved Vineyard


Blog by Dal Stanton

When I first saw the Meer before me on the eBay auction block, I was first attracted by the patina showing on the combination smooth and sculpted surfaces.  The base of the billiard bowl showcases two opposing sculpted frescoes, one with the vineyard in expectation of fruit, and the other with the fulfillment – a rack of grapes appearing from behind the grapevine leaves.  Hope and fulfillment are always pleasing themes for reflection as one smokes a bowl of his (or her!) favorite blend.  The patina of the aging meerschaum is concentrated at the base of the stummel, encompassing the frescoes and then gradually thinning and lightening toward the rim and toward the shank.  The other characteristic that drew my attention was the color and taper of the Bakelite stem completing the bent billiard flow.  It just looked good to me.  I have no idea of a carver as there are no markings on the Meer, and the only information from the seller was that its origins were in Europe – it was a gift to the original owner by his sister who lived in Belgium in the 1970s.  Taking it from the ‘Help Me!’ basket, I place it on my work table here in Sofia, Bulgaria, and record the Meer’s condition when it came to me. The characteristics and make-up of meerschaum are not widely understood – I know because I was among those who looked at the white coral-like material and wondered what exactly it was!  The word ‘meerschaum’ has German origins, literally meaning ‘sea foam’.  This brief description from Meerschaum.com is helpful:

Meerschaum is a very rare mineral, a kind of hard white clay. Light and porous structure of the pipe keeps the smoke cool and soft. The pipe itself is a natural filter which absorbs the nicotine. Because of this peculiarity, meerschaum pipes slowly change their colors to different tones of gold and dark brown. This adds an esthetic enjoyment to its great smoking pleasure. The longer a pipe is smoked the more valuable it becomes due to the color change. Today many old and rare meerschaums have found a permanent place in museums and private collections.

Meers are popular because they require no breaking in, no cake, and no resting between smokes. Many consider Meers to be a cooler and dryer smoking experience.  The one main issue with Meers is that they don’t like to be dropped on hard floors – that is never a good thing!  Most Meerschaum is mined in Turkey and for the curious who want to know what exactly the material is, one last excerpt from Altinok Meerschaum’s facts page:

The geologist knows the light, porous Meerschaum as hydrous magnesium silicate. The pipe smoker knows it as the perfect material for providing a cool, dry, flavorful smoke. The mineral itself is the fossilized shells of tiny sea creatures that fell to the ocean floor over 50 million years ago, there to be covered and compressed over the ages by layer upon layer of silt. Profound movements in the earth’s crust raised the creamy white stone of Meerschaum above sea level. There men eventually discovered it and created an incomparable pipe from it. The first record of Meerschaum as a pipe dates from around 1723.

The stummel on the Meer before me has a lot of grime and dirt with nicks showing his age and that he has been well used.  The challenge with Meer is always how to clean and restore but not to remove the patina, which for a Meerschaum, is the honorific equivalent of the respect owed to those blessed with gray hair and long life in the Bible.  The rim has thick lava and the bowl has moderate cake which will need to be removed with care – cake is not needed on a Meer!  The more daunting questions focus on the stem.  The obvious challenge is the large chip on the end of the stem which also has removed almost half of the button.  I could prepare for this repair by ordering and having someone bring from the US to Bulgaria Behlen’s Medium Yellow Furniture Powders to form a putty patch.  I will attempt to repair the stem with the help of others – we’ll see!  The other challenge that I was not able to discern from the eBay pictures, was the push tenon.  The mortise was threaded for a screw in tenon but the tenon I see connected to the stem has no threads and only engages the mortise as the mortise narrows after the threads.  You can see how much of the tenon is engaged by the coloration (last picture above) – only about half.  When I test the engaged tenon, there is a bit of a wiggle to the stem and it isn’t solidly seated as one would expect.  While the stem, when connected to the shank is usable, it isn’t ideal.  I’ll give some thought to this challenge and perhaps seek counsel.

Leaving the question about the approach for the tenon, I decide to start on the clean-up of the stummel.  I first clean the rim by using cotton pads wetted with isopropyl 95% – I just want to see how much of the lava and stain will come off.  Not much did.  I then decide to use a medium grade sanding sponge and lightly top the rim – not aiming to take off the meerschaum but to break through the crusty stuff and remove the burnt areas.  That did the trick.  Pictures show the progress. I can now see the inner edge of the chamber wall and using both a pin knife and the Savinelli Pipe Knife carefully I ream the bowl and remove the cake.  I follow this by using 240 grit paper and sand the walls to remove more of the carbon. I wasn’t satisfied with the 240 grit so I rolled up some coarser 120 grit wrapped around a Sharpie Pen and that did the trick. Much nicer.  I complete the reaming with cleaning the bowl with a cotton wipe wetted with isopropyl 95%.  The fire chamber looks good.  To remove the blackening on the inner ring of the rim, I give it a very gentle bevel with 240 grit sanding paper rolled.  The pictures show the progress. With the bowl reamed I clean the mortise internals.  Using pipe cleaners and Q-tips, dipped in isopropyl 95%, I discover quickly that I’m not able to get a pipe cleaner through the mortise through the draught hole.  I twist, turn and angle – it feels like there’s an obstruction.  I blow through the mortise and find that air is moving through without pressure build up.  Finally, the pipe cleaner moved through.  Looking more closely in the mortise with a directed light I see in the throat of the mortise just beyond the end of the threading appears to be a plastic tubing.  I manage to take a picture of it.  I’m not sure if this is part of the internal system or something broken off and lodged. Yet, this plastic tube is what the tenon is engaging.  With great difficulty, I can probe the area what appears to be beyond the tubing and find the airway which seems to be a sharp turn up from the angle of the mortise’s drilling as the pipe cleaner emerges from the plastic tubing.  This doesn’t seem right.  I’ll research more to see what the tubing is.  The mortise is clean, so I move to the cleaning the externals of the bowl.To clean the external surface of the stummel, I use undiluted Murphy’s Oil Soap with a cotton pad as well as scrubbing the sculpted lines of the vineyard frescoes.  The amount of grime on the surface becomes apparent as from the before and after pictures.  The pictures show the progress. I then sanded the bowl with micromesh pads not to remove every scratch, which is a sign of character and age, but to restore the shine of a vital meerschaum surface.  I wet sanded the surface using pads 1500 to 2400 then dry sanded using micromesh pads 3200 to 4000.  I was not aggressive but careful not to damage the patina.  I like the result.Regarding the stem and tenon questions I referenced above, I sent a note off to Steve and about the push-pull tenon system and what to do with this Meer.  In the end, I decide to order a new replacement system.  I sent a note and measurements off to Tim at http://www.jhlowe.com/ and am waiting for his recommendations.  Since I live in Bulgaria, ordering parts from the States is no small thing as I have it sent to someone coming and they carry it for me.  Saves a bit on postage. With the tenon situation on hold and on order, I turn to the technical part of this restoration that I’ve been anticipating for some time.  Repairing the Bakelite stem or per Steve, possibly a similar material called Amberoid, has been a subject of my research.  The stems most often associated with Meerschaums are the attractive, rich honey yellow color.  The challenge in a repair is matching the yellow color and glass-like texture of the Bakelite or Amberoid.   When I researched this question, I came across Reborn Pipes contributor, Joyal Taylor’s (aka holymolar) 3-part series on patching amber colored stems in 2014.  Starting at the first essay, Stem Patch Using Amber Super Glue, Part 1, I benefited from Joyal demonstrating not only what did work well, but what didn’t.  Also of benefit were the comments many others contributed at the end of the blogs.  So, thanks to Joyal’s trial and error approach, I’m able to jump to a solution in Essay 3 that worked best for him.  I hope I can emulate his success!  Before beginning on the repair, I want the stem internals to be clean.  Taking pipe cleaners dipped in isopropyl, I go to work on the stem.  The resistance was a bit more than I expected.  The cavity behind the screw-in tenon was gummed up good and I expended several Q-tips and a sharp and spade dental tools helped scrape the cavity walls to break up the gunk.  There is some dark staining on the internal airway but the pipe cleaners are now coming out clean.In essay 3, Joyal employed the use of Medium Yellow Behlen Furniture Powder (pictured below) which I found on eBay at this LINK.  Previously, he had employed amber colored superglue which came out too clear – lacking the opaque quality needed for a good match.  In the second essay, he tried to employ a mixture of Fiebing’s yellow and orange leather dyes and thick superglue.  He found that the chemistry of the dyes caused the superglue to setup instantly.  Also in essay 2 he mixed StewMac 2-part clear epoxy with Fiebing’s yellow and orange dyes, which mixed well, but the results were less than satisfactory – for both the hue and the texture.  The final essay he tried the powder approach using Behlen Medium Yellow with extra thick superglue and the results were the best.  Below I picture the match-up between the colors of the powder and the stem.  Not bad.  Joyal’s final assessment was helpful for the stem I’m looking at now:

This time I tried Behlen’s yellow powder w/ StewMac’s thick clear superglue.  This is the best so far. Good color and opaque. Some of the powder didn’t mix in but it all polished smoothly. I had to leave the patch thick at the edge because every time I tried to sand it – smooth it [next] to the acrylic, I would remove more of the original color from the acrylic and have to add more patch material. Oh well, this may be as good as I can do, for now.

The last observation is helpful because it lets me know that the basic solidity of the patch could be ‘softer’ relatively speaking, than the stem material so that he was removing more collateral stem material than he wanted.  So, off we go!  I begin the patch on the Meer’s Bakelite stem by taking another close-up focusing on the patch areas.  The patch has two parts.  First, the side of the stem chipped off parallel with the right-side stem edge until it enters the button area.  At this point the break encompasses the entire corner – stem and button.  It appears to me the break was caused by dropping the Meer on a hard surface and the impact point was the end of the stem.  The second part of the patch is to rebuild the button.  To do this, I’ll apply a ‘surplus’ amount of the patch putty not only to the damaged, missing part, but over the entire button.  This will allow me to shape a new button with adequate edges.  To mix with the Behlen powder I have a newly acquired bottle of BSI Extra Thick Maxi-Cure CA glue.  I’ll start the mixture aiming at a 50/50 ratio and eyeball things.  I want to mix it well so that the powder is fully dissolved.  I’m also not sure how much time I have before the new CA glue starts setting.  I first take 240 grit sanding paper and rough up the entire patch area to increase the bonding potential between the Bakelite and patch putty.  Now, I construct a ‘slot mold’ for the button.  The slot area is shaped like a concave canoe that the button edges encompass.  I need to keep putty out of this area and form a mold of sorts for the putty.  The results of this mold would remind one of the Wolverine in X-Men.  As menacing as it appears, the center toothpick anchors the mold in the airhole and the ‘wing-picks’ are wedging the edges. The folded index card forming the mold I cover with smooth tape so it won’t adhere to the putty.  Prep done, I pour some Behlen powder in a plastic egg crate to double as a mixing trough.  With tools and toothpicks at hand to serve as putty trowels, I add BSI Extra Thick Maxi-Cure CA to the powder and begin mixing.  Well, if this were a science experiment it would remind me of my first chemistry set in 5th grade.  Every 10-year-old with a new chemistry set sees the formula included for a ‘skunk bomb’ and tries it as his first experiment.  I was no exception.  After adding the glue to the powder and mixing, the mixture began to smoke and harden very quickly.  After running the smoking egg crate to the bathroom and adding water to the mix, the smoke stopped and I return to the work table and record my science experiment with a picture capturing the toothpick forever encased in the hardened yellow putty.  The pictures show the progression. Now fully in step with Jowal’s methodology of ‘Trial and Error’ progress, I ask the question, what happened?   I’m not sure, but my guess is that I started with too much powder and adding the glue to it was not sufficient to keep it in liquid form.  My guess is that the rapid hardening created the reactions (chemical energy!), which created the smoke, leading to my emergency procedures.  This time I will approach the process like I do with a charcoal and super glue mix – put both powder and glue on an index card together and mix more gradually and see what happens.  Well, I’ve proven that the methodology is not the culprit.  Again, smoke was produced from the mixture on the index card while I started applying the putty to the stem.  At this point, I’m thinking that the new glue I’m using might be the problem.  I’ll try again with a glue I’ve used in the past.  Thankfully, I could remove the hardened putty that did make it to the stem, by carefully scraping with my thumb nail.  The bright side of this is that the color match with the stem looks great!  Lesson 2 learned – what not to do.  Pictures show the progression of lesson 2. While contemplating the next step, an email came in from Tim at J. H. Lowe in Ohio, and as expected, his note is very helpful:

The regular push-pull set is what you need. Are there threads inside the mortise? There are two sizes of these sets but the larger one is only used when the threads are very worn out and the oversize mortise part has to be fitted in the shank to fix this kind of worn out repair sleeve. I sell these by the each for $3 and by the dz. for a discounted price. You’ll need to change out the stem peg and the sleeve in the Meers pipe repair.

I responded by ordering 3 of each size so I’ll have some on hand for future projects.  So, in a couple weeks, the new push-pull system order will arrive with a friend coming to visit Bulgaria.  By that time, the rest of the Meerschaum Carved Vineyard should be ready and waiting with a quick finish to the restoration.

For the third go – I repeat roughing the patch area with 240 grit sanding paper to remove putty residue from Lesson 2.  Then, after replacing Wolverine, I change glues using Hot Stuff Special ‘T’ CA glue and mix the same way that I did in Lesson 2, placing a puddle of glue alongside the Behlen Medium Yellow powder and gradually mix by drawing the powder into the glue until (hopefully) the mixture reaches a molasses like consistency.  If it doesn’t ‘smoke’ this time, we’ll know the problem of Lessons 1 & 2. Unfortunately, the ‘smoking’ is repeated and the putty hardened very quickly.  My conclusion to the problem, and the pictures below show the progression of my solution.  The problem is that I’m adding too much Behlen powder to the mix or not enough glue.  I’m estimating that instead of a 50/50 mixture, I need an 80/20 ratio of glue to powder.  I’m not sure of the chemistry involved, but the smoke produced happens when the mixture hardens.  I had more time gradually to build up the patch with the greater glue ratio.  Of course, the question remains, will the lesser powder content change the color match or texture?  We’ll see.  The pictures show the several cycles of building the patch around the button area.  I had only so much time before the hardening would happen and I would make another small batch.  The last picture shows the successfully removed Wolverine mold and the success of guarding the slot area from the putty.  The proof of this yellow pudding will be in the filing, sanding and shaping of the Behlen powder and superglue putty patch.  I use needle files and 240 sanding paper to do the initial shaping.  Starting from the slot side – the end of the stem, I like to create a baseline by re-establishing end by removing the excess.  After removing excess putty on the end, I find the original button.  Since the left side of the button needs to be totally rebuilt, as it was broken off, I use the remaining right side of the button and slot shape to help me form the left side of the slot so it will match. With the baseline established, using the flat edge needle file, I begin to contour the general proportions of the button – lower then upper.  The pictures show the gradual progress. With the general contours of the button established, I then score a line with the flat needle file to mark the upper button lip edge.  With this edge established, I then file down the score line to establish the lip.  I turn the file vertically and use the short edge as a saw and set the edge deeper.  I like to have that edge established so that I can then begin to remove methodically the excess patch putty more accurately to the left of the lip on the second picture below.  After removing as much of the excess putty as possible with the flat needle file, to avoid collateral filing into the Bakelite, I then use 240 grit paper to smooth the surface and remove the putty.  The upper bit looks good so far!  The pictures show the progress. I flip the stem over and repeat same process starting with defining the bit and creating a lip to guide the excess putty removal.  While I work, I’m keeping an eye on the right side (lower in the picture below) of the stem where the major stem rebuild was.  I recall Joyal’s observations of having to keep the patch high because during the smoothing and blending process sanding on the edge of the patch was taking too much of the stem material in the process.  He then described having to refill with more patch the ‘border’ between patch and stem.  The pictures show the progress on the lower bit area. The next two pictures show the completion of the filing and use of 240 grit sanding paper.  I then use 600 grit paper to smooth and blend more and finish with briskly rubbing with 0000 steel wool.  At this stage of the stem repair, I look at the patch areas (3rd picture) and the use of Behlen Furniture Powder Medium Yellow and Special ‘T’ CA glue is strong.  Building up the chip area and missing button portion wasn’t easy but it looks good.  The color is good though it has a speckled quality to it created by small air pockets in the patch which were exposed during the sanding. This I have found is normal.  To fill the pockets, I apply a dab of Hot Stuff CA glue on the stem patch and then ‘paint’ it over the patch using a toothpick.  I do the same with the button lips – upper and lower.  I repeat sanding with 600 grit and then steel wool (I forgot to take pictures of filling the air pockets!).  The pictures show the progress. With the repairs to the stem completed, using micromesh pads 1500 to 2400 I wet sand the stem.  Following this, I dry sand the stem using pads 3200 to 4000 and then, 6000 to 12000.  The Bakelite (or Amberoid, I’ll have to figure out how to tell the difference) stem gradually shines up nicely with each successive micromesh cycle.  The pictures show the progress.I follow the micromesh cycles with applying Blue Diamond compound to the stem with the cotton cloth Dremel wheel set to the slowest speed.  I then mount the carnauba cotton cloth wheel on the Dremel and give the stem 3 coats of carnauba wax.  I follow the carnauba with a hand-buff using a microfiber cloth. Wow!  I like it. The Bakelite or Amberoid has the appearance of glass – the patch has no textural differences with the original stem.  The last two pictures are flipped to show what I’m seeing after the buff. Stem completed for now – the new push-pull tenon system should be in transit. With the stem completed and on hold for the tenon, I look to complete the stummel of this Meer Carved Vineyard.  With of the unique characteristics of Meerschaum pipes, they’re like wine – they get better with age!  For Meerschaums, their value increases with use as the oils in the tobacco interact with the unique composition of the Meerschaum the bowl will change color gradually, darkening to the golden, honey brown which is its patina.  The Carved Vineyard displays this growing patina and to enhance this natural coloring process, treating the stummel with bees’ wax is the long-used practice of choice.  This is my first application of bee’s wax to a Meer and Charles Lemon’s, of Dad’s Pipes, descriptive posts have been helpful as I’ve done my research (See: Quick Clean-up of a Tulip Meerschaum Sitter).  One thing very much available in Bulgaria is bees’ wax, which I found in a local outdoor market at the honey kiosk.  My price was 3BGN for 100gr (Translation: $1.63 for 1/5 pounds).  I don’t know if it’s a deal or a steal.   After I unwrap the package, I break off some chunks of the bee’s wax and put them in a small mason jar, which I’ll be able to keep unused wax for the next Meer treatment.  Using my hot air gun, I melt the wax in the mason jar.  After melting the wax, I hold the Meer over the hot gun to warm up to better absorb the wax.  Blame it on Bulgarian winters, but when I finish warming the Meer, the wax has already cooled down and congealing!  So, a more rapid wax melting follows, and a re-warming of the Meer stummel.  I used a Q-tip cotton swab to paint the bowl with the melted bee’s wax.  I was careful to paint the sculpted vineyard lines – getting the wax in the nooks and crannies.  I put the stummel aside to cool.  Since this was my first time to apply the bee’s wax treatment to a Meer, I was a little surprised how thick the congealed wax was on the stummel after it cooled.  It could be that the Meer wasn’t hot enough and the wax was cooling too quickly.  Either way, the Meer received a treatment!  After cooled, I try buffing with a towel to remove the thicker waxy residue, and I discover that it’s not too easy.  I’m thinking that the wax is too thick and it congealed to fast (3rd picture below). I improvise and I think the improvisation benefited this Meer.  Using a Q-tip as a brush, I start passing the thick-layered bees’ wax stummel over the air gun – like passing over a lit candle, it liquefies the wax on the portion impacted by the heat.  As the wax liquefies, I paint it into the surface – working it in well and removing the excess with the Q-tip. This time applying wax around the Meerschaum seems to absorb the wax instead of being smothered by it. It didn’t take long and the application of bees’ wax is complete (4th picture below)!  Then, before the stummel cooled down, while yet warm, I buff the stummel with a towel and then with a microfiber cloth and WOW.  I’m a believer.  The shine and deepening of the patina is evident!  The pictures tell the story. With the Meerschaum’s stem and stummel complete – almost – I set both aside waiting for the arrival of the push-pull tenon from the US.  I’m beginning to wonder whether this Meer Carved Vineyard should go to The Pipe Steward store, or remain in my collection – often I have that problem 🙂 !

A few weeks later the push-pull tenons arrive via a friend who was willing to carry them to Bulgaria.  I open the package sent by Tim West at J.H. Lowe in Columbus, Ohio, and have my first look at what a new push-pull system looks like.  I unscrew the old tenon and easily screw the new one in place.  The mortise sleeve’s threads worked perfectly as well.  The problem though, is that it will not screw all the way in.  Previously, I identified a tubing of sorts deeper in the mortise which was the only thing the old tenon was locking into – though poorly.  My first inclination was to cut the new mortise tenon sleeve so that being shortened it would fit in the limited space.  It was then that I started questioning whether what I was looking at was part of the design or that it was in fact, the left-over remains of the bottom end of the old mortise sleeve which had broken off.  After looking closely at the inner tubing, I can see fragments of the old break.  Ok!  Now I understand that I need to exorcise this vagabond mortise sleeve. I first try wedging a small flat head screw driver in the tubing to ‘unscrew’ it by turning it counter-clockwise.  I was hoping that it might be loose, but will not budge.  So, using appropriately size drill bits and wood screws, gradually I clear out the obstructing portion by shaving off the material of the old sleeve which I think might be acrylic. I am careful to keep the bits and screws straight so they do not nick the Meer threads.  This was not an easy or fast process, but eventually I was satisfied to remove most of the old sleeve – leaving only a very thin ‘skin’ over the threaded area deeper in the mortise, which may indeed help in keeping the mortise cleaner.  After this, I screw the new insert into the mortise and trim and sand the protruding ‘head’ of the sleeve to improve the fit and alignment of the mortise and stem.  I also sand down the tenon diameter to improve its fit into the sleeve.  I’m pleased with the results.  The pictures show the replacement of the push-pull tenon system.  I’m pleased with the stem rebuild that has blended very well with the Bakelite stem and has put this Meerschaum back in service for a new steward. The patina of the Meerschaum Carved Vineyard has a very healthy start and will only season more with good, aromatic tobaccos.  I also like the blending of smooth and carved Meerschaum – a very stylish pipe.  If you would like to adopt this Meerschaum Carved Vineyard, look at the Pipe Store in my new blog site at ThePipeSteward.com.  The profits of my pipe sales go to help women and children who have been sexually exploited and trafficked through the Daughters of Bulgaria, an organization we work with here in Bulgaria.  Thanks for joining me!

The Striking Grain of a GBD Americana – Made in London England Bent Billiard


Blog by Dal Stanton

When I saw this pipe on the eBay auction block, I was drawn to it first by the grain.  The dark veins of grain were an anomaly and immediately the questions that came to my mind were, “Is that natural or were the darker veins introduced through the manufacturing processes of GBD?  Or, are they discolorations that came afterwards through aging?  The questions raised my curiosity enough to stand back and look at the pipe itself – a GBD Americana half Bent Billiard.  The grain beyond the dark veins were interesting – one side of the stummel was almost exclusively a pattern of peacock feather eyes – bird’s eye grain, but larger and flowing.  The other side appeared as a tree flowing up from the heal of the stummel and fanning out midway to the rim, with more bird’s eye grain taking the form of the foliage of the tree.  Unapologetically, I’m a briar grain addict!  Well, with the winning bid cast, the GBD made its way from the United States to my “Help Me!” basket here in Sofia, Bulgaria.  Here are the pictures that first got my attention on eBay – the black vein grain and the flowering tree: This attractive Bent Billiard has markings on the left side of the shank of, “GBD” (oval encircled) over “Americana”.  The right side of the shank bears, “Made in London” (circular lettering) over “England” with the shape number “508” immediately to the right.  The bottom of the shank has “M” imprinted standing alone.  The traditional brass GBD rondel garnishes the stem. The story of GBD pipes is an interesting one starting in France in 1850 with an unexpected partnership, not coming from businessmen, but fellow pipe makers who felt they could make a go of it.  This excellent article, Finding Out Who Created GBD – Story of a Pipe Brand – Jacques Cole was reposted on Reborn Pipes and is an excellent read for framing a historical appreciation for a pipe name and its development – GBD.

Who were these creators? Ganneval, Bondier and Donninger were three ‘Master Pipemakers’ who got together in Paris in 1850 to manufacture meerschaum pipes. It was a bold decision as these were troubled times in France. Charles Louis-Napoleon Bonaparte has returned after the 1848 revolution and become President of the Republic. Following a coup d’etat in 1851, he made himself Emperor Napoleon III in 1852. He was incidentally a keen pipesmoker and may well have owned one or more early GBDs.

 The pipe of Emperor Napoléon!  Does it get much better than this?  The picture to the left bottom is not Napoleon depicted, but with pipe in hand, the ‘charge’ gives one an image to imagine!  The focus of the ‘GBD’ enterprise in the late 1800s was primarily the production of meerschaum pipes but in the 1850s, with Saint-Claude’s discovery of briar and its special qualities for making lasting, heat-resistant pipes, GBD adapted and added briar to its list of materials.  GBD boasted in the end of the 19th Century as having 1500 models that customers could choose from – though Pipedia’s article on GBD clarifies this unbelievable number as counting each shape three times due to three different stem materials used.  GBD straddled its French identity and its adopted English identity through various acquisitions and changes in ownership, yet, keeping the initials of the founders firmly in place.  Pipedia’s history is helpful to understand these historical iterations:

There is a very simple explanation for GBD’s program to turn more “British”: GBD became a British company soon after the turn of the century! In 1902 Marechal and Ruchon sold GBD to A. Oppenheimer & Co. in London. Charles Oppenheimer had founded this successful trade business in 1860 as an import-/export house. His brothers David and Adolphe and brother-in-law Louis Adler soon joined him. Adolphe took over when Charles went to Germany as British ambassador. Briar pipes were among the first products traded. The business relation to GBD in Paris began as early as 1870. Being the most important customer in the English-speaking world, Oppenheimer & Co. were designated as sole distributor for Great Britain, the USA and Canada in 1897.

Though English owned, pipe production continued in Paris and soon Oppenheimer acquired two factories in Saint-Claude in 1906, increasing its production.  Also during this period, Oppenheimer continuing to expand, built a pipe factory in London, but this operation failed to live up to expectations until the genesis of WW I when demand for pipes increased for the front line and production fell in the French factories as men were called to the front lines.  The shift of GBD being identified more distinctly as a British pipe emerged after the close of the war even though production continued in London and France through the 1920s.  I find the next Pipedia excerpt interesting because it marks well how GBD had fully transitioned from its origins, the handshake of 3 French pipe makers, to a macro-business continuing through the 1900s.

In 1920 Oppenheimer had purchased BBB (Blumfeld’s Best Briar, formerly A. Frankau) and little later Loewe & Co. and large shares of Comoy’s of London. The economic crisis in the early 1920s induced the foundation of Cadogan Investments Ltd., named for its seat at Cadogan Square in London. The Cadogan group was a superordinated holding company, in order to tune all activities of Oppenheimer’s brands in the pipe industry. Whereby an extensive independence of the single brands was preserved. Remember, the Oppenheimers and Adlers weren’t pipe specialists, but rather sales people who depended on their experts in the British and French plants.

This link is to a 50 page catalog featuring Oppenheimer’s product line – it is fascinating.  The index page is pictured below.  In 1952 the Paris factory moved to Saint-Claude and since the 1980s most GBD pipes come from London.  The higher-end GBD pipe lines are of good quality and many feel they stack up well against the array of Dunhill offerings yet more affordable.  The Pipe Phil history of GBD says that the Saint-Claude pipe factory closed in 1981 leaving only London as the producer of GBD pipes.This list comprises the better grades of GBD pipes in descending order: Pedigree, Pedigree I, Pedigree II, Straight Grain, Prodigy, Bronze Velvet, Virgin, Varichrome, Prestige, Jubilee, New Era, Prehistoric, International, Universe, Speciale Standard, Ebony, Tapestry, New Standard, Granitan, Sauvage, Sierra, Penthouse, Legacy, Concorde.

According to the José Manuel Lopes, the Americana before me now is a GBD second associated with L&H Stern, Pioneer, and Appleby.  The closest indicator of dating of this GBD Americana comes from Pipe Phil that GBD’s metal stem rondels were discontinued after 1981 when GBD merged with Comoy.  After seeing Reborn Pipes’ contributor, Al Jones’ comments in several GBD discussion threads, I sent him a note with some questions and pictures about this Americana.  His response was helpful and his description of ‘Odd Duck’ helps me place this pipe in context:

Dal:

You’ve got an odd duck! 

Typically, the stamping used on pre-Cadogan pipes is the straight line COM, “London, England” stamp (see attached) combine with the brass rondell stem logo.  Cadogan era pipes (made after 1981) have the round “Made in London” (with England under) COM, as shown on your pipe.  But, they typically have stamped stem logos. I see these pipes occasionally, and my assumption is they were made after the merger, until the brass rondell inventory was exhausted. One common denominator on these pipes is a single letter.  I have no idea as to what it may mean, but M is frequently used. These pipes also had many more finish names, like your Americana, that were not seen before.  Comoy’s started doing the same thing, adding lines and letters just after the merger. I’ll look forward to seeing the restored pipe, it looks like a good candidate.

Thanks,

Al With Al’s ‘Odd Duck’ description in place, my best summation of this GBD Americana, is that it is placed after 1981, but in the early 80s, after the Cadogan merger, but before the brass rondel bucket emptied which more than likely indicates a cost-saving measure that may indicate a lowering of GBD quality – perhaps, only my guess.  I took a quick look in the early 80’s GBD catalog listings on Chris’s Pipe Pages, perchance to find a listing for an Americana, but came up empty.

With a greater appreciation for the name and history of the GBD Americana pipe before me, and the other GBDs waiting in my “Help Me!” basket, I take additional pictures on my work table to fill in the story and take a closer look. I like the appearance of this GBD Americana bent Billiard.  The cake build up in the chamber is thick and will need to be removed to the briar for a fresh start.  The rim is covered with lava flow and will need cleaning before I can see what lies beneath.  I’m interested to see what happens with the dark briar veins on the stummel surface when I clean it up with Murphy’s Soap.  I detect some pits and dents on the stummel surface – normal wear and tear.  The stem shows significant oxidation coupled with moderate teeth chatter and some dents on the bits.  The first thing I do to begin the restoration and recommissioning of this GBD Americana is to plop the stem into an Oxi-Clean solution for a good soak to raise the oxidation. After soaking several hours, I pluck the stem out of the Oxi-Clean bath and the solution did the job of raising the oxidation.  After I take a picture, I wet sand the stem using 600 grit sandpaper that takes the mother-load of oxidation off.  I continue using 0000 steel wool to remove more oxidation and work the grooves around the button.  I also work around the GBD rondel with the steel wool, working on the oxidation and shining the brass as well.  The pictures show the progress.I then take pipe cleaners dipped in isopropyl and clean the internals of the stem.  There was not too much resistance and the pipe cleaners returned clean very quickly.

Time to work on the stummel.  I begin by removing the moderate cake build up in the chamber.  I first put a paper towel down on the work space to collect the carbon dust and then take the Pipnet Reaming Kit and I use two smaller of the 4 blades available.  Starting with the smaller blade, I turn it until the crunchy resistance of the carbon cake is absent, then I move up to the next larger blade removing the cake.  Following the reaming blades, I use the Savinelli Pipe Knife and fine tune the reaming by scraping the chamber walls removing even more carbon.  Then, I roll 240 grit sanding paper around a Sharpie Pen and sand the chamber walls.  Finally, I use a cotton pad wetted with isopropyl 95% to remove the residue carbon dust and clean the chamber.  Inspecting the wall of the chamber, all looks good – no problems detected.  The pictures show the progress. I like working on a clean pipe so I turn now to the internals of the stummel.  Using pipe cleaners and cotton swabs dipped in isopropyl 95% I attack the mortise and the airway. The tar and oils are not putting up too much resistance and the pipe cleaners and swabs start coming through clean.  Later, I will give the internals a salt/alcohol soak to clean the stummel further and freshen the pipe. With the internals clean, I now turn to the external surface.  I’m anxious to see what the Murphy’s Soap does regarding the dark veins on the surface – I’m not sure if it’s actual dark grain color or something else.  I use undiluted Murphy’s Soap with cotton pads and bristled tooth brush to scrub the surface and remove the grime.  To clean the rim, I also employ use of a brass bristle brush which will clean but not damage the wood.  Without a doubt, I am looking at an amazing piece of briar with dark, blackish veins in the grain – unique and striking.  The surface itself is in good shape.  I detect very small fills but they are solid and will easily blend.  The rim shows damage on the front-left edge – possibly scorching from lighting the pipe over the rim.  There is also a bevel on the inner rim. To remove the damage to the rim and to reestablish crisp lines, I will lightly top the GBD – only taking off as much as needed.  I use a chopping board on my work table with a sheet of 240 grit paper over it.  I invert the stummel and rotate the stummel in a circular motion – careful not to lean to the softer damaged area of the rim. I take a picture mid-way to show progress.  After removing enough of the top, I then switch to a 600 grit paper and give the rim a few more rotations on the topping board, primarily to smooth the rim.  Burning and discoloration remain on the inner rim after the topping.  I take 120 grit paper, tightly rolled, and cut a new inner rim bevel.  I follow with 240 grit paper rolled, then a 600 grit rolled paper to complete the bevel.  The pictures show the rim’s progress. With the stummel before me, I decide to proceed with sanding the externals.  I first use a light grade sanding sponge, followed by the micromesh pads from 1500 to 12000.  In sets of three, I wet sand using micromesh pads 1500 to 2400, followed by dry sanding with pads 3200 to 4000, and then concluding also dry sanding with pads 6000 to 12000.  The grain in this GBD Americana is unique and the way the grain emerged through the micromesh cycles was striking.  The pictures show the sanding process. I now clean and freshen the internals of the stummel more and I use kosher salt and alcohol to soak the stummel.  The kosher salt will leave no residual taste as will regular iodized salt. I first stretch and twist a cotton ball to stuff down the mortise acting as a wick to draw out the tars and oils.  I then fill the chamber with kosher salt and set it in an egg carton where it will have the right angle and be stable.  Then using a dropper, I fill the chamber with isopropyl 95% until it rises above the level of the salt.  I top it off after a few minutes because the alcohol is drawn down initially into the mortise and the cotton wick.  I then set the stummel aside for several hours to soak.  The pictures show the progress.With the stummel soaking, I start the stem polishing process.  I first work around the GBD rondel using a small piece of Mr. Clean Miracle Eraser.  I detect left over oxidation ringing the rondel in the vulcanite.  I do not want to bear down on the rondel with an abrasive so I’m hoping that Mr. Clean will do the job and the result confirms this.  Previously, when I removed the oxidation with 600 grit paper, it cleaned the button area of teeth chatter very well.  I detect on both the upper and lower lip edges residue oxidation that was shielded by the lip overhang.  I fold a piece of 240 grit paper to create a sharp blade/edge and sand the lip edge.  This removes the oxidation as well as sharpening the button definition.  I follow doing the same with 600 grit paper and then buff the bit, upper and lower with 0000 steel wool.  The pictures show the fine-tuning stem work. I’m ready to begin the micromesh pads polishing process.  First, using pads 1500 to 2400, I wet sand the stem, followed by pads 3200 to 4000 then 6000 to 12000, I dry sand the stem.  After each cycle of 3, I apply Obsidian Oil to revitalize the vulcanite and take a picture to mark the progress.  The GBD stem rondel has a pop with the black backdrop of the newly revitalized vulcanite stem.  The pictures show the progress. Back home after a day at work, I’m looking forward to finishing and recommissioning this GBD Americana for service to a new steward.  The salt and alcohol soak has had all day and there isn’t that much discoloration of the salt – hopefully this means there wasn’t that much left to clean!  I thump the bowl on my palm to dislodge the used salt and dump it.  I then take a dry paper towel and wipe out the excess salt from the chamber and after removing the cotton wick, I use multi-sized round bristle brushes to remove excess salt from the airway and mortise.  Then I complete the job by wetting a cotton swab and a pipe cleaner with isopropyl 95% and plunge them, only to discover that the internals were indeed cleaned and ready to go. With the stummel cleaned and stem waiting in the wings, I reassemble the pipe to get a bird’s eye view of things.  It does not take long to decide not to apply a stain, but to leave the natural finish on this striking and graceful Bent Billiard.  The color combinations of the black veins and black stem, the golden briar and the brass stem rondel are eye-catching.  This is one nice looking pipe! I use white diamond compound with a felt wheel mounted on the Dremel at the lowest speed.  Before I apply the compound, I purge the wheel of old compound using the edge of the Dremel’s adjustment wrench.  I apply the compound to both stem and stummel. I rotate the wheel over the surface, not applying much downward pressure on the surface but allowing the RPMs of the Dremel and the compound to do the work.  After the White Diamond, I mount a cotton cloth wheel at the same lowest speed, and apply Blue Diamond compound to both stummel and stem.  With the compounds completed, I buff the pipe with a flannel cloth not so much to shine it but to remove the excess compound dust before I apply wax.  With the carnauba wax I mount the cotton cloth wheel, increase the speed one notch faster, 2 with the fastest being 5.  I apply several coats of wax to stem and stummel.  I finish the polishing process with a hand buff using a micromesh cloth to deepen and bring out the shine.

This GBD Americana Bent Billiard has perhaps the most striking briar grain I have yet to see.  The black veined grain gives a marbling effect that draws the eyes to look closer.  When one looks closer the grain is a myriad of shapes and bird’s eye swirls that make me ponder again one of God’s little creations.  Then, the black grain on the left side of the stummel, dips underneath the heel, and emerges on the right side as straight vertical grain resembling a mature tree, beginning with the roots, then trunk, replete with foliage fanning out above as it reaches toward the rim – a virtual canvas.  If I decide to sell this pipe (I’m conflicted, this one may indeed be a keeper!), you will see it in the store at my blog site, The Pipe Steward.  All the profits of pipes that I sell go to help the Daughters of Bulgaria – the organization we work with here in Bulgaria helping women and children who have been sexually exploited and trafficked.  Thanks for joining me!

 

 

 

Who would have guessed that there was a Beauty in this Beast


Blog by Steve Laug

Sometimes you have to look past the state of a pipe to really see what could be present underneath all of the layers of dirt and grime. You have to have the right perspective as well. You need to be able to see these pipes as well loved rather than abused; as a favourite pipe rather than a neglected one. This the context in which the next pipe that crossed my worktable is to be viewed. Here is the back-story. Not too long ago I received an email from a friend of mine named Jim, whose pipes I have worked on in the past. He had an interesting story to tell me and a request. I thought rather than tell the story for him I would let him tell it himself. Here is his email in full:

Hey Steve,

I have been hunting about 1200 acres of Farm and Woodland Property owned by an area farmer and old friend of mine named Stephen Lehner. Steve knows I am a pipe aficionado, and approached me the other day with a pipe that had belonged to his father. I was able to get a little history of how this pipe came to be in this abysmal condition. Steve’s father was rather hard on his pipes. As the original owner of this pipe, Steve said his dad, in the latter years of his life, was not given to cleaning his pipes. His cleaning routine, if you could call it that, consisted of digging any ash and unburnt tobacco from the bowl with a pocket knife, then grasping the pipe by the stem, toward the mouthpiece/lip area, and banging it violently against any nearby hard object – trees, brick walls, car mirrors. It was hard enough that Steve’s son, Shawn, remarked that the old man actually damaged the mirrors on his trucks! Mr. Lehner’s pipes were so abused, that he routinely broke stems, necessitating that he acquire new stems – some of which were not well fitted.

In any case, Steve handed me this pipe, stating that it is one of a very few connections he has to his late father, and asked if I could do a cursory cleaning so he could display it as a keepsake (He is not a pipe smoker). I thought the pipe was interesting, if in bad condition. I cannot clearly make out any markings. On one side, there is a partially legible stamping, “…vage” with some cursive writing below it which I cannot make out. On the other side, I can read the number “75.”  I think it is a bulldog style. The tenon will not enter all the way into the mortise, and I am not sure if that is because there is so much crud inside or because it is not the correct bit.  The bowl is heavily caked and cracked. It also looks as though there was some ad hoc rustication on the bowl, as well. The bowl shows a distinct area of impact where it was banged during cleaning as well.

I attached some pix so you could behold this wonder:Once I saw the pictures I was quite taken back by the sheer beastly look of this old pipe. It had quite literally been beaten to death. The bowl was cracked on the outside of the bowl that started at the front of the bowl and extended to almost the back side. There was a second crack below that on the front of the bowl extending from the bottom of the first crack and extending toward the other side of the bowl. The bowl was so badly caked that I could not even get my pinky finger in the bowl. I tried to blow through the end of the shank and I was unable to get any air through the bowl. The finish was dirty and sticky to touch. The worm trail rustication ran over the bowl surface but was filled in with dirt and grit. From the photos it appeared that the shank inside was incredibly dirty. I think that it is fair to say this pipe was a stranger to pipe cleaners. The stem that was in the shank was not a fit. It was of smaller diameter than the shank. The slot in the stem was almost clogged.

After reading his email and looking over the photos I wrote back to my friend. I was pretty certain from the look of the rustication and the shape number he gave me that the pipe was a GBD. The three letters that he could read on the left side of the shank were age. That led me to look in the GBD list I have and concluded that the pipe was a GBD Sauvage. I looked up some information on a chart I have of GBD lines and knew that the pipe was originally sold with a light brown stain, smooth bowl with deep carved lines to hide flaws. It was similar to a Savinelli Sherwood, but much deeper carved lines. The GBD shape number 75 was a Rhodesian with a1/4 Bent Saddle stem. While this old pipe was a mess it was awfully hard to tell if it ever was a Rhodesian. I sent him this information in my reply.

He wrote back and said he wondered if I would be willing to tackle the restoration on this one. If so he would send it to me. I wrote back and said I would do the work. I guess I will find out if my guesses on the brand of this pipe were correct. I would know more once it arrived.

The pipe arrived and it was indeed a mess. On top of the beat up old pipe, the reek of Middleton’s Cherry pipe tobacco filled the room when I opened the box. My daughters immediately commented on how strong the smell was. I examined the pipe with a lens to see if I could identify the pipe. It was stamped on the left side of the shank with the GBD logo in an oval over Sauvage over Collector in script. On the right side of the shank it is stamped Made in England over 75 which is the shape number. The next photos show what the pipe looked like when I received it. I took a close up photo of the rim to show the absolute dreadful condition this pipe was in when it arrived. The bowl had a thick cake that still reeked of the aroma of burnt Middleton’s Cherry pipe tobacco. The rim had been hammered to what looked like the point of no return – though I would not know for sure until I had removed the cake and the buildup on the rim top. The stem was a replacement one and it was obviously a poor fitting one. The diameter of the stem and the shank were not a match and the tenon could not be pushed into the shank because of the grit and tar built up inside. The button had been flattened by biting and there were tooth dents on it and also on the top and bottom sides. I would definitely need to make a new stem for the pipe. I decided to start by reaming the bowl back to bare wood. I wanted to see if the cracks on the outside continued into the bowl. I fully expected the bowl to fall apart once the carbon was removed and ceased to hold everything together. I started reaming with the smallest cutting blade on the PipNet pipe reamer and worked up to the largest cutting head. I finished reaming the bowl with a Savinelli Fitsall Pipe Knife.I rolled a piece of 80 grit sandpaper on my index finger and sanded the inside of the bowl. I wanted to be able to clearly see if the cracks on the outside continued into the bowl. The second photo below shows the inside of the bowl. The crack on the left side of the bowl did not seem to show through inside. The one on the front of the bowl still needed some more work to be certain but it also looked like it did not show through. Notice the buildup on the rim it probably protected the top of the bowl to a large degree.I scraped the rim with a pen knife to peel off the cake that overflowed on the top. I carefully held the blade against the surface of the rim and scraped it slowly until all of the buildup was gone. Underneath all of the buildup the rim was in rough shape. It had been beaten pretty hard and the damage was quite extensive. The rim top showed signs of being knocked about hard against that truck mirror mentioned above. If this pipe could have talked I would love to hear the stories it could tell.I topped the bowl on the topping board using 220 grit sandpaper. I decided that I would sand it until the top of the rim was smooth and the damage on the outer edge of the rim was minimized.With the rim topped and smooth I wiped the bowl down with acetone on cotton pads to remove the grime and clean up the surface so I could assess the next steps in dealing with the external cracks on the left side and bowl front. I used a microdrill bit on my Dremel to drill pin holes at each end of the cracks in the bowl. The length of the bit ensures that I will not be able to drill too far and go into the bowl itself. There were five distinct ends to the series of cracks in the briar.I used a dental pick to clean out the cracks with surprisingly had closed tighter once the cake was removed from the bowl releasing the pressure. Once they were clean I pressed briar dust into the crack surfaces and the drill holes in the bowl. I dripped clear super glue on the cracks and into the plugs in the drill holes. I gave the repair several more coats of briar dust and super glue until the surface was filled. The pictures tell the story. I sanded the dried repair and the rest of the bowl with 220 grit sandpaper to remove the excess briar dust and glue. I wiped the bowl down with alcohol on a cotton pad. I used a Black Sharpie pen to colour in the worm trail rustication around the bowl sides. I had done some research and found that the rustication on the Sauvage line had been darker than the stain on the bowl.I used the drill bit from the KleenReem Pipe reamer to drill out the buildup in the airway from the mortise to the bowl. It was thick and hard so the drill bit took several passes through the airway to clean it out. I used a dental spatula to scrape out the thick, hard tars that lined the walls of the mortise. I scrubbed out the mortise and airway with alcohol, cotton swabs and pipe cleaners until the internals were clean.I stuffed the bowl with cotton balls until they were just below the edge of the rim. I put a pipe cleaner in the airway to wick the alcohol into the shank. I used an ear syringe to fill the bowl and shank with alcohol. I set the bowl upright in an ice cube tray and let it sit over night to draw the oils out of the briar. In the morning I took a photo of the darkened cotton balls. I used a dental pick to pull them out of the bowl. I cleaned out the shank and the bowl with cotton swabs to remove all the excess alcohol. I let the bowl dry.I stained the bowl with a dark brown aniline stain thinned 50/50 with alcohol to make it more transparent. I flamed the stain and restained it. I repeated the process of staining and flaming the surface until the briar had even coverage. I buffed the bowl with Blue Diamond on the buffing wheel and then took the following photos to send to Jim to show him the state of the bowl at this point in the process. There were still scratches in the finish that would need to be polished out but the bowl was showing promise and beauty was emerging from the beast. I left the pipe on my work table while I traveled to Idaho for my mom’s 90th birthday. I stay with my brother Jeff when I am there and as usual he had a batch of pipes for me. There were some amazing pipes there but what caught my eye this time was the stem I needed for this Sauvage. It was slightly bigger in diameter than the shank but it would not take much to fit it to the pipe. When I got home I lightly sanded the tenon with a Dremel and sanding drum until it fit snugly into the mortise. I took the photo below to show the new stem and the one that was with the pipe when it arrived. I took photos of the stem to show the difference in diameters of the shank and the stem. You can also see the deep tooth marks in the top and bottom sides of the stem near the button.I sanded the diameter with a sanding drum on the Dremel. I do this with the stem inserted in the mortise so that I can remove as much of the excess vulcanite as possible without damaging the briar on the shank. I nicked the edged of the briar but fortunately the nick was not deep. I also lightly sanded the top and underside of the stem with the Dremel and minimized the tooth marks. I sanded the areas on the stem where the tooth marks had damaged the vulcanite with 180 grit sandpaper and smoothed out the surface damage. What remained were the deeper tooth marks. I wiped down the surface of the stem with alcohol on a cotton pad to remove the debris and dust from the tooth marks. I filled the remaining tooth marks with black super glue and set the stem aside to dry.When the repairs had cured I sanded them with 180 grit sandpaper to blend them into the surface of the stem. I sanded the saddle portion of the stem to remove the marks left behind by the sanding drum.I put the stem in the shank and sanded the stem and shank with 220 grit sandpaper to make the transition really smooth. I could have done this differently but there was enough damage to the shank that the sanding would smooth out the briar as well. I wet sanded the stem and shank with 1500-2400 grit micromesh sanding pads to smooth out the scratches on the briar and the vulcanite. I was able to remove most of the scratches. The rest would come out with more elbow grease. I cleaned out the inside of the stem with pipe cleaners and alcohol until they came out clean. I used a sharp knife to bevel the airway into the stem. I have found that doing this directs the airflow from the bowl to the button. I put the stem in the shank and took the following photos. There is still a lot of polishing to do but the pipe is beginning to look pretty decent. I continued sanding with the 3200-12000 grit micromesh sanding pads to polish the stem. After each set of three pads I rubbed it down with Obsidian Oil and sanded some more. After the last pad I gave it a final coat of the oil and let it sit to dry.I buffed the bowl and stem with Blue Diamond on the buffing wheel and then gave both the bowl and the stem multiple coats of carnauba wax. I buffed it with a clean buffing wheel to raise the shine and hand buffed it with a microffibre cloth to deepen it. The finished pipe is shown in the photos below. I am repairing and refitting the original stem to send back with the pipe as well. Once it finished I will buff the two stems and finish removing any scratches that can still be seen in the pipe and then send it back for the surprise that Jim has in mind for it. Thanks for looking.

Refreshing a Stanwell Gilt Edged 124 Ivarsson Design


Blog by Steve Laug

I received an email a few weeks ago from Mario. He has been following the blog for some time now and had enjoyed reading the posts. He wrote that he had purchased a pipe on Ebay for a good price. He attached some photos of the crack in the shank and wondered if I would be willing to take it on. I wrote back and asked for some photos so he sent me the following two photos. The first shows what appears to be a crack in the shank just ahead of the gold band between the shank and the stem. I have circled the damaged area in red in the photo below.stan1The second photo shows the shank end of the pipe. The band wraps over the end of the shank which was a plus to my mind. The band was tight on the shank according to the seller. My thinking was that the band would hold the crack together and it would be easier to work with. (The tenon on the stem is also a 9mm filter stem).stan2I wrote back and told him I would be glad to work on it. He wrote back when the pipe arrived at his place. As he looked it close up he wrote that the crack did not look as bad as he had expected. It appeared to be possibly a flaw in the briar. He also wrote that the end of the flaw near the band did extend to the edge of the band. He packed up the pipe and sent it to me in Vancouver. When it arrived I loved the look and shape of the pipe. The long shank and the shape of the bowl work well together. The gilt ring around the outer edge of the bowl and around the shank is what gave the pipe its name. It is stamped Stanwell of Gilt Edged on the left side of the shank. On the underside it reads Made in Denmark. On the right side of the shank it reads 124 which is the Stanwell Shape number. According to information compiled by the late Bas Stevens regarding Stanwell shapes the 124 is a freehand, long conical shank, with a short saddle mouthpiece. It was designed by Sixten Ivarsson. Here is the link to the full blog post that Bas gave permission to post on rebornpipes: https://rebornpipes.com/2013/09/03/stanwell-shapes-compiled-by-bas-stevens/

I took the following photos of the pipe when it arrived and before I started to work on it. You can see the damage to the rim – including both dents and a slight burn on the back inner edge toward the right side. There were also some dents on the top of the shank just ahead of the crack in the briar. The pipe was sold as clean and restored but it was far from clean by the smell of tobacco and the oils in the shank and stem.stan3 stan4There was some tar and oil on the top of the rim so I wiped it off with a cotton pad and took the following close up photo. It is hard to see but there were light dings in the rim top and the damage at the rear which I have circled in red.stan5The stem was clean on the surface but there were ripples and ridges from buffing as well as some slight tooth indentations on both sides near the button and on the button.stan6I sanded the damaged/flawed area on the top of the shank and probed it with a dental pick. Interestingly if it was a crack it was sealed tightly and there were no soft spots in the surface. It also appeared that the top finish had run slightly leaving a sag mark on the shank. I examined it with a bright light and lens and could see that the flaw ended a good 1/8th inch before the band and that the other ended. I decided to not drill the ends of the crack because it was a tight fit and also because when I looked at the inside I could see no trace of the crack coming through. I filled it in with clear super glue and when it dried I sanded it smooth with 220 grit sandpaper.stan7I cleaned up the rim top with 220 grit sandpaper and lightly beveled the inner edge to clean up the burned spot. I did not want to bevel it too much but only enough to match the rest of the rim bevel. When I finished shaping it I sanded it with 1500-2400 grit micromesh sanding pads to remove any scratch marks. I steamed out the dents on the top of the shank and polished them and the repair with micromesh sanding pads. I stained the rim edge and repair with a medium brown stain pen. I used a black Sharpie pen to continue the grain marks through the repair on the shank.stan8I buffed the pipe with Blue Diamond on the buffing wheel and hand buffed it with a microfibre cloth. I took the following photos of the pipe and sent copies to Mario. We are both really pleased with the way the pipe has come out to this point.stan9 stan10Here are some close up photos of the shank repair and the rim clean up. It looks much better than when I began the work.stan11I set the bowl aside and started to work on the stem. I sanded both sides with 220 grit sandpaper and took the photos to show the marks, ripples and dents on the surfaces.stan12I cleaned out the tenon area with alcohol, cotton swabs and pipe cleaners to remove all of the oils and tars in airway and the area where the filter would have been. It took a lot of pipe cleaners and cotton swabs to remove all of the debris. The next photo shows about half of the cotton swabs and pipe cleaners that I used on the stem.stan13I examined the inside of the mortise and airway with a pen light and could see that the shank was thickly caked with a hard coat of tars. I used a dental spatula to scrape away the debris in the mortise. It took a lot of scraping to remove the buildup to see the briar. I cleaned out the shank and airway with alcohol, cotton swabs and pipe cleaners until it was clean. The pipe smelled much cleaner though still smoky.stan13a stan14I pressed cotton balls into the bowl and rolled a cotton pad and inserted it in the shank. I used an ear syringe to fill the bowl with alcohol. I tipped it so that the alcohol ran into the shank. I filled it until the cotton was covered in the bowl. I set the bowl aside to let the alcohol do its work in drawing the oils out of the briar. I set the bowl aside and turned to the stem.stan15I finished sanding it with the 220 grit sandpaper to remove all of the ripples and dents in the stem surface. I polished the stem with micromesh sanding pads – wet sanding it with 1500-2400 grit pads and dry sanding it with 3200-12000 grit pads. After each set of three pads I rubbed the stem down with Obsidian Oil. After the last rubdown of oil I set the stem aside and let it dry.stan16 stan17 stan18I let the cotton balls and alcohol sit in the bowl for 6 hours. I took the following photo of the darkened cotton balls. I removed the cotton balls and cleaned out the shank, airway and bowl with cotton swabs and pipe cleaners. I was able to remove a lot more of the tars in the shank.stan19Once the shank was clean and the walls were clean and had dried I put the stem in place on the shank. I buffed the pipe and stem with Blue Diamond on the buffing wheel. I gave the bowl and stem several coats of carnauba wax and buffed it with a clean buffing pad. I hand buffed the pipe with a microfibre cloth. The finished pipe is shown in the photos below. The stem is smooth and glassy, the rim is much better and looks smooth, and the flaw/crack in the shank is smooth to touch and virtually invisible.  It will be heading back to Mario this week and I look forward to hearing what he thinks of his pipe now. Thanks for walking along with me through this restoration.stan20 stan21 stan22 stan23 stan24 stan25 stan26 stan27 stan28 stan29

Refreshing a Tiny L&Co. Billiard


Blog by Steve Laug

This is the final pipe of the lot of pipes I received from the pipe man in Eastern Canada who picked up an amazing lot an auction. The kind of price he paid makes me envious! This one is an older Loewe and Company graceful and diminutive pipe. It is stamped on the left side of the shank with L&Co. in an oval. On the right side of the shank it is stamped Loewe over England W.

When I received the pipe I took the following photos of it to give you the big picture of this tiny pipe. The stem was in good shape but had the most oxidation of the lot that was sent to me. There were small tooth marks and chatter on the stem near the button on both sides. The finish was dirty but in decent shape. The rim was worn and there were some dents and dings on the top surface. The inner edge of the bowl was slightly out of round. Someone had reamed the pipe back to bare wood but the internals were very dirty. loewe2 loewe3I took a close up photo of the rim to show its condition. The finish was worn on the rim as well as darkened and dented. You can see the damage to the inner edge of the bowl as well.loewe4The next two photos show the oxidation on the stem. It is hard to see the tooth chatter and marks but they are present and will need to be dealt with.loewe5I also took some photos of the stamping. While not perfect you can read the stamps quite well and see the details that I mentioned above.loewe6I reamed the bowl with a Savinelli Fitsall Pipe Knife to clean up the inside of the bowl. The bowl had already been reamed and there were only slight remnants of a cake in the bowl.loewe7With the bowl clean I used a 1500 grit micromesh sanding pad to smooth out the rim and take off the carbon buildup on top. It also worked to take off the scratches in the briar.loewe8I used a folded piece of 220 grit sandpaper to clean up the out of round rim and bevel that were present. It did not take too much sanding and it looked as good as new.loewe9I used a dark brown stain pen to touch up the rim. The colour of the stain was a perfect match to the colour of the stain on the bowl. I stained the bevel and the top of the rim.loewe10I cleaned out the inside of the mortise and the airways in the shank and the stem with alcohol, pipe cleaners and cotton swabs. The pipe was quite dirty in these areas and took a bit of scrubbing to get the grit out of the airways.loewe11I sanded the stem with 220 grit sandpaper to remove the oxidation and the tooth marks and chatter. Several of them were quite deep so I “painted” the tooth marks with the flame of the lighter to lift them to the surface of the stem. They all raised to the surface and a bit of sanding smoothed out the damage.loewe12I polished the stem with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I rubbed the stem down with Obsidian Oil after each set of three pads. I set the stem aside to dry.loewe13 loewe14 loewe15I buffed the pipe and stem with Blue Diamond on the buffing wheel to polish the minute scratches that still remained in the vulcanite and the finish of the briar. I gave the bowl and stem multiple coats of carnauba wax. I buffed the pipe with a clean buffing pad to raise the shine and then hand buffed it with a microfiber cloth to deepen the shine. The finished pipe is shown in the photos below. This evening I packed the pipes and sent them Express Post back to the pipe man in Eastern Canada. I am hoping he enjoys his “new” pipes and adds them to his rotation. Cheers. Thanks for looking.loewe16 loewe17 loewe18 loewe19 loewe20 loewe21 loewe22 loewe23 loewe24

 

Hole in the Wall Gold Mine: Butz-Choquin Cocarde Major Rhodesian


Blog by Dal Stanton

Even though it was a snow trudging kind of day, making it to the ‘Hole in the Wall’ paid off again.  I mentioned this visit before when I was writing up the restoration of the Stanwell Silver Mount.  On this visit, I saw the Stanwell for the first time, but didn’t bite.  The next time I would!  On this visit, I found another very nice example of St. Claude, France’s claim to fame as an historic center of pipe production – rivaling the UK for market share in Europe.  When I saw the Butz-Choquin Cocarde Major in the pipe basket on the cluttered Hole in the Wall shelf, my initial reaction was its size – a hefty guy.  My first assessment was that it was a Bulldog shape, then I noted the large rounded shank – a Rhodesian or a Bullmoose?  This one is going home with me regardless!  I looked in the basket for a good pipe to bundle and I saw an attractive, diminutive, Bent Billiard Sitter with a swan neck stem – unmarked, but a very nice looking pipe.  When I got home I took a quick picture of the bundled pair and put them in the ‘Help Me!’ basket for later attention.butz1 butz2When I take the BC Cocarde Major out of the basket, I am anxious to recommission this nice-looking Rhodesian, I decide.  The first thing I do is pull up Google Translator and insert Cocarde Major in the French to English machine.  I did not study French in school so help is appreciated.  I want to know if special meaning is attached to this St. Claude BC.  Cocarde translated into English as the word, ‘Cockade’ which was defined as, a rosette, roundel or knot of ribbons worn in a hat as a badge of office or party, or as part of a livery. With a little looking on the internet, I found these interesting French examples of Cocardes.butz3With this meaning for ‘Cocarde’ it put doubt in my mind regarding my original thought that ‘Major’ referred to large or big.  Attaching Major to the idea of the French symbol of national pride, it is most likely pointing to a level of rank, or when ‘Major’ is attached to another rank (e.g., sergeant-major) it denotes the ranking of one superior among those of the same rank.  I emailed a colleague living and working in Toulouse, France, whose command of the language could help.  His comments confirmed what I was thinking:

The word cockade refers to a national symbole for the French, like “cocarde tricolore’ refers to the French flag which is, of course, one of the most important symbols of the French people and national pride.  It has many meanings, but for example official cars or planes have this symbol on it.  You are right about the word Major, refering to a military grade. Used as an adjectif, “majeur” it means big.   I would conclude that this is simply the name of the pipe.  You can’t translate it literally.  The pipe’s name implies in my opinion that it is a symbol of French pride, like the French insignia for a general in the military.

With the symbols of French pride stamped on this BC Rhodesian, I have a greater appreciation for the pipe when I take more pictures now on my worktable.butz4 butz5 butz6 butz7 butz8The stampings on the left side of the shank are “Butz-Choquin” in an arched script over “Concarde” over “Major”.  On the right side is, “St Claude” arched over “France” over “1028”, the BC shape number.  Per Pipedia’s history of the name, when Jean-Baptiste Choquin of Metz, started out as a tobacconist and the business prospered.  In 1858, one of his employees, one Gustave Butz, fell for his boss’ daughter and they were married.  That same year, Butz and Choquin came together to form the enterprise that is now known as Butz-Choquin, and eventually moved the operation from Metz to St. Claude, known as “the world capital of the briar pipe”.  Looking on the internet, I found another BC shape ‘1028’ but was called a ‘Bourbon Major’.  The shape was that of a Bulldog, with the diamond shank.  I know there is debate regarding the difference between Bulldog and a Rhodesian classification, but I am happy with Bill Burney’s descriptive difference in the Pipedia shapes Chart, that the difference between the two is, the Rhodesian has a round shank and the Bulldog, a diamond.

So, looking more closely at the BC Rhodesian in front of me, I see that the surface is generally in good shape – striking grain patterns.  There are two noticeable fills that need addressing.  There is also a chip over the shank, where the double grooves meet – the grooves forming the border between the upper and lower cones of the Rhodesian stummel.  The chamber has thick carbon cake buildup and needs removal down to the briar for a fresh start.  The stem has very little oxidation and a couple distinct clincher tooth marks on the top bit and chatter above and below.  The stamped ‘BC’ stem marking is in good shape but the white color needs touching up.  The following pictures show the question areas on the stummel – mainly fills and the chip.butz9 butz10Even though the oxidation is minor, I put the stem in an Oxi-Clean bath for a few hours to raise the oxidation to the surface.  I first cover the stem ‘BC’ stamp with petroleum oil.  Turning to the stummel, I take the Pipnet Pipe Reamer kit and use the two smaller blades of the four available and remove the cake using first the smallest, then graduating to the next larger when the blade stops meeting resistance.  This cake is hard and crusty but vacates in short order.  I fine tune the reaming with my Savinelli Pipe Knife.  I’ve grown to like this handy tool.  What The Pipe Smoker blog says about it is spot on:

Basically, a three-sided scraper, it can be placed in the chamber exactly where it needs to be placed and then cake is scraped off with a simple movement of the wrist. It allows full control over where the cake is being reduced. It has a rounded tip, which means that it will not damage the bottom of the bowl. It makes no difference, whether the chamber is straight or conical, I can use the same tool on either. It requires no adjustment. 

After the Savinelli pipe knife scrapes the chamber wall, I wrap 240 grit paper around a Sharpie pen and sand the chamber removing the last vestiges of carbon.  I then wipe the bowl with a cotton pad wetted with isopropyl 95%.  The chamber looks great.  I fold up the paper towel and my work station is clean again.  Pictures show the progress.butz11 butz12 butz13 butz14I then switch to the internals of the stummel and clean the mortise and airhole with pipe cleaners and cotton swabs dipped in isopropyl 95%.  After some extended effort, pipe cleaners and cotton swabs are coming out clean.  Later, I’ll add another measure of cleaning by giving the stummel a kosher salt and alcohol soak.  I like to go the extra mile when I’m preparing a pipe for a new steward.  The picture shows the progress.butz15Turning to the stummel externals, I remove the grime on the surface and clean the rim.  I use undiluted Murphy Oil Soap with cotton pads.  I use a bristle tooth brush as well to clean the double grooves circling the cone.  I also employ a brass brush to clean the lava and grime off the rim.  The pictures show the progress.butz16Time to fish the stem from the Oxi-Clean bath.  It’s amazing that even when the stem looks to have little oxidation, the Oxi-Clean bath raises the oxidation to the surface.  I wet sand with 600 grit paper to remove the bulk of the oxidation from the vulcanite and then follow-up using 0000 steel wool. Throughout this process, I give care to work around the ‘BC’ stem stamping.  Pictures show the progress.butz17With the tooth dents on the upper bit, I attempt to remove by using a lit candle’s heat to raise the indentations by expanding the vulcanite but it wasn’t working well.  So, I apply a small drop of super glue to the spots and then apply an accelerator to cure the glue.  After a few minutes, I use the flat edge needle file to file down the superglue patches to the vulcanite surface.  While I have the file out, I file the button lip, upper and lower, to give them more definition.  I follow with applying 240 grit paper to remove the file marks and to fine tune and blend the superglue patches.  I follow with 600 grit paper and then 0000 steel wool.  The pictures show the progress.butz18 butz19 butz20 butz21I clean and freshen the internals of the stummel further with a Kosher Salt/alcohol soak for several hours.  I set the stummel in a sturdy egg carton and twist a cotton ball and feed it into the mortise, pushing it in with a straight wire.  I then fill the chamber with kosher salt which is not iodized – which can leave a taste.  Then, I fill the chamber with isopropyl 95% until it surfaces above the salt.  The pictures show the process.butz22The next morning, the salt/alcohol soak had run its course and from the darkening of the salt and the cotton wick, the process effectively cleaned and freshened the stummel internals even after the plethora of pipe cleaners and cotton swabs.  I dump the old expended salt and thump the stummel on my palm, then use a paper towel and wipe the bowl.  I use bristle brushes to clean the mortise and again, pipe cleaners through the airway to finish the cleanup.  As billed, the soak works.  Pictures show the soak results.butz23With the internals of the stummel clean, I clean the internals of the stem.  Using pipe cleaners dipped in isopropyl 95% I work on the stem.  After I begin, even though the ¼ bent saddle stem is not an extreme bend, I’m surprised that I am not able to move a pipe cleaner through the stem without difficulty.  Finally, I pass a bristled pipe cleaner through and move it back and forth, hoping that it loosens up the passageway. It doesn’t.  I decide to use the technique that Charles Lemon used on Dad’s Pipes (See here: Link) of expanding the airway by heating the stem and moving a pipe cleaner through.  Just to be on the safe side, I draw an outline of the stem’s bend to use as a template for a comparison after I re-bend the pipe back to the original.  I first straighten the stem by warming it with a heat gun until the vulcanite becomes pliable.  After inserting a pipe cleaner through the stem, I then reheat the stem and return the stem to the ¼ bend.  Now, back to the original curve comparing to the template, without difficulty I complete the cleaning of the stem using isopropyl dipped pipe cleaners moving freely through the airway.  I also clean the crud out of the slot with a dental probe.  Pictures show the process.butz24 butz25Before starting the micromesh phase to raise the luster of the BC bent stem, I use Miracle Eraser on the ‘BC’ stem stamp to remove the oxidation without applying an abrasive to the stamp.  It does seem to help.  Then, I wet sand the stem using micromesh pads 1500 to 2400, followed by dry sanding with 3200 to 4000, then 6000 to 12000.  I complete each set by applying Obsidian Oil to revitalize the vulcanite.  To watch the stem gradually pop, is an amazing process.  This Butz-Choquin is cleaning up nicely.  I set the stem aside to dry.butz26 butz27Now I return to the stummel and take a close look.  After cleaning with Murphy’s Soap, I detect about 4 or 5 fills on the surface that need addressing. The fills are solid but with some, I’m able to scrape of the upper layer of the fill.  There is also a chip in the double grove going around the stummel.  With the smaller fills, that are not pitted, I use dye sticks, starting with a lighter hue and graduating to a darker hue, until the blend is best.  I then use a lightly dampened cotton pad with isopropyl 95% to dab the areas to blend further with the surrounding briar.  The pictures show the progress.butz28 butz29With those more pitted, I mix a bit of superglue and briar dust to form a putty and apply on the pitted fills.  Carefully, I also paint the groove chip and before the putty start hardening, I clear overflow putty from the grooves with a sharp dental probe.  I use an accelerator to cure the briar dust putty patches more rapidly.   After a short time, I sand each putty fill to bring it to the briar surface.  I first carefully use a flat needle file to work the putty hills down to almost surface level then I use 240 grit paper to sand to the surface level.butz30 butz31 butz32Decision time.  I want to restore this Butz-Choquin as close to the original shade as I can.  I discovered on TobaccoPipes.com a BC in the same shape group as the Cocarde Major – 1028.  In the picture below, the shade of the stummel is light and I think I can achieve this by simply sanding the stummel and restoring the briar to its original natural luster – MINUS what appears to be an acrylic finish below. I can still decide to apply a stain at the end of the sanding process after I have a better idea of the briar as it emerges.  The shape below is a BC Cocarde 1025 – the only difference I detect is the tapered stem versus the saddle stem.butz33First, I want to freshen the rim lines and re-cut an inner bevel which will look better and remove discoloration on the inner rim edge.  The rim has a subtle slant toward the chamber.  I cut the initial bevel using a coarse 120 grip paper rolled tightly.  When I reestablish the bevel, I follow by sanding with 240 grit sanding paper.  I then sand the stummel using a medium grade sanding sponge, followed by a light grade sanding sponge.  I am careful to work around the stampings on the sides of the shank.  Before I move on to the micromesh sanding, I use dye sticks to help blend the fill patch areas that are not yet blending.  After applying the dye stick, I then lightly dab the area with a cotton pad slightly wetted with alcohol.  This helps blend with the surrounding briar.  The pictures show the progress.butz34 butz35 butz36 butz37I follow by using micromesh pads 1500 to 2400 and wet sand the stummel.  After this, I dry sand using 3200 to 4000 then finish with pads 6000 to 12000.  I then run a toothpick through both grooves connecting the upper and lower domes of the Rhodesian to remove residue remaining from the sanding process.butz38 butz39To step back and take in the big picture, I reunite stem and stummel and take a picture.  I see two distinct briar dust putty fills that are looking like I should have used a clear superglue fill instead.  They are darker than the surrounding grain environment – not an ideal situation.butz40I decide I can live with the fill on the upper cone, next to the rim.  It is smaller and I hope that it will blend after applying a light brown stain which is looking like will be needed.  With the larger lower fill, I will delicately try reaming the fill with the point of a Dremel tool to remove the putty.  Depending on how that goes, the next step will be to shape the fill somewhat so that the shape is less circular and flows more with the surrounding grain pattern.  Then, I will fill the new hole with clear superglue, sand and again be back to where I am now – hopefully with better blending.  Phase one seems to go well – very carefully.  With the Dremel tool I clean the putty fill and shape the pit circle to flow with the grain.  I then spot-glue and use accelerator to cure the new clear patch.  Looking good so far.   I use a flat needle file to remove the superglue fill mound almost to the briar surface, then I use 240 grit paper rolled, to strategically stay on top of the glue to bring it down to surface.  I follow with 600 grit, then steel wool, then the full array of 9 micromesh pads, 1500 to 12000.  I touch up a bit with a light dye stick and blend with a cotton pad with a bit of alcohol.  I am now back to where I was at the beginning of the detour. The fill is still visible, but doesn’t jump out proclaiming, “Here I am, Boys!”  The pictures show the detoured progress.butz41 butz42 butz43 butz44Now, to promote blending throughout the entire stummel, I use Fiebing’s Light Brown Leather Dye.  I warm the stummel to open the grains to receive the dye.  Using a doubled-over pipe cleaner I liberally apply the dye over the stummel careful to achieve full coverage, rim and grooves.  I then flame the aniline dye with a lit candle and the alcohol immediately burns off, setting the dye in the grain.  To achieve total coverage, I repeat the process above after a few minutes, complete with flaming.  I put the stummel aside to rest and I’ll return to it after work this evening.butz45One last task to do before heading to work.  I want to freshen the ‘BC’ stem marking with white acrylic paint.  I put a small dab of paint over the ‘BC’ and then use a toothpick to spread the paint, making sure the marks are fully covered.  Tonight, after the paint is fully cured, I’ll scrape off the excess leaving a fresh Butz-Choquin stem.butz46Back home and ready to go.  The white acrylic paint has fully cured on the stem marking.  I take a toothpick and gently scrape the excess paint away using the side of the toothpick.  Doing this, the toothpick passes over the top of the stamping leaving the indentations fully renewed.butz47Time to ‘unwrap’ the fire crusted stummel after applying Fiebing’s Light Brown Leather Dye.  Using the felt wheel, I set the speed of the Dremel to the slowest possible and using Tripoli compound, after purging the wheel of old compound with the sharp edge of the Dremel’s adjustment wrench, I remove the crust from the stummel.  I take a picture to show this process.  After the crust is removed, I use cotton pads wet with isopropyl 95% to wipe down the stummel.  I lighten the stummel’s hue a good bit aiming for the original as closely as possible and to blend the dye across the grain.  When I reach the hue that looks good, I switch to a cotton cloth wheel mounted on the Dremel, and after reuniting stem and stummel, I apply Blue Diamond compound both.  I’m loving watching the grain on this BC Cocarde Major Rhodesian start popping – it is truly an amazing process and the components of such fine abrasion produce such a result in the briar. When completed with Blue Diamond I give the pipe a buff with a felt towel, not so much for shining but to remove residue compound before I apply the wax.  After mounting the cotton cloth wheel on the Dremel, I increase the speed to the second slowest speed and apply several coats of carnauba wax to stem and stubble.  When finished, I rigorously hand buff the pipe with a micromesh cloth.butz48 butz49The grain on this Rhodesian is placed perfectly to enhance the proud, chin forward carriage of the stummel.  The horizontal flame grain crosses the heel of the stummel and flows to the sides terminating in bird’s eye – a beautiful showpiece of briar that is well-suited to bear the name of French pride – Cocarde Major.  This Butz-Choquin Rhodesian, another traveler from St. Claude, is looking for a new steward.  I sell the pipes I restore and give the profits to benefit the work we do here in Bulgaria with the Daughters of Bulgaria – rescuing women and children who have been trafficked and sexually exploited.  If you are interested in adding this Butz-Choquin Cocarde Major Rhodesian to your collection, you can find it at the store at my blog site, The Pipe Steward.  Thanks for joining me!butz50 butz51 butz52 butz53 butz54 butz55

Rejuvenating a Made in Leeds, England Ben Wade Natural Grain Lovat


Blog by Steve Laug

This little Ben Wade Lovat is the fourth pipe of the lot from Eastern Canada that I am restoring for a pipe man from there who sent it to me. It is stamped on the left side of the shank BEN WADE over Natural Grain and on the right side of the shank it reads Made in Leeds over England and a shape number 20 V near the bowl shank junction. The finish was natural and either unstained or stained with a light tan stain. The grain is quite good on the pipe. The rim is in rough shape from having been knocked on hard surfaces to remove the dottle. There were dents, dings and roughening. The bowl was slightly out of round. The stem was good quality vulcanite and has light oxidation at the joint of the stem and shank. There was tooth chatter and tooth marks on the top and bottom side near the button.ben1 ben2I took some close up photos of the rim and the stem. You can see the damage to the outer and inner edges of the rim as well as dents in the rim top. The cake has been poorly reamed from the bowl and there were some gouges in the briar walls that will need to be sanded out. The stem photos show the tooth chatter and marks as well as the small band of oxidation next to the shank.ben3 ben4I have always heard that the Ben Wade Company made quality English made pipes prior to its purchase by Herman Lane but I did not have any idea of the history of the brand. I did a bit of research on it and found the following helpful information on Pipedia. The link follows the quoted portion.

The company was founded by Benjamin Wade in 1860 in Leeds, Yorkshire, where it was located for over a century. Ben Wade started as a pipe trader, but yet in the 1860’s he established a workshop to produce briar pipes. The pipes were made in very many standard shapes – always extensively classic and “very British”. Many models tended to be of smaller dimensions. Ben Wade offered a very high standard of craftsmanship and quality without any fills. Thus the pipes were considered to be high grade and a major competitor to other famous English brands. The often heard comparison to Charatan seems to be a little bit inadequate because those days’ Charatans were entirely handmade.

In the II World War the factory was destroyed by German air raids on Leeds. But the Ben Wade family decided to re-build it immediately after the war and pipe production was re-started soon and successfully linked to the fame from the pre-war years. Even though the owner family decided to leave pipe business and sell off the firm. The family went into negotiations with Herman G. Lane, president of Lane Ltd. in New York at about the same time as the Charatan family. Lane Ltd. bought both firms in 1962.

Herman G. Lane had been Charatan’s US sole distributor since 1955 and Charatan always remained his pet child. But Ben Wade was treated in another way by its new owner. The fabrication of pipes was reduced and the factory in Leeds was closed in 1965 finally.

So this was the end of Ben Wade pipes stamped “Made in Leeds, England”. https://pipedia.org/wiki/Ben_Wade

The pipe I was working on was stamped “Made in Leeds, England” thus effectively dating it to the period the company was owned by the family. I know that it was made before the closing of the factory in 1965. So I had the last date it could have been made. Judging from the age of the rest of the auction lot my guess would be that this pipe also came from the 1930s. The style and cut of the stem leads me to place it in that period.

I cleaned up the reaming in the bowl with a Savinelli Fitsall Pipe Knife and took the cake back to bare wood. It took some work to smooth out the gouges in the bowl walls. I was able to remove many of them leaving only a remnant behind. I wrapped a dowel with sandpaper and sanded the bowl walls after I had reamed it.ben4a ben5To remove the damage to the rim edges and the top I topped the bowl on the topping board. I did a minimal topping to just even things out and clean up the surface.ben6I scrubbed the bowl surface with acetone on cotton pads to remove the grime and oils that were embedded in the bowl sides. I wanted to get the briar clean so I could retain the natural finish.ben7 ben8I used a folded piece of 220 grit sandpaper to give the inside rim a light bevel to bring the bowl back into round. I also used in on the outside edge to soften it.ben9With the bowl clean I lightly sanded it with a medium and a fine grit sanding sponge to take out the scratches and smooth out the finish. I sanded it with 1500-2400 grit micromesh sanding pads as well. When I had finished sanding it I wiped it down with a last wipe of alcohol on a cotton pad in preparation for giving it a light coat of oil. I rubbed the bowl down with olive oil and polished it by hand.ben10 ben11I set the bowl aside and turned my attention to the stem. I sanded the entire stem with 220 grit sandpaper to remove the oxidation and the tooth chatter. I “painted” the tooth marks in the stem with a lighter flame until they lifted. I sanded the damaged areas with the sandpaper until the surfaces were smooth and showed no more sign of tooth damage.ben12I wet sanded the saddle portion of the stem with 1500-2400 grit micromesh pads and then used Rub ‘n Buff European Gold to fill in the portions of the BW stamp that still showed on the stem surface.ben13I cleaned out the interior of the mortise and the airways in the shank and the stem with alcohol, cotton swabs and pipe cleaners until they were no longer dirty and oily. As you can see from the photos below it took a few swabs and cleaners to get to that point.ben14I polished the stem with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I rubbed the stem down with Obsidian Oil after each set of three pads. After the final rubdown with oil I set the stem aside to dry.ben15 ben16 ben17Once the oil had dried I buffed the bowl and stem with Blue Diamond on the buffing wheel and then gave them both multiple coats of carnauba wax. I buffed the pipe with a clean buffing pad to raise the shine and hand buffed it with a microfibre cloth to deepen the shine. The finished pipe is shown in the photos that follow. It came out quite nice with the grain popping through over the bowl and shank. The pipe will soon join the others in the lot on the return trip to Eastern Canada. Thanks for looking.ben18 ben19 ben20 ben21 ben22 ben23 ben24 ben25

 

An old Sasieni Sashar London Made 901 Billiard


Blog by Steve Laug

The third pipe I worked on from the pipe man in Eastern Canada who picked up that old lot at an auction is one that is stamped on the left side of shank with the name Sashar over London Made. On the right side of the shank it is stamped with the shape number 901. The rim was worn and whoever cleaned the pipe before I got it removed a lot of the finish. The inner bevel of the rim had a burned area on the right front side. The outer edges of the bowl were worn. The stem was good quality vulcanite and had light oxidation and tome tooth marks on both sides of the stem near the button. The inside of the shank and the stem was very dirty with tars and oils. There was a stinger in the tenon that extended into the bottom of the bowl. There was a light cake in the bowl that would need to be cleaned up as well.sas1 sas2I remembered that the Sashar line was made by Sasieni. I could not remember any other information on the brand. I did a Google search and found that there was a write up on rebornpipes – go figure. I looked and it was a blog that Al Jones wrote on a Sashar pipe that he worked on. Here is the link https://rebornpipes.com/2016/12/19/sasieni-sashar-restoration/.

I did some more searching and found a short writeup on Wesley’s – a pipe shop in South Africa about the pipe brand. It was under a heading there entitled SASIENI. I quote from that site the following: “Joel Sasieni started as an apprentice with Charatan, moved to Dunhill when it opened in 1910, and started his own company in London in 1918 making high grade pipes largely for the US market. They also manufactured pipes under the brand name Sashar (specifically for South Africa) for pipes a little down the line. The company was sold in 1979 and the pipes are now made by a completely different firm.” http://www.wesleys.co.za/refurb04.html

Now I had a bit of information on the brand. It was a Sasieni made pipe manufactured under the Sashar brand name for South Africa. Armed with that information I turned to working on the pipe. I took close up photos of the rim top and inner edge as well as the tooth marks on the stem. In the photo of the bowl you can see the damage on the inner edge of the bowl. The bowl was slightly out of round and there was a burn mark evident mid rim on the right side of the bowl.sas3 sas4In order to clean out the airway in the stem I needed to remove the inner tube from the tenon. I heated it with a lighter until the oils and tars holding it in place warmed up. I wrapped the jaws on a pair of pliers and used it to turn the inner tube out of the tenon. With the tube removed I was able to clean out the airway without impediment.sas5I used a folded piece of 180 grit sandpaper to rework a bevel on the inner edge of the bowl. Once I had the bevel cut I worked on it again with 220 grit sandpaper and 1500 grit micromesh sanding pads. I rolled a piece of 220 grit sandpaper into a tube and wrapped it around a dowel and then my finger to sand the inside of the bowl and clean up the remaining cake on the walls.sas6 sas7I used a dark brown stain pen to restain the top of the rim and the inner and outer edge of the bowl. I spot coloured it with a black Sharpie pen and blended the two together to get the finish to match the rest of the bowl.sas8I used a wet cloth and a butter knife to steam out the dents in the back side of the bowl. I heated the knife in the flame of the burners on my kitchen stove. When hot, I folded a wet towel against the dents in the briar and laid the hot knife on the wet cloth. It generated a fair amount of steam. I repeated the process until the dents were lifted.sas9 sas10I used 99% isopropyl alcohol, cotton swabs and pipe cleaners to clean out the mortise and the airway in the shank and the stem. They were not too dirty so it took very few cleaners to clean it. Once the stem was clean I put the inner tube back in place in the tenon.sas11I sanded the tooth chatter on the stem at the button with 220 grit sandpaper to remove it and the few tooth marks that were also present on both sides of the stem near the button.sas12I polished the stem with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I rubbed the stem down with Obsidian Oil after each set of three pads. After the last set of pads I gave it a final coat of oil and let it sit and dry.sas13 sas14 sas15I buffed the bowl and stem with Blue Diamond on the buffing wheel to polish the briar and the vulcanite. I gave them both multiple coats of carnauba wax and buffed it with a clean buffing pad to raise the shine. I hand buffed it with a microfibre cloth to deepen the shine. The finished pipe is shown in the photos below. It is ready to go back to its owner in Eastern Canada. Thanks for looking.sas16 sas17 sas18 sas19 sas20 sas21 sas22 sas23

New Life for a KBB Yello-Bole Sandblast 2705 Billiard


Blog by Steve Laug

This is the second pipe that was sent to me by a fellow Canadian for a cleanup and restoration from the lot he had picked up in a local auction for a great price. This one is an older Yello-Bole sandblast billiard with the KBB cloverleaf on the underside of the shank. It has a great looking rugged sandblast on the bowl that highlights the grain. The overall finish appeared to be in good shape though the crevices in the blast were dirty. The bowl had been cleaned before the auction and there was some scratching on the bowl walls. There was still an overflow of tars in the finish that remained on to the rim in the parts that were not damaged. The outer edge of the rim had the look of a pipe that had been smoked hard and knocked out on anything close at hand no matter what it did to the pipe. There were nicks and dings all the way around the rim top and edges. The first five photos that I have included are ones that I received from the pipe’s owner when he emailed and asked me about repairing his find. The first is an overall view of the pipe. yb1The second and third photos are close up shots to clearly show the extent of the damage to the rim top and outer edges. As far as I could see from the photos the inner edge of the rim appeared to be in great shape. The outer edge was another story.yb2The last two photos he sent show the fit of the stem against the shank and the stamping on the underside of the shank. From the first photo it did not appear that the stem was properly seated in the shank. My experience has been that the stems on these older Yello-Bole pipes had an excellent fit but when tars collected around the walls of the shank surrounding the spade stinger the stem would not properly seat. I was hopeful this would be the case with this one. The second photo shows the clear stamping on the underside. It is stamped with the four digit shape number 2705 which is a billiard number and after the 5 is the letter u. The KBB cloverleaf is followed by the classic Yello-Bole stamp and under that it reads Algerian Bruyere.yb3When the pipe arrived I snapped some photos of the condition of the pipe before I started the cleanup. The stem had light oxidation and the yellow O logo was perfect. The inside of the shank was quite dirty so my assumption regarding the reason that the stem did not seat properly was correct. Unfortunately before I took the photos I had done some cleaning on the rim top and edges. I used a sanding block on the edges to knock off loose debris and a dental pick on the rim. I touched up the raw briar with a black Sharpie pen because I have learned that when it is mixed with a dark brown stain I can get a match to the colour of the stain on the bowl. blast1 blast2At this point in the process I used a brass bristle tire brush to scrub out the crevices and sandblast on the top surface. I did this to prepare the rim for restaining, to clean out the blast crevices and to smooth out some of the roughness I have found that this brush does a great job in lifting the dust and tar while not damaging the briar. The brass bristles are soft and do not scratch the briar but make easy work of the tars and build up on the rim of a blast. I scrubbed the inner beveled edge with the brush and it came out looking undamaged. The sandblast reappeared on the rim top as well.blast3I used the black Sharpie pen again to add a dark colour in the chips and nicks in the finish around the edges and the top of the bowl. When that was finished I stained the bowl with a dark brown aniline stain thinned 50/50 with isopropyl alcohol. I fired the stain with a lighter and repeated the process until I was satisfied with the coverage on the bowl. You can see that the nicks along the edges of the rim look very good. The rim top needs to be polished and it will look the same after I have waxed and buffed it.blast4 blast5I probably should have cleaned up the inside of the bowl earlier but as I worked on the rim first it almost escaped my notice. In the last photo above I could see the cake in the bowl and what appeared to be some damage to the inside wall of the left side. I used a Savinelli Fitsall Reaming knife to take the cake out of the bowl. I was able to ream back the walls and the apparent damage disappeared. I used a pen knife to scrape the hard tars that had collected in the shank and mortise. I was amazed at the amount of powder that came out of the shank. It was thick and black and proved my point made earlier about it keeping the stem from seating properly against the shank.blast6I scrubbed the mortise and the airways in the stem and the shank with 99% isopropyl alcohol, pipe cleaners and cotton swabs until I removed all of the grit and grime from those areas. I cleaned the spade stinger with alcohol and pipe cleaners and polished it with 0000 steel wool until it shone.blast7The pipe smelled of old aromatics and even with the bowl and shank clean the smell was present. I stuffed the bowl with cotton balls and used an eye dropper to fill it with isopropyl alcohol. I have found that cotton balls work as well as Kosher salt does and it is not as messy. I put a cotton swab in the shank up to the entrance of the airway into the bowl as it wicks alcohol into the shank and draws out the oils in that area. I put the pipe bowl upright in an ice-cube tray and let it sit over night to let it do its magic. The second photo shows the cotton balls, discoloured with the oils after sitting 8-9 hours. Once I removed the cotton balls I scrubbed out the shank and airway to remove any remnants of alcohol left behind and set the bowl aside to dry.

I have written about this alternative to the salt and alcohol treatment in an earlier blog that can be read here. https://rebornpipes.com/2013/02/10/sweetening-a-pipe-an-alternative-to-the-salt-and-alcohol-treatment/blast8I sanded the stem with 220 grit sandpaper to remove the light oxidation and the light tooth chatter at the button. It did not take too much sanding to remove those from the stem.blast9I polished the stem with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. This is my normal routine and if you have been following the blog for any length of time you know that I always follow this procedure with the stems. Between the 4000 grit pad and the 6000 grit pad I buffed the stem with White Diamond and then went on to use the final three grits of micromesh pads. I gave the stem a rubdown with Obsidian Oil after each set of three pads and after the last set put it aside to let the oil dry.blast10 blast11 blast12I hand waxed the bowl with Conservator’s Wax and buffed it with a shoe brush. I find that the wax does not clump in the crevices of a sandblast finish like carnauba does so I always hand wax this kind of finish. I buffed the stem with Blue Diamond on the buffing wheel and gave it multiple coats of carnauba wax. I buffed the bowl and stem with a clean buffing pad to raise the shine and then hand buffed it with a microfibre cloth to deepen the shine. The finished pipe is ready to go back across Canada to its owner. It is a beauty and I think he will enjoy it. Thanks for looking.blast13 blast14 blast15 blast16 blast17 blast18 blast19 blast20

 

Reworking a very damaged Toogood’s Make “A” Billiard 12F.


Blog by Steve Laug

I was contacted by a fellow Canadian who had just picked a nice selection of 6 older pipes at an auction. He picked them up for a very good price. Five of the six pipes were in very good shape. There was an older Dunhill Duke St. SW Lovat, an L&Co small billiard, an older KBB Yello-Bole 2705 sandblast billiard, a Ben Wade Natural Grain Lovat, a Sashar billiard made by Sasieni for South Africa and this older Toogood’s Make A billiard. The little billiard is stamped on the left side of the shank 12F and next to that is Toogood’s over Make over A. On the top of the shank flowing down the right side it reads Made in over England over Sun Dried over in Surrey. I was unfamiliar with the brand and I could not find any information on it on the web. My usual sites did not give me any information. I checked in my copy of Who Made That Pipe and information that the brand was made by Mason & Toogood. It listed 12 different variations on the brand. I have included a screen capture of the section from the book that shows the brand.too1aI searched the web for information about Mason & Toogood in Surrey, England but I could not find anything under that heading either. Perhaps some of you reading this may have some information on this brand.

I took some pictures of the pipe before I did any clean up or restoration on it. I chose to work on this one for the challenge more than anything else. I knew that even once it was restored it would not have any particular value but I like the challenge and enjoy seeing what I can do. You can see the deep gouges on the right side of the bowl from the rim down about ¼ inch. There were also some deep marks and scratches just below the gouges. I took photos of the side of the bowl and also from the top down showing the depth and extent of the damage to the right side.too1 too2I took a photo of the stamping on the shank sides to record the information and to see if any of you recognize it once you see the photos.too3I took some close up photos of the damaged bowl side and the rim top. These show the depth of the gouge and the deep nicks on the rim and the bowl side. It was in rough shape and would take some patience to rebuild the side and the rim.too4I reamed the bowl back to bare briar with a Savinelli Fitsall Pipe Knife in preparation for the work on the side and rim top.too5I decided to top the bowl on the topping board to remove the damage on the rim top. The gouges on the top of the rim were not as deep as the side. The photo below shows the rim top after topping the bowl.too6The next series of photos show the rebuild of the rim edge, top and side of the bowl with a mixture of clear super glue and briar dust. I layered on the glue and the dust to bring the level of the side up to the same thickness and height as the rest of the bowl.too7I sanded the repaired area with 180 grit sandpaper to smooth out the repair and blend it into the surface of the bowl. Once I had it smoothed out I sanded it with 220 grit sandpaper to smooth out the scratches. The next series of photos show the progress of the repair at this point.too8 too9I sanded the bowl repair with a medium and a fine grit sanding sponge and then with 1500-3200 grit micromesh sanding pads. I was able to remove the scratches in the briar with the sanding pads. I stained the bowl side with a dark brown stain pen to match the rest of the bowl colour. This was the first coat of stain. I would follow it with darker coats to try to blend it in better with the bowl side.too10I sanded the freshly stained rim and bowl side with 1500-3200 grit micromesh sanding pads to remove the scratches that showed up on the pipe after the first coat of stain. I restained the bowl side and top with a dark brown aniline stain and flamed it with a lighter. I gave it a second coat and repeated the flaming of the stain to set it in the grain.too11I buffed the bowl with White Diamond on the buffing wheel to raise the shine. The photo below shows the bowl at this point in the process. I still needed to blend the repair into the briar with a black Sharpie Pen. The photos below show the repair before the black Sharpie touch ups.too12The stem was in pretty decent shape with light oxidation. The stem had an aluminum inner tube that was set in the tenon and seemed extend quite a ways up the inside of the airway in the stem.too14I sanded the stem with 220 grit sandpaper to remove the scratches and the tooth chatter on the stem surfaces at the button on both sides. I smoothed out the surface of the stem and then polished it with micromesh sanding pads. I wet sanded with 1500-2400 grit sanding pads and dry sanded it with 3200-12000 grit pads. I rubbed the stem down with Obsidian Oil after each set of three pads. After the final sanding pad I gave it a last rub down with the oil and set it aside to dry.too15 too16 too17I buffed the bowl and stem with Blue Diamond on the buffing wheel. I gave it multiple coats of carnauba wax and buffed it with a clean buffing pad to raise the shine. I hand buffed it with a microfibre cloth to deep the shine. The repair still shows on the right side; but the pipe is useable and it looks pretty good. The repair blends into the stain on the rest of the bowl. It is smooth to touch and the rim also is in good order. The finished pipe is shown in the photos below. I took some close up photos of the repaired side and rim to show how they look up close. While I still do not know who made the pipe, I like the look of the pipe. The maker laid out the pipe to flow with the grain. The straight and flame grain on the bowl sides, front and back sides looks great and the sandblast on the bottom of the bowl and shank looks good. Thanks for looking. too18 too19 too20 too21 too22 too23 too24 too25 too26 too27