Tag Archives: repairing bite marks

Refurbishing a Tired Preben Holm #1 from the Mumbai Bonanza Lot


Blog by Paresh Deshpande

I am a big fan of Free Hand pipes!!! I love the way these pipes fit in to the hand and the creativity of the carver can be really appreciated in these pipes. And a freehand pipe made by the renowned Danish pipe carver, Preben Holm, is my dream come true. To be very honest to you all, the PH estate pipes that are available nowadays on eBay are very expensive and well nigh out of my reach. So when Abha, my wife, sent me pictures of the Mumbai Bonanza lot, I was immediately attracted to one free hand pipe that screamed PREBEN HOLM and when she confirmed that it was indeed one, I knew I was lucky. I say lucky because of the circumstances in which I made a purchase of this lot of 30 pipes and thereafter, the pipes that I received in this lot. I have given a gist of this purchase in the paragraph below. Well, the PREBEN HOLM is finally on my work table now!

I was fortunate enough to have heeded the advice of my dear friend and mentor, Steve, and struck a deal with a junk collector from Mumbai. He did not know what he was selling and I did not know what I was buying as we reside in different cities!! The argument that Mr. Steve presented was that if not anything, I shall at least have some spares and this was logical. I struck a deal and here are pictures of the pipes that I received in this lot. This lot contains some very nice collectible pipes, a few well known brands and some mediocre brands. Overall, with seven Dunhill pipes, a Preben Holm #1 FH, a couple of “Made in England” Pete System pipes, a couple of  Charatan’s Belvedere, Custom-Bilt, Stanwell and other assorted pipes, I would say that I had struck a decent haul!!! This is indeed my “Mumbai Bonanza”.

This 14th pipe that I decided to work on from this find, is a smallish Free Hand pipe with a bone shank extension and is indicated in yellow colored arrow in the picture below. It is stamped on the bottom of the shank towards the shank end as “PREBEN HOLM” in block capital letters over “HAND CUT” in a fancy script over “COPENHAGEN” over “DENMARK” again in block capital letters. The left side of the shank is stamped with an encircled numeral “1”. All the stampings are crisp and easily readable. The stem is devoid of any logo.To research this brand and line/ model in specific, I referred to pipedia.org in an attempt to date this pipe and understand the significance of the numeral # 1, if it was a shape code or grading code. However, there is nothing on this numbering system, except on Preben Holm “Private Collection” where the grading system starts with 101, 202 up to 808 in ascending order. And this is definitely not from “Private Collection” line!! I even visited rebornpipes.com in the hope that I would be able to unravel the mystery shrouding this pipe, but to no avail.

But nonetheless this is a PREBEN HOLM and is staying with me. Any reader who has any information or knowledge about this pipe is earnestly requested to share it with us on rebornpipes!

INITIAL VISUAL INSPECTION
The smooth stummel has some beautiful straight grains on the front, back and sides of the stummel. On either side of the stummel, is an elegantly contoured elevation which makes for a nice and comfortable hold with the thumb and the middle finger while smoking. The front of the stummel rises above the back making for a downward sloping rim top surface. The upper portion of the rim top flares out in a typical PH design and adds a distinct feature to the appearance of the pipe. The stummel surface is covered in dirt and grime giving the stummel a dull and lackluster appearance. There are a one/ two likely fills, noticeably on either side near the shank and stummel junction and another couple near the foot. These will be clear when the stummel is cleaned of all the grime. A thick layer of cake can be seen in the chamber. The backwards sloping plateau rim top surface has nice knobby raised portions and the portion of crevices formed, is covered in thick overflow of lava, dirt, dust and grime. The condition of the inner walls of the chamber and rim top surface will be known once the cake has been taken down to bare briar and the rim top crud has been scraped off completely. The inner rim condition appears to be in good condition with no burn/ charred surfaces. Only once the stummel has been thoroughly cleaned that I can be sure of my initial appreciation. In spite of the thick cake, the chamber odor is, surprisingly, not strong and should be addressed once the cake has been taken down to the bare briar and the shank internals have been thoroughly cleaned. The draught hole is dead center at the bottom of the chamber and should be a great smoker. The shank end is adorned with a horn shank end extension which is pinched in the middle and then flares outwards matching in profile with the rim top. The shank extension is dry and has darkened nicely due to absorption of all the oils over the years of smoking. This will add a nice classy touch to the overall appearance of the pipe once cleaned and hydrated. The shank extension end and mortise are blocked with accumulated dried gunk, adversely affecting the airflow. The fancy vulcanite stem is heavily oxidized and has calcification deposits towards the button end. There are deep tooth marks on the lower and upper stem surface in the bite zone and appears that the previous owner has literally chomped on the bite zone of the stem. The lower stem surface is cracked near the button edge and is circled in red. The button edges also have bite marks, in fact, they are badly worn out. The tenon and horizontal slot shows accumulated oils and tars. The oxidation in the space between the three squares, in descending size from the tenon end to slot end, is going to be a bear to get rid of but once nice and shiny will elevate the appearance of the overall pipe manifold times. Along with the stems of other pipes in line for restoration, I immersed the stem of this Preben Holm in a mix of one part Hydrogen Peroxide 20% with one part hot water after I ran a couple of pipe cleaners dipped in alcohol through the stem air way. A couple of hours later, the stem oxidation on all these stems were raised to the surface. The pictures below show the stem after it was removed from this bath. The appearance is definitely not for the fainthearted, to say the least!!After I had fished out the stem from the Hydrogen Peroxide bath, I scrubbed it with Magiclean sponge and followed it up with a wipe of cotton swab and alcohol. I further scrubbed the stem surface with 0000 grade steel wool. The loosened and superficial layer of oxidation was easily removed and revealed the condition of the stem.. There are deep bite marks in both the upper and lower bite zone. The bite marks are deep enough to cause significant thinning of the surface and complete disfigurement of the button edges. The deeper oxidation that was pulled to the surface would require more abrasive techniques.

THE PROCESS
I started the restoration with the stem repairs as this would take the maximum of my time to clean, repair and spruce up the stem. I cleaned the internals of the stem using hard and normal bristled pipe cleaners and isopropyl alcohol. The heap of pipe cleaners tells the sordid tale of the stem condition. With a pointed dental tool, I scraped out the entire dried gunk from the slot. I addressed the deeper oxidation by sanding the entire stem with a folded piece of 150 and followed by 220 grit sand paper. Once the oxidation was completely removed, I wiped the surface clean with a cotton swab and alcohol and rubbed a little Extra Virigin Olive oil to hydrate the stem. I flamed the damaged button edge and the nicks and dents with the flame of a lighter. This helps the vulcanite to rise to the surface as it has an inherent property to regain its original shape when heated. At this stage, I could clearly make out the extent of damage to the lower surface and the extent of the crack in the bite zone. This was further accentuated due to heating with the flame of a lighter. The upper surface too has a couple of deep tooth marks. Just for the information of statistically oriented reader, to get the stem to this stage it took better part of the afternoon and well past mid night!! Continuing with the stem repair, with a dental spatula, I probed the area around crack from inside the slot end with the aim of dislodging only the thin and loosened stem surface. Once the thin and loose stem surface was removed, I was certain that the rest of the stem surface around the crack was solid. I inserted a triangulated index card covered in transparent tape in to the slot. The tape prevents the mix of superglue and charcoal from sticking to the index card. I mixed superglue and activated charcoal powder and generously applied it over the bite zone on either side, including over the button and set it aside to cure.While the stem fill was set aside to cure, I started with cleaning of the stummel as I was keen to know the condition of the walls of the chamber. With size 1 head followed by head size 2 of a PipNet pipe reamer, I took the cake down to bare briar. Using a folded piece of 180 grit sand paper, I sand out the last traces of cake and expose the walls of the chamber. I wiped the chamber with a cotton pad dipped in isopropyl alcohol to remove the carbon dust left behind by all the reaming and sanding process. Once the chamber walls were cleaned out, I was pleased to note a pristine chamber with no signs of heat fissures/lines/pits. Next, I cleaned out the internals of the shank and mortise. Using my dental tool, I scraped out all the dried oils, tars and gunk that had accumulated in the shank airway and mortise. The amount of crud that was scrapped out and the condition of the pipe cleaners that were used leaves no surprise why air flow through it was restricted. I finished the cleaning by running a few pipe cleaners dipped in isopropyl alcohol. I also wiped the shank with cotton buds and alcohol. With this cleaning, all old smells in the pipe are history. The pipe now smells clean and fresh.With the internals of the stummel now clean, I cleaned the external surface using a hard bristled toothbrush and Murphy’s Oil Soap. I diligently scrubbed the rim top surface to remove the entire dust, dirt and lava overflow that was embedded in the crevices of the plateau rim top surface. With a soft bristled brass wired brush, I removed the overflowing lava from the rim top surface and cleaned the internals of the shank with a shank brush and dish washing soap to remove what little crud remained in the shank. I rinsed it under running tap water and wiped the stummel dry with an absorbent soft cotton cloth. Once I had wiped the stummel dry with paper towels and soft cotton cloth, I saw a couple of small and superficial fills on the left side of the bowl, near the bowl and shank joint and one at the foot of the stummel. These fills are marked in yellow circle. Very carefully and painstakingly, I completely removed the old fill with a pointed dental pick. I cleaned the fill of all the debris of old fill material, wiped it with alcohol and refreshed the fill with a drop of clear CA superglue in each fill and set it aside to cure overnight. By next day, the fill was nice, hard and well set. With a folded piece of 220 grit sand paper, I worked the fill till I had achieved a nice blend with the rest of the stummel surface. It turned out much better than I had anticipated. I further sand the entire stummel surface with the same grit sand paper to address the minor scratches and further smooth the stummel surface in preparation for a polish by micromesh pads. The plateau rim top surface still did show areas where the overflow of lava was still embedded in the crevices. With a dental pick, I diligently scraped each and every spot to remove the deposit of lava. I am now pleased with the cleaning of the rim top surface.I subjected the stummel, including the bone shank extension, to a complete cycle of micromesh polish, wet sanding with 1500 to 12000 grit pads. I wiped the stummel with a moist cloth after every grit pad to remove the sanding dust left behind by the pads. This also helps in monitoring the progress being made and ensures early corrective action. I am happy with the progress being made till now. Next, I rub a small quantity of “Before and After Restoration Balm” in to the briar, the bone shank extension and the plateau rim top surface with my finger tips and work it deep in to the surface and let it rest for a few minutes. The balm almost immediately works its magic and the briar now has a nice vibrant appearance with the beautiful straight grain patterns on full display. The contrast of the dark browns of the grain with the light hues of the rest of the stummel adds an interesting dimension to the appearance of the stummel. I further buffed it with a horse hair brush to further deepen the shine. I was slightly perturbed by the dark coloration taken on by the bone shank extension and shared pictures of the same with my mentor, Steve, who reassured me that this phenomenon is normal and should be good when the balm has been completely absorbed and polished subsequently. With this assurance, I move ahead with the stem repairs.

Using a flat head needle file, I reshaped the button and roughly matched the fills with the rest of the stem surface. I sanded the fills with a folded piece of 180 grit sand paper and followed it up by further sanding the stem with 320, 600 and 800 grit sand papers to achieve a perfect blending of the fills with the stem surface and a crisp button edge on either side of the stem. In my exuberance to cross the finish line, I completely missed out on taking pictures of this stage in restoration. My sincere apologies for this miss….

Using the micromesh pads, I completed the polishing cycle by wet sanding the surface with 1500 to 3200 girt pads. I had read that White diamond polish is between 3600 and 4000 grit of micromesh pads and best used between these two. I decided to give this a try to see if there is any difference in the final stem finish. I mount a fresh cotton buffing wheel on to my hand held rotary tool and apply white diamond polish and buffed the stem. I wiped the stem with microfiber cloth and go through the remaining pads, dry sanding with 4000 to 12000 grit pads. The stem looks great with the fills nicely matched with the rest of the surface. I rub a little quantity of Extra Virgin Olive oil in to the stem surface and set it aside to be absorbed by the vulcanite.To complete the restoration, I mount a cotton cloth buffing wheel on to my hand held rotary tool and applied several coats of carnauba wax. I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further and remove any residual wax from in between the plateaus of the rim top surface. The finished pipe looks amazingly beautiful and is now ready for its long second innings with me. I only wish it could share with me its life story of the past years while I enjoy smoking my favorite Virginia blend in it or maybe an English blend!! P.S. I earnestly would like to request all the readers to help me with the grading and dating this pipe. The only thing that is confirmed is that this is definitely not one of the high grade pipes from Preben Holm what with the fills that were seen on the stummel, but nevertheless, it’s a PH!!!!

There is only one more pending write ups which I shall be tackling before I undertake to restore a pipe which my dear friend and mentor, Steve, had sent me about a year back with the intention of providing me an opportunity to test my own skills. I wish to thank each one for sparing their valuable time to read through this write up and sharing this journey with me.

Restoring an Interesting Acorn # 7472 from Stanwell


Blog by Paresh Deshpande

One of the pipes in my Mumbai Bonanza lot which intrigued me no end was a small Acorn shaped pipe from the Danish pipe maker, Stanwell. I prefer large pipes and so this pipe was always being relegated to the next-in-line project status. Finally I decided to break the shackles of resistance and brought it to my work table as the next project. It’s a Stanwell pipe with shape code # 7472.

I was fortunate enough to have heeded the advice of my dear friend and mentor, Steve, and struck a deal with a junk collector from Mumbai. He did not know what he was selling and I did not know what I was buying as we reside in different cities!! The argument that Mr. Steve presented was that if not anything, I shall at least have some spares and this was logical. I struck a deal and here are pictures of the pipes that I received in this lot. This lot contains some very nice collectible pipes, a few well known brands and some mediocre brands. Overall, with seven Dunhill pipes, a Preben Holm #1 FH, a couple of “Made in England” Pete System pipes, a couple of  Charatan’s Belvedere, Custom-Bilt, Stanwell and other assorted pipes, I would say that I had struck a decent haul!!! This is indeed my “Mumbai Bonanza”.

This, then, is the 13th pipe that I decided to work on from this find and is an Acorn shaped pipe indicated in blue colored arrow in the picture below. It is stamped on the bottom middle half of the smooth surface of the shank as “# 7472” over “MADE IN DENMARK”. Towards the shank end, it is stamped as “STANWELL” in its trademark inverted arch in block capital letters. The stem bears a plain “S” logo on the left side of the stem.Now coming to the research of this brand and line/ model in specific, I referred to pipedia.org and as expected there is an extensive research on this pipe and even has a separate page on Stanwell Shape numbers and Designers, a study compiled by Stanwell collector and an undisputed authority on these pipes, Basil Stevens. However, there is nothing on this particular shape and number, in fact, this shape and number does not find any mention. I even visited rebornpipes.com in the hope that I would be able to unravel the mystery shrouding this pipe, but to no avail.

The only input I received was from Steve was that this is most likely a Sixten Ivarsson carved pipe, but nothing to date and confirm. Any reader who has any information or knowledge about this pipe is earnestly requested to share it with us on rebornpipes!

INITIAL VISUAL INSPECTION
The stummel has beautiful sandblast patterns on the uniquely shaped stummel with a short neck and a nice flow to the shape profile of the pipe. The sandblasted stummel is covered in dirt and grime of yesteryear. This should clean up nicely. The stummel surface is solid with no damage to the external surface. The dark browns of the raised sandblast contrast beautifully with the black stain of rest of the stummel. A thick layer of cake can be seen in the chamber. The sandblasted thin and inward curving rim top surface is covered in thick overflow of lava, dirt, dust and grime. The condition of the inner walls of the chamber and rim top surface will be known once the cake has been taken down to bare briar and the rim top crud has been scraped off completely. The inner rim condition appears to be in good condition with no burn/ charred surfaces. Even the outer rim edge appears to be in a decent condition. Only once the stummel has been thoroughly cleaned that I can be sure of my initial appreciation. In spite of the thick cake, the chamber odor is, surprisingly, not strong and should be addressed once the cake has been taken down to the bare briar and the shank internals have been thoroughly cleaned. The draught hole is dead center at the bottom of the chamber and should be a great smoker. The shank end and the mortise are blocked with dried gunk, adversely affecting the airflow.The delicate vulcanite saddle stem is heavily oxidized and has calcification deposits towards the button end. There are deep tooth marks on the lower and upper stem surface and appears that the previous owner has literally chomped on the bite zone of the stem. The button edges also have bite marks, in fact, they are badly worn out. The horizontal slot shows accumulated oils and tars.Along with the stems of other pipes in line for restoration, I immersed the stem of this Stanwell #7472 in a mix of one part Hydrogen Peroxide 20% with one part hot water after I ran a couple of pipe cleaners dipped in alcohol through the stem air way. A couple of hours later, the stem oxidation on all these stems were raised to the surface. After I had fished out the stem from the Hydrogen Peroxide bath, I scrubbed it with Magiclean sponge and followed it up with a wipe of cotton swab and alcohol. I further scrubbed the stem surface with 0000 grade steel wool. The loosened and superficial layer of oxidation was easily removed and revealed the condition of the stem. It was not as horrifying as I had imagined it to be during the initial inspection. There are deep bite marks in both the upper and lower bite zone. The bite marks are deep enough to cause significant thinning of the surface and complete disfigurement of the button edges. The deeper oxidation that was pulled to the surface would require more abrasive techniques.THE PROCESS
I started with cleaning of the stummel as I was keen to know the condition of the walls of the chamber. With size 1 head followed by head size 2 of a PipNet pipe reamer, I took the cake down to bare briar. Using a folded piece of 180 grit sand paper, I sand out the last traces of cake and expose the walls of the chamber. I wiped the chamber with a cotton pad dipped in isopropyl alcohol to remove the carbon dust left behind by all the reaming and sanding process. Once the chamber walls were cleaned out, I saw very minor and superficial beginnings of heat fissures/ pits all along the chamber walls. I shall address this issue by a simple bowl coat. I used my smaller of the two fabricated knife to gently scrap away at the overflow over the rim top surface while being careful not to damage the sandblast on the rim top. I was pleased to find the inner and outer edge of the rim intact and without any burn or char marks. Next, I cleaned out the internals of the shank and mortise. Using my dental tool, I scraped out all the dried oils, tars and gunk that had accumulated in the shank airway and mortise. The amount of crud that was scrapped out and the condition of the pipe cleaners that were used leaves no surprise why air flow through it was restricted. I finished the cleaning by running a few pipe cleaners dipped in isopropyl alcohol. I also wiped the shank with cotton buds and alcohol. With this cleaning, all old smells in the pipe are history. The pipe now smells clean and fresh.With the internals of the stummel now clean, I cleaned the external surface using a hard bristled toothbrush and Murphy’s Oil Soap. I diligently scrubbed the stummel to remove all the dust and dirt that was embedded in the crevices of the sandblast. With a soft bristled brass wired brush, I removed the overflowing lava from the rim top surface and cleaned the internals of the shank with a shank brush and dish washing soap to remove what little crud remained in the shank. I rinsed it under running tap water and wiped the stummel dry with an absorbent soft cotton cloth. Once I had wiped the stummel dry with paper towels and soft cotton cloth, I thought I saw a fill on the left side of the bowl, near the bowl and shank joint. It was perfectly matched and blended with the sandblast on the stummel and stained in dark as seen on other surfaces of the stummel. It is marked in yellow circle. My fears were confirmed when I probed it with a dental pick. Very carefully and painstakingly, I completely removed the old fill with a pointed dental pick. I cleaned the fill of all the debris of old fill material, wiped it with alcohol and refreshed the fill with a mix of clear CA superglue and briar dust and set it aside to cure overnight.By next day, the fill was hard and well set. With a folded piece of 220 grit sand paper, I worked the fill till I had achieved a nice blend with the shape and contours of the stummel. It turned out much better than I had anticipated. With a soft wire brass brush, I again cleaned out all the debris that lodged itself in the sandblast surface as a result of all the sanding and use of briar dust.Next, I rub a small quantity of “Before and After Restoration Balm” in to the briar with my finger tips, work it deep in to the sandblasts and let it rest for a few minutes. The balm almost immediately works its magic and the briar now has a nice vibrant appearance with the beautiful sandblast patterns on full display. The contrast of the dark browns of the raised sandblast with the dark black of the rest of the stummel adds an interesting dimension to the appearance of the stummel. I further buffed it with a horse hair brush. The last picture is of the side that had the refreshed fill and even the most discerning reader will be hard pressed to accurately pin point the fill. With the stummel nearly completed, I turned my attention to the stem repairs. I masked the stem logo “S” with a whitener pen to protect it during the sanding process. I cleaned the internals of the stem using hard and normal bristled pipe cleaners and isopropyl alcohol. With a pointed dental tool, I scraped out the entire dried gunk from the slot. I addressed the deeper oxidation by sanding the entire stem with a folded piece of 220 grit sand paper. Once the oxidation was completely removed, I wiped the surface clean with a cotton swab and alcohol. I flamed the damaged button edge and the nicks and dents with the flame of a lighter. This helps the vulcanite to rise to the surface as it has an inherent property to regain its original shape when heated. At this stage, I noticed that the bite zone on the upper stem surface has a crack which extends over to the button. This was further accentuated due to heating with the flame of a lighter. Continuing with the stem repair, I inserted a triangulated index card covered in transparent tape in to the slot. The tape prevents the mix of superglue and charcoal from sticking to the index card. I mixed superglue and activated charcoal powder and generously applied it over the bite zone, including over the button and set it aside to cure. Once the mix had cured, I removed the index card from the slot.Using a flat head needle file, I reshaped the button and roughly matched the fills with the rest of the stem surface. However, things rarely happen as you want them to happen and in this case, a few air pockets were revealed. With a permanent black marker I darkened the air pockets and spot filled them with clear superglue. Once the superglue had cured (I had set it aside overnight), I sanded the fills with a folded piece of 180 grit sand paper. I followed it up by further sanding the stem with 320, 600 and 800 grit sand papers to achieve a perfect blending of the fills with the stem surface and a crisp button edge on either side of the stem.Using the micromesh pads, I completed the polishing cycle by wet sanding the surface with 1500 to 3200 girt pads. I had read that White diamond polish is between 3600 and 4000 grit of micromesh pads and best used between these two. I decided to give this a try to see if there is any difference in the final stem finish. I mount a fresh cotton buffing wheel on to my hand held rotary tool and apply white diamond polish and buffed the stem. I wiped the stem with microfiber cloth and go through the remaining pads, dry sanding with 4000 to 12000 grit pads. The stem looks great with the fills nicely matched with the rest of the surface. I rub a little quantity of Extra Virgin Olive oil in to the stem surface and set it aside to be absorbed by the vulcanite. To complete the restoration, I mount a cotton cloth buffing wheel on to my hand held rotary tool and applied several coats of carnauba wax. I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further and remove any residual wax from in between the sandblasts.The finished pipe looks amazingly beautiful and is now ready for its long second innings with me. I only wish it could share with me its life story of the past years while I enjoy smoking my favorite Virginia blend in it or maybe an English blend!! P.S. There was only one more issue that needed to be addressed and one that could not be ignored, being a functional issue. After I had reamed and sanded the chamber walls, I had observed very minor and superficial beginnings of heat fissures/ pits all along the chamber walls. I addressed this by mixing activated charcoal and plain yogurt to a thicker consistency, just enough that I would spread easily and applied it evenly all along the chamber walls after inserting a folded pipe cleaner through the draught hole to keep it open. Once dry and set, this will not only protect the walls but also aid in faster build up of cake.There are two more pending write ups which I shall be tackling before I undertake to restore a pipe which my dear friend and mentor, Steve, had sent me about a year back with the intention of providing me an opportunity to test my own skills. I wish to thank each one for sparing their valuable time to read through and once again request you for any inputs or advice on dating and designer of this pipe.

Back to Bob Kerr’s Estate – Linking Peterson’s “Kapruf” 9BC with the 56 shape number


Blog by Steve Laug

With this Peterson’s “Kapruf” 9BC I am turning again to work on a few more pipes from Bob Kerr’s estate. This is the first of the Peterson’s that I am working on. I am cleaning them for the family and moving them out into the hands of pipemen and women who will carry on the trust that began with Bob and in some pipes was carried on by Bob. In the collection there were 19 Peterson’s pipes along with a bevy of Dunhills, some Comoy’s and Barlings as well as a lot of other pipes – a total of 125 pipes along with a box of parts. This is the largest estate that I have had the opportunity to work on. I put together a spread sheet of the pipes and stamping to create an invoice. I was taking on what would take me a fair amount of time to clean up. I could not pass up the opportunity to work on these pipes though. They were just too tempting. I decided to take a break from working on his Dunhills to work on a few of the other pipes. The first of them is a really nice Peterson. It is a shape that is one of my favourites so this one will probably stay with me.

I love these older Peterson’s 9BC shapes and find that the sandblast versions really are a favourite of mine. This one has a rugged sandblast finish with lots of nooks and crannies in the briar. It is a beauty! The pipe is stamped Peterson’s “Kapruf” over London Made England. That is followed by the shape number 9BC over 56. The valleys and ridges of the sandblasted grain showing through the grime and dirt are a mixture that leaves a rich texture. It had a rich reddish brown stain that does not look too bad. There was a thick cake in the bowl and lava overflow filling in the blast on the rim. The edges of the rim and top are dirty but look pretty pristine under the grime. It was a beautiful pipe that was dirty and tired looking. The stem was lightly oxidized with the typical tooth marks and chatter on both sides that I have come to expect from Bob’s pipes. He obviously loved the Peterson’s as much as he did his Dunhills. The P-lip button had some light damage to the top surface. Jeff took photos of the pipe before he started his cleanup work on it.Jeff took photos of the bowl and rim top to show the cake in the bowl and the lava build up on the edges of the bowl. It was thick and hard but hopefully it had protected the rim and edges from damage. The edges look pretty good. Jeff took photos of the sides and heel of the bowl to show the condition of the finish. You can see the beautiful undulations of the sandblast. There is a lot of dust and grime filling in the valleys. Jeff took photos of the stamping on the smooth panel on the underside of the bowl and shank. The stamping was readable as you can see from the photos. The London Made over England stamp is faint but readable under a light. The pipe also bears the same 9BC over 56 stamp that Al Jones (upshallfan) noted on the on his previous blog and had called a mystery pipe (https://rebornpipes.com/2019/07/25/peterson-shape-56-mystery/).Jeff took photos of the top and underside of the stem showing the deep tooth marks and scratching, oxidation on the stem surface and wear on the edges of the button. The “P” logo on the stem is long gone but the robust p-lip button is in very good condition.Al Jones had written a couple of blogs on the Peterson’s Kapruf 9BC so I turned to rebornpipes to refresh my memory through Al’s blogs (https://rebornpipes.com/2015/06/03/peterson-9bc-kapruf-pre-59/). I quote from there and also include some of the catalogue pages from the blog.

I didn’t know much about the Kapruf line. It is described in a 1960’s catalog as: “A fine sandblast finish distinguishes this range of light natural grained pipes with their distinctive red colouring. Very popular with sportsmen.”

The second page shows the 9BC shape.  I have boxed the shape in with a red box for quick reference. Al had also written a blog about another “Kapruf” 9BC he had picked up that was not stamped with the 9BC stamp but with a shape number 56. Interestingly the one I am working on is stamped with both numbers. I quote from a pertinent section of that blog on the shape number (https://rebornpipes.com/2019/07/25/peterson-shape-56-mystery/).

Well, the Shape 56 mystery is now resolved…Well, further sleuthing from the world’s foremost Peterson authority yielded an answer – which came directly from a blog entry here on rebornpipes, by our very own Steven Laug. In 2015, Steve posted a catalog from Canadian importer, Genin, Trudeau & Co. which shows their unique numbering system. I even comment that the Shape 56 looks like a 9BC! So, all the while, the answer was hiding on this blog! Below is that brochure page showing the Shape 56. Steve comments that the postal code used in the address dates the brochure to between 1962 and 1969. I guess not many Canadians appreciated the shape, so they are pretty uncommon. Thanks to Mark Irwin for his superior memory and to Steve for making this type of ephemera available, you never know when it will come in handy.

I have included both the link to the document for you to check out and a page from it that shows the 9BC/56 connection Al noted above (https://rebornpipes.com/2016/09/13/petersons-pipes-brochure-from-genin-trudeau-co-montreal-quebec/). I have put a red box around the shape number to make identifying it simpler. Be sure to check out the document as it is very informative.I turned to an article on Pipedia by a good friend, the late Mike Leverette entitled A Peterson Dating Guide (https://pipedia.org/wiki/A_Peterson_Dating_Guide;_A_Rule_of_Thumb). While the one I have in hand is slightly different in terms of stamping it is an English made Peterson that bears the stamp London Made England. I quote from the section by Mike on the English pipes.

English made Peterson pipes actually spans between the pre-Republic and Republic eras. In 1895, Peterson opened a shop in London England that lasted until the late 1950s or early 1960s. So the English Era, for a simplified date, will be from 1895 through 1959. The stamps Peterson used in London and that we have seen are:

  • Made in England – block format
  • Made in England – circle format
  • Made in London
  • Made in London England
  • Simply, London England.
  • Great Britain

I went to the full article on Peterson pipes after this to try to pin things down a bit more clearly (https://pipedia.org/wiki/Peterson). I believe the pipe is from the Republic Era – 1950 – 1989. I quote the pertinent section of that article below:

1969/70 – The ‘Made in England’ stamp was discontinued with the closing down of the London based factory. Although Peterson has always prided itself in being an Irish made pipe, Peterson had also maintained a pipe factory in London since 1899.

English made Peterson pipes actually spanned the period between the pre Republic and Republic eras.

In 1899, Peterson opened the first in a series of several successive shops in London, England, that lasted until the late 1960’s/70s.

1899 – 53, New Broad St. E.C.

1910 – 7, Hills Pl., Oxford St. W.

1915 – 21, Mortimer St. W.

Finally moving to 74/77 White Lion Street until 1970.

So the English Era, for a simplified date, will be from 1899 through to around 1970. The stamps Peterson used in London are:

    • Made in England block format
    • Made in England circle format
    • Made in London
    • Made in London England
    • Simply, London England
    • London Made over England block format
    • Great Britain

With that information in hand I knew what I was dealing with in terms of the stamping and the age of this pipe. I knew from the information from both Mike’s Pipedia article and the longer article that the pipe was made during the Republic Era prior to the closer of the London based factory. My thinking is that it came from the final factory location on 74/77 White Lion Street which closed down in 1970. That fits the time frame of many of the pipes from Bob Kerr’s estate.  I also knew that the pipe was brought into Canada by the Canadian importer, Genin, Trudeau & Co. in Montreal, Quebec. Noting above that the catalogue postal code puts it in the late 60s early 70s which also fits the story. Now it was time to work on the pipe.

With over 125 pipes to clean from Bob’s estate I took a batch of them to the states with me on a recent visit and left them with Jeff so he could help me out. Jeff cleaned the pipe with his usual penchant for thoroughness that I really appreciate. This one was a real mess and I did not know what to expect when I unwrapped it from his box. He reamed it with a PipNet pipe reamer and cleaned up the reaming with a Savinelli Fitsall Pipe Knife. He scrubbed out the internals with alcohol, pipe cleaners and cotton swabs until the pipe was clean. He scrubbed the exterior of the bowl with Murphy’s Oil Soap and a tooth brush to remove the grime and grit on the briar and the lava on the rim top. The finish looks very good with good looking grain around the bowl and shank. Jeff soaked the stem in Before & After Deoxidizer to remove the oxidation on the rubber. When the pipe arrived here in Vancouver for the second stop of its restoration tour it looked very good. I took photos before I started my part of the work. I took some close up photos of the rim top and also of the stem surface. I wanted to show what an amazing job Jeff did in the cleanup of the rim top. The rim top looks very good. The sandblast finish is very nice. The bowl looked very good. I also took close up photos of the stem to show the deep tooth marks on the top and underside. The “P” logo on the stem was long gone though I could see a faint ghost of it on the left side. I took a photo of the stamping and was able to capture all of it. Even the illusive London Made over England portion shows up. Since this is another pipe Bob’s estate I am sure that some of you have read at least some of the other restoration work that has been done on the previous pipes. You have also read what I have included about Bob Kerr, the pipeman who held these pipes in trust before I came to work on them (see photo to the left). Also, if you have followed the blog for long you will already know that I like to include background information on the pipeman whose pipes I am restoring. For me, when I am working on an estate I really like to have a sense of the person who held the pipes in trust before I worked on them. It gives me another dimension of the restoration work. I asked Brian if he or his wife would like to write a brief biographical tribute to her father, Bob. His daughter worked on it and I received the following short write up on him and some pictures to go along with the words including one of Bob’s carvings. Once again I thank you Brian and tell your wife thank you as well.

I am delighted to pass on these beloved pipes of my father’s. I hope each user gets many hours of contemplative pleasure as he did. I remember the aroma of tobacco in the rec room, as he put up his feet on his lazy boy. He’d be first at the paper then, no one could touch it before him. Maybe there would be a movie on with an actor smoking a pipe. He would have very definite opinions on whether the performer was a ‘real’ smoker or not, a distinction which I could never see but it would be very clear to him. He worked by day as a sales manager of a paper products company, a job he hated. What he longed for was the life of an artist, so on the weekends and sometimes mid-week evenings he would journey to his workshop and come out with wood sculptures, all of which he declared as crap but every one of them treasured by my sister and myself. Enjoy the pipes, and maybe a little of his creative spirit will enter you!

Now on to the rest of the restoration on this pipe that links the two shape numbers that Al referred to – the 9BC and the 56. Since Jeff had done such an amazing clean up job on the bowl it was very easy for me. I only had to rub the bowl down with Before & After Restoration Balm. I worked it into the surface of the briar with my fingertips and a horsehair shoe brush to clean, enliven and protect it. I let the balm sit for a little while and then buffed with a cotton cloth and shoe brush to raise the shine. Mark Hoover’s Balm is a product that I have come to appreciate and one I use on every pipe I have been working on. I set the bowl aside and turned my attention to the tooth marks in the stem. I painted the surface of the stem with the flame of a Bic style lighter. Since vulcanite has “memory” heat will lift much of the tooth damage. The photos show the marks that remain after the heat treatment.To repair these deeper tooth marks, I filled them in with clear super glue and set the stem aside to dry. Once the glue cured it would be a matter of blending the repairs into the surface of the stem with sandpaper.Once the repairs had hardened I also sanded them to blend them into the surrounding vulcanite with a folded piece of 220 grit sandpaper. I followed the 220 grit sandpaper with 400 grit wet dry sandpaper to minimize the scratching. The two papers combined do a great job in blending the repairs. I wiped the stem down with Obsidian Oil and set it aside to dry.  I polished out the scratches with micromesh sanding pads – wet sanding with 1500-12000 grit pads. I wiped the stem down after each sanding pad with Obsidian Oil. I polished it with Before & After Pipe Stem Polish – both Fine and Extra Fine. Once I had finished the polishing I gave it final coat of oil and set it aside to dry. I am on the homestretch with this pipe and I really look forward to the final look when it is put back together and polished and waxed. I put the bowl and stem back together. I polished the bowl and stem with Blue Diamond to polish out the scratches in the briar and the vulcanite. I gave the bowl multiple coats of Conservator’s Wax and the stem multiple coats of carnauba wax. I buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The pipe polished up pretty nicely. The valleys and ridges of the sandblast looked good with the polished black vulcanite. This 1969/70 Peterson’s “Kapruf” 9BC/56 Bent billiard was a fun pipe to work on thanks to Jeff’s cleanup work. It really has that classic Peterson look in a sandblast “Kapruf” finish that catches the eye. The combination of various brown stains really makes the pipe look attractive. It is a comfortable pipe to hold in the hand and I think that as it heats with smoking that over time the finish will darken and look even better. The finished pipe is shown in the photos below. The dimensions of the pipe are Length: 5 ½ inches, Height: 2 inches, Outside diameter of the bowl: 1 3/8 inches, Chamber diameter: ¾ of an inch. This one is staying with me as I carry on Bob’s legacy each time I fire up a bowl. I have a lot more to work on include 18 more Petersons. Perhaps one of those will catch your attention. Thanks for reading this blog and my reflections on the pipe while I worked on it. This is an interesting estate to bring back to life.

Breathing Fresh Life into an Inherited Ben Wade “The Gem” from the Year 1900!


Blog by Paresh Deshpande

It’s been a while since I have worked on any of my grandfather’s pipe collection that I have inherited after his demise a few years ago. Amongst the collection, this small quaint Ben Wade was beckoning me for a long time. It is now that I decided to work on it. I had one Ben Wade without a stem, that Steve had taken back to Canada from his visit to India to fashion a stem from his bag of spares. This prompted me to fish out this Ben Wade and work towards its restoration.

This small sized straight Bulldog is typically classic British shape, with a diamond shank and a horn stem with a threaded bone tenon. The shank end is decorated with a sterling silver ferrule with embossed leaves, which is loose and came off easily. On this ferrule are the stamp details which will help in determining the vintage of this pipe. The silver shank ferrule is stamped as “A & Co” over a series of three hallmarks running from the left near the bowl end to the end of the shank on the right.The first hallmark is an “Anchor” in a shield shaped cartouche and identifies the city of Birmingham in England where the silver was crafted. The second hallmark is a passant Lion in a cartouche which signifies that the band is silver and that it was crafted by a British silversmith. The third hallmark is a square cartouche with the small letter “a” in the box which is a date letter that will give the year of the making of the pipe. Steve had recommended a site which he frequents while dating silver hallmarked pipes. Here is the link which helped me identify the city mark as Birmingham and further following the link on Birmingham date letter chart on the same page brought me to a separate page with all the letters along with the period in which they were stamped. I found the letter which matched to the one seen on the pipe in my hand and I can now say with authority that this silver ferrule is from the year of manufacture1900!! Unfortunately, the site did not allow me to copy/ edit and reproduce the relevant charts for including in this write up.

https://www.925-1000.com/british_marks.html

The next stamp which I researched was the “A & Co” stamp over the three hallmarks. I conferred with The-Beard-of-Knowledge on all things pipe, Steve and he suggested that I visit http://www.silvercollection.it and sure enough I got the information that I was looking for. I reproduce the relevant information from the site and also the link for those who may need to refer when researching their pipes.

http://www.silvercollection.it/englishsilvermarksXA.html

A business which is supposed to have been established in 1781 at Mitcham, Surrey, by William Asprey (died 1827).

CHRONOLOGY:
Francis Kennedy, c. 1804-c. 1841
Kennedy & Asprey, c. 1841-1843
Charles Asprey, 1843-c.1872
purchased the business of Charles Edwards, c.1857
Charles Asprey & Son, c.1872-c.1879
Charles Asprey & Sons, c.1879-c.1888
acquired Leuchars & Sons
C.& G.E. Asprey, c.1888-c.1900
Asprey (& Co), c.1900-1909
acquired Houghton & Gunn, 1906
acquired William Payne & Co, 1908
Asprey & Co Ltd, 1909- 1998
Asprey & Garrard, 1998-2002
Asprey & Co Ltd, 2002

The relevant stamping is highlighted in blue. The period/ vintage of the ferrule now perfectly matches and confirmed that it is from the year 1900.

With the year of make of the ferrule established as 1900, I wanted to confirm if this matched with the year of manufacture of the pipe itself. This is essential since the makers did stock up on such silver ferrule before they even made pipes for them. The stampings on the pipe itself should provide some clues to the link with the vintage of the pipe. The pipe is stamped as “B W” in a rectangle over “THE GEM”, all in golden block capital letters. There are no other markings on this pipe, not even COM stamp.I searched pipedia.org for information on this brand and further confirmation on dating this pipe. There are some interesting details on this brand and makes for an interesting read. I have reproduced some snippets of the information from pipedia.org which are relevant to dating this Ben Wade.

The company was founded by Benjamin Wade in 1860 in Leeds, Yorkshire, where it was located for over a century. Ben Wade started as a pipe trader, but yet in the 1860’s he established a workshop to produce briar pipes. The pipes were made in very many standard shapes – always extensively classic and “very British”. Many models tended to be of smaller dimensions. Ben Wade offered a very high standard of craftsmanship and quality without any fills. Thus the pipes were considered to be high grade and a major competitor to other famous English brands.

In the second World War the factory was destroyed by German air raids on Leeds. But the Ben Wade family decided to re-build it immediately after the war and pipe production was re-started soon and successfully linked to the fame from the pre-war years.

Before the second war Ben Wade clustered their offerings into three price points: “Ben Wade” included the higher end pipes (eg the Larnix, Super Grain, Selected Grain, etc), “BW” included the mid-level pipes (eg Statesman, Natural Grain, County, etc), and “BWL” were the least expensive (eg Hurlingham, Adelphi, Tense Grain). Champion was in the last group, and in the 1930s at least retailed for 2/6.

Even though the owner family decided to leave pipe business and sell off the firm. The family went into negotiations with Herman G. Lane, president of Lane Ltd. in New York at about the same time as the Charatan family. Lane Ltd. bought both firms in 1962.

From the above it is confirmed that the Ben Wade that I have inherited is from the family era and from the era before the second war, placing it before 1939. Now, I had read somewhere that it was common for pipe makers not stamp the pipe with the COM stamp in early 1900s and this was confirmed by Steve. Thus, to sum up all the information researched to date this particular piece, it is safe to conclude that this pipe is likely to have been made in the year 1900!! My inheritance indeed has some very nice and very old pipes.

INITIAL VISUAL INSPECTION
In the month of January this year, I had restored a Loewe Kenton from my inherited pipes that was nicely reamed with no overflowing lava over the rim top (https://rebornpipes.com/2019/01/17/restoring-a-classic-british-billiard-loewe-co-pipe/) and now this is the second pipe which is without a layer of cake in the chamber. However, the rim top surface is darkened and covered with lava overflow. I searched through the remaining large carton of inherited pipe for another pipe which is sans cake, but did not find any. Coming back to the pipe on my work table, the rim inner edge is mighty uneven, most probably a result of using a knife blade and shows signs of darkening due to charring. However, the outer edge is without any damage. The walls of the chamber are in excellent condition with no signs of heat fissures/ lines, but slightly uneven. A little magical touch from Pavni, my daughter who specializes in making the chamber smooth should address this issue. The stummel surface has developed a nice patina over 119 years of its existence and I have no intentions of destroying it during the restoration. Therefore, the few dents and dings that are visible shall stay and be a part of the pipes history through the years. Maybe, micromesh polishing will address a few of these dents and scratches. I wouldn’t say that this pipe has beautiful grains all round because it does not!! But yes, there is a smattering of some straight grains in the cap of the stummel and few on the shank while rest of the stummel has just some swirls of grains here and there. Even though the stummel is covered in dust, dirt and grime from years of uncared for storage, through it all the pipe still has a feel of quality maybe because of the shape or the proportions, I am not able to pin point exact reasons, but the pipe shouts vintage and quality!! The double ring separating the cap from the rest of the stummel is filled with dirt and dust, but is intact with no chipping or unevenness, which is surprising. At this stage of my initial inspection, in order to see the condition of the shank end and mortise, I tried to separate the bone stem from the shank end. The stem would not budge. I had no desire of applying more force for the fear of breaking the bone tenon inside the mortise and this would have really complicated the restoration for me as well as the originality of the pipe would have been compromised. I wanted neither and so in went the entire pipe in to freezer for a chill. A few hours later, I took the pipe out from the freezer and slightly heated the shank end. Once satisfied, I gingerly turned the stem with success. A little coaxing and finally the stem and shank were separated. Whew! What a relief. However, when I tried to reattach the two, there was a slight gap between the stem and the shank end and indicated with red arrows. I am sure that with the cleaning of the shank/ mortise of the entire gunk, the fit should improve. After the stem was separated from the shank end, the sterling silver ferrule too fell out easily. I will have to fix it with superglue. A closer examination of the mortise confirmed that it is clogged with accumulation of oils, tars and gunk of yesteryear. The threads too are covered in the gunk and most probably the cause of the incorrect seating of the stem in the mortise.The horn stem itself appears dull and lifeless and has tooth chatter on both the surfaces of the stem. The slot is perfectly round and correct for the time period of the pipe and shows accumulation of dried tars and dirt. The button edges, however, are sharp and sans any damage with a little dirt embedded at the bottom of the edges. I could make out one crack emanating from the right bottom edge of the diamond saddle and extending to more than half the length of the saddle panel. This crack is shown by a yellow arrow. The dark and light hues taken on by the stem over the years should polish out nicely and will add an additional touch of class to this classy pipe. THE PROCESS
Pavni, my youngest daughter loves to help me in pipe restoration in her free time and her forte is getting the walls of the chamber as smooth as a baby’s bottom. With a folded piece of 220 grit sand paper she completely evened out the wall surface. Once she was through with her sanding regime, I cleaned out the internals of the shank and the mortise with a few hard and regular pipe cleaners dipped in isopropyl alcohol. I also cleaned out the threads in the shank end with cotton buds and alcohol. With a sharp knife, I gently scraped away the lava overflow from the rim top surface. I followed it up by cleaning the external surface of the stummel with hard bristled tooth brush and Murphy’s oil soap. I rinsed it under running tap water and dried it with paper towels and a soft cotton cloth. I diligently scrubbed the rim top surface with a scotch-brite pad and Murphy’s oil soap to remove the remaining lava overflow. With this step on this particular project, I achieved two results; firstly, the gold lettered stamping on the shank was consigned to past tense and secondly, a couple of fills were revealed (marked in yellow arrows) at the front of the bowl and in the bottom left panel of the diamond shank. Thankfully, there is no charring over the inner and outer edge or the rim surface. I removed the old and loosened fills from the front of the bowl and one on the shank that was closer to the bowl. The old fill at the shank end; I let it be as it would be covered with superglue while attaching the silver ferrule. Next, I decided to address the issue of darkened rim top surface and uneven inner edge by topping the rim on a piece of 220 grit sand paper. The progress being made was frequently checked as I had no desire to lose any briar estate than absolutely necessary. Once satisfied with the result, I wiped the rim top surface with a moist cloth. The darkened rim top has been addressed completely, however, the inner rim edge is still uneven (though greatly reduced) with slight charred edges. I address these issues by simply running a piece of 220 grit sand paper along the inner rim edge without creating a bevel, but a nice rounded even surface.Next issue to be addressed was the fills. As mentioned above, I had cleaned out the old and loose fills using my sharp dental tool. I filled these with a mix of superglue and briar dust using the layering technique. Using a toothpick, I first spot fill superglue in to the surface of the intended fill and press briar dust over it. I repeat this process, if need be, till the fill is slightly above the rest of the surface. Once all the fills are covered, I set the stummel aside to cure. Once the fills are sufficiently hardened, which is quite rapid, I sand it with a flat head needle file to achieve a rough match with the rest of the stummel surface. I follow it up by sanding with a piece of 220, 600 and 800 grit sand papers to a perfect match. Discerning readers must have noted that I did not sand the entire stummel surface. This was because, as I had decided earlier that I would maintain the aged patina that the briar had taken on over the 119 years.At this stage, I decided that I would tackle the stem repairs as addressing the crack observed on the diamond saddle would require curing time and while the stem repair is curing, I could get back to the stummel, saving on time. I began by first cleaning the bone tenon and the stem surface with a cotton swab and alcohol to remove all the dirt and gunk from the surface. I was contemplating whether or not to drill a counter hole to prevent the crack from progressing further and after weighing the cons, I decided not to do so. The probability of the stem chipping or the crack developing further was reason enough for me to avoid this drilling. I filled this crack with plain superglue and set it aside to cure. The CA superglue would seep and spread inside and stabilize the crack. During his visit, while discussing various aspects of pipe restorations, Steve had made a passing comment that in his experience the best way to preserve the patina on a briar if you need to sand it is to dry sand the stummel with 1500 to 12000 grit micromesh pads. I followed his advice and went ahead and dry sanded the entire stummel surface with 1500 to 12000 grit micromesh pads. The results are amazing. The stummel has now a deep and rich dark brown coloration and this will further deepen once I go through the polishing and wax application regimen. Most of the readers would have noticed that the double ring separating the cap from the rest of the stummel shows accumulation of briar dust and grime. Also the fills are darker than the rest of the stummel surface. I have noticed it too and will clean the rings at the end as the polish and wax would also be accumulating in these gaps subsequently. The issue of the fills was addressed by staining the fills and surrounding surface with a dark brown stain pen. I set the stummel aside overnight for the stain to set. The blend is near perfect and should blend further after application of balm and carnauba wax polish.The superglue applied over the crack was by now well cured and had seeped in to the crack as well. I sand the entire stem and the fill in particular, with a worn piece of 220 grit sand paper. This helped to address the tooth chatter seen in the bite zone as well as blend the fill with the rest of the stem surface. I followed it up with dry sanding the stem with 1500 to 12000 grit micromesh pads. I wiped the stem with a moist cloth after every three pads to remove the resulting bone dust. To finish, I applied a liberal coat of Extra Virgin Olive oil and set it aside to be absorbed by the porous bone. I am very pleased with the way the contrasting dark browns and lighter grains in the bone are now highlighted. Once polished further, this will further add a touch of class to an already chic looking Bulldog!! I applied petroleum jelly over the bone tenon and tried the fit of it in to the mortise after temporarily attaching the silver ferrule over the shank end. The alignment and seating of the two was spot on. I separated all the parts again and continued further. While the stem was being hydrated with olive oil, I went back to work the stummel. The stain had set well by this time. I applied a little “Before and After Restoration” balm with my fingers and rubbed it deep in to the stummel surface. This balm rejuvenates the briar and the transformation in the appearance of the stummel is almost immediate. The fills are now so well blended in to the briar that it is difficult to spot them. The only part that needs TLC is the sterling silver ferrule. I polish the ferrule with a very soft powder specifically available locally, and widely used by jewelers, for polishing of silver. I align the ferrule stampings with the stummel stamping on the shank and fix it over the shank with a little superglue. The contrast that this shiny ferrule provides against the dark brown of the stummel looks fantastic.Next, I ran a thin and sharp knife through the double cap ring and cleaned it. To finish, I re-attach the stem with the stummel and mount a cotton cloth buffing wheel on to my rotary tool. I set the speed at about half of the full power and applied several coats of carnauba wax over the stummel and the stem of the pipe. I finished the restoration by giving the pipe a rigorous hand buff using a microfiber cloth to deepen the shine further. The completed pipe, with dark brown hues of the stummel contrasting with silver ferrule and the shiny dark browns and lighter grains in the bone stem makes for a visual treat. The pipe looks lovely, fresh and vibrant; the photographs speak for themselves. Thank you for your valuable time. P.S. This was the last pipe that I had restored during my leave from my work. The following write ups are now on pipes that I have already restored after returning to my work place. I shall sorely miss the help that Pavni, my 10 year youngest daughter and Abha, wifey dear, extend in my work. There are about 40 odd pipes that I have carried with me and which have been cleaned by Abha. So the next couple of months are going to be interesting. Keep following rebornpipes.com for some nice, unique and interesting pipes from here in India in the near future.

Oh, missed out on one aspect!! I tried to repaint the shank stamp with a gold glitter pen towards the end, but it would just not stay. Any suggestion would definitely help me mark this oldie as well as for future.

 

New Life for a Mystery Pipe – an Imported Sterling Briar Author


Blog by Steve Laug

The next pipe in the queue is a ¼ Bent Author that Jeff picked up from an auction he follows in Michigan. It is a great looking pipe with some beautiful grain – swirls of birdseye, straight and flame grain around the bowl and shank. The carver did a great job utilizing the block of briar to maximize the grain. The pipe is stamped on the left side of the shank. It reads Sterling with Imported arched over the Sterling name and Briar arched underneath. The pipe was filthy with a thick cake in the bowl and overflowing lava on the back of the beveled rim top. There was some burn damage and darkening on the back inner edge of the rim but it was hard to know how badly damaged it was until it was cleaned up. There were some nicks in the outer edge of the bowl as well. Even though it was dirty there was some nice grain peeking out from under the grime. The exterior of the briar was dirty and dull looking – lifeless after sitting unused for years. The bent tapered stem is vulcanite and has no marking or stamping. It is good quality vulcanite but is pitted all over both sides. There are some tooth marks and chatter on both sides near the button. There was a tarnished Sterling Silver band on the shank with the following Hallmarks – a rampant lion (.925 silver stamp), an anchor (the Birmingham assay office) and an upper case letter “T” which will give me some idea of the date on at least the band. The photos below tell the story and give a glimpse of the pipe before clean up. I took photos of the bowl and rim to capture the condition of the pipe before Jeff did his cleanup work. There was significant darkening on the rim top and a cake in the bowl flowing over as lava on the back top edge. The inner edge showed some burn damage to the back side and rim top. The outer edges of the bowl had some nicking from the pipe being knocked out against something hard.Jeff took some photos of the side and underside of the bowl to show some of the issues with the old finish. It was more scratched than nicked but it was very worn looking on the underside of the bowl. You can also see the tarnish on the silver band in the photos.He took a photo of the stamping on the left side of the shank. It reads as noted above. The stamping is well done and readable. The photo of the silver band shows the hallmarks as noted above.The stem had some oxidation but was good quality vulcanite. There was some wear on the button edges and some tooth marks and chatter on both sides near the stem. The surface was also pitted and worn looking.I remembered working on a similar brand but was not sure how the Imported Briar stamped (which is usually used on USA made pipes) with the Hallmarks identifying the Sterling Silver band as Birmingham made and bearing a “T” date stamp. The conflicting information had several possible resolutions. One was that the pipe could be an American made pipe and the band added as bling later in its life time. Another would be that the pipe was made in England for export into the USA and the band was original. At this point I was not sure what to think about the situation. More work was necessary to see if I could gain some insight.

I turned first to the Pipephil website (http://www.pipephil.eu/logos/en/logo-s12.html). There was some information on a brand that was stamped Sterling Hall that was made by Briarcraft in New York City. The stamping was very different from the one in my hands. The stamping on Pipephil was Germanic script and had the Shield B logo of Briarcraft. The one that had in hand had neither one of those. The Aged Imported Briar stamp was also longer and different from the arched Imported Briar in block letters around the uppercase block STERLING. So at this point I was not sure there was a link to Sterling Hall. I have included a screen capture of the stamping for you to compare with the one above on this pipe.I turned to my other go to site for information – Pipedia. I looked in the British makers list for Sterling pipes but there was nothing listed. I turned to the same in the USA makers list and again it was not listed. I decided to have a look at the listing for Briarcraft and see if I could possibly find some pertinent information (https://pipedia.org/wiki/Briarcraft). I quote:

Richard Kliethermes Sr. was the founder of Briarcraft. First located on Pipetown Hill Rd, Spring Valley, NY., it moved later to 66 Central Ave., Spring Valley, NY. After the death of RK Sr., business was run by Richard Kliethermes Jr. († 1943) and was quite prosperous between 1920 and 1940. The company closed in 1950.

Briarcraft Pipe Company was very prosperous between 1920 and 1940 and usually feature a diamond shield logo. They also produced a line of seconds under the following names: Airo, Arcadian, Briarmeer, Smokemaster, Cavalcade, Hallmark, Sterling Hall, and Wimbledon. They closed their doors in 1950.

Briarcraft was started by Richard Kliethermes Sr. and located on Pipetown Hill Rd, Spring Valley, NY. It received its power from a dam on Hyenga Lake, later it moved to 66 Central Ave., Spring Valley, NY. At first it was housed in a 2 story frame building and later a 2 story stone building was added. Upon the death of RK Sr., business was run by Richard Jr, between 1920 and 1940 it was second in size to Frank Medico pipes. All the briar root was imported from Africa, with the start of WWII, imports stopped and a briar like root was imported from S. Carolina. Richard Kliethermes Jr. was the inventor of a pipe known as Smokemaster, which used a doubled up pipe cleaner in the bit to absorb tobacco juice. With the decline in business during WWII and the following 5 years it closed its doors 1950.

I have highlighted in red text the name Sterling Hall. There is no other help with the brand and there was nothing to link it to the Sterling I was working on. The other interesting thing of note in the above information is that the pipes were usually stamped with a Diamond Shield logo. The word “usually” could apply to this one not having a stamped logo.

I also checked in my copy of Who Made that Pipe (WMTP) by Herb Wilczak and Tom Cowell, copyright 1997. There I found a bit more help. There were several listings for the Sterling pipe and also variations on the name. I did a screen capture of the section showing the brands.In the above chart you can see that Arlington Briars in the US and Comoy’s, Delacour Bros and Orlik made them in England. You can also see that Kapp & Peterson made them in Ireland and Stanwell also had a Sterling brand made in Denmark. There was also a Sterling Band brand listed under Wally Frank in the US. It was pretty easy to say that the pipe in hand was not a Stanwell or Peterson made pipe so that left others that interested me.

I turned to the section on Arlington Briars to see if there were any ties there to help me get a better picture (https://pipedia.org/wiki/Arlington). I quote a part of that article and highlight the section that may give some insight. Again there is nothing certain in the article tying the brand to this company.

According to José Manuel Lopes, “North American brand that belonged to Arlington Briar Pipes Corp., Brooklyn, New York, founded in 1919. In the 1940s, Ludwig Rosenberger gave the company new life, and it continued until the 70s. His son, Mel Rosenberger, has recently launched the DiMonte brand. Jack Uhle was also linked to Arlington.” Arlington, as far as known, mainly operated as a sub-contractor for other brands. The Jobey pipes are said to be made by Arlington at an unknown point of time. Arlington’s own pipes are seldom seen.

I checked out the article on Pipedia on Delacour Bros. to see if there was a tie. But it did not have enough information to be truly helpful (https://pipedia.org/wiki/Delacour_Brothers).

I also checked the section on the Comoy’s and the Orlik article that pertained to seconds lines and there was no tie to the Sterling in either of them.

I then turned to the last noted make from the above WMTP chart – Wally Frank. I thought maybe that was a possibility as they had many companies make pipes for them. Here is the link on Pipedia (https://pipedia.org/wiki/Wally_Frank). I quote a portion of the article here for my purposes and have highlighted the portion that is interesting to this discussion:

Their numerous private-label pipes were made by many makers, including Charatan, Sasieni, Weber, and many others. Wally Frank, Ltd. also owned the Pioneer brand of meerschaum pipes, made from both Turkish and African meerschaum. In addition to importing pipes, he had many pipes made in his own name and also employed pipemakers like Peter Stokkebye, Svend Bang, and Ed Burak (who later became the owner of Connoisseur). As a result, each Wally Frank pipe must be individually evaluated on its own merit.

I have run into a dead end on the research of this pipe. I do not know where else to turn with looking for the brand. What I do know is that the most that can be said about this pipe is that it is certainly a USA Import Pipe. How it came to have a British Hallmarked Silver band on the shank is shrouded in mystery and I will probably never figure out the connection. Perhaps one of you readers can shed some light on the brand. If so let us know. Onto working on the pipe itself!

Jeff did his usual thorough cleaning of the pipe. He reamed the bowl with a PipNet Pipe reamer to take the cake back to bare briar. He cleaned up the reaming with the Savinell Fitsall Pipe Knife. He scrubbed the exterior of the pipe with undiluted Murphy’s Oil Soap and a tooth brush. He rinsed the bowl off with warm tap water to remove the grime. He scrubbed out the mortise and the airway in the shank and stem with pipe cleaners, cotton swabs and isopropyl alcohol until they were clean. He soaked the stem in Before & After Deoxidizer and when it had done its magic, rinsed it off the exterior and in the airway with warm water. He dried it and buffed it with a soft clot to remove the oxidation. I took the following photos of the pipe before I did my part in the restoration. I took a photo of the bowl and rim top to show its condition after Jeff had scrubbed it. You can see the darkening and the damage on the back inner edge of the bowl. You can also see the nicking on the outer edge of the bowl. The stem looked very good other than the few tooth marks on the surface of both sides ahead of the button. There was also some damage to the sharp edge of the button that would need to be dealt with. The silver band looked good.I took a close up photo of the stamping on the shank. The reflection of the flash makes it hard to capture the stamping on the band but it has the following Hallmarks – a rampant lion (.925 silver stamp), an anchor (the Birmingham assay office) and an upper case letter “T” which will give me some idea of the date on at least the band.I decided to figure out the potential date on at least the silver band. I found another helpful website on British silver hallmarks that covered hallmarks dating from 1743 to 2024 (https://www.silvermakersmarks.co.uk/Dates/Birmingham.html).I know that the graphic is small but check the link. When you are on the site you can click on the date letter you are looking for and it will give you every listing on the chart with that letter. I clicked on the “T” link which I have included below and it took me to a listing of the T dates (https://www.silvermakersmarks.co.uk/Dates/Birmingham/Date%20Letters%20T.html).

The date that corresponded to the hallmarks on the band were those listed for 1943. When I clicked on the date I was taken to a larger view of the stamp. I have included that here as well.

So at least I could be certain that the band for the pipe was Sterling Silver that bore the Birmingham hallmark Anchor and the date stamp of a capital T which identified it as having been stamped in 1943.

The trouble was I could not link it to the manufacturer of the briar… ah well. There always remains a bit of mystery in these restorations.

I decided to address the issues with the rim edges of the bowl first. I filled in the deep nicks and gouges on the outer edges of the bowl with clear super glue. Once the repairs had cured I sanded them smooth with a folded piece of 220 grit sandpaper. I also worked on the inner edge of the rim to remove the damage to the back side of the bowl. Once I beveled the inner edge of the rim to bring it back to round, I decided to continue my ongoing experiment with a new product from Mark Hoover of Before & After Products. This one is a product he labels briar cleaner and it has the capacity of absorbing grime and dirt from the surface of briar. I rubbed the bowl down with some of his Briar Cleaner to see how it would work in this setting. In speaking to Mark he noted that the product is completely safe to use. The main product is even FDA approved edible. I rubbed it onto the bowl and rim top with my finger tips and worked it into the grime and grit on the bowl. I let it sit on the pipe for about 5 minutes before I rubbed it off with a microfibre cloth. I rinsed it under warm running water to remove the residue. I was pleasantly surprised by how clean the surface on the bowl looked when I was finished. I polished the bowl and rim with micromesh sanding pads – wet sanding with 1500-12000 grit pads. I wiped the bowl down after each pad to remove the sanding debris. My goal was to further remove the darkening on the both the rim top and the outer edges of the bowl. I worked some Before & After Restoration Balm into the surface of the briar with my fingertips to clean, enliven and protect it. I let the balm sit for a little while and then buffed with a cotton cloth to raise the shine. Mark Hoover’s Balm is a product that I have come to appreciate and one I use on every pipe I have been working on. While there is still a bit of darkening on the rim it is still quite a stunning pipe. Have a look at the bowl now. With the bowl finished I set it aside and turned my attention to the stem. I wiped the surface down with some Obsidian Oil and dried it off. I filled in the deep tooth marks on both sides and repaired the edge of the button with clear super glue.Once the repairs had hardened I used a needle file to redefine the sharp edge of the button and to flatten the repaired areas. I sanded the stem with 220 grit sandpaper to smooth out the surface of the repairs and blend them into the stem. I started the polishing of the surface with 400 grit wet dry sandpaper. I polished the stem with micromesh sanding pads – wet sanding it with 1500-12000 grit pads. I wiped the stem down with a damp cloth after each pad. I further polished it with Before & After Pipe Polish – both Fine and Extra Fine. I wiped it down with a coat of Obsidian Oil and set it aside to dry. With both parts of the pipe finished I put the pipe back together again and I polished the bowl and the stem with Blue Diamond polish on the buffing wheel. I gave the bowl and the stem multiple coats of carnauba wax. I buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The pipe polished up pretty nicely. The rich finish and the interesting grain on this briar came alive with the buffing. The finish on the briar works well with the polished black vulcanite stem. The finished pipe is a well-proportioned, nicely grained shape that I would call an Author. Have a look at it with the photos below. The dimensions are Length: 5 ½ inches, Height: 1 ½ inches, Outside diameter of the bowl: 1 ½ inches, Chamber diameter: 7/8 of an inch. This beautiful mystery pipe is bound to be a great smoker. Was it made in England or the USA? Were the band English and the pipe American? I am not sure we will ever know for certain. But it was an interesting mystery to research and restore. Thanks for walking through the restoration with me.

 

Restoring a Dr. Grabow “Commodore” #39


Blog by Paresh Deshpande

After we bid our farewells to my Guru and Mentor, Steve Laug and his brother, Jeff, (Dal had left a couple of days earlier) I felt a void. All of a sudden there was nothing to look forward to, no pipe talks, no planned activities, nobody to share a smoke with and above all, their mere presence was being missed by Abha, my wife and both daughters, not to mention me too! It was my youngest daughter, Pavni, who suggested that we restore a pipe!! What a suggestion that was! Our spirits immediately soared and I pulled out my “MUMBAI BONANZA” pipe box to select one pipe.

The one that caught our collective attention was a pick axe shaped pipe that we had come to associate with Kriswill as I have inherited a few. However, this had a “Spade” stamped on its stem in white. It was a Dr. Grabow.

For those readers who have missed out on my previous work, I was fortunate enough to have heeded the advice of my dear friend and mentor, Steve, and struck a deal with a junk collector from Mumbai. He did not know what he was selling and I did not know what I was buying as we reside in different cities!! The argument that Mr. Steve presented was that if not anything, I shall at least have some spares and this was logical. I struck a deal and here are pictures of the pipes that I received in this lot.     This lot contains some very nice collectible pipes, a few well known brands and some mediocre brands. Overall, with seven Dunhill pipes, a Preben Holm #1 FH, a couple of “Made in England” Pete System pipes, a couple of  Charatan’s Belvedere, Custom-Bilt, Stanwell and other assorted pipes, I would say that I had struck a decent haul!!! This is indeed my “Mumbai Bonanza”.

The eleventh pipe that we decided to work on from this find is a pickaxe shaped pipe and is indicated in red colored arrow in the picture below. It is stamped on the right side of the shank as “COMMODORE” in block letter over “DR. GRABOW” again in block letter. The shape code “# 39” is also stamped on the right side towards the shank end and away in the middle of the two lines. The left side of the shank is devoid of any stamping, which is slightly unusual as most of carvers and makers prefer to stamp their pipes on the left. The stem bears the famous “Ace of Spades” logo in white, embedded on the left side of the stem. Now coming to the research of this brand and line/ model in specific, I referred to pipedia.org and as expected there is an extensive research on this pipe and even has a separate page on the dating of Dr. Grabow pipes, starting from the Linkman era to later pipe lines and numbers which makes for an interesting read and is highly recommended. This research has been done by Russell McKay, and is from his website DrGrabow-pipe-info.com. Here is the link to the page on pipedia.org:

https://pipedia.org/wiki/Dr._Grabow_Models_(Series,Line)_Names_Through_the_Years

I found what I was looking for in the list of most “newer” Dr. Grabow pipe names and is reproduced below;

COMMODORE (c1964) — First appears in a magazine ad for $7.95 as early as 1964. Like the Sculptura, later models were sandblasted in a “big” blast circa 1967-69 (See “Sculptura” for details.)

From the above information, it is evident that the pipe currently on my work table is from the period 1967-69, even though the line was first introduced in 1964 since the stummel is beautifully sandblasted. With this input on the vintage of this pipe, I move ahead with the restoration of this 50 plus years old pipe!

INITIAL VISUAL INSPECTION
I usually start my initial visual inspection by going over the chamber first. However, in this particular pipe, I was so drawn by the beautiful sandblast on the stummel that I decided to change the order and start with the stummel.

The stummel boasts one of the most beautiful sandblast patterns with the front of the bowl having circular blasted pattern and from the outer most part of this blast ring, the sandblast that radiates from the front of the stummel and moving around to the sides and back of the stummel with the cross grains and the straight grains forming an intricate crisscross patterns. It is a visual treat to say the least and difficult to explain in mere words! The following two pictures of the cleaned stummel will give the readers an idea of the sandblast patterns on the stummel.The sandblasted stummel is covered in dirt and grime of 50 plus years of its existence. This should clean up nicely. The stummel surface is solid with no damage to the external surface. The dark browns of the raised sandblast contrast beautifully with the black stain of rest of the stummel. A thick layer of cake can be seen in the chamber. The sandblasted rim top surface is covered in thick overflow of lava, dirt, dust and grime. The condition of the inner walls of the chamber and rim top surface will be known once the cake has been taken down to bare briar and the rim top crud has been scraped off completely (thankfully readers cannot see or hear me muttering silent prayers!!). The inner rim condition appears to be in good condition with no burn/ charred surfaces. Even the outer rim edge appears to be in a decent condition. Only once the stummel has been thoroughly cleaned that I can be sure of my initial appreciation. In spite of the thick cake, the chamber odor is, surprisingly, not strong and should be addressed once the cake has been taken down to the bare briar. The shank end has a metal band around the center and this metal band extends inside the shank with threads, over which the threaded stem stinger is seated in to the mortise. Thankfully, the band and threads are all intact. The mortise is blocked with dried gunk, adversely affecting the airflow. The metal band is dull and dirty in appearance.The stem is an “Adjustomatic” type (a patent for stem to shank threading system, later Patent #2461905 which was filed on 25th January 1946 by David P. Lavietes). This patent allows the stem to be turned in the shank for a perfect alignment without having to detach the two. The stem is attached to the shank by a threaded “tool” stinger (again patented by the brand way back in 1924 and upgraded over the years) and the stem can be turned over this stinger for alignment of the shank and stem. Unfortunately, the previous owner had this stinger cut ahead of the threaded portion so that the attachment of the stem to the shank is not affected at all. The vulcanite stem is heavily oxidized and has calcification deposits towards the button end. There are a few deep tooth marks on the lower and upper stem surface. The button edges also have bite marks. The stinger opening and the horizontal slot shows accumulated oils and tars. The threaded portion of what remains of the stinger is covered in dried dust, dirt and grime. The alignment of the stem and shank skewed with the stem being overturned to the right.THE PROCESS
I started the restoration with cleaning of the stummel as I was keen to know the condition of the walls of the chamber. With size 1 head of a Castleford pipe reamer, I took the cake down to bare briar. Using a folded piece of 180 grit sand paper, I sand out the last traces of cake and expose the walls of the chamber to ascertain that there are no cracks/ heat fissures. I wiped the chamber with a cotton pad dipped in isopropyl alcohol to remove the carbon dust left behind by all the reaming and sanding process. I was happy to note that the walls of the chamber are in pristine condition without any heat fissures or pits. The inner and outer edge of the rim are intact and without any burn or char marks. Next I decided to address the stem. I cleaned the internals of the stem using hard and normal bristled pipe cleaners and isopropyl alcohol. The stem airway and the open ended stinger were filthy as can be made out from the number of pipe cleaners that were used up in the cleaning process. I cleaned the complete stem with a cotton swab and alcohol to remove the calcification from the button end and thereafter flamed the stem surface with the flame of a lighter to raise the tooth indentation to the surface. I scrubbed and cleaned the portion of the stinger that remained. I liberally applied petroleum jelly to the stinger to protect it and dropped the stem in to the “Before and After Deoxidizer” solution which Jeff had lugged all the way from Idaho, USA for me. This solution, which has been developed by Mark Hoover, has reduced my time in working on removing stem oxidation by ¼ and should form a part of the list of ‘must have’ items for restoring a pipe.While the stem was soaking in the “Before and After Deoxidizer” solution, I cleaned out the internals of the shank and mortise. Using my fabricated tool, I scraped out all the dried oils, tars and gunk that had accumulated in the shank airway and mortise. The amount of crud that was scrapped out leaves no surprise why air flow through it was restricted. I finished the cleaning by running a few pipe cleaners dipped in isopropyl alcohol. I also wiped the metal band and the threads with cotton buds and alcohol. With this cleaning, all old smells in the pipe are history. The pipe now smells clean and fresh.With the internals of the stummel now clean, I cleaned the external surface using a hard bristled toothbrush and Murphy’s Oil Soap. I diligently scrubbed the crevices formed by the sandblast to remove all the dust and dirt that was embedded in between. With a soft bristled brass wired brush, I gently removed the overflowing lava from the rim top surface and rinsed it under running tap water. I wiped the stummel dry with an absorbent soft cotton cloth. I am very pleased with the way the stummel has cleaned up. The sandblast looks absolutely gorgeous. Next, I rub a small quantity of “Before and After Restoration Balm” in to the briar with my finger tips, work it deep in to the sandblasts and let it rest for a few minutes. The balm almost immediately works its magic and the briar now has a nice vibrant appearance with the beautiful sandblast patterns on full display. I further buff it with a horse hair shoe brush. With this, I keep the stummel aside and turn my attention to the stem repairs. While I was working on the stummel, Abha, my wife had in the meanwhile fished out the stem from the ‘Before and After Deoxidizer’ solution after a soak of about 6 hours. She rinsed it under running tap water to remove all the sticky solution that remained on the surface. She also let the water run through the stem airway and blew through it to dislodge the solution that remained inside and followed it up with a thorough cleaning with Mr. Magiclean sponge and 0000 grade steel wool. She finished her part in cleaning of the stem with a vigorous rubbing with a microfiber cloth. This removed nearly all of the oxidation from the stem surface, however, the deep tooth indentations at the button edge and in the bite zone still needed to be addressed. And as is her habit, she did not take any pictures of this process.

I began my part of stem repairs by sanding the stem with a folded piece of 220 grit sand paper. This helps in getting rid of what little oxidation remained while providing a smooth surface for the intended fills to reconstruct the damaged bite zone on both surfaces and also the button edges. I wiped the stem surface, particularly the damaged areas, with a cotton pad and alcohol to remove any traces of dirt and grime. I prepared a mix of CA superglue and activated charcoal and carefully applied it over the damaged bite zone on both surfaces, and button edges and set it aside for curing over night. I had applied this mix in sufficient thickness which would help during the filing and sanding to match the fills with the stem surface and shaping the button. Once the fills had cured sufficiently, using a flat head needle file, I reshaped the button and roughly matched the fills with the rest of the stem surface. I followed it up by further sanding the stem with 320, 600 and 800 grit sand papers to achieve a perfect blending of the fills with the stem surface and a crisp button edge on either side of the stem. Using the micromesh pads, I complete the polishing cycle by wet sanding the surface with 1500 to 12000 girt pads. The stem looks great with the fills nicely matched with the rest of the surface. I rub a little quantity of Extra Virgin Olive oil in to the stem surface and set it aside to be absorbed by the vulcanite. The only issue that remains unaddressed at this stage is the issue of overturned stem. Being an adjustomatic stem, I fixed the stem in to the shank and tried to turn the stem to match the shank applying just adequate pressure. However, the stem would not budge. Not wanting to create further complications like broken stinger or wearing down of the threads, I unscrewed the stem from the shank. With the flame of a lighter, I heated the aluminum stinger to a point where the stem was just about able to rotate on the stinger. I reattached the stem to the shank while the stinger was still warm, and turned it till the alignment was perfect as I desired and set it aside to cool down. Actually the reasoning behind heating the stinger is that the gunk which accumulates on the stinger and further percolates inside is loosened, thus freeing the stem.

To complete the restoration, I mounted a cotton cloth buffing wheel on to my hand held rotary tool.  I set the speed at about half of the full power and applied White Diamond compound to the entire pipe. I wiped/ buffed the pipe with a soft cotton cloth to clear it of any leftover compound dust. With a cotton buffing wheel earmarked for Red Tripoli, which has a finer grit than White compound, I buffed the stem to a fine glossy finish. I then mounted another cotton cloth wheel on to the polishing machine and applied several coats of carnauba wax. I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further. The finished pipe looks amazingly beautiful and is now ready for its long second innings with me. I only wish it could share with me its life story of the past 50 plus years while I enjoy smoking my favorite Virginia blend in it!! P.S. I have to admit to the readers of this blog that I had completed this project in the month of May 2019 but I kept procrastinating on the write up. To be honest, I find doing the write up on any project more tedious and difficult than working on the project itself and Steve will bear with me on this fact. And the fact that English is not my first language further makes it all the more challenging. There are nine more pending write ups which I shall be tackling before I undertake any new restoration, God!! I don’t want to scare myself!! I wish to thank each one for sparing their valuable time to read through and any inputs or advice is always welcome.

Gifting My Dear Friend, Dal Stanton, an Alexander Zavvos Hygrosystem Pipe


Blog by Paresh Deshpande

Steve, his brother, Jeff and Dal Stanton, The Pipe Steward, were on a visit to India in early May 2019. It was a fun filled week and also a great learning. I have always admired the finish that Dal imparts to the pipes he restores while I am amazed at the speed, the measured quantum of work that Steve puts in his restoration processes and also the profound knowledge that he has on all things pipes!! I was fortunate to see and learn these nuances first hand. I had a desire that there should be a unique pipe which all three of us should have (Jeff being a non smoker) and had laid down for myself, the following parameters for identifying THAT PIPE!

(a) Both should not be having this pipe in their personal collection (knowing well that this would be a very tall order!!)

(b) The pipe must have some historical significance and should have made a contribution to the world’s pipe history.

(c) It must come from a well known carver or manufacturer.

The pipe selected is an ALEXANDER ZAVVOS HYGROSYSTEM, PAT.No 87033, made in the 1970s-80s. What followed was an extensive and prolonged hunt for two such pipes of which the first one was purchased from one seller on Pinterest and the second was on eBay. These pipes were received separately and the last delivery materialized a couple of days prior to the arrival of these esteemed guests. Here are both the pipes as I received them.Since Mr. Dal was the first to arrive in India, he was given a choice between the two. He selected one with an Apple shape and the remaining willy-nilly came to Steve. At that point in time, both Dal and I discussed that it would be the Apple shape that Steve would have selected but… It’s Dal’s pipe now. The stamping on the Apple is crisp and easy to make out. It reads on the left of the shank as “ALEXANDER” over “HYGROSYSTEM” over a square with letter “Zb” over “GREECE”. The right side of the shank is marked as “EX # 207- *”, denoting the shape code, size and grade (?). The bottom of the shank bears the stamping “PAT No. 87033” over “06/ 89”, which I believe is the date code indicating that the pipe was made in June of 1989. I re-searched this pipe on pipedia.org and reproduce excerpts of information on this pipe carver, in his own words, and his immense contributions to the Greek pipe industry in particular and entire world’s pipe community.

I am Alexandros Zavvos, born in Molos, Thermopylae, near Lamia. Since I was a child I had an inclination for art, starting with painting. I studied Radio-electronics, and at age 23 I got involved with commerce with a capital of 150.000 drs. in 1962.

I entered the pipe business where I met, by total chance, with Mr. Libero G. Albanese, first technician and producer of briar-wood models in Kalabria, Italy. When I told him that I am Greek, he almost prayed, saying that we Greeks have the best briar in the world for pipe-making! From that moment on I understood that this fellow is in love with his work – and he transmitted that to me instantly!

From mid-1962 to 1963 I searched all over the world for a college or a school in order to be taught the art of pipe-making, but in vain – there were none. Moreover, I wasn’t able to make it through the big European pipe-makers of that time (British, Italian, Danish). I was convinced that only through experience there was a chance of me becoming what I wanted.

In 1964 I started the commercial briar-wood model production, in 1965 I constructed empirically my first pipe and in 1967 I started the vertical production (this is from the briar Greek woods to the consumer) – maybe there is no other factory in the world producing smoking pipes vertically.

In 1970 I started the research, which was accomplished in 1984, on the 1st generation hygrostatic system. In that same period we founded, my brother and I, our factory in Lamia for the production of ebony epistomes.

Today, 40 years later, I have successfully arrived at the production of the 5th generation hygrostatic pipe. I will finish by saying that this pipe, to what concerns the pleasure it provides, has nothing to do with that pipe for peace, offered by American Indians.        

Update:Today I am saddened by the news that Alexander passed away on February 10th, 2015. Our thoughts and prayers are with his family and friends. We are very thankful for his contributions to the World of pipes. —sethile (talk) 21:00, 12 February 2015 (UTC). 

The description given by the seller on eBay was equally informative and I reproduce the same for the readers to get a fair idea of the famed Hygrosystem that has been incorporated into the construction of this pipe.

A patented Hygro-system pipe by the greatest and most known (now deceased) Greek pipe manufacturer Alexander (Zabos / Zavvos). His old pieces are by now becoming rare and sought after, as his son who took over the business is not equal to the father. His stamp (Z with a B lower) comes from the two consonants in his name the way it is spelled in Greek. Very big and well known European pipe makers have purchased top briars from Alexander Zavvos, since the Greek briars are among the best in the world.

A few things about Alexader Zabos’s patent : The hygrostatic system  is the result of 35 years research and experience. It is based on the Bernoulli principle, has been allowed to be patterned (No 87833) by the Greek Ministry of Industry and Energy. Unlike most filter or no-filter pipes, the Alexander Hygrostatic Pipe reduces drastically moisture and other heavy residue (such as tar etc), which otherwise could be inhaled into our lungs and extinguishes a bitterness and a burning on the tongue.

Alexander Zavvos’s Hygrosystem pipes were quite expensive if bought new (the cheapest had a value of 160-170 euros) and have become highly collectible after the death of the manufacturer.

From the above information, it is safe to infer that this pipe is from the first generation of the hygrosystem pipes from Alexander Zavvos and made in March 1989.

I have given a detailed description on deconstructing this line of pipes and also a detailed explanation, as I understood it, on the application of the principle employed in the hygrosystem for which these pipes became famous, in my previous write up on a similar pipe which is on its way to Steve in Vancouver, Canada. Here is the link to that article, https://rebornpipes.com/2019/08/02/gifting-my-mentor-and-dear-friend-steve-an-alexander-zavvos-hygrosystem-pipe/

INITIAL VISUAL INSPECTION
This is a very ornate and beautiful pipe with a perfect shape, size and hand feel with a delicate and a smallish stem. The forward heavy weight of the pipe does not lend itself to clenching and would best be enjoyed while being held in the hand. The brass band at the shank end, the vulcanite band at the shank end of the aluminum shank extension and again a brass band at the tenon end of this shank extension should add a nice classy touch to the pipe’s appearance once polished and it also helps to break the monotony of the briar. The stummel has beautiful mixed grain with a combination of straight on the sides and front with bird’s eye and swirls over the heel and shank. All this beauty is hidden under the accumulation of dirt and grime over the years. The stummel has numerous dents and ding over the entire surface. However, save for one large fill (marked in yellow arrow) and unlike the pipe which will be going to Steve, there are no major issues of fills or cracks that I foresee on this stummel. The outer rim edge curves inwards to form a narrow rim top surface  and shows a slight overflow of lava on the rim top and the surface itself is peppered with numerous dents and dings which should be easy to sort out by sanding the rim top with a piece of 220 grit sand paper.The chamber has a thick and even layer of cake which shrouds the condition of the walls of the chamber. However, the feel of the bowl is solid and I hope there are no major surprises here. There is a brass ring at the shank end which extends inside the shank with threads on to which the aluminum shank extension is screwed in. This brass ring should add a bit of glitz to the pipe appearance once polished. The mortise is clogged and heavy crust of dried oils and tars are clearly visible. This will take some effort to clean out.The screw-in aluminum shank extension that houses a filter is covered in oils and tars. Also the smaller aperture pipe protrusion at the stem end is covered in gunk and tars. The vulcanite band at the shank end and the brass band at the tenon end will need to be polished. The briar at the tenon end is nice and solid with no damage, and that’s a big relief having experienced the challenges firsthand with Steve’s pipe, how difficult it is to address issues on this part of the pipe. The wood gasket which is housed in the tenon end of the shank extension has been dislodged from its place and is stuck on to the tenon. The vulcanite stem with its fused briar at the tenon end is generally in good shape, save for the broken and missing nearly half of the stem. The break is at an angle and only a tiny portion of the button end on one side is available to me as a reference. This should be more than sufficient for me to undertake a complete rebuild of the missing portion of the stem. The stem is very lightly oxidized and the fused and decorative briar saddle, though covered in oils, tars and grime, is intact. The tenon is dirty and clogged with all the gunk and dried oils and tars left behind by the previous owner of this pipe. I took a few close-up pictures of the stem and broken edge of the stem for the readers to better assimilate what I would be dealing with during the stem rebuild. I have the option of cutting off the stem at the point of break and thereafter rebuild and shape a new button on either side, but this would drastically shorten the already short stem and toss the symmetry of this beautiful pipe right through the window. And remember, my dear readers, that this pipe is being sent to my dear friend and a pipe restorer par excellence, Dal!! He is a perfectionist, to say the least. I intend to use the intact part of the stem as a guide for determining the length of the stem, the flare at the button end and the length of the slot and I would be attempting all this by eyeballing all the measurements as I do not have any Vernier calipers for exact measurements. I know, that’s hell of a lot of eyeballing that I would be doing during the restoration.THE PROCESS
It is the stem reconstruction that takes the most amount of time what with all the curing, sanding, refilling if needed, shaping and polishing and, therefore, I always prefer to start with repairs to the stem. Firstly, I sand off the area of intended fill with a piece of 220 grit sand paper. This not only evens out the surface for the fill but also gets rid of the oxidation which would otherwise show itself through the fills as a brown patch after polishing. This was followed by cleaning up the internals of the stem and the tenon with regular and bristled pipe cleaners dipped in 99% pure isopropyl alcohol. With a dental pick, I scrubbed out the dried gunk from the tenon and from along the broken button end edges. I had seen Dal use a folded triangular index card while reconstructing a broken button end whereas I always used a petroleum jelly (Vaseline) coated pipe cleaner inserted in to the air way to keep it open. My method, though effective, was time consuming as I had to completely reshape the slot thereafter. However, in this instance, since there was nothing to support or hold the folded index card on the other side, I perforce had to fall back on my time tested method of using a pipe cleaner coated with petroleum jelly (Vaseline). I prepared a slightly thin (just thick enough to form a drop but not runny enough to fall down) mix of CA superglue and food grade activated charcoal and applied it over the broken stem area. I also applied this mix over the intact side lip edge to make it even. To get the flare which was evident on the intact side of the stem, I applied a thick blob of this mix and held it sideways so that the mix forms a droplet. Thereafter I maneuvered the drop to the desired shape till it hardens and harden it does so quite rapidly. Once this layer had cured, I applied another layer of the mix. The trick here is that this type of reconstruction needs to be done in layers to a thickness more than the adjoining stem surface. This, thereafter, can be filed and sanded down to match the stem surface. I did exactly as described above and set the stem aside to cure. The following pictures will give you a general idea of what I have described above. Once the mix had cured hard, I went about shaping these fills to match the overall profile of the stem, with a flat head needle file. I was very careful with my use of the needle file, eyeballing the profile frequently. An hour later and I had achieved a rough match profile to the original stem as it would have been before the break. I even had a rough button profile shaped out in conjunction with the intact button edge. Eager to use my newly acquired slot shaping tool, this was an ideal candidate to use it for the first time. Well, this tool is much more effective than using a tightly folded piece of 220 grit sandpaper to shape the slot. I am very happy with the progress being made. From my experience (and I have done many!!) it usually takes a week to reach this stage and here I was on only my third day of working on the stem!!And then a set back! As I was shaping the slot, a chunk of the fill did not feel like staying and just left its place, leaving behind a gaping hole. It is marked in yellow arrow.Such chipping is to be expected and undaunted I again prepared a mix of superglue and activated charcoal, this time more glue and lesser of charcoal. Since I now had both the edges of the slot, I decided to use the folded index card. Once the index card was in place, I applied this mix over the chipped area and set it aside to cure. I also took this opportunity to fill in a few air pockets which were beginning to show as well as increase the button edges on either side.A curing time of nearly 12 hours later, the fill was nicely set and hard enough to start reshaping the slot and the button edge and further fine tune the stem profile and finish. Using a flat head needle file, I file away at the fill and roughly shape the button edge on either side of the stem. I am comfortably placed with the progress being made so far, so to say. As expected, I observed a couple of air pockets and also that one of the lip edge had been filed down more than the other and was dotted with many air pockets. I addressed these issues with a layer of superglue and charcoal powder mix. However, in this mix, the percentage of superglue was higher than the charcoal powder. I set the stem aside to cure. I would have ideally applied black CA glue, but…don’t have it.Moving ahead, I reamed the chamber with size 2 head of the PipNet reamer. Using my smaller sized fabricated knife, I further reamed out the cake from places where the PipNet reamer could not reach. I gently scrapped out the lava overflow from the thin rim top surface and followed it with sanding the chamber walls with a 220 grit sand paper. How I miss my younger daughter, Pavni, who specializes in smoothing the chamber walls and removing every trace of the old cake. Dal, I know you would have loved to have a pipe that your “Bollywood Queen” had worked on, but hope I have come close to her finesse!! Once the cake was taken down to bare briar, the walls of the chamber were found to be smooth and flawless. The draught hole is dead center and at the bottom of the chamber. I am sure that this will be a nice smoker! Removing the overflow of lava from the rim top revealed a thin surface that is peppered with numerous dents and dings. I continued with cleaning of the stummel and worked the mortise using the smaller fabricated knife first to scrap out the dried out gunk, oils and tars left behind by the previous steward. The amount of grime scrapped out is a testimony to the efficacy of this Hygrosystem, I say. A few pipe cleaners dipped in alcohol later, the shank is clean. Now that the chamber and shank internals are clean, I move ahead with the external cleaning of the stummel.I cleaned the externals of the stummel with Murphy’s oil soap and toothbrush. Rinsing under tap water (remember, I am in India and its hot here and even the tap water is equally warm!!) revealed just a few fills in the briar on left back side of the stummel and nearer to the rim top and these have been marked by yellow arrows. To be honest, I feared a rerun of the nightmare that I just went through while restoring Steve’s Alexander Zavvos Hygrosystem pipe! Not the case this time around, Thank God for such mercies!!! The stummel has a number of small dents and dings, which should be addressed when I sand the stummel with a piece of 220 grit sand paper followed by complete micromesh pad polishing cycle. I do not intend to be overly aggressive with the 220 grit sandpaper as I wish to preserve as much of the old patina as I can. Beautiful straight and mixed grains are now clearly visible. This should turn out to be a beautiful looking pipe, I think. I began removing the old fills and preparing the stummel for a fresh fill. Using my dental tools, I progressed to removing the fills. The fill on the left back side of the stummel was large and deep while the two on the rim top were smaller in size but deep.At this point in the restoration, I decided to address the issue of old odors in the chamber and shank by subjecting it to a cotton and alcohol bath. I wrapped some cotton around a folded pipe cleaner, keeping the tip of the pipe cleaner free of wrapped cotton as this would be inserted through the draught hole in to the chamber. This would form the wick for the shank. I tightly packed the chamber with cotton balls and filled it with 99% pure isopropyl alcohol using a syringe and set it aside. By next day, the cotton and alcohol had drawn out the all the old tars and oils from the chamber and max from the shank. I let the stummel fills dry out completely and after all the alcohol had evaporated, proceeded to fill the deep gouges with CA superglue and briar dust using the layering technique where I put down a thin layer of superglue in to the fill and press briar dust in to this fill over the glue. I continue with this till the fill rises above rest of the stummel surface. Once all the gouges were filled up, I set the stummel aside to cure for the next 24 hours.I file the raised mounds of the patched fills with a flat needle file. The only drawback of the layering technique is that a number of air pockets are revealed after the filing. This time was no exception and I refilled the exposed air pockets only with superglue and set it aside to cure.Since there was still time before I hit the bed, I decided to address the stem. I sand the fill with a needle file to a rough match with the surface of the stem. For a better match, I further sand the entire stem with a folded piece of 220 grit sand paper. I topped the slot on a piece of 220 grit sand paper to even it out. The repairs looked good at this stage.With the stummel fills nicely cured, it was time again to work on it. Using a flat head needle file, I sanded the fills and followed it by sanding with worn out folded piece of 150 grit sand paper. The fill has blended in quite well. However, I shall strive to further achieve a near perfect blend during further sanding and polishing with micromesh pads.I again worked on the stem, filing with a needle file and followed with sanding with a piece of 220 grit sand paper. With my slot tool, I carved out and shaped the slot. Here, the intact part of the stem gave me an idea of the extent of the spread of the slot from the edge. I achieved the desired shape and size by just visual estimations. I sand the slot end on a piece of 220 grit sand paper. I am happy with the way the stem reconstruction including the buttons and the slot, has shaped up till this point. I rubbed a little Extra Virgin Olive oil in to the stem surface for it to be absorbed and hydrate the vulcanite and set it aside. With the stem repairs well under control and progressing steadily, I turn my attention to the stummel once again. I address the dents and dings with further sanding of the entire stummel and the thin rim top using a worn out piece of folded 150 grit sand paper followed by a 220 grit paper. The dents and dings on the stummel and rim top are addressed to a large extent. What dents and dings remained, I let them be as a part of the history associated with the pipe and its previous owner. While going through with the micromesh polishing cycle, I extend this care to the brass band at the shank end. The now nicely shining brass band adds a touch of class to the pipe and helps in breaking the monotony of the pipe.I rubbed some “Before and After” restoration balm. This product has been developed by Mark Hoover and it helps to enrich and enliven the briar. For me it is an absolute “must have” item in my list of items for pipe restorations. I rub this balm in to the briar and set it aside for some time. I turned my attention back to the stem. I sanded the stem, including the briar insert at the tenon end with a 220 grit paper and progressively moving to 600 and 800 grit sand papers. As expected, a clean and neat looking stem stared back at me. I rubbed a little Extra Virgin Olive oil in to the stem surface to hydrate it and set it aside to be absorbed in to the vulcanite.I was satisfied with the way the stem has now turned out. I finished the stem reconstruction by polishing the stem with micromesh pads, wet sanding with 1500 to 12000 grit pads. I applied a small quantity of Extra Virgin Olive oil to the vulcanite stem and rubbed some “Before and After” restoration balm before setting it aside.I had undertaken restoration of two of the three parts of this pipe, the stem and the stummel, and now turned my attention to the third and last part, the aluminum shank extension. This part was in pristine condition, save for the accumulated oils, tars and gunk which I had already cleaned out from the aluminum tube, the smaller aperture tube and the wide shank extension at the stem end, and yes, I had missed out on taking pictures and documenting this step. I went through sanding the vulcanite band and the briar insert with a folded piece of 220, 400 and 600 grit sand papers in that order. I cleaned the aluminum tube protrusion and the threading with a brass wire brush. I further polished it with a 0000 grade steel wool followed by dry sanding with all the nine pads of micromesh. The aluminum tube is now clean and shining. I finished the cleaning regime of the tube and threads in the shank extension by polishing it with a multipurpose liquid polish.This was followed by micromesh polishing cycle, wet sanding these components of the shank extension, including the brass band, with 1500 to 12000 grit pads. I rubbed some “Before and After” restoration balm and set it aside. This part definitely adds some nice class to the overall appearance of the pipe.I cleaned out the wood gasket which makes the fit of the tenon in to the shank extension airtight with cotton buds dipped in alcohol. I applied a little Extra Virgin Olive oil to this gasket, inside and outer surface to hydrate the wood and set it aside to be absorbed by the wood. When I had initially dismantled the pipe, this gasket came out attached to the tenon. However, close observation of the outer surface of the gasket points to the fact that the gasket was stuck inside the shank extension towards the stem end. I did not sand the outer surface to a smooth finish as I wanted to keep the surface rough when I applied superglue and reaffixed it inside the shank extension.Nearing the home run, I decided to stain the stummel and the rim top surface with a dark brown stain in the hope that it would help in a nice blending of the one and only major stummel fill. I heated the stummel surface with my heat gun to open up the pores on the stummel so that the stain is well set while being careful that I do not overheat the fill, a lesson learned while restoring Steve’s Alexander Zavvos pipe. I dipped a folded pipe cleaner in Feibing’s Dark Brown leather dye and liberally applied it over the heated surface, flaming it with the flame of a lighter as I went ahead to different self designated zones of the surface. This helps in the setting of the stain in the grain of the briar.I was not very comfortable in heating the aluminum shank extension and the briar insert on the stem as this could result in warping of the vulcanite band and the briar inserts on the shank extension and stem. I decided to use a dark brown stain pen instead. I applied the dark brown stain over the briar inserts of the shank extension and stem. I set both the stummel and shank extension aside for the stain to dry and get completely absorbed in the surface.The next evening, approximately 18 hours later, as Dal describes, I began to unwrap the stain in the hope to see beautiful grains. I mount a felt cloth buffing wheel on my hand held rotary tool and setting the tool at its slowest speed, again my recent experience while working on Steve’s pipe came in handy and the damage that can be caused due to heating while using the felt buffing wheel still fresh in my memory; I began to peel off the stain from the stummel surface first. The stain was peeled out gradually. This was followed with wiping the stummel with a cotton swab and alcohol to lighten the stain a little as it was too dark for my liking. This also helps in cleaning the surface of all the residual stain and highlighting the grain. Now, the fear that besieged me was the stain running down Dal’s hand as he smoked the pipe and so I set the stain by again heating the stummel surface with the heat gun. Unfortunately in my exuberance, I missed out on taking pictures of this step.

I felt as though the stummel, shank extension and the stem appeared patchy, though when I shared pictures with Abha, my wife, she found them to be nice, smooth and shiny. However, I decided to go with my instinct and dry sanded the entire pipe with 1500 to 12000 grit micromesh pads, aluminum tubing and brass bands included. Now I am satisfied by the appearance of the pipe at this stage and ready to move on to the final stage of polishing. Next, I mount a cotton cloth buffing wheel and setting the speed to ¼ of the full power, I applied a thick coat of carnauba wax over the stummel, aluminum shank extension and the stem. I worked the complete pipe till the time all the wax was absorbed by the briar. The pipe now boasts of a beautiful and lustrous shine. I vigorously rubbed the pipe with a microfiber cloth to deepen the shine and also clean away any residual wax that had been left behind. I am very happy with the way this beauty has turned out.Before re-assembling the pipe, I once again thoroughly cleaned the internals of the shank, aluminum shank extension and the stem airway with pipe cleaners and ear buds dipped in isopropyl alcohol. I also fixed the wooden gasket with superglue in to the stem end of the shank extension. I checked the draw to make sure that the airways in the shank, extension and stem are open. The draw is nice, smooth and open and somewhat similar to the draw experienced on a Peterson’s P-lip stem. I also applied a little Vaseline over the threads of the aluminum shank extension and the wood gasket to protect and keep it soft.To finish, I reassembled the complete pipe and gave it a final buff with a microfiber cloth to deepen the shine. This dude has come a long way when it started its journey in June 1989 and now 30 years later, it shall soon be traveling all the way to Bulgaria to serve my dear friend and fellow pipe restorer, Dal Stanton while he reminisces about his visit to me, Abha, Mudra and his Bollywood Queen!! I sincerely thank all the readers to have spared their valuable time in going through this write up. P.S. This project has been very close to my heart as this pipe is intended to be with my friend and guide, Dal as a memento of his visit to my family in India, fond memories of which will always stay with me. I hope that whenever he sits down with this pipe, packs it with his favorite tobacco, LANE BCA and fires it up, the first whiff reminds him of us here in India.

Some readers must have observed that the fill still stands out as a sore thumb, but I would like to assure you that it’s the smooth glossy surface of the highly polished superglue that reflects more light than the surrounding and hence is more prominent. To the naked eye, however, it is not so evident. Any inputs and suggestions are always valuable to me and most appreciated as they help me grow and improve.

Lastly, I thank everyone for sharing the joy that I experienced while working on this pipe.

 

 

 

Gifting my Mentor and Dear Friend, Steve, an Alexander Zavvos Hygrosystem Pipe.


Blog by Paresh Deshpande

When Steve, his brother, Jeff and Dal Stanton, The Pipe Steward, were on a visit to India, I had a desire that there should be a unique pipe which all three of us should have (Mr. Jeff being a non smoker) and had laid down for myself, the following parameters for identifying THAT PIPE!

(a) Both should not be having this pipe in their personal collection (knowing well that this would be a very tall order!!)

(b) The pipe must have some historical significance and should have made a contribution to the world’s pipe history.

(c) It must come from a well-known carver or manufacturer.

I began this selection with going through my own personal modest collection, rather my Grandfather’s collection to which I have made miniscule additions. Amidst all the WDCs, Charatans, Comoy’s, Barlings, Ben Wades, Stanwells and Kriswills, there was this one pipe which was very different. Very early in my association with Steve, we had discussed this pipe which Mr. Steve had not come across (which was unbelievable!!!) and did not own a pipe from this carver, but was very much interested in it. An oblique enquiry from Dal also confirmed that he did not have this make. Well, this helped me zero in on this pipe to be gifted to my friends during their visit to India. The pipe selected is an ALEXANDER ZAVVOS HYGROSYSTEM, PAT.No 87033, made in the 1970s-80s. What followed was an extensive and prolonged hunt for two such pipes of which the first one was purchased from one seller on Pinterest and the second was on eBay. These pipes were received separately and the last delivery materialized a couple of days prior to the arrival of my esteemed guests. Here are both the pipes as I received them.Since Dal was the first to arrive in India (and being the youngest amongst arriving guests…LoL), he was given a choice between the two. He selected one with an Apple shape and the remaining willy-nilly came to Steve. At that point in time, both Dal and I discussed that it would be the Apple shape that Steve would have selected but… Well after working on Steve’s pipe, am I glad that the Dublin came to Steve as it provided me with an opportunity to present my first ever rusticated pipe to the person who has introduced me to this art and mentored me all along. Thank you Steve for being with Abha and me on this journey.

The stamping on the Dublin is pretty worn out and hard to make out. However, the stampings on my pipe and that on Dal’s is pretty crisp and clear. It reads on the left of the shank as “ALEXANDER” over “HYGROSYSTEM” over a square with letter “Zb” over “GREECE”. The bottom of the shank bears the stamping “PAT No. 87033” over “03/ 89”, which I believe is the date code indicating that the pipe was made in March of 1989. This stamping is visible only under a white light with a magnifying glass and the area around the stampings has bubbled up skin surface, something akin to chipped paint.I researched this pipe on pipedia.org and reproduce excerpts of information on this pipe carver, in his own words, and his immense contributions to the Greek pipe industry in particular and entire world’s pipe community.

I am Alexandros Zavvos, born in Molos, Thermopylae, near Lamia. Since I was a child I had an inclination for art, starting with painting. I studied Radio-electronics, and at age 23 I got involved with commerce with a capital of 150.000 drs. in 1962.

 I entered the pipe business where I met, by total chance, with Mr. Libero G. Albanese, first technician and producer of briar-wood models in Kalabria, Italy. When I told him that I am Greek, he almost prayed, saying that we Greeks have the best briar in the world for pipe-making! From that moment on I understood that this fellow is in love woth his work – and he transmitted that to me instantly!

From mid-1962 to 1963 I searched all over the world for a college or a school in order to be taught the art of pipe-making, but in vain – there were none. Moreover, I wasn’t able to make it through the big European pipe-makers of that time (British, Italian, Danish). I was convinced that only through experience there was a chance of me becoming what I wanted.

In 1964 I started the commercial briar-wood model production, in 1965 I constructed empirically my first pipe and in 1967 I started the vertical production (this is from the briar Greek woods to the consumer) – maybe there is no other factory in the world producing smoking pipes vertically.

In 1970 I started the research, which was accomplished in 1984, on the 1st generation hygrostatic system. In that same period we founded, my brother and I, our factory in Lamia for the production of ebony epistomes.

Today, 40 years later, I have successfully arrived at the production of the 5th generation hygrostatic pipe. I will finish by saying that this pipe, to what concerns the pleasure it provides, has nothing to do with that pipe for peace, offered by American Indians.

Update: Today I am saddened by the news that Alexander passed away on February 10th, 2015. Our thoughts and prayers are with his family and friends. We are very thankful for his contributions to the World of pipes. —sethile (talk) 21:00, 12 February 2015 (UTC).

The description given by the seller on eBay was equally informative and I reproduce the same for the readers to get a fair idea of the famed Hygrosystem that has been incorporated into the construction of this pipe.

A patented Hygro-system pipe by the greatest and most known (now deceased) Greek pipe manufacturer Alexander (Zabos / Zavvos). His old pieces are by now becoming rare and sought after, as his son who took over the business is not equal to the father. His stamp (Z with a B lower) comes from the two consonants in his name the way it is spelled in Greek. Very big and well known European pipe makers have purchased top briars from Alexander Zavvos, since the Greek briars are among the best in the world.

A few things about Alexader Zabos’s patent: The hygrostatic system  is the result of 35 years research and experience. It is based on the Bernoulli principle, has been allowed to be patterned (No 87833) by the Greek Ministry of Industry and Energy. Unlike most filter or no-filter pipes, the Alexander Hygrostatic Pipe reduces drastically moisture and other heavy residue (such as tar etc), which otherwise could be inhaled into our lungs and extinguishes a bitterness and a burning on the tongue.

Alexander Zavvos’s Hygrosystem pipes were quite expensive if bought new (the cheapest had a value of 160-170 euros) and have become highly collectible after the death of the manufacturer.

From the above information, it is safe to infer that this pipe is from the first generation of the hygrosystem pipes from Alexander Zavvos and made in March 1989.

DECONSTRUCTING THE PIPE
In my quest to understand the functional principal of the famed HYGROSYSTEM used in this pipe, I began by first dismantling the pipe. The pipe was dismantled in three parts; first the stummel, secondly the aluminum screw-in shank extension which has an aluminum tube to house a filter, probably a 6 mm, and lastly vulcanite stem with a fused briar wood saddle. From my appreciation, it is the shank extension which forms the critical component in the famed Hygro-System, at the stem end of which a smaller aperture pipe protrusion is seen. A similar sized protrusion is seen at the tenon end of the vulcanite stem. The fit of the tenon in to the aluminum shank extension is made air tight with a thin ring of briar wood (not leather, as it is not pliable at all).APPLICATION OF BERNOULLI’S PRINCIPLE IN THE HYGROSYSTEM

Bernoulli’s principle states that an increase in the speed of a fluid occurs simultaneously with a decrease in pressure or a decrease in the fluid‘s potential energy. This is applicable to flow of gases also.

In simple layman’s understanding, the above principle states that “Pressure is inversely proportional to the speed of the liquid or gaseous flow”. So how does this principle work in the hygrosystem of this pipe? To explain application of this principle, refer to the picture of the pipe below that I have drawn:(a) Hot smoke along with heavy particulates of oils, tars and moisture from the chamber enters the mortise and expands due to width of the mortise. As a result, speed is reduced. High pressure is created in the mortise.

(b) Once the smoke enters in to the aluminum shank extension, it is compressed and speeds up considerably creating a low pressure area. Due to the low pressure, heavy particles like oils, tars and moisture settle down and are trapped in the filter in the aluminum tube of the shank extension.

(c) The speed is further increased when the smoke passes through the smaller aperture tube due to further compression, shown in green arrows, further lowering the pressure. When this smoke leaves the smaller aperture tube and enters the wide stem end of the shank extension, there is a sudden increase in pressure. This sudden variation in pressures results in heavy particulates settling down and only smoke, being lighter, propelled ahead.

(d) Similar pressure changes are affected when the smoke passes through the wide tenon and through the smaller aperture tube in the stem, further precipitating the heavy particulates of oils, tars and moisture. The end result is a pure smoke without any oils or tars.

The above understanding is my own reasoning based on my learning of science till Graduation level. Any corrections or clarifications from more knowledgeable readers is always enriching and welcomed.

INITIAL VISUAL INSPECTION
Starting with the rim and rim top surface, there is a slight overflow of lava on the rim top and the surface itself is peppered with numerous dents and dings which should be easy to sort out by topping the rim top. The rim edges are sans any serious damage, save for an odd chip on the outer edge, marked in blue arrow.The chamber however tells a very different story. There is a thin layer of cake which has taken on a grey coloration, which is a first for me, by the way. The way the cake appears to the eye, I suspect a few heat lines in the walls of the chamber towards the back and right side. I just hope that the issue is not a major one and just a bowl coating should suffice. Well, I shall cross the bridge when I reach it. There is strong smell emanating from the chamber which should be addressed to a great extent once the chamber has been reamed and the shank has been cleaned. The stummel surface has signs of accumulated dirt, dust and grime and should clean up nicely. It was surprising to note that these accumulations are in patches, almost following the cross grains seen on the right and front and over the entire shank. The left side, which has some beautiful bird’s eye grain, is clean. There are a large number of dents and dings all around the stummel surface. The shank surface has bubbled up near and around the stampings towards the shank end. Just near to the shank and bowl junction, I could make out a very thin line running all round the shank forming a circle (marked in yellow arrow). This worries me as at this stage, I am not sure about the extent of the depth of the crack. Also along this crack line, I could make out one fill. All in all, this is going to be a challenging restoration to get it back to being smoke worthy. There is a brass ring at the shank end which extends inside the shank with threads on to which the aluminum shank extension is screwed in. This brass ring should add a bit of glitz to the pipe appearance once polished. The mortise is clogged and heavy crust of dried oils and tars are clearly visible. This will take some effort to clean out.   The screw-in aluminum shank extension that houses a filter is covered in oils and tars. Also the smaller aperture pipe protrusion at the stem end is covered in gunk and tars. The briar coating at the top of this extension is chipped at one place (marked in yellow arrow) exposing the underlying aluminum shank extension. At the stem end of this extension, the brass ring is missing (marked in orange). I don’t have any brass rings and hence will have to improvise one that will fit. The vulcanite stem with its fused briar saddle at the tenon end is generally in good shape, save for the broken button end. The stem is very lightly oxidized and has minor tooth chatter on the lower lip surface towards the button end. The lower button itself shows minor tooth marks. Rebuilding of the missing button portion of the upper surface and reshaping of the lower button shouldn’t pose any major issue. The tenon is dirty with all the gunk and dried oils and tars left behind by the previous owner of this pipe. THE PROCESS
Since any stem reconstruction takes the most amount of time what with all the curing, sanding, refilling if needed, shaping and polishing, I always prefer to start with repairs to the stem. Firstly, I sand off all the tooth chatter and the area of intended fill with a piece of 220 grit sand paper. This not only evens out the surface for the fill but also gets rid of the oxidation which would otherwise show itself through the fills as a brown patch after polishing. This was followed by cleaning up the internals of the stem and the tenon with regular and bristled pipe cleaners dipped in 99% pure isopropyl alcohol. With a dental pick, I scrubbed out the dried gunk from the tenon and from along the broken button end edges. I had seen Dal use a folded triangular index card while reconstructing a broken button end whereas I always used a Vaseline coated pipe cleaner inserted in to the air way to keep it open. My method, though effective, was time consuming as I had to completely reshape the slot thereafter. Therefore for this repair, I decided to adopt Dal’s method. I appropriately folded an index card and covered it with a transparent tape which prevents the superglue and charcoal mix from sticking to the card. This is how it appears and fits in to the broken stem.I prepared a thick mix of CA superglue and food grade activated charcoal and applied it over the broken button area. I also applied this mix over the lip edge to make it even and cover the tooth marks. Once this layer had cured, I applied another layer of the mix. The trick here is that this type of reconstruction needs to be done in layers to a thickness more than the adjoining stem surface. This thereafter can be filed and sanded down to match the stem surface. I did exactly as described above and set the stem aside to cure.First layer.Second layer.Third layer.Final layer.

Once the mix had cured hard, I went about matching these fills with a flat head needle file and followed it up with a piece of 220 grit sand paper. As expected, I observed a couple of air pockets and also that one of the lip edge had been filed down more than the other and was dotted with many air pockets. I addressed these issues with a layer of superglue and charcoal powder mix. However, in this mix, the percentage of superglue was higher than the charcoal powder. I set the stem aside to cure. After the stem fills had cured, I repeated the process explained above to match the filled surface with the stem surface using needle files and sand paper. Now the lip edges are even, however, the air pockets persist. It’s very frustrating, I know but you have to be equally persistent. I applied a layer of clear CA superglue (would have ideally applied black CA glue, but……don’t have it) and set it aside. To take my mind off the troublesome stem repair, I decided to tackle the issue of missing brass band from the stem end of the shank extension. Working with limited spares, materials and tools has its advantages. It forces you to think out-of-the-box for ways around the hurdle, many a times with startling and successful results but you pay the price in terms of time penalties. Well, time I have aplenty!!! I decided to fabricate a brass ring of adequate thickness. My fabricator informed me that it would not be possible to make one with this width as he had only wires and not strips of brass. No issues, I had two rings made!! These rings fit perfectly and add a nice unique touch. These should polish up nicely. I shall fix these rings towards the end of the restoration process. Moving ahead, I reamed the chamber with size 1 and 2 head of the PipNet reamer. Using my smaller sized fabricated knife, I further reamed out the cake from places where the PipNet reamer could not reach. I gently scrapped out the lava overflow from the rim top surface. I followed it with sanding the chamber walls with a 220 grit sand paper. How I miss my younger daughter, Pavni, who specializes in smoothing the chamber walls and removing every trace of the old cake. Steve, hope I have come close to her finesse!! Once the cake was taken down to bare briar, my initial fears of heat fissures/line were confirmed, with the only difference being that these were not linear but pits, another first for me. These pits were only on the right side of the stummel and marked in yellow.  To use J B Weld or only a bowl coating (which I prefer) would suffice, shall be decided later. Removing the overflow of lava from the rim top revealed a surface that is peppered with numerous dents and dings. Other than these issues, the walls of the chamber are even and solid. I still did not have the inclination to work on the stem (actually it’s the fear of unknown result of the last fill!!) and continued with cleaning of the stummel. I worked the mortise using the dental tool first to scrap out the dried out gunk, oils and tars left behind by the previous steward. The amount of grime scrapped out is a testimony to the efficacy of this HygroSystem, I say. A few pipe cleaners dipped in alcohol later, the shank is clean. Now that the chamber and shank internals are clean, the smells though reduced, is still prevalent.Staying with the stummel, I cleaned the externals with Murphy’s oil soap and toothbrush. Rinsing under tap water (remember, I am in India and its hot here and even tap water is equally warm!!!!) was the start of my nightmare and prolonged conversations with Steve and on our FB messenger group. Here are the pictures first; description of my observations will follow subsequently. Just follow the arrows… As I had noted during my initial inspection, the hairline crack towards the bowl end is now prominently visible and marked with yellow arrows in each picture. This hairline crack runs all around the shank and is joined end-to-end. This still was okay as I had anticipated it, but what surprised me, or rather rocked my feet, was the thick fill of putty running all around the shank end. The same is marked with blue arrows. This fill runs in a more perfect circle than the one near the bowl shank joint and right through the middle of all stampings!! Aargh……There goes the stampings… Sorry Steve, hope you understand.

As if the hairline crack and the all-round fill at the shank end was not enough, the right side of the stummel is…. Actually, I am lost for words and the words that come to my mind are most definitely unprintable and I definitely have no desire for a rap on my knuckles from Steve. Have a look at the pictures and please decide for yourself a suitable description. There is not an inch on the right side of the stummel and shank that is free of any fills. Undaunted, I began the arduous journey of removing the old fills and preparing the stummel for a fresh fill. Using my newly acquired dental tools which were procured when Steve, Jeff, Abha and I had gone around the town shopping for tools for pipe resto work, I progressed to removing the fills. This is how the pipe appeared after the old fills were removed, a cheesecake pipe!!!! The fills were large and deep. The only saving grace was the crack near the bowl shank joint was only superficial and the fills on it would act as counter hole, what am I writing!! It’s a complete circular crack. The long and short of it is that the crack is stable and going nowhere damaging the structural integrity of the pipe. At this point in the restoration, I decided to address the issue of old odors in the chamber and shank by subjecting it to a cotton and alcohol bath. I wrapped some cotton around a folded pipe cleaner, keeping the tip of the pipe cleaner free of wrapped cotton as this would be inserted through the draught hole in to the chamber. This would form the wick for the shank. I tightly packed the chamber with cotton balls and filled it with 99% pure isopropyl alcohol using a syringe and set it aside. Immediately a few seconds later, the alcohol started oozing out of all the fills. The pipe appears to be shedding tears at its present condition, and so am I. I shared these pictures with my FB messenger group friends inquiring whether to discard the pipe or continue and ways to progress ahead with the restoration. The unanimous reply was to continue and rustication was the way ahead. Well I moved ahead with my work on the pipe but was not sure about the rustication part. Here is how the pipe appeared at this stage in restoration: By next day, the cotton and alcohol had drawn out the tars and oils from the chamber and max from the shank.I let the stummel fills dry out completely and after all the alcohol had evaporated, proceeded to fill the deep gouges with CA superglue and briar dust using the layering technique. I my part of the world, the moment briar dust came in to contact with the glue it becomes rock hard even after trying every trick that Dal had shared with me and Steve when we were together in India. Therefore, I adopted the layering technique where I put down a thin layer of superglue in to the fill and press briar dust over the glue. I continue with this till the fill rises above rest of the stummel surface. Believe you me readers, I spent an entire evening working well past midnight, to get all the gouges filled up. I set the stummel aside to cure for the next 24 hours. Still working on the stummel, I file the raised mounds of the patched fills with a flat needle file. The only drawback of the layering technique is that a number of air pockets are revealed after the filing. This time was no exception and I refilled the exposed air pockets only with superglue and set it aside to cure. Since there was still time before I hit the bed, I decided to address the stem. I sand the fill to match the surface of the stem. For a better blending, I further sand the entire stem with 220. I topped the slot on a piece of 220 grit sand paper to even it out. The repairs looked good at this stage. With the stummel fills nicely cured, it was time again to work on it. Using a flat head needle file, I sanded the fills and followed it with further sanding with a folded piece of 220 grit sand paper. Again the same sordid story, the fills revealed numerous air pockets through which the briar dust was seen. In my quest to make this restoration as perfect as possible, it refilled these air pockets with superglue and briar dust. This time around, I mixed a minuscule amount of briar dust with superglue and surprise! The mix remained pliable for just enough seconds in which I could apply it over the fills. Again I set the stummel aside to cure. This sure is trying my patience and stubbornness. I shall prevail, is what I have decided. Since the glue and briar dust mix had hardened immediately, but not hard enough to use a flat head needle file on it, I decided to address the issue of the numerous dents, dings and scratches on the rim top surface. To do this, I spread out a patch of 220 grit sand paper on my work table. Firmly holding the patch in my left hand and the stummel in my right, I gave a few firm rotations to the rim top over the sand paper patch. I continued the process, checking ever so frequently, till I was satisfied with the result. The rim no appears pristine and even. This was the only uneventful part in the entire restoration, LoL!!The fills on the stummel having sufficiently cured, I went ahead and filed the fills with a folded worn out piece of 150 grit sand paper and followed it up with sanding with a piece of 220 grit sand paper. My reasoning for not using a flat head needle file was that maybe the hard abrasiveness of the file is causing the fill to come out exposing the air pockets. But no, the air pockets still showed themselves in all their ugliness. I decided to press on with the process, even though Steve was still gently prodding me to take the rustication route. This was followed up with micromesh polishing cycle. I wet sanded the stummel going through with 1500 to 12000 grit pads. Intermittent wiping of the stummel with a moist cloth helps firstly, to remove the sanded dust and secondly, gives an idea of the progress being made and areas which needed more attention. The stummel has taken a beautiful sheen where there are no fills, but the right and front of the stummel and the shank tells a different story, it does not look presentable to put it mildly. While going through with the micromesh polishing cycle, I extend this care to the brass band at the shank end. The now nicely shining brass band adds a touch of class to the pipe and some bling too!!I shared the above pictures with Steve and asked for suggestions for the way ahead. He suggested applying some “Before and After” restoration balm as it may also help in further blending the fills. As he was suggesting this, there was a ping on my mobile and there were some pictures of beautifully rusticated pipes that Steve had done over the years. I just smiled and went ahead with applying the balm and see the results. The results were not encouraging at all to say the least. To be honest, the thought of going the rustication route to salvage this pipe had started taking roots in my head, mind you head and not the heart! Disappointed with the stummel appearance at this stage, I turned my attention back to the stem. I had sanded the stem, including the briar insert at the tenon end with a 220 grit paper. I picked it up from there and progressively sanded the entire stem with 600 and 800 grit sand paper. I expected a clean and neat looking stem to stare back at me, but what I saw made me cringe. The top of the button showed some beautiful white spots of air pockets (marked in circle)!! Why, why can’t this restoration progress without any hiccups? I decided to take a break and cleaned out my work table. I loaded my large W. O. Larsen bent brandy pipe with my favorite G. L. Pease Virginia blend, Telegraph Hill (thanks Steve for this pipe and the tobacco, though my gift to you is testing my endurance and determination!) and went out and sat down in the lawns closing my eyes. I thoroughly enjoyed my smoke and came back refreshed. I rubbed a little Extra Virgin Olive oil in to the stem surface to hydrate it and set it aside to be absorbed in to the vulcanite.I had undertaken restoration of two of the three parts of this pipe, the stem and the stummel, and this had proved to be tedious and frustrating. I left them aside in various stages of progress and now turned my attention to the third and last part, the aluminum shank extension. The only issue that I had seen in my initial inspection was that of the chip and bubble in the surface of the briar coating over the aluminum insert. I picked out the bubble and lo, behold, the small chip instantly transformed itself in to larger than life sized!!!! The thickness of the coat was very thin, a few microns, maybe, and instantly peeled of like wall paint. I immediately realized that I am in for a long haul on this one too. Here is what happened and for comprehension, reproducing the picture taken during the initial inspection.It was interesting to note that the aluminum shank extension had a nice design, indicated with a yellow arrow, below the briar finish coat and the coat was pressed on to it. That the coat is heated and wrapped around is evident from the fact that this design can be seen on the intact coat surface. I decided to address the issue of chipped coating by filling it with a mixture of briar dust and superglue. I set the shank extension aside to cure after applying the mix. I missed out on taking pictures of the fill.While fill on the shank extension was curing, I decided to complete the stem repairs. I completely gouged out the area with air pocket for a fresh fill. With a black marker I darkened the fill and thereafter spot filled it with a mix of charcoal powder and superglue, superglue being more than charcoal and set it aside to cure. The mix hardened immediately and I continued with sanding and shaping the button. The fills and stem reconstruction came out good and I was satisfied with the way the stem has now turned out. I followed it up with sanding the entire stem with a folded piece of 220, 400 and 600 grit sandpaper in that order. I finished the stem reconstruction with a polishing with micromesh pads, wet sanding with 1500 to 12000 grit pads. I applied a small quantity of Extra Virgin Olive oil to the stem and set it aside. The fill on the shank extension had cured and I progressed with filing it with a flat head needle file followed with a sanding with a piece of 220 grit sand paper. I further matched the fill with the rest of the surface by sanding the entire wood coating on the shank extension with folded pieces of 400 and 600 grit sand papers. In the pictures below, one may think that there are air pockets in the fill; however, the fill is solid without any air pockets. I also evened out the edges over the aluminum extension in preparation for fixing the two fabricated brass rings, described above. Staying with the shank extension, I cleaned out the aluminum tube protrusion and the threading with a brass wire brush. I further polished it with a 0000 grade steel wool. The aluminum tube is now clean and shining. I finished the cleaning regime of the tube and threads in the shank extension by polishing it with a multipurpose liquid polish.Now it was time to affix the two fabricated brass rings. I applied a little superglue over the exposed aluminum protrusion of the shank extension towards the stem end and fixed the rings over it. I polished the shank extension, the aluminum tube and the two brass rings included, with micromesh pads, wet sanding with 1500 to 12000 grit pads. The shank extension now has a nice shine and the aluminum tube looks like new. The fill does show through in all its awfulness, but this will blend in nicely when I stain and subsequently polish it further. I applied a little “Before and After” restoration balm and buff it with a microfiber cloth after 20 minutes.I cleaned out the wood gasket which makes the fit of the tenon in to the shank extension airtight with cotton buds dipped in alcohol. I applied a little Extra Virgin Olive oil to this gasket, inside and out, to hydrate the wood and set it aside to be absorbed in the wood. When I had initially dismantled the pipe, this gasket came out attached to the tenon. However, close observation of the outer surface of the gasket points to the fact that the gasket was stuck inside the shank extension towards the stem end. I did not sand the outer surface to a smooth finish as I wanted to keep the surface rough when I applied superglue and reaffixed it inside the shank extension.Now that I had completed the restoration and reconstruction of the shank extension and stem respectively, I turned my attention back to the stummel with all its imperfections. Even at this stage, while on Face time with Steve he suggested that I rusticate the stummel. However, when he saw the reluctance, he suggested that I should try to blend the fills, which were standing out like sore thumbs, with a darkest stain available to me. I decided to stain the stummel and the rim top surface with black stain first and later with a dark brown stain in the hope that the contrast would help in a nice blend. I heated the stummel surface with my heat gun to open up the pores on the stummel so that the stain is well set. I mixed black stain powder with isopropyl alcohol and liberally applied it over the heated surface, flaming it with the flame of a lighter as I went ahead to different self designated zones of the surface. This helps in the setting of the stain in the grain of the briar. Similarly, I applied the black stain over the wood of the shank extension. I set both the stummel and shank extension aside for the stain to dry and get completely absorbed in the surface. The next evening, approximately 18 hours later, as Dal describes, I began to unwrap the stain in the hope to see beautiful grains. I mount a felt cloth buffing wheel (for the first time I admit, as I had only recently purchased these) on my hand held rotary tool. Setting the tool at its slowest speed as Dal had explained to me that a felt cloth wheel generates tremendous heat, I began to peel of the stain from the stummel surface first. But, hell there was no unwrapping at all!!! Not an iota of stain was buffed out. Therefore, I decided to increase the speed of the rotary tool a notch higher and still no result. I further upped the ante and took the speed regulator to half of the full power. Now the stain was peeled out gradually. This was followed with wiping the stummel with a cotton swab and alcohol to lighten the stain a little as it was too dark for my liking and this also helps in cleaning the surface of all the residual stain. But as soon as I reached to the right side of the stummel, I started seeing the dreaded patches where the fills got removed. Same for the shank extension!!! Here are the pictures as I saw the after effects of this buffing. Following are my observation on the stummel at this stage:-

(a) The stain had not set in over certain fills. These stood out like red blisters and are gory to look at.

(b) The fills had come out at certain spots. This was due to my mistake. I had either heated thestummel too much prior to staining or could be that I erred in my handling of the newly acquired felt cloth buffing wheel. Unknowingly, I got the stummel overheated, ditto for the shank extension.

It was extremely frustrating to say the least. Now I had option of either refilling the spots or “RUSTICATING” the stummel and the shank. To the readers, I would like to inform that during the process of filling and subsequent sanding of the stummel there were numerous, or countless I say, times when I had to spot fill small pockets and repeat the sanding of these small spots. I really had no desire to go that route as it would have literally meant starting from square one!! And it has already been nearly 25 days that I have been working on this pipe (and simultaneously on Dal’s pipe too with its own share of challenges!). I decided to go the path pointed by my mentor and rusticate the stummel. I messaged Steve about this decision and his first response was a terse “Good”!!! Before I could forward a message lamenting further about not having suitable tools, he sent me a link on rebornpipes.com about how to make rustication tool from a Philips screwdriver. From the speed and swiftness with which he forwarded the link, it appeared as if he had anticipated this. Here is the link and is a must read for all new exponents of this art. https://rebornpipes.com/2012/11/03/making-a-rustication-tool-out-of-a-phillips-screwdriver/

The article is worded very simple and articulate enough for anyone to follow and make a rustication tool for oneself.  Lucky for me, I had ordered a DIY rotary tool kit with complete accessories and this kit included all the tools that were essential to make myself a rustication tool. Shown below are a few pictures of the tools used and the completed rustication tool. With this, I geared myself for the first ever rustication of a pipe amidst a lot of trepidation. It was after a lot of effort that I had laid my hands on a pipe from this maker with this system, was meant to be a gift for someone I admire and as such did not want to ruin it. However, if you do not take a step further, you never progress and never learn and so I began the process of rusticating the bowl and shank.

I first wiped the stummel with a cotton pad and isopropyl alcohol to clean the surface and lighten the dark stain. The rim and about half an inch below the rim was in decent shape and I decided to maintain a smooth ring atop the rustication. Since I did not have a masking tape, I used a transparent tape to demarcate the area that I wanted to keep smooth that is the rim top and about half an inch below the rim outer edge. Similarly, I covered whatever little that remained of the stamping. This is a very essential step as I realized during rusticating that it is very easy to lose track and transgress over the areas and stampings which you wish to preserve. To rusticate, I firmly held the stummel in my left hand and with my right hand and began gouging out the briar. The technique is to firmly press the pointed four prongs of the modified Philips screwdriver in to the surface, rotate and pull out the removed chunk of briar. During the entire process, I kept sharing pictures of the progress that I was making, with Steve. As Steve suggested, I was pretty aggressive in my rustications. Once I had completed the rustications over the intended areas, I removed the transparent tape and cleaned the entire stummel with a soft bristled brass brush to remove all the debris from the rusticated surface. Here is how the stummel appeared after the cleaning process. I am happy with the way the stummel appears at this stage. I wanted to smooth out the jagged edges left behind by the screwdriver. I decided to scrub the entire stummel with a hardwired bristled circular brush mounted on my rotary tool. I hoped that this would thoroughly clean the rustications, smooth out the rough edges, and remove the chipped surface which could not be removed by the soft wired brass brush while adding a new dimension to the rusticated surface. Well, honestly I am not sure about the last aspect that I had hoped to achieve, but the other objectives we successfully achieved. I cleaned the smooth and rusticated surface with a cotton swab dipped in isopropyl alcohol to remove the sticky mark left behind by the tape and clean the rusticated surface in preparation for application of black stain. Once satisfied with the cleaning, I heated the stummel with my heat gun and applied a coat of black stain as described above. I set the stummel aside to set the stain in the surface. Once the stain had dried, I did observe a few spots that missed the application of the stain. However, I am not overly concerned with this, as these spots would eventually get stained when I apply the second coat of dark brown. Once the stain had set in well, I again warmed the stummel with my heat gun. This helps the stain to be absorbed and set further in to the briar. This heating also helps in reducing/preventing the stain from bleeding onto one’s hands while smoking or that is what I have read. I mounted a felt cloth buffing wheel on my rotary tool and gently buffed the entire stummel surface. Not wanting to repeat my previous mistake, I kept the speed of the rotary tool at its minimum. It took some time before I was finally able to remove the crust formed by the black stain. I wiped the stummel with a cotton swab and alcohol to remove any excess stain and followed it up sanding the raised rustication with a folded piece of 220 grit sand paper. This was followed up by carefully dry sanding of the entire stummel, especially the raised rustications with 1500 to 12000 grit micromesh pads. This not only lightened and highlighted the rustications, but would also provide a smooth surface for the next coat of dark brown stain. I was contemplating either a cherry red or oxblood stain apart from the dark brown as suggested by Steve, for the next coat. Also the present look of the stummel was equally beautiful. So there I was, at cross roads for deciding stain or no stain for the second coat. I decided to go by Steve’s suggestion as he is more experienced and as also this was to be his pipe. Here is how the pipe appeared before I applied the second coat of dark brown stain. I buffed the stummel with a horse hair shoe brush to remove any sanding dust resulting from the micromesh sanding. I applied a small quantity of “Before and After” restoration balm to rehydrate and rejuvenate the briar and set it aside for some time. Thereafter, I buffed and cleaned the stummel with a microfiber cloth. I applied a second coat of dark brown stain over the stummel and the shank extension, going through the same method as described above and set them aside for the stain to set. However, in my exuberance to cross the finish line, which by the way was now within sight, I completely missed out on taking pictures of this stage. Once the stain was set, I wiped down the stummel with a cotton swab and alcohol to remove any excess stain and lighten it from the raised rustications. Mounting a felt cloth buffing wheel on my rotary tool, I went about removing the crust formed by the stain over the raised rustication. The second coat of brown stain has added another layer of texture to the appearance of the stummel and aluminum shank extension. I like the way the stummel now appears to the eye. Now, the fear that besieged me was the stain running down Steve’s hand as he smoked the pipe and I shared this anxiety with him. He suggested that I should set the stain by again heating the stummel surface with the heat gun and this is exactly what I did. Next, I mounted a cotton cloth buffing wheel and setting the speed to ¼ of the full power, I applied a coat of carnauba wax over the stummel, aluminum shank extension and the stem. I worked the complete pipe to a beautiful and lustrous shine.I followed this wax polish by a mounting a clean cotton buffing wheel on the rotary tool and cleaned the stummel surface to remove any excess wax that had lodged itself in the rustications. The last issue that remains unaddressed is the thin chamber wall on the right side of the stummel. I had an option of either applying JB Weld or using plain bowl coating. I decided to go with the latter as, in my appreciation, this should suffice and also, in case my appreciation goes awry, I know Steve would apply JB Weld to make it functional again. Had this pipe been for anyone else, I would have applied JB Weld followed by a layer of bowl coat, just to be sure.Before re-assembling the pipe, I once again thoroughly cleaned the internals of the shank, aluminum shank extension and the stem airway with pipe cleaners and ear buds dipped in isopropyl alcohol. I also fixed the wooden gasket with superglue in to the stem end of the shank extension. I checked the draw to make sure that the airways in the shank, extension and stem are open. The draw is nice, smooth and open and somewhat similar to the draw experienced on a Peterson’s P-lip stem. I also applied a little Vaseline over the threads of the aluminum shank extension and the wood gasket to protect and keep it soft.To finish, I reassembled the complete pipe and gave it a final buff with a microfiber cloth to deepen the shine. This dude has come a long way from being on the verge of being discarded, to be my first ever attempt at rustication, to being my first gift to my Guru and mentor, Steve. I am pleased with the way this pipe has turned out and I sincerely hope that Steve likes it too. This pipe will soon be on its way to another part of the world, Vancouver, Canada to be precise, to be enjoyed and to serve my dear friend while he reminisces about his visit to me, Abha, Mudra and Pavni. I sincerely thank all the readers to have spared their valuable time in going through this long, and at times repetitive, write up. P.S. This project has been a great learning, with its fair share of frustrations and moments of euphoria, both of which are memorable to me. I enjoyed researching and understanding the working principle employed in this pipe. Any input and suggestions are always valuable to me and most appreciated as they help me grow and improve.

I Really Love the form and shape of Older C.P.F. Meerschaum Pipes


Blog by Steve Laug

Not too long ago Jeff was contacted by a fellow who we have bought pipes from in the past. He has always been a good source of pipes for us and sold us some great pipes including a few C.P.F. pipes. He wrote to say that he had a few more pipes to sell and wondered if we were interested. He said that one of them was a small cased meerschaum pipe with a Redmanol stem. The pipe had been smoked and was worn but in otherwise good condition. The case had a stamp in the cover that read Warranted Genuine Meerschaum in and oval with a star. The shank had a silver band with the C.P.F. in an oval logo over Sterling. Jeff had him send us some photos of the pipe so we could have a look at it before making an offer. I have included a collage of those photos to give a general idea of what the pipe looked like and what attracted us to it. We made a deal – need you have doubted when you saw the C.P.F. oval logo on the Sterling shank band. We had the pipes shipped to Jeff in Idaho. When it arrived Jeff unpacked the pipe and did a quick examination of the pipe before he cleaned it up. He took photos of the case and the pipe. The logo on the inside of the case shows that it is a Meerschaum and warranted as such. The Star on the case is similar to others we have seen on C.P.F. pipes. The photos of the pipe in the case show the general external condition of the bowl. Jeff took the pipe out of the case and took a photo of the exterior of the pipe from above. It shows the cake in the bowl and the wear on the rim top as well as the slight darkening on the rim.Jeff took a close up photo of the rim top and bowl to show the cake and the darkening in the meerschaum. He also took a photo of the underside of the bowl and though it is a bit out of focus it is nonetheless clear enough to show the general condition of the pipe. He took a photo of the stamping on the band showing the C.P.F. oval logo over the Sterling stamp. You can also see the chipping on the Redmanol stem next to the shank band. The alignment of the stem to the shank is perfect so that we can assume that the tenon is in very good condition.The next photos show the condition of the Redmanol stem. There is tooth chatter on both sides near the button and some chipping in the surface of the button.This afternoon I was going through one of the bags of pipes I brought back from Idaho with me on my last trip. It was the same group of pipes that had contained the unsmoked and smoked C.P.F. pipes. In the bag I found a small brown leather covered case. I had forgotten what was in it so I took it to my desk and opened it up. Inside the case was the small C.P.F. pipe that I had seen when I was visiting with Jeff. It was time for me to work on it.I took the pipe out of the case and examined it. Jeff had done his usual thorough work in cleaning up this pipe. He had reamed the bowl with a Savinelli Fitsall Pipe Knife to scrape out the cake. He scrubbed the exterior and interior with Murphy’s Oil Soap and a tooth brush to remove the grime filth on the meerschaum. He cleaned the internals with alcohol, cotton swabs and pipe cleaners until the inside was clean. The pipe looked very good and other than a little rim colouring was in excellent condition. The stem was in good shape other than the chips along the shank band and the tooth marks on the top and underside of the stem that would need to be dealt with in the restoration. I took photos of the pipe before I started my part of the restoration work. I took a close up photo of the meerschaum rim top and bowl to show the condition of the meer bowl after Jeff had cleaned it. The finish looked really good and there was only a very little colouration on the rim top. The silver band looked really good and the C.P.F. Logo and the Sterling stamp were very readable. The photos of the Redmanol/Bakelite stem show its general condition. It was very clean but had some chipping on stem at the junction of the band and the stem. There were tooth marks on both sides on button edges. The bone tenon was in very good condition and just a little darkening.The next photo shows the stamping on the left side of the band. It is clear and readable. The stamping reads as noted above. The band is stamped with the C.P.F. in an oval logo over STERLING.I have included the following information with each of the blogs on C.P.F. pipes because I always want to keep the historical context in mind as I work on these. The link to the blog follows (https://rebornpipes.com/2013/04/14/some-reflection-on-the-historical-background-on-cpf-pipes/). I quote a pertinent part of the blog below:

From my reading and research it seems to me that C.P.F. brand was discontinued sometime in the 1910-1920 range. Again, turning to Bill Feuerbach I found that he notes the following, which pins down the time frame of the discontinuation of the brand more specifically, “I have a C.P.F. Chesterfield in our office display that has a nametag from way before my time that says 1900 C.P.F. Chesterfield. It looks like most other Chesterfields you’ve seen, including the military type push stem, except this stem is horn and not vulcanite. As far as I have gathered the C.P.F. brand was phased out sometime around 1915.” Interestingly, he noted that the Chesterfield name and style was later introduced in the KB&B, Kaywoodie and Yello-Bole lines. He says that the 1924 KB&B catalog shows KB&B Chesterfields…

… From my research I believe that we can definitively assert that the C.P.F. logo stands for Colossus Pipe Factory. The brand was purchased by KB&B sometime between 1884 and 1898 and that it continued until 1915. That time frame gives help in dating some of the older C.P.F. pipes you or I might find. It can be said that prior to the dual stamping it is fairly certain that the pipe is pre-1884 to 1898. After the dual stamping it can be placed post 1898 until the closure of the brand line in 1915. C.P.F. made beautiful pipes.

From that information I can tentatively date the pipe to the period prior to 1884-1898 when KB&B bought the brand because of the single C.P.F. stamp on the band. At any rate it is another old meerschaum pipe that is lightly smoked. The story of its journey to Jeff and me this long after the date it was made is another mystery. This is another of those pipes that makes me wish that it could share its story with us. I can only imagine the journey it has had even minimally from the bits that I do know. It traveled from the Colossal Pipe Factory in New York City to Florida and then on to Idaho Falls in journey that began in the 1880s and ended in 2019. Now it is has further traveled by air to Vancouver, Canada, as far west as it can go and remain on the same continent… what a well-traveled pipe. Armed with that information it was not time to work on the pipe.

I decided to begin with the stem damage at the junction of the band and stem. There was chipping in the Redmanol/Bakelite at that point that needed attention. The first photo below shows the chipping. I built up the edge with clear super glue. At the same time I filled in the tooth marks on the button with super glue. I set the stem aside to let the glue cure. I polished the meerschaum bowl and rim top with micromesh sanding pads – wet sanding with 1500-12000 grit pads and wiping the bowl down after each pad. The bowl began to take on a real shine after each set of pads. I set the bowl aside and went to work on the stem. The repairs had cured so I sanded them with a folded piece of 220 grit sandpaper to smooth out the surface of the repairs and blend them into the stem material – Bakelite or Redmanol. I polished it with 400 grit wet dry sandpaper to smooth out the scratches and begin the polishing process.I polished the stem with micromesh sanding pads – wet sanding it with 1500-2400 grit pads and dry sanding it with 3200-12000 grit pads. I wiped it down with Obsidian Oil after each sanding pad. I gave it a final coat of Obsidian Oil after the final sanding pad and set it aside to dry. By now if you have read rebornpipes for very long you will have figured out that I love these old C.P.F. pipes. There is some serious thought that they were carved by European trained craftsman who were skilled pipemakers. These pipemakers were brought to the US by the Colossal Pipe Factory to make pipes. Many of the shapes, bands and stems have such high quality workmanship involved that I really think there is truth to this story. This is little bent Meerschaum with a Redmanol/Bakelite stem is a real beauty.

I screwed the bowl back on the base and carefully polished stem and the bowl with Blue Diamond polish on the buffing wheel carefully avoiding the stamping on the shank. I gave the stem multiple coats of carnauba wax. I hand rubbed the bowl with some beeswax. I buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The pipe polished up pretty nicely. The pipe really alive with the buffing. The rich contrasting white of the meerschaum on the bowl works well with the polished red of the stem. The finished pipe has a rich look that is quite catching. Have a look at it with the photos below. The shape, finish and flow of the pipe and stem are very well done. The dimensions are Length: 3 3/4 inches, Height: 1 1/2 inches, Outside diameter of the bowl: 1 1/4 inches, Chamber diameter: 5/8 of an inch. This is another one that I will be adding to my collection. It fits in the C.P.F. niche group that I have been building. The shape and feel in the hand is perfect. Since this one is already well smoked it will be an easy pipe to load and fire up. Thanks for walking through the restoration with me as I restored and reworked this old bent meerschaum from 1884-1898. It is always a treat for me to work on a piece of pipe history especially when I have learned a bit of the story behind it.

Restoring another Schoenleber Hand Made – A 5 Pot


Blog by Steve Laug

The next pipe in the queue is another pipe from the batch of pipes I am cleaning up for Alex – this one is another Schoenleber Hand Made – a straight shank Pot shaped pipe with some beautiful grain around the bowl and shank. The pipe does not appear to have been stained but sports the same look as the Malaga pipes that I have been working on. The carver did a great job utilizing the block of briar to maximize the grain. The pipe is stamped on the left side of the shank and reads Schoenleber over Hand Made. On the right side of the shank it is stamped Imported Briar. On the right side next to the bowl/shank junction there is a number 5 which is either a shape number or size designation. The taper stem is vulcanite and has no marking or stamping. This is another nice looking piece much like many of the pipes Alex is picking up. The bowl had a thick cake and lava flow and some darkening on the rim top. The exterior of the briar was dirty with grime and dust. The stem had deep tooth marks and chatter on both sides near the button. The stem was oxidized and there was a thick coat of calcification on the stem for the first inch ahead of the button. The photos below give a glimpse of the pipe before clean up. I took a photo of the bowl and beveled rim top to capture the condition of the pipe before I started my cleanup work. There was significant darkening on the top of the inwardly beveled rim at the back of the bowl. The bowl had a thick cake that flowed over the rim top. The inner edge appeared to have some damage but the outer edge of the bowl appeared to be in excellent condition. The stem was in rough condition with deep tooth chatter and deep tooth marks on both sides of the stem near the button and on the button. I also took a photo of the right side of the shank to show the stamping. The stamping is readable in the photo below and is as noted above – Schoenleber over Hand Made. On the opposite side it reads Imported Briar. There is also a 5 at the shank/bowl junction on the right side. When I was working on the other Schoenleber pipes in Alex’s collection I had looked up information on the brand. I am quoting that information once again on the blog for this pipe. I quote the article in full (https://pipedia.org/wiki/Schoenleber).

Louis Schoenleber lived in North Arlington N.J. and was an Austrian immigrant and skilled artisan in pipe making. His hand carved pipes were available in his shop, ‘Schoenleber’s Newark Pipe Shop’, at 26 Branford Pl., Newark NJ, thought to open in the 1920’s. Schoenleber’s carried a full line of tobaccos as well as related pipe smoking accessories. It’s thought the shop operated until the late 1960’s, and Louis Schoenleber died in 1976. It’s also fairly certain they may have sold to other brands such as Jelling, also in Newark and are very similar in design and finish.

There was also an advertising card on the site that I have included below. It speaks to my assumptions about the curing process and the finishing process on the pipe. It also connects the pipe to Schoenleber’s Newark Pipe Shop in Newark, N.J. It also has a comment on the fact that pipes were made to order.I started the restoration by reaming the bowl with a PipNet pipe reamer and took the cake back to bare briar. I sanded the interior walls with 220 grit sandpaper wrapped around a piece of dowel.I scraped the rim top with the sharp edge of a pen knife to remove the thick lava coat. I sanded the remaining lava and darkening to the rim top rim with 220 and 400 grit sandpaper. I was able to remove the darkening and smooth out the rim top. I cleaned the mortise and the airway in both the shank and the stem with alcohol, cotton swabs and pipe cleaners. I scrubbed the mortise and airway until it was very clean and the pipe cleaners and cotton swabs came out clean.I polished the bowl and rim with micromesh sanding pads – wet sanding with 1500-12000 grit pads. I wiped the bowl down with a damp cloth pad after each pad to remove the sanding debris. I worked some Before & After Restoration Balm into the surface of the briar with my fingertips to clean, enliven and protect it. I let the balm sit for a little while and then buffed with a cotton cloth to raise the shine. With the bowl finished I set it aside and turned my attention to the stem. I painted the tooth marks in the stem with a Bic lighter to try to raise the deep marks. I scraped the surface with a knife and removed the buildup of calcified spittle and oxidation. I sanded it with 220 grit sand paper and wiped down the tooth marks and chatter with a cotton swab and alcohol. I dried it off with a cotton swab. I filled in the remaining tooth marks with black super glue and set it aside to dry.Once the repairs cured, I used a needle file to file the button edge to redefine it and give it a sharp edge. I lightly filed the button top and bottom to give it a smoother definition. The filing made the sanding a bit simpler as it took the excess material down to the surface.I sanded the filed stem surface with 220 grit sandpaper to remove the filing marks on both sides of the stem. I am happy with the stem surface once that was done. I started the polishing of the surface with 400 grit wet dry sandpaper. I polished the stem with micromesh sanding pads – wet sanding it with 1500-12000 grit pads. I wiped the stem down with a damp cloth after each pad. I further polished it with Before & After Pipe Polish – both Fine and Extra Fine. I wiped it down with a coat of Obsidian Oil and set it aside to dry. With both parts of the pipe finished I put the pipe back together and polished the bowl and the stem with Blue Diamond polish on the buffing wheel. I gave the bowl and the stem multiple coats of carnauba wax. I buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The pipe polished up pretty nicely. The rich oil cured finish and the grain came alive with the buffing. The finish on the briar works well with the polished black vulcanite stem. The finished pipe is a well-proportioned, nicely grained ¼ straight Pot shaped pipe. Have a look at it with the photos below. The dimensions are Length: 5 1/2 inches, Height: 1 1/2 inches, Outside diameter of the bowl: 1 1/2 inches, Chamber diameter: 7/8 of an inch. This Schoenleber Hand Made 5 Pot will be going back to Alex soon to join his growing collection of American made pipes. Thanks for walking through the restoration with me on another of Alex’s pipes.