Tag Archives: Stem repairs

The Brief, Shining History behind an Italian Dublin and Its Easier Than Usual Refurbish


Robert M. Boughton

Copyright © Reborn Pipes and the Author except as cited

 

 

— “The Treachery of Images” (1929, also known by the translation of the message on it, from the French, “This Is Not a Pipe”), an oil on canvas painting by the great Belgian Impressionist, René Magritte (1898-1967)

 

 

INTRODUCTION

Sometimes I wonder if the D in P.A.D. shouldn’t be replaced with S for Serendipity, in the sense of being in the right place at the right time, or with still more sneaky spin, Fate with a capital F.  Then my sense returns, and I realize the musing rationale is only a symptom of the Disorder.  My most recent bout with this overwhelming inner turmoil was lost within minutes after I chanced (yeah, right) to read an informative and enthusiastic, yet brief, account of a little known but masterful creator of hand-carved Italian pipes in the 1980s and into the early ‘90s.  Thinking of an assertion in the post that claimed the brand in question is difficult to find as a sort of challenge, I clicked on eBay and searched for the name.  Indeed, only two samples popped up, as well as a nice, dark brown pipe sleeve.  Not really able to afford either pipe, or the $11 sleeve for that matter, I was nevertheless torn between both and knew I had to have one.  The source of the information that set my P.A.D. careering is an acquaintance on the Smokers Forums UK, on the Pipes page.  The gentleman’s SF handle is fishnbanjo, which I suppose indicates two things he enjoys very much other than pipes.  He and most everyone who knows him at all shortens the moniker to the simpler Banjo, which is also, after all, a kinder, gentler re-nicknaming than Fish, or even Fishn.

‘The title of the post caught my eye before I noticed it was started by Banjo: “The stepchild of Italian pipes.”  I always enjoy Banjo’s contributions because of the rugged good looks of the pipes he has a knack for acquiring and his keen knowledge of the subjects he covers, and when it comes to pipes the brands of which, most of the time, I find I have never heard but without fail would like to own.  Often spoken in pipe smoking circles is the comment, “That pipe looks good on you,” which is one of those statements that of course in intended to be courteous and friendly but, when considered in literal terms, is preposterous.  Somehow, though, with Banjo the expression is more à propos than anyone I’ve ever seen, even if only in excellent selfies.

His own looks being a cross between Spencer Tracy, who played the down-on-his-luck old Cuban fisherman in the 1958 classic movie version of Hemingway’s The Old Man and the Sea, and Anthony Quinn, who reprised the role of Santiago in a 1990 TV remake, are complemented to perfection by his good, strong, masculine, bold taste in pipes.  Here he is in an example of one of those apparent self-photos, from the Capitello post I had the good fortune to find.  The self-portrait really is quite good since I decided to contact Banjo and ask for his permission to use it in full rather than lop off the top half of his head for the silly sake of protecting his privacy without even knowing if he minded. When Caminetto Pipes (1968-1979, the official Caminetto Period) stopped production, all by hand, the assorted partners went their own ways. Giuseppe Ascorti produced Sergio pipes for a short time before forming the company bearing his own last name with his son Roberto; Luigi Radice opened Radice Pipes, and Enzo Galluzo, who was the official carver for Caminetto and had worked at Castello and later Ascorti’s shop, founded the Capitello Pipe Company with his partner on the business end, Corrado Ripamonti, c. 1982.  Capitello closed in 1991, according to Banjo “because [Galluzo’s] distributor never paid him for the pipes he sold and without money to pay the bills a great, not well-known company ended its run.”  In 1986, by the way, two years after the death of his father, Roberto Ascorti started the New Caminetto Period.

Banjo wrote, with nostalgic eloquence, of Capitello being the first Italian pipe manufacturer in the 1980s to use oil curing.  The process was patented by the Alfred Dunhill Company Ltd. on November 14, 1918, just 28 days before the signing of the Armistice – at the 11th hour of the 11th day of the 11th month – that officially ended World War I (“the War to End All Wars”).  Dunhill’s Patent №. GB119,708 involved immersing natural-finish stummels in olive oil for several weeks before drying with hot air and sandblasting away large rough parts of the early irregular results.  Whether old Alfred in fact invented the procedure is debated, but I’m not going there today, so relax.  At first the use of oil was for aesthetic reasons only, as it gave the outer area of the stummel greater luster.  Pipe collectors and scholars giving every indication of being quarrelsome when it comes to just about everything, the rough effect that seems to have led to the creation of the Shell pipes (and is also the reason for the reddish tinge to the briar in that line) is yet another subject of discord in certain rarefied circles, with an emphasis on circles being never-ending. At any rate, the unavoidable consequences of Dunhill’s approach were unusual shapes that could not be classified according to the official charts until oil curing was “perfected” some years later.

Returning to Banjo’s humble eloquence, he wrote of buying the pipe more than 30 years ago from “someone with much more experience than I who told me it would color much like a Meerschaum does.”  As would most experienced pipesters familiar with the differences of wood and meerschaum, Banjo had his doubts, but he liked the huge, pebbled specimen, so why worry about it?  I can’t help thinking and interjecting the notion that such a refreshing thought process could benefit certain more vocal experts.  To Banjo’s lasting surprise, his old pipe indeed continues to color, just like a well-aged meerschaum.  Banjo noted that today it is difficult to imagine the gorgeous piece of work in the virgin finish he first viewed it.  I suspect it looked something like this other Capitello, minus the smooth finish.

Capitello Airlecchio 773, courtesy Haddock’s Pipes

Capitello’s peculiar, more common designs and crafting include the following.

Corinzio Two Columns Sandblasted Belge, courtesy amaxwell1_eBay

Wax Drip Gotico, courtesy Pipephil

My remaining opening comments are few enough to wrap up in short order, which I will now do.  As far as the farfetched-sounding idea of smoking a wax-dipped pipe goes, see the last link in my Sources below before passing judgment.  Concerning the somewhat confusing list of Italian names – both for some of the companies mentioned and more to the point Capitello and its various lines – my curiosity got the better of me.  As a result, I discovered they have real meanings, and here they are.

  1. Capitello – capital. I sense a dual meaning here, as in the seat of power of a government, etc., as well as the monetary distinction
  2. Caminetto – literally, fireplace, but also used to describe a very hot, small space where objects are forged by craftsmen
  3. Radice – a surname that also means root
  4. Castello – castle
  5. Corinzio – Corinthian. No, not the Corinthian leather used in a certain car promoted by Ricardo Montalbán, but Corinthian architecture, the last and most ornate of the three main orders of ancient Greece and Rome that was characterized by columns. Hence, the Corinzio Two Columns Belge shown above.  I did not find Belge anywhere.
  6. Gotico – Gothic
  7. Jonico – Ionian, or pertaining to the second primary architectural order of ancient Greece and Rome

RESTORATION

The nomenclature is crisp, although I had to edit the color and brightness levels of the photos above to make the stampings clear: on the left shank, lowercase “Capitello,” in quotations with the closing mark in subscript, above JONICO, and below that, to the right, a small square with what appears to be an Ionic column matching the brand’s logo as shown in this photo of a genuine Capitello stem, courtesy of Pipephil.

The symmetry of the classic Dublin shape combined with corresponding tight, vertical grain on the bowl except for the rear, which is more mottled, and the way all of it points to the flawless large bird’s-eye of the rim, transfixed every brain cell I possess related to reason.  My power to resist, at $26.99 with about two days of bidding left and only three other buyers interested, turned to mush like a clay or meerschaum pipe after being retorted with Everclear.   I’m happy to say I never made that mistake but have heard pained accounts from more than one friend who has, none of them more than once.  Thus, I bid $100 on the pipe, thinking that if the bidding inched up $1 at a time I would be safe.  Foolhardy but true!  Not another bid was made.

Scrutinizing each of the plentiful photos taken well and from every angle, except for the color that was a little darker, the only flaw I detected was the worse than average looking but single rim burn.  The description noted the inclusion of a replacement stem which, in my excitement, I must admit I did not notice was left only halfway turned into the shank in the photos.  I should have expected something was up with that. 

The pipe arrived from Daytona Beach, Florida only two days after shipping despite Irma’s devastation that left 80%+ of the power in that area off the grid.  I inspected the pipe, and almost all of it looked very good.  I love the olive wood ferrule.  I tried to tighten the stem.  No-go.  Less than halfway, the Ebonite screeched.  Halfway, I stopped with the certainty the tenon would break if I were to continue.

Now, adjusting the tenon circumference took only a few minutes before it fit as though hand-crafted for the Jonico.  I should add that the stem was straight and needed a gentle curve, as well as removal of slight, almost imperceptible rough edges along the sides, left-over signs of the machines that stamped them in groups.

But the end of the shank was rounded, which I had seen with a few new and restored estate pipes I bought over the years.  I just hadn’t ever given much attention to the stem fittings on these pipes.  My first impulse, therefore, was to order a stem that was the correct diameter for the shank, specifically an army mount, but then I thought, “Why wait?”  Scanning through my photos of various such pipes, I noticed that the one common trait of the stems used is that they look good on the given pipes.  That being true enough for now with mine, and its destination being my shelf, I proceeded to the required stem work until the army mount stem arrives.

I started with feather-light, focused sanding using 400-grit paper followed by micro-meshing from 1500-12000.  This stem was so shiny when I unwrapped it with the pipe that the first sight of it made me fear it might be plastic and hope it would turn out to be acrylic.  The distinct odor of burned rubber and Sulphur that rose to my nose upon sanding cleared that up.   Having already pre-heated the oven to 220° F., I slipped a regular cleaner through the stem’s airhole and placed the whole thing on a small sheet of aluminum foil.After 15 minutes in the cooker, the stem was pliant.  I used the complex tool in the following shot to accomplish most of the task that called for the slightest curve of almost nothing but the mouthpiece.  I returned the stem, already somewhat cooled, to the oven for a few more minutes and made the final, tiny bend by hand, with a cooking mitten and rag of course.  Then I ran cold water from the tap over it and removed the cleaner. As I mentioned earlier, the burn on the rim in the eBay photos worried me, and my un-ease grew when I had my first Close Encounter of the Third Kind.  The concern wasn’t whether I could fix it but how far I would need to go to do so.  The reason was the depth of the affected areas, from the rim scorch that was isolated to one spot but crept into the chamber and ate away at the top of the inner wall most of the way around the top right side.  By no means was this even close to bad as I have come to understand the word in terms of pipe rim repair, but I did not want to alter the uniform, hearty thickness of the wall any more than could be avoided.  With this pipe, re-sizing the rim with a file was like to sacrilege, yet the idea did cross my mind in a sinful flash before I rejected it at the thought of eliminating any significant fraction of a millimeter of the wonderful bird’s-eye.  Have a closer gander at the unfortunate but far less egregious degradation to the inner right rim this beautiful Dublin withstood.I began the only aspect of the refurbish that could be called any kind of challenge with the gentlest approach, purified water and a soft cotton cloth over the entire stummel.  While a fair amount of soot, skin oil and whatnot came off, no amount of scrubbing made a dent, as it were, on the blemish.  Fine grades of sand paper had no effect, either, and so, I worked my way down the numbers and up the grits to my two-in-one sanding sponge, half 180 and the other 150.  Focusing on the deep rim burn spot, I went at it with the 150.  My hand a blur and breaking out in a sweat all over, the removal of the single little spot took closer to 10 than five minutes.  But I’ll be a turkey’s behind if the dang thang didn’t disappear on me!  I reversed the harsh effects of the 150-grit sponge, minimal as they were because they only rid the fine Mediterranean briar of something that had no place pocking it, with 220- and 400-grit paper before the full scale of micro-mesh pads.  While I was in the groove with the micro-mesh, I did the whole stummel.  I remember coming across one scratch big enough to warrant 320-grit sandpaper, but to save my life I can’t remember where it was, and now it’s gone.  Oh, well.  C’est la vie!

Happy with the absence of the nasty, pernicious burn mark, I found an old, small favorite piece of 150-grit paper that’s perfect for pipe chambers and, focusing again, only on the upper circle inside the chamber, succeeded in eliminating the unwanted beginning of a groove caused by what I can only imagine was a drunken fit of excessive lighting (as in the previous owner passing out while flicking his Zippo and only coming to when he burned his thumb).  I followed the 150-grit strip with the 220- and 400-grits again, and after much careful tapping and blowing of soot and wiping the chamber clean with a piece of paper towel and alcohol, I saw that the damage was repaired, and the chamber was down to bright, clean briar as far as I had gone.  Repeating the process in steady advances down the chamber, 30 or so minutes more passed before the entire inside of the chamber was down to the wood. The end of this special restoration nigh, the time had come to re-stain the rim that had lost more than a little of its fine darker color.  I rejected the notion of making the Capitello Jonico Dublin a two-tone, which is one of my favorite habits with many pipes, and chose instead to apply a couple of Qwik-Koats of Lincoln Brown Boot Dye, alcohol-based.  You know I had my Bic handy to flick, but at least I was sober, safe and sane.Taking off the charred stain and returning the rim color to the original shiny dark brown was simple with 1800 followed by 4000-12000 micro-mesh.

As a general rule, I don’t leave the cleaning and retorting of a pipe’s insides until just before the last step, but this time I became so wrapped up in the stem bending, burn removing and, for the first time, eliminating all but the ghost of the original owner’s tobacco char that I just forgot until the mental checklist time arrived.  Whomever the previous owner was loved this pipe despite the one misadventurous rim burn incident.  I can tell, because I only needed six regular cleaners half-soaked in alcohol with the dry ends to follow up each run through the shank before the last came out clean both sides.  Also, the retort was fast and easy with only three Pyrex test tubes of alcohol boiled through the pipe.

Strolling from the living room to the “workshop” (my bedroom still, for now, but next month or November at the latest I’ll start paying an old-time rent control-level extra charge for the spare third bedroom in the house and begin assembling the proper tools for this work), I plugged in the electric buffer.  Before that, I asked the cats to leave, which they did because for some reason they don’t like the noise of the machine.  I closed the door and freshened the brown Tripoli wheel I’ve been using to give more luster to the wood, made sure there were no papers or other light objects that might blow away nearby, and turned on the juice.  The whir of a wood buffing wheel is one of the happiest sounds I know.  Lightly turning the wooden stummel with confident firmness over the spinning cloth buffer is likewise one of the finest feelings, because of the completion it brings to another project.

The brown Tripoli buffing finished, I wrapped a clean cotton cloth around the wood and, with both hands, worked the excess compound and a couple of streaks, part of it deeper into the stummel and the rest onto the cloth.  I’ve been doing this lately instead of the alternative clean buffing wheel method, and it works just as well.  Then I repeated the process with a coat of Carnauba wax, and after rubbing it with another cotton cloth gave it one more roll on the Carnauba wheel before the final rub-down.  I buffed the stem with a single coat of Carnauba and rubbed it smooth of excess wax.  For now, it is aligned with the shank as close to an army mount as I could approximate with a regular narrow tapered stem.

CONCLUSION

René Magritte had a brilliant, often hilarious imagination fueled by his wild, wicked (as my generation used it to mean “awesome” or “totally [rad]”) sense of humor, even if he apparently didn’t smoke a pipe – or anything else.  Take a close look at this photo of him as a young man, cribbed from Pinterest, and you’ll see the cigarette in his mouth appears to be backward, if it’s a cigarette at all and not a pencil.  If I had to guess, and I do, I would say he appreciated the beauty of everything in life as he saw it.  Pipes being a big part of culture during Magritte’s too-short time in this world before he moved on to the Totally Surreal Higher Place, my take on the painting I used as an atypical opening quote is that it is at the very least double-edged: the artist’s rendering of a pipe in a piece of art does not make it a pipe, and the conspicuously bland billiard he chose to create with paint and paper, without doubt using the greatest consideration of the multitude of options available to his ingenious mind, is something one might find on a basic pipe chart if they were as well illustrated as this work.  That is why I chose the subtle example of the surreal to open this blog.  Look at any pipe made by Capitello, and if you speak French, you would exclaim, “C’est une pipe [That’s a pipe]!”

SOURCES

http://www.pipephil.eu/logos/en/logo-c2.html
https://dutchpipesmoker.wordpress.com/tag/oil-curing/
https://patentscope.wipo.int/search/en/result.jsf
http://loringpage.com/pipearticles/First%20Shell.htm
https://pipedia.org/wiki/Dunhill
http://www.pipephil.eu/logos/en/infos/wax-drip-pipes.html

Restoring a Georg Jensen Royal Navy Hand Made 93 Bent Apple


Blog by Steve Laug

The photos of this Georg Jensen bent apple made the pipe look pretty good. The sandblast finish look pretty good and the stain is mottled but look like it may have been intended to look that way. The bowl had a cake but not too thick and the lava overflow on the rim top appeared average and not much work. The stem was lightly oxidized with most of the oxidation occurring around the button. There was the characteristic GJ stamp on the left side of the stem. It looked like the stem had worn one of the rubber bite guards as the sludge that usually accompanies the removal of those was on the stem. There was tooth chatter on both sides of the stem and a deeper tooth dent on the underside near the button. The pipe was stamped Royal Navy over Hand Made in Denmark with the shape number 93 on a flat smooth band on the underside of the shank. There was a black and brass band on the shank end. My brother took photos before he did his cleanup work on the pipe. The next two close up photos of the rim and bowl show the general condition of the pipe. You can see the buildup of tar on the rim filling in the details of the sandblast. You can also see the damage to the outer edge of the rim where it had been banged out against a hard surface.Jeff took some close up photos of the sides and bottom of the bowl to show the condition of the finish. It was dirty and spotty. It appeared to be a heavy plasticized finish on top of the stain coat. There were some dark spots on the front and bottom of the bowl.Jeff also took photos of the stamping on the underside of the shank and the stamping on the left side of the stem.The next two photos show the condition of the stem. The first one shows tooth chatter and wear on the button face as well as the top side of the stem. The second one shows a deep tooth mark on the underside against the button. There is also a deep mark on the sharp edge of the button next to the tooth dent.This Georg Jensen Hand Made Royal Navy 93 came to me clean and ready to restore. Jeff had reamed the bowl with a PipNet pipe reamer and cleaned it up with a Savinelli Fitsall Pipe Knife. He scrubbed out the 9mm filter mortise and the airways in the shank and filter holder in the stem with alcohol, cotton swabs and pipe cleaners. He scrubbed the bowl and rim top with a tooth brush and Murphy’s Oil Soap. He rinsed it with running water to remove the grime and the soap. He soaked the stem in an OxyClean bath to remove the oxidation. I took photos of the pipe before I started restoring it. One of the most frustrating things for me in pipe restoration is bowls that have been coated with a thick coat of some kind of plastic finish. That is what was covering the briar on this Jensen. The brass band with two black rings on the shank added a nice touch but I could hardly see if for the shiny plastic coat over the surface of the briar. I took a close up photo of the rim top and bowl after the cleanup Jeff had done. He did a great job removing the debris from the rim top it was clean and the sandblast finish was visible.The oxidation on the stem was mostly at the end near the button. The photos show the tooth mark on the underside very clearly.I took the stem off the shank and the band fell free of the shank end. It would need to be reglued and held in place until it dried.I dropped the bowl in an alcohol bath to soak. I was hoping that the alcohol would soften the topcoat on the bowl and let me work over the finish. I was not sure it would but it was worth a try. I left it to soak and addressed the stem.I sanded the stem with 220 grit sandpaper to remove the oxidation and the tooth chatter on the surface of the stem. The dent on the underside of the stem was deep enough that I wanted to see if I could heat the dent to raise it. I used a Bic lighter to paint the surface of the stem with the flame. The heat raised the dent to the surface. I polished the stem with micromesh sanding pads – wet sanding it with 1500-2400 grit pads. After the first set of three pads I used some Rub’n Buff European Gold to fill in the GJ stamp on the side of the stem. I applied it with a cotton pad and rubbed off the excess. Once it dried I used the 3200-12000 grit pads to dry sand the stem. After each micromesh sanding pad I rubbed the stem down with Obsidian Oil to enliven the vulcanite. After the 12000 grit pad I set the stem aside to dry. I took the stummel out of the alcohol bath and used a brass bristle wire brush to break down the plastic coat on the briar. I worked at it until the surface of the bowl was dull and lifeless. I wiped it down with acetone and a cotton pad and repeated the process until I had removed the majority of the plastic coat.  I put some all-purpose glue on the end of the shank and spread it around the perimeter of the inset made for the band. I pressed the band in place on the shank end and wiped away the excess glue. It did not take too long for the glue to set and the band to be solidly in place on the shank.Now it was time to address the lighter areas on the front and the back of the bowl. I decided to use a black Sharpie Pen to colour in the low spots on the grain in between the ridges. I ran the pen across the flow of the sandblast to highlight these spots on the rim and the back and the front of the bowl. It would be a nice contrast with the rich chocolate brown stain that was on the bowl.I buffed the bowl with Blue Diamond on the buffing wheel to blend in the black of the pen and the chocolate brown of the rest of the bowl. I took the following photos to show how well it blended into the finish. I put the stem back on the bowl and buffed the entire pipe with Blue Diamond once again. I gave the bowl multiple coats of Conservator’s Wax and the stem multiple coats of carnauba. I buffed the pipe with a clean buffing pad to raise the shine. I hand buffed the pipe with a microfibre cloth to deepen the shine. The photos below show the finished pipe. The reflection of the polished brass band on the black of the vulcanite stem looks really good. The contrast of the blacks and browns in sandblast finish are really quite stunning. The dimensions of this pipe are Length: 6 inches, Height: 1 ¾ inches, Bowl diameter: 1 ¼ inches at the top of the rim, Chamber diameter: 7/8 inches. It a great looking pipe and one that will make a good smoker. It is drilled for a 9mm filter but can easily be used without one or a converter can be purchased from various online sources to slide into the 9mm tenon and change it into a regular pipe. If you are interested in this pipe send me an email to slaug@uniserve.com or a message on Facebook. I will be putting it on the rebornpipes store later today. Thanks for looking.

One Seriously Frustrating Refurb – a Broken Down Hilson Fantasia 206 Dublin


Blog by Steve Laug

The last of Steve’s pipes the remained for me to work on was a Hilson Fantasia. It is a Dublin shaped pipe made of resin with a meerschaum insert. It has a yellow coloured bowl and shank with swirls of green that are scattered throughout the pipe. When Steve sent me the box of pipes to work on I told him this one was not worth the effort to clean it up. It was in really rough shape on both the stem and the bowl insert. But in the end I decided to clean it and the Pipe just so he could see what these resin bowl pipes were like. I have cleaned a few of these up over the years that have almost psychedelic patterns in the resin. They are really a product of the 60s and 70s in my opinion. I took the following photos of the pipe before I started the clean up to show the general condition and give you some idea why I said the pipe was not worth cleaning up. The pipe really was in rough condition. The meerschaum bowl was not readily identifiable and there was major damage to the rim top. There chunks of the inner bowl missing from the top at the back edge of the bowl. There was a seriously thick cake in the bowl that was fuzzy with dust and debris. The outer resin bowl was covered with a layer of lava. The stem would not fit in the shank the way it was supposed to which signaled that the shank was cake with about as much debris and the bowl. The stem was oxidized and there were tooth marks on both the top and the underside at the button. The button itself was worn away and no longer clearly defined. The outer resin bowl was in pretty good shape with no deep scratches or gouges. I was hoping that once I reamed the bowl it would be intact lower down. I was basing that hope on the fact that Hilson used block meerschaum and not pressed meerschaum for their bowls. That made the quality of the lining far better and I have rarely seen a Hilson meerschaum lining cracked or broken.The next two photos show the stamping on the pipe. On the underside of the shank it is stamped Belgium and on the right side it is stamped with the shape number 206. The normal stamping on the stem was long gone. So it no longer read Hilson Fantasia. For the identity I am going with the stamping that is visible, the shape and material of the pipe for calling it a Hilson Fantasia.The photos of the stem show the condition of the oxidation and tooth marks on the surface as well as the worn condition of the button.I had previously researched the Hilson Fantasia for a blog I already did on a previous restoration. (https://rebornpipes.com/2016/07/05/is-it-really-a-plastic-smoking-pipe-what-is-a-hilson-fantasia/) On that blog I wrote of what I had found out about the brand. I had learned that the Hilson Fantasia was made in Belgium as this one was stamped. It originally came out as a meerschaum lined pipe with an outer bowl made of a new material that they called pipenite. From what I can find out about the material they call pipenite, it was a specially designed polyester resin. It was light weight and fairly indestructible. The block meerschaum insert was something that Hilson turned into a specialty. I had found a catalogue page on Chris’ Pipe pages, http://pipepages.com/hilson.htm that confirmed my guess regarding the 60s/70s look of the pipe. I have once again included a catalogue page from a 1962 Wally Frank Catalogue that was on the pipepages site. The write up on the Hilson Fantasia is entertaining to read in terms of the sales pitch that is delivered.I have also written about some of the history of the brand on a previous blog on Hilson Double Ecume pipes. If you are interested in reading about the history of the brand click on the following link: https://wordpress.com/post/rebornpipes.com/40547. In addition the following link on the Estervals Pipe House website gives a good summary of the history of the brand for those of you who want to read more: http://www.tecon-gmbh.de/info_pages.php?pages_id=70.

Now for the cleanup of the Fantasia! I carefully reamed the bowl with the smallest cutting head of the PipNet pipe reamer and cleaned up the inside of the bowl with a Savinelli Fitsall Pipe knife. I say carefully because I did not want to damage the meerschaum insert in the bowl but I wanted to remove the rock hard cake in the bowl.I topped the bowl carefully using a medium and a fine grit sanding pad. I wanted to smooth out the surface of the rim and remove the lava that was on top. I wanted to remove the lip of lava that had formed on the top of the bowl. The second photo below shows the cleaned rim top and also the damage that was very evident at the back edge of the bowl and around the sides. I cleaned out the shank of the pipe with a thin pen knife to scrape away the hardened tars that lined the inside walls. I followed that with a sanding stick and many pipe cleaners, cotton swabs and alcohol before the shank was clean.The inner edge of the bowl was pitted and uneven so I sanded it with a piece of 220 grit sandpaper to smooth it out and to clean up the damaged area at the back of the bowl. It was not perfect but it looked better than when I started.I took the stem out of the Before & After Pipe Stem Deoxidizer and wiped it down with a cotton pad. I cleaned out the inside of the stem with pipe cleaners and alcohol to remove the left over deoxidizer. The photos below show that it removed most of the oxidation but there were some stubborn spots left. The tooth dents are also very clear in the next photos of the stem. I wiped the stem down with alcohol and filled in the dents with a black super glue. I set the stem aside to let the repairs cure. When the glue had cured I worked on the fit of the stem in the shank. The tenon was still too big for the stem to sit properly in the shank so I sanded it down with 220 grit sandpaper. There were some high spots on the tenon that needed to be rounded out and cleaned up. Once that was completed the stem fit perfectly.Once the fit of the stem was correct, I turned to work on the stem itself. I wanted to blend the patched areas into the surface of the stem and also recut and redefine the button with needle files. I used a knife-edge needle file to redefine the sharp edge of the button and give it form. I also used it to flatten out the repaired areas on both sides of the stem.I smoothed out the repairs with 220 grit sandpaper and worked to blend them into the surface of the stem. I was a little concerned in that the repairs seemed to look almost red against the surface of the still oxidized vulcanite. I would have to work that to see if I could blend it in more. At worse the repairs will show but the pipe will be smokable.Now the frustration heightened – I really should have listened to my initial thoughts on this pipe. It was not worth working on. But I did not listen and now one of the reasons became more apparent. I polished the stem with micromesh sanding pads. The more I polished them the more the two repaired spots on the top of the stem showed a red colour. I have never had that happen before. I cleaned the stems before patching them with alcohol and dried them off. I used black super glue for the repairs, like I have many times before. Yet this time the repairs show a red tint. I have no idea what is going on with this repair. Fortunately it is one that I am calling finished. It was just a quick clean up on a badly damaged pipe. The stem is functionally very good just those spots are irritating. I used micromesh sanding pads to polish the stem – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I rubbed the stem down with Obsidian Oil after each pad and set it aside to dry after the 12000 grit pad. I was irritated with the way the pipe looked – both bowl and stem. They were ragged looking still and even though they were better they were not what I like to see in a finished pipe. I was finished though as I decided that more work would not improve the damaged pipe. I buffed the bowl and stem with Blue Diamond on the buffing wheel. I hoped that the buffing might blend the repairs into the surface of the stem. While they certainly looked better they still showed. The overall look of the pipe was much better than when I started. The damage to the back side top edge of the meerschaum bowl liner was significant but the pipe was still able to be smoked. It was clean and would certainly make a workable yard pipe. I have boxed the pipe with the rest of Steve’s pipes and have them packed and ready to send to Dawson Creek. I am hoping he enjoys the lot and gives them a good workout in the days ahead. Thanks for looking.

 

Cleaning up a sad “the Pipe” Billiard


Blog by Steve Laug

I have hinted at the fact that my friend Steve from Dawson Creek included two pipes in his box of pipes for me to refurbish that I had relegated to a “not worth doing” category. One of these was a Hilson Fantasia – Resin bowl and shank with a meerschaum lining and a plastic pipe stamped “the Pipe” that has a pyrolytic graphite bowl lining and a phenolic resin exterior. When I was working on the last one, the Kriswill made Danish Crown pipe I thought I would just do a clean up on these two just to be able to send a clean batch of pipes back to Steve.

I decided to begin working on the pipe labeled “the Pipe”. I have never paid attention to these pipes and have actually never had one in hand until this moment. I have avoided buying them or even being gifted one of them. I just was not interested in this combination of phenolic resin and pyrolytic graphite at all. I am generally intrigued by the unusual as those of you who follow the blog know, but this one had no draw for me. It was a bit of a mess. The bowl had a crumbling cake that was uneven. It had flowed over the rim top leaving it a mess. The outer edge of the bowl had been knocked against hard surfaces to empty the bowl leaving behind characteristic dents and chips. The right side of the bowl and the entire shank was scratched with deep scratches that carried on up the stem. The top and underside of the stem was also covered with bite marks and tooth chatter. The pipe looked pretty sad with all of the damage. I wondered if I could make it look any better and to be honest, if there was a point to doing so.

I took photos of the pipe before I started for comparison sake. Once I was finished I could look back and see if my work had made any difference at all. I wanted to get a quick education regarding the manufacture and date of this brand of pipes. My gut feel was that it was a product of the 60s and 70s. I looked up the brand on Pipedia and found that it began in 1963. There was a good summary of the history of the brand there. The Super-Temp Corporation who started making plastic pipes with pyrolytic graphite bowl liners made it. They called them “the Pipe”. In 1965, Super-Temp contracted to market their unique pipes through Venturi, Inc., the company that sold Tar Gard cigarette filters. Colors and stripes were added to the pipes that were offered circa 1967. About 1970, THE SMOKE pipes were added to the line – they were non-traditional shapes with a less expensive bowl liner. Venturi pipes were added around 1972 – they had no liner in the bowls at all. The pipes were out of production by 1975 (https://pipedia.org/wiki/Super-Temp). If you would like to read more about the brand, including a comprehensive history visit Dr. Billie W. Taylor’s site http://www.thepipe.info/. He is a collector of the Super-Temp Corporation pipes. He is a source of incredible information if you want to tap into it.

I took a close up photo of the bowl and the rim top to show the condition of both. The cake is heavy in the bowl and overflowing onto the black rim. It is hard to see because both the bowl insert and the exterior of the pipe are black. You can also see the damage on the outer edges of the bowl.The stem damage was one of the most worrisome parts of this restoration. The scratches running both the length of the stem and across the stem had left deep marks. Underneath and on top of those scratches there was a lot of small tooth marks and chatter that would need to be sanded out. The scratches extended up the top side and partly up both the right and left side of the shank. There were even scratches on the right side of the bowl. It was almost as if the pipe had road rash from being dragged across concrete or asphalt. The stem was not vulcanite so it would be hard to polish. It was going to be an interesting part of the work on this pipe. The stamping on the left side of the shank was very clear and readable. It was deeply embossed and no amount of sanding to remove the scratching would damage it. The stem was held snug in the shank by a rubber grommet that fit over the tenon. This was replaceable as the rubber wore out and air leaked by. I reamed the bowl with a PipNet pipe reamer and carefully took the cake back to the graphite bowl insert. I left a little cake to protect the insert and cleaned it up with a Savinelli Fitsall Pipe Knife. Using the knife I scraped the bowl back to bare walls and scraped the rim top free of the buildup of lava that was there.I scraped the top of the bowl with the edges of the Savinelli Fitsall Knife to remove the lava build up. Once I had the majority of it off I polished the rim with 1500 grit micromesh sanding pads to polish both the bowl insert and the rim top. I sanded the outer edges of the bowl to smooth out the damage to the edge of the bowl.I polished the entire bowl with 1500-2400 grit micromesh sanding pads. I wiped the bowl down after each pad using a damp cotton pad. I worked on the left side of the bowl and the top and left side of the shank where there were a lot of deep scratches running both vertically and horizontally on both. I polished the shank and bowl with 3200-12000 grit pads. I wiped it down after each pad with the damp cotton pad. When I finished with the 12000 grit pad I buffed the bowl on the buffing wheel using Blue Diamond to polish it further. The photos below tell the story. With the bowl finished for now, I turned to work on the horrendous damage to the stem. It was in rough shape as was seen in the above photos. I sanded the surface of the stem with 220 grit sandpaper to remove the scratches. It took a lot of sanding but I was able to remove almost all of them on the top and underside of the stem. I ran a pipe cleaner through the stem to clean out any debris that might have been in the airway before continuing on the stem. I used black super glue to fill in the small tooth marks on the top and underside of the stem at the button. I sanded the repaired areas with 220 grit sandpaper until the repairs blended into the surface of the stem. I polished the stem with micromesh sanding pads – wet sanding it with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I rubbed the stem down with Obsidian Oil after each pad. After the final 12000 grit pad I gave it a last coat of the Obsidian Oil and set it aside to dry. I had already spent quite a few hours working over the badly gouged and scratched stem and I was able to remove many of the scratches. I tried to lightly buff the pipe to remove more of them but the nylon stem resists buffing too much as it heats quickly and melts. I decided to call the pipe finished at this point. It was not going to get much better without many more hours of work that I am unable to give it. I buffed the bowl on the buffing wheel with Blue Diamond to buff out some more of the scratches on the shank and right side. I gave the bowl a buff with a clean buffing pad. I polished the stem with Before & After Pipe Polish – both fine and extra fine. I did not bother giving the stem a carnauba coat as it is plastic and the wax does not do much. I hand waxed the stem with Conservator’s Wax to polish it more. The finished pipe is far from perfect but it is better than when I started. I will box it up later this week when I finish the Hilson Fantasia I have left and then mail it back to Steve in Dawson Creek, BC. Thanks for looking.

 

On Bending and Straightening Amber Stone Stems


Blog by Robert M. Boughton

Copyright © Reborn Pipes and the Author except as cited

No amount of experimentation can ever prove me right.  A single experiment can prove me wrong.

— Albert Einstein (1879-1955), German-born theoretical physicist and winner of the 1921 Nobel Prize for his discovery of the law of the photoelectric effect, received in 1922 (don’t ask why – the answer in some ways is more complex than Relativity)

THE POWER OF PERSUASION

This is the most difficult pipe restoration blog I’ve ever written, for the things about which it is not.  It is not about an antique gold-banded KB&B Blue Line Bakelite, c. 1910-1914.  A friend of mine won that distinguished, classic shaped pipe from the pre-Kaywoodie era for a very low price on eBay, and I offered, for a small fee, to restore it.  It is not about the still older gold band CPF Best Make turned lion’s head meerschaum, c. 1898, that only lacked a bone tenon to be complete.  As much as I dislike the cliché, I poured my heart and soul into that pipe since 2013 in a true labor of love to return the 19th century treasure to its original structural form.  The simple act of restoration was – and remains – intended as a tribute to the man most of the readers here know as my good friend and mentor, Chuck Richards, who gave it to me.

It is not about either of these things, or the writing between the lines as it were, but some choice details are relevant.  For example, the connection between the two pipes named above is their stems.  The Blue Line’s is Bakelite, the world’s first synthetic plastic, which could be colored dark brownish red.  The Best Make’s genuine dark red amber stem comes from wholly organic-based resins from exotic, extinct trees that were washed away by large bodies of water and fossilized into mineral form 10-100 million years ago.

The focal point of this blog is the immediate but temporary solution to a series of events that still has not been resolved.  Never in my wildest apprehensions, during the last several years of taking some truly ruined pipes and making them whole again, did I conceive that something seeming to be simple could become so bloody banjacked , as the Irish might put it with good cause.  At first, I intended to include the details as usual, in a single account of the finished project.  And so, with a little help from a friend, I adapted my thinking, draft after draft, to write this aspect of the overall restoration into a single blog.  To be brief, here is what happened.

My friend (the one who owns the Blueline, Daryl Loomis), holds the status of co-top buyer of my pipes, numbering five so far, with someone else who came and went in short order.  Daryl also let me restore one of his own pipes before, a gorgeous Redmanol Socket system pipe related to this one by its maker, KB&B, and the Redmanol of its construction that was consumed by the General Bakelite Co. in 1922.  Thereafter, Redmanol was classed as Bakelite despite certain superior qualities.  For extensive details on Bakelite’s origins and development, see the fourth link in my Sources.

At any rate, without going into details that will be covered in my eventual blog on the full restoration of the Blueline, there was a mishap – oh, the understatement! – wherein the bone tenon was crushed.  The photo below was taken after I Super Glued the bits and pieces of the shank end of the tenon, minus the powdered remains, as best I could.This catastrophe was followed close on its heels by a second calamity that left the Bakelite stem ruined, as far as I am concerned., other than for use with some unforeseeable shop pipe.  There is no way I will place a stem I broke, or anyone else did for that matter, on a paid restoration, even though, for obvious reasons, I’m refunding the small fee.  And so, with the immediate goal being to return the Blueline in a condition that it can be smoked as soon as possible, I am left with no alternative than using the genuine cherry red amber stem from my Best Make pending the acquisition of a Bakelite replacement.  Here is the Bakelite stem after I was done with it, in the negative sense of the expression.

Top view Bakelite stem

Bottom of Bakelite stem, broken

Open end with both sides of the break shown on either side

Steve wrote an excellent blog called “What Is the Amber Used in Pipe Stems and How Do You Bend It?” in 2013, but had never tried the theoretical guidelines proposed.  He still has not had occasion to attempt the unusual process.  In other words, it occurred to me, I would be the guinea pig to test the theories.  The prospect was not appealing given the potential for destroying my 119-year-old amber stem for the sake of “progress” in this obscure field of pipe restoration.  Steve’s blog is a trove of information about amber in general and the article from Scientific American on how amber stems were once custom-crafted and bent per the specifications needed for a specific pipe.  Steve raised some good questions in his fine blog that can be read at the third link below.

ABOUT BENDING AMBER

Having spent a great deal of time pouring over every word of Steve’s piece as it related to bending amber, from the viewpoint of having an immediate job to do so, I was left with still more troubling questions.  The key concerns were:

  1. Since amber stems were made and shaped for specific pipes, could they be re-bent later for replacements on other pipes? After all, bending a stem once is one thing, while bending it back is another.
  2. If so, what might be the effect of age, which tends to make amber more brittle, on a stem?
  3. Was my hope that the answers to the first two questions just that, wishful thinking, or put more plainly, a crock?

WARNING AND DISCLAIMER: The method I am about to describe, although it worked beyond my wildest dream, does not follow the better, safer steps set forth in the article upon which Steve’s blog is based.  Read his blog and, if you already possess or have the means to acquire the equipment described, or the wherewithal to fashion your own versions, please do so.  Also follow the other procedures described.  I am taking responsibility for my own mistake(s) that made this drastic measure necessary but will not be responsible for anyone else’s misfortunes!

Having abandoned myself to the certainty that my efforts would either turn out well or the whole thing would go awry in the most hideous way, I didn’t bother re-visiting Steve’s blog when I reached the desperate state of mind necessary to go through with the “experiment.”  Instead, I winged it.  The following pic shows my beloved 1898 amber stem not only in the bent form in which it was hand-fashioned by some unknown but master CPF meerschaum crafter late in the century before the one preceding the current, but as I still feared would be the last time I saw it in any recognizable form.OK, here’s what I did.  Pre-heating the oven, instead of the 210° or 220° F. temperature I’ve always used for regular stems, on a whim, if you will (since I was throwing everything else to the wind), I cranked it up to 335°.  Steve’s blog states that the process does not even involve an oven and the softening temperature of amber is about 150° C. ((302° F.). I just now confirmed that he was, no surprise, correct.

Therefore, 335° F., or 168° C., was a little high.  Placing the stem on a piece of aluminum foil, I forgot to put anything through the airway to prevent more than likely collapse until about a minute after I closed the oven door on it. 

Snapping to my terrible lapse of memory, I grabbed a regular pipe cleaner and bolted to the oven, where I found the stem very hot already but the airway still intact, and inserted the cleaner through it.

I also checked after only 10 minutes more (thank God), and found the amber stem had straightened itself!  Not only that, but when I touched the stem on the piece of aluminum, it had a bizarre limpness to it.  My heart was racing as I removed the aluminum foil with the stem from the oven and placed it on the counter.  Picking up the stem with care using both hands on either end of the cleaner, I saw the middle sag downward with gravity.

Sure for a few seconds that I would become ill and have to rush to the sink to vomit, I got a hold of myself and moved my hands to both ends of the stem, at which time I found it was so soft it reminded me of the hilarious old cartoons with Bugs Bunny or whatever Toon character flopping a broken arm about like a cooked noodle.  Of course, I didn’t play with the stem, but rushed it to the aforementioned sink and ran cold water over the whole thing until it was firm again and cool.The cleaner came out with no resistance.  Needless to say, I sighed in relief and wiped the sweat from my brow.  The experiment was a success!

Bakelite above, amber below. I know the bone tenon is backward!

And the amber stem with the KB&B Blueline stummel that’s ready for the temporary amber substitute as soon as I have a suitable new tenon.

CONCLUSION

In my most recent, exultant email to Steve, I wrote: “As the attached pics show, I finally got the gumption to go for it, and believe it or not it was the easiest bending material I’ve ever worked with.  Lucite was a dog when I re-stemmed the BW Preben Holm, but 10 minutes in the oven and the amber not only straightened itself but was like Gumby to the touch — no, like a children’s cartoon of someone with a broken arm!”  I attached a couple of photos.

His immediate, doubtful reply told me I was correct in my assumption that Steve didn’t really know what would happen, either.  He wrote, with apparent doubt, “Was the stem a true amber stem or is it the Bakelite one that you sent pictures of?”

I responded that the stem I baked was without doubt amber, then sent this added comment: “PS: I decided to crank the temp up to 335, also, on a hunch.  It may

have been reckless, but it worked perfectly.  I’m planning on writing the process up in my blog on the Blueline.”

Steve wrote back the following words a short time later, and I appreciate them very much, although I don’t know for sure that I “discovered” the process, other than my own oven method.  “Thanks for experimenting, Robert.  That is an incredible discovery.  Do a separate write up on just the bending of amber.  I think that alone will be a must read for those of us who love to restore old pipes.  Thank you for being reckless.”

Until then, I didn’t understand just how risky this little exercise in stem repair was.  But Steve’s power of persuasion being formidable, I took his advice for the blog.

I found the following quote, from a September 1924 Time magazine write-up on Bakelite, amusing in its revelation of the fantastic and egotistic personality of Bakelite’s founder, Leo H. Baekeland, not to mention the influence his company’s PR department must have had in its writing.

“From the time that a man brushes his teeth in the morning with a Bakelite-handled brush, until the moment when he removes his last cigarette from a Bakelite holder, extinguishes it in a Bakelite ashtray, and falls back upon a Bakelite bed, all that he touches, sees, uses, will be made of this material of a thousand purposes.  Books and papers will be set up in Bakelite type.  People will read Bakeliterature, Bakelitigate their cases, offer Bakeliturgies for their dead, bring young into the world in Bakelitters.”

Hubris? Indeed!  But still, it’s amazing stuff.  By the way, the lawyers at Bakelite know something about Bakelitigating from their 1922 Patent infringement suit against the Redmanol Chemical Products Co. and the Condensite Co.

Last, but not least, I wish to thank Steve for his blog and invaluable help throughout the ordeal of my collapsing Blueline restoration, and Troy Wilburn for his wonderful blog on another Blueline and its dating.

SOURCES

http://www.elvenkrafte.com/bakelite%20presentation.htm

https://rebornpipes.com/2015/06/06/spiffing-up-a-kbb-blue-line-bakelite-poker-1908-1914/

https://rebornpipes.com/2013/02/23/what-is-the-amber-used-in-pipe-stems-and-how-are-they-bent/

https://rebornpipes.com/2016/07/05/the-scintillating-antique-kbb-redmanol-pipe/