Tag Archives: contrast staining

Cleaning Up a Third Wrecked Pipe for a Fellow Pastor in Vancouver – A VB Apple


Blog by Steve Laug

Lately I am not taking on more work for repairs from email or online requests as I am just too busy. I still get the odd referral from the local cigar and pipe shop that I feel obligated to repair or restore. They tend to be spread out a bit so I can fit them in among the other work that I am doing for estates. Earlier this week I received a phone call from a fellow who had been referred to me by the shop. In our conversation he said that he had some pipes that the stems were all loose on and he wanted to know if I would be able to help him. I have learned to not make any arrangements until I have the pipes in hand and have examined them. He came over Friday afternoon to let me have a look at the pipes. He handed me a bag and inside there were four or five extra stems that he had brought for my use. There were also three old and tired pipes. They were in very rough shape. Two were apple shaped pipes stamped VB and one was a Croydon billiard. The stems were indeed loose on two of the pipes and stuck on the third pipe. The bowls were clogged with a thick cake to the degree that I could not even get my little finger in them. The stems had a thick layer of calcification and some tooth marks. They needed a lot of work.

We talked about the pipes and that he had held them for a long time hoping for a repair. He had spoken with the cigar and pipe shop and they had led him to me. Now he could actually have a hope of smoking them again. In the course of the 30 minute or so conversation he asked me what I do for work. I told him I was a Presbyterian minister working with an NGO dealing with the sexual exploitation and trafficking of women and children in 7 countries and 12 cities around the world. We talked about that a bit then he laughed and told me he was a United Church Minister who had taught in a variety of schools as well as pastored various parishes. We had a great conversation and I took the pipes and told him we would connect again once I had them finished.

The last pipe from the threesome is on the table now. It was probably in the best shape of the three pipes. It was in rough condition but not as bad as the previous two pipes. The bowl was clogged in precisely the same manner – a thick hard cake and no air would pass through the shank. The finish was shiny with varnish and worn and spotty with blackening on the right side of the bowl and both sides of the shank. It appeared to be an oily black not a burn. The rim top was a real mess with thick hard lava overflowing all around the bowl onto the rim. The stem was loose in the shank and was oxidized with calcification extending for about an inch up the stem from the button. In the midst of the calcification were the same deep tooth marks that appeared to be rounded rather than sharp so I may well be able to lift them out with a lighter flame. The slot in the button was plugged with a pin hole sized airway going through it. This third pipe is exactly like the others and I honestly do not know how this pipe was smoked the last time it was used. This was another of those pipes that I really dreaded working on because I just sensed that one thing would lead to another and the restoration would be almost endless. I took photos of the pipe before I started to record this anxious moment! I took some close up photos of the bowl and stem to show what I was dealing with on this pipe. You can see the density of the cake. It is not totally clear in the photo but the bowl is filled on the second half of the bowl and packed solid. This bowl appeared to be the only one that he had not reamed with a knife. The bowl was not slanted and the cake was evenly heavy all the way around the bowl. The rim top is rough as noted above and looking at the photos it too appears to have been used as a hammer. It is very rough to touch. The stem is a mess as can be seen. There is some oxidation and a thick coat of calcification from the button forward. That too is rock hard. Both the stem and the shank are plugged with no air passing through them.I took a photo of the stamping to show the brand on the pipe. It is a brand I have never heard of or worked on. There is little information available on it. It is stamped VB on the left side of the shank and Prima on the underside.Fortunately it was the same brand as the second pipe that I worked on. The only difference was the stain and the PRIMA stamping on the underside of the shank. I did some digging on the brand to see what I could find out with this additional information and there was nothing more to be found. I am including what I found on the previous VB pipe on Pipephil’s index page (http://www.pipephil.eu/logos/en/index-en.html) I found my first and only clue. Under the section called logos with two letters I found the VB listed. It took me to a listing under Holiday pipes. There was no further information on the country of origin or on the maker other than Holiday. I checked on pipedia as well and there was nothing. I have included a copy of the screen capture of the listing on Pipedia (http://www.pipephil.eu/logos/en/logo-h3.html#holiday).After posting the first VB pipe I received two comments on the blog regarding the stamping. I really appreciate getting information like this so if you ever have info please do not hesitate to send it. Here is what the first commenter, Liebaart sent me:

The VB logo is from the Vinche Company, a Belgian distributor. See their page: https://www.v-k.be/documents/catalog.xml?lang=en&open=NAV%5CPIJPEN%5CVINCHE&from=0

The second commenter, Joris D. Sutter (may be the same gentleman) sent the same information. The V.B logo refers to the company Vinche, a Belgia distributor. Have a look at their website here : https://www.v-k.be/documents/catalog.xml?lang=en&open=NAV%5CPIJPEN%5CVINCHE&from=0

This was very definitive information for me. I now knew that the pipe was from the Vinche Company a Belgian distributor. I am still wondering though if the pipe was made in Holland as suggested previously… the new information does not negate that possibility!

Once again I could no longer postpone starting the work on this old pipe. It was the last of threesome and I could return them to the old pastor. And besides that this is what I do – I am a pipe refurbisher. It was time to get started on this beast. I learned from the previous two pipes in the lot that the cake and calcification were very hard. I dropped the stem in a Oxyclean bath and the bowl in an alcohol bath. I figured while I worked on other pipes the cake and calcification would begin to soften a bit.When the pipe and stem had been soaking for about 4 hours I pulled them out of the respective baths. The bowl looked better externally. The alcohol had cut the shiny finish and removed some of the grime on the bowl. The cake in the bowl was definitely softer so I think it would be easier to remove. The stem came out and the bath had removed much of the oxidation and calcification. It had also softened what remained. The photos below show what I saw.The alcohol bath had softened the hard cake enough that I could directly ream it with the PipNet pipe reamer using the third cutting head. It easily worked through the cake and I was able to take it back to the bare walls of the bowl. I wanted to check and see if there was damage like there had been on the other two pipes. The good news was it was free of damage. I cleaned up the edges and bottom of the bowl with a Savinelli Fitsall Pipe Knife. I sanded the inside of the bowl with 220 grit sandpaper wrapped around a piece of dowel to further smooth out the bowl. I broke through the clogged airway in the shank with a piece of stiff wire. I topped the bowl on a topping board with 220 grit sandpaper and removed the damaged areas on the surface. Once I had finished the rim top was flat now I could deal with the edges of the bowl. I filled in the damage on the edges of the bowl with clear Krazy Glue and Briar dust. Once it dried I cleaned up the topping once again and then used a folded piece of 220 grit sandpaper to smooth out the inner and outer edge of the bowl. With the bowl reamed and the rim top repaired and clean I decided to work on the exterior of the bowl. It was unbelievably grimy and sticky. I scrubbed it with a tooth brush and undiluted Murphy’s Oil Soap. I rinsed it under warm running water to wash away the soap and debris. I repeated the process until the exterior was as clean as I was going to get it at this point. I dried it off with a cotton cloth and took photos to show the result. I cleaned the mortise and the airway in the shank and stem with pipe cleaners, cotton swabs and alcohol. I used the drill bit on a KleenReem tool to clean out the “crud” (hardened tars and oils) in the airway in the shank. I scraped the inside of the mortise with a pen knife. I opened the slot in the button with a dental pick and pushed pipe cleaners through the debris in the stem. I scraped away the majority of the calcification with the pen knife while I was cleaning the stem. Once I had finished – many pipe cleaners and cotton swabs later the airway was unobstructed to the bowl and the pipe had begun to smell clean. I sanded the exterior of the bowl and rim with a medium grit sanding sponge to remove the nicks, scratches and remnants of the original finish. I sanded the strange dark stains on the right side of the bowl and both sides of the shank at the same time. While I w not able to remove them I reduced them enough that I was hoping the stain I was going to use would cover them. I stained the bowl and shank with a Fiebing’s Tan Stain. It has a nice reddish tint to it that shows up once I have buffed and sanded it. I applied the stain, flamed it with a lighter and repeated the process until I was happy with the coverage. I would carry on with the bowl in the morning. The stain would dry overnight.In the morning when I got up I took photos of what the bowl looked like after the stain had cured all night. There are wet looking patches but they are not wet…just shiny! I wet sanded with 1500-12000 grit sanding pads to smooth out the finish on the bowl and prepare it for staining. I wiped the bowl down after each pad with a damp cloth to remove the dust and debris from sanding. I worked some Before & After Restoration Balm into the finish of the bowl, the rim top and shank with my fingertips to clean, enliven and protect it. I find that the balm really makes the briar come alive again. I let the balm sit for a little while and then buffed it with a cotton cloth to raise the shine. The pipe really looks good at this point. It looks much better than when I took it out of the bag. I set the bowl aside and turned my attention to the stem. I “painted” the surface of the stem with the flame of a Bic light to raise the tooth marks. It raised them all some but two small dents remained on both sides of the stem.I filled in the remaining tooth marks with clear Krazy Glue and let it cure. I like the clear glue on this kind of stem as it dries clear and the black of the stem shows through making for a very good blend with the existing material.Once the repairs cured I reshaped the button edge with a needle file. I flattened out the repaired spots at the same time. The stem was beginning to take shape.I sanded the repaired areas on both sides of the stem with 220 grit sandpaper to blend them into the surface of the stem. I followed that by sanding them with a folded piece of 400 grit wet dry sandpaper to begin the polishing.I polished the stem with micromesh sanding pads – wet sanding it with 1500-12000 grit pads. I polished it further with Before & After Pipe Stem Polish – both fine and extra fine. I wiped the stem down with Briarville’s No Oxy Oil to preserve and protect the stem. This was another challenging pipe to work on and I did the heavy work without Jeff. I put the stem back on the bowl and polished the bowl and stem with Blue Diamond polish on the buffing wheel. I gave the bowl and the stem multiple coats of carnauba wax. I buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The grain pops through enough to let us know it is there and my repairs to the rim of the bowl blend in really well. I am pleased with the look of the pipe. It really has exceeded my expectations for it when I first took it out of the bag it was in when dropped off. The contrast between the reddish, tan stain of the briar and the polished black vulcanite stem look very good together. The pipe feels great in my hand and I am sure that it will feel even better radiating the heat of a good smoke. It must have been a fine smoking pipe judging from the condition it was when I received it from the pipeman who dropped it off. Have a look at it with the photos below. The dimensions are Length: 5 ¾ inches, Height: 1 ¾ inches, Outside diameter of the bowl: 1 ¼ inches, Chamber diameter: ¾ of an inch. I am looking forward to what the old clergyman thinks of his second “new” pipe. I think he will enjoy it for many years to come and perhaps it will pass to the next pipeman who will hold it in trust. Thanks to each of you who are reading this blog.

Restoring a Karl Erik Ekstravagant Handmade In Denmark Tulip


Blog by Steve Laug

Every so often I receive pipes from pipemen and women who want them to be sold and the proceeds go to the NGO I work for in my real job! It is an organization called the SA Foundation Canada (www.safoundation.com) and it provides long terms housing, recovery and skill development for women and their children escaping sexual exploitation and trafficking. The organization is based in Vancouver, Canada but has projects in 7 countries and 12 cities globally. It is an organization that is cutting edge in the recovery process for these women and their kids with a success rate of over 70% globally. That simply means that out of every 100 women who enter our program 70 do not go back to their previous lifestyle. It is an amazing organization to work for and it has big vision and a commitment to thinking globally and acting locally. The admin and fundraising costs are 10% meaning that of every dollar donated $.90 goes to the work of providing for the recovery, care and training of the women and their children.

I am posting four pipes that have been donated for this cause. I am donating the restoration work on them and the individuals are donating the income generated by the sale of the pipes. This is the third of those pipes – first was a Nording Brandy 13, second was a Chimera Churchwarden and now this Karl Erik Ekstravagant Tulip. It is a beautiful pipe that has stunning grain. The stamping on the shank reads Karl Erik in a circle over Handmade in Denmark with Ekstravagant underneath that. The pipe is in excellent condition. There was some damage and burn marks on the rim top and inner edge as well as some darkening on the rim edges. The stem is acrylic with a golden fancy KE on the top. It has some light tooth chatter and marks near the button. There was also a long scratch on the underside of the stem running mid stem toward the button. The bowl and shank were dirty from light use but there was no cake in the bowl. I took some photos of the pipe before I started working on it. It really is a stunning pipe and feels great in the hand. I took photos of the rim top to show the damage that is present on the top and on the inner edge of the bowl. It almost looked as if the bowl had been knocked out against concrete. I took photos of the stem as well to try to capture the condition of the stem. The top side was dirty and dull but there were no tooth marks or chatter. The underside looked good other than a deep scratch that ran from the button edge forward on the stem for about an inch. I took a photo of the COM stamp on the underside of the shank and it reads as noted above. It is clear and readable with the stamp running around the circle.I wanted to know a bit more about the Ekstravagant stamping on this pipe. I have worked on quite a few pipes from Karl Erik (Karl Erik Ottendahl) over the years but this was the first with the Ekstravagant stamping. I turned to the Pipedia article on KE pipes for help with this (https://pipedia.org/wiki/Karl_Erik). From there I learned that these pipes were large pipes entirely handmade by Karl Erik Ottendahl.

I quote in part from that article below.

During all periods he had made some of his own handmade pipes, but he felt that the responsibility of managing the factory did not give him the freedom he wished he had. Accordingly, in 1990, he went back to work on his own. He believed that he could produce better work if he worked alone, though his principle reason was simply that he missed the quiet, pleasant atmosphere that a one man shop afforded him. According to him, he has been much happier since he returned to make pipes all by himself. Certainly, the results reflect his rediscovered happiness with the pipe making craft.

Though Karl Erik’s favorite briar mostly came from Morocco or Greece, but he frequently purchased elsewhere, too. He didn’t consider the briar origin to be particularly important provided the briar was well cured. Therefore, he simply purchased the best briar he could find, rather than purchasing from only one or two regions.

Concentrating on more classical influenced shapes Karl Erik’s style emphasized the wood over all other contributing factors by allowing the grain to determine the ultimate shape of the piece. He further emphasized the natural, organic, flowing shape of his bowls with hand cut stems and a broad variety of decorating materials.

Now it was time to work on the pipe. I decided to address the issues with the rim top first. I chose to use the least intrusive method first. I steamed the nicks and dents to no effect. I sanded it with a folded piece of 220 grit sandpaper to try to remove the damage. You can see the effectiveness of this in the first photo below. I carefully worked on the inner edge of the rim with a folded piece of 220 grit sandpaper. I worked slowly so as not to damage the rim top. It took a little work but I was able to remove some of the burn damage that marred the inner edge but there were some deep burns on the back edge of the bowl that would require stronger methods. I turned to stronger measures and carefully top the bowl on a topping board with 220 grit sandpaper. I needed to address the deep nicks in the surface and the edges – both inner and outer and this was the means I chose. It took care of the majority of the issues and minimized the burn mark at the front and back of the bowl. It was not gone but it looked better. I used a folded piece of 220 grit sandpaper to work on the inner edge. I wanted to give it a slight bevel to clean up the burn damage. While it was not perfect it was much better. I did not want to sacrifice the roundness of the bowl to do more work on it so I left it.I polished the rim top and edges of the bowl with micromesh sanding pads. I wet sanded it with 1500-12000 grit sanding pads and wiped it down with a damp cloth after each pad. The rim top came out looking very good. The darkening was lessened and the damage was smoothed out. The rim was looking very good at this point.  I stained the top of the bowl with a blend of Oak and Cherry stain pens. This combination matched the stain on the rest of the bowl perfectly. I am pretty happy with the look of the rim top at this point in the process.I worked some Before & After Restoration Balm into the surface of the briar with my fingertips and let it sit for about 10 minutes. I buffed it off with a soft cloth. It is a product that I have really come to appreciate. Mark Hoover crafted it to enliven, clean and protect briar. I use it on every pipe I work on and find that with a single application the briar comes alive with deep glow. Because the pipe looked so clean I forgot to clean out the internals. I went back and cleaned out the mortise and the airway in the shank and stem with alcohol, cotton swabs and pipes cleaners. The shank was quite dirty but the airway in the stem was pretty clean. I repeated the scrubbing until the cleaners came out clean.I set the bowl aside and turned my attention to address the deep scratch in the stem. It was really a gouge that had carved a line from the button forward. It was not a crack lest you might think so. I examined it in detail with a lens and the stem was solid. I wiped down the area with a cotton swab and alcohol and then filled in the gouge with clear Krazy Glue. Once the repair cured I used a folded piece of 220 grit sandpaper to blend the repair into the stem surface. I polished the area I had sanded with 400 grit wet dry sandpaper.Denicare Mouthpiece Polish is a gritty read paste that I have been using as a pre-polish for the mouthpieces. It removes a lot of very minor scratches and works well in removing the hard to get area in the crease of the button. I work it on with my fingers and then scrub the stem with a cotton pad and wipe it off when finished.  I avoided the gold stamping on the topside to protect it from over buffing.I polished the acrylic stem with micromesh sanding pads – wet sanding it with 1500-12000 grit pads and wiping it down with a damp cloth between each set of pads. The stem began to take on a deep shine. I used Before & After Pipe Polish – both Fine and Extra Fine to finish the polishing. By this point the stem looks great and the gouge is gone! Once I finished I put the stem back on the shank and carefully buffed the pipe with Blue Diamond polish using a lightly loaded pad and a soft touch. I wanted to raise a shine and buff out some of the small scratches in the briar and the acrylic stem. I gave the stem a vigorous polish being careful around the stylized gold KE on the stem top. I gave the bowl and the stem several coats of carnauba. I buffed the pipe with a clean buffing pad and hand buffed it with a microfiber cloth. The finished pipe is shown in the photos below. It is a great looking Karl Erik Ekstravagant Tulip shaped pipe whose sale price is going for a great cause. The dimensions of the pipe are Length: 6 inches, Height: 2 ½ inches, Outer Bowl Diameter: 1 ½ inches, Chamber Diameter: ¾ of an inch. The pipe will soon be on the rebornpipes store and you can purchase it and support a very worthy cause. Thanks for walking with me through the restoration.

Breathing Life into a Worn and Beat up Dunhill Shell Briar EC Canadian for Alex


Blog by Steve Laug

In a previous blog I mentioned that around Christmas time I got together with Alex to enjoy some great hot cocoa, smoke our pipes and talk about all things pipes. I also gave him a batch of pipes that I had finished from his stash and he gave me a few more to work on for him. I always have a great time when we get together and this time was no exception. He greeted me at the door with slippers and an old smoking jacket. I took my seat in the living room among his latest pipe finds and was handed a great cup of cocoa. I set it down and we both loaded out pipes with some new Perretti’s tobacco that he had picked up. We touched the flame of the lighter to the tobacco and sat back and blissfully enjoyed the flavour. As we did Alex walked me through his latest finds. There were some amazing pipes to look at and savour. I already wrote about the Dunhill Bamboo Tanshell with a lot of nice colour happening around the bowl. I refreshed that pipe for him and wrote about it here – https://rebornpipes.com/2020/01/08/refreshing-a-dunhill-tanshell-w60-t-1962bamboo-lovat-for-alex/.

He also pulled another Dunhill from the pile of new pipes that he wanted me to work on. It was the exact opposite of the Bamboo in terms of condition. The Bamboo was relatively clean and he had already enjoyed a few bowls through it so it was a quick and easy refresh. This one was a real mess! It was another sandblast. This time it was a Shell Briar Canadian. I carefully took it in my hands and examined it. It was in very rough shape with many cracks in the briar. Alex knew the issues with the pipe but he wanted to know if I could repair it. I assured him that of course it could be repaired and the current cracks stopped. But all repairs to the cracks would essentially be cosmetic and though he could not see them they were still present. The ones going through into the bowl would need to be treated as well. I have repaired many of the pipes that I smoke in this manner and they continue to serve me undamaged for many years after the repair so I was just giving him the facts. He was fine with that and said to go ahead. So I took it home with me.

When I got home I laid it aside and tonight took it up to work on it. I examined the pipe to see what I was working with and took some photos. You can see from the first four photos below that there was something redeeming about the pipe. I think that is what Alex saw. It is a really nicely shaped Canadian. The right side of the bowl was dirty but looked very good. The back of the bowl and right side were full of cracks that went virtually the length of the bowl from the rim top to at least shank height. The rim top had significant damage to the inner edge and the crack on the right side went through to the interior and on top. The stem was pockmarked, dirty and oxidized with tooth chatter and marks on both sides just ahead of the button. Overall the pipe a wreck. I took photos of the pipe before I started my cleanup and restoration. Look closely at the second and third photos. You will see the cracks. I took a close up photo of the rim top and the back and right side of the bowl to show the crack damage. I have pointed out the cracks with red arrows for easy identification. The inner edge of the rim also shows burn and poor reaming damage. I took photos of the stem as well. The vulcanite was pitted, oxidized and calcified in the crease of the button. There were some tooth marks and chatter on the stem near the button but otherwise it looked pretty good. The pipe was stamped on the heel and underside of the shank with the following nomenclature: EC (the designation for a Canadian) followed by Dunhill over Shell Briar. That is followed by Made in England with a number 3 in superscript next to the D. This tells me that the pipe was made in 1963. After that there is a circle with a 4 in it designating the size of the pipe followed by the letter S which is the designation for Shell Briar pipes. The stamping was clear and legible which actually surprised me given the condition of the rest of the pipe.I think Jeff has spoiled me with working on clean pipes so I decided to start by cleaning up this one. I wanted it clean even before I began to work on the repairs. I find that the cleaning also helps me see things in the finish that I would otherwise miss. I scrubbed the exterior of the bowl with Murphy’s Oil Soap and a tooth brush to remove the debris from the nooks and crannies of the sand blast as well as from the inside of the cracks. I rinsed the bowl with warm water and dried it off with a cotton cloth. Once that was done the cracks were very clear but so was the natural beauty of this Canadian shape! With the exterior clean I worked on the interior. I reamed the bowl with a Savinelli Fitsall knife. I did not want to risk the pressure that is put on the bowl sides by the PipNet reamer. I scraped the cake out until the walls were clear. I sanded them smooth with a dowel wrapped in 220 grit sandpaper.I cleaned out the mortise and the airway from the shank to the bowl with pipe cleaners, cotton swabs and alcohol. I worked on it until the airway was clean and the pipe smelled clean! I cleaned the stem at the same time working around the buildup on the tenon and stem face as well as the airway and the slot. I used alcohol, pipe cleaners and cotton swabs for this as well. I was surprised at how clean the internals of the stem were. I expected it to be horrid.With the bowl clean it was time to begin the reconstructive surgery on the bowl. I used a lens to trace the cracks to their end. All of them began at the rim and worked downward. I marked the end with a correction pen (thanks for the tip Paresh). Once I had them marked I used a Dremel and microdrill bit to drill a small hole in the end of the crack to stop it from spreading. Once I had the holes drilled I filled them in with briar dust and clear Krazy Glue (CA Glue). The cracks were numerous so I took a few photos to show the extent of the repairs. My method is a bit different from Dal’s due to my glue. I fill in the crack with the glue and press the parts together. It dries quickly and with no internal pressure holds together well. I go back and fill in the cracks in the bowl with briar dust. I use a dental spatula and pick to work them into the cracks. I put a top coat of Krazy Glue to seal it. I repeat the process until the repair is complete. In the case of the large crack that goes into the interior of the bowl I pressed dust into it as well and the glue from the outside held it in place. I will give it a coat of JB Weld to protect it once I finish the bowl. Once the repairs cure I work over the repaired areas with a brass bristle brush to knock of the loose dust and bits of glue that are on the surface. I used my Dremel and sanding drum to smooth out the interior walls of the bowl and the repair to the crack on the right side of the rim top. I think that the repair is starting to look pretty good.With the repairs cured and the interior and high spots smoothed out it was time for some artistry to bring the Shell finish back to the bowl sides and rim top. I started the process by working over the repaired areas with a wire wheel on my Dremel. I worked over the areas around the sides of the bowl and the rim top. It was starting to look right. The shininess of the repairs was reduced and the finish began to show through. Now it was time to etch the surface of the briar with the Dremel and burrs. The photos that follow show the three different burrs that I use to cut the grooves to match the sandblast. The burrs worked to cut a pretty nice match in the briar.I used the wire brush again to clean off the dust left behind by the burrs. It is hard to tell from the photos but the pattern is really close to the surrounding areas of the briar bowl and shank. With the carving done approximating the sandblast finish under the repairs it was time to stain the bowl. I have found that with a Shell Briar finish I have to use a Mahogany and a Walnut stain pen to match the rest of the bowl. I streak on the Mahogany first and fill in the Walnut around the rest of the finish. I blend them together and the finished look is hard to distinguish from the original stain. I moved on to round out the inner edge of the rim and minimize the damage. I used a folded piece of 220 grit sandpaper to carefully give the inner edge a very light bevel. Once I was finished with the shaping I ran a Walnut Stain Pen around the freshly sanded edge to blacken it.With the finish repaired and restained I rubbed it down with Before and After Restoration Balm. It is a product developed by Mark Hoover to clean, enliven and protect briar. I worked it into the briar with my finger tips and a horse hair shoe brush. I let it sit for about 10 minutes and buffed it off with a cotton cloth. You can see the results below. With the exterior finish and the repairs completed it was time to mix up a batch of JB Weld to coat the inside of the bowl and protect the walls where the cracks went through. I mixed the Weld and put a pipe cleaner in the airway to keep the weld from sealing off the airway in the bowl. I applied the mixture to the walls with a dental spatula. Once had the walls covered around the area of the cracks I set the bowl aside to cure. I did not put the mixture in the heel of the bowl as it was solid and had no issues. I set the bowl aside and turned to address the oxidation, tooth marks and chatter on the stem surface. The stem was in good condition with some minor pitting. I used a folded piece of 220 grit sandpaper to sand out the tooth marks, chatter and oxidation. I started the polishing with 400 grit sandpaper. The stem is starting to look very good.I have been using Denicare Mouthpiece Polish as a pre-polishing agent. It is a gritty, red paste that does a great job in removing the oxidation remnants in the crease of the button and also polish out some of the lighter scratches in vulcanite. I rub it on with my finger tips and scrubb it with a cotton pad. I buff it off with another pad.I finished polishing the stem with micromesh sanding pads – wet sanding it with 1500-12000 grit pads and wiping it down after each pad with a damp cotton pad to remove the dust. I polished it with Before and After Pipe Polish – both fine and extra fine. I finished by wiping the stem down with some No Oxy Oil that  received from Briarville Pipe Repair to experiment with. Once the JB Weld repair had cured I sanded the walls of the bowl to remove the excess material and to make sure the mixture was primarily in the damaged areas of the bowl walls. The repair looked very good. I mixed a batch of pipe mud composed of sour cream and charcoal powder and applied a coat of it to the bowl to protect the walls while a cake formed. I know Alex hates bowl coatings as much as I do but this one is essential given the nature of the cracks. It is just a precautionary step and the coating dries neutral and imparts no taste to the tobacco. After a few bowls you do not even know it is there. After mixing it well I applied it to the walls of the bowl with a folded pipe cleaner. I aim for a smooth coating that will dry dark and black and be almost invisible. When it dries the mixture does not have any residual taste. Once it was coated I set the pipe aside to dry. The mix does not take too long to dry. In about an hour it is dry to touch and almost black. After 24 hours it is black and smooth. The last photo below has been drying about two hours. The only remaining damp spot is in the bottom of the bowl. Once I finished I put the stem back on the shank and carefully buffed the pipe with Blue Diamond polish using a lightly loaded pad and a soft touch. I wanted the shine but not the grit filling in the crevices of the sandblast bowl. I gave the stem a vigorous polish being careful around the white spot. I gave the bowl several coats of Conservator’s Wax and the stem several coats of carnauba. I buffed the pipe with a clean buffing pad and hand buffed it with a microfiber cloth. The finished pipe is shown in the photos below. It is a great resurrection pipe for Alex and looks better than when I began the process. The dimensions of the pipe are Length: 5 ½ inches, Height: 1 5/8 inches, Outer Bowl Diameter: 1 ¼ inches, Chamber Diameter: ¾ of an inch. The pipe will soon be heading back to Alex so he can continue to enjoy it. Thanks for walking with me through the restoration.

A Challenging Restoration of a Peterson’s System 3, Irish Free State Stamped Pipe


Blog by Paresh Deshpande

This pipe had been on my ‘to do list’ for long but since it came without a stem and as I did not have one, this project was kept pending since long. Now that I have received my large consignment of estate vulcanite and bone/ horn stems, including one Pete System P-lip stem, I couldn’t help but fish out the Pete stummel again to work on.

Most of my fellow pipe restorers would have turned away from this project that I had decided to work on next. To be honest, I would have led the pack in just consigning this pipe to history, but for the provenance of this Peterson’s System pipe. This pipe had once belonged to my grandfather and from the condition that it was in; it was apparently one of his favorite pipes!!

Well, the pipe that is now on my work table is in a pretty badly battered condition and came without a stem. There are ample signs of this pipe having been repaired earlier and extensively smoked thereafter. The stampings are all but worn out and can be seen under a bright light and under a magnifying glass. The left side of the shank bears the stamp “PETERSON’S” over “SYSTEM” over an encircled # 3. The pipe bears the COM stamp of “IRISH” over “FREE STATE” that is stamped perpendicular to the shank axis in two lines and very close to the shank end. The ferrule has the usual three cartouche with first having Shamrock, the second a Prone Fox and lastly a Stone Tower. Stamped above the cartouche are the letters “K & P” and is stamped below as “PETERSON’S” over “DUBLIN”. Having worked on quite a few old Peterson pipes from my inheritance and few from my Mumbai Bonanza, I was pretty sure that this pipe dates to 1920- 30 time period. To confirm this and also refresh my memory, I turned to my favorite site rebornpipes.com and to a write up “A Peterson Dating Guide; a Rule of Thumb” by Mike Leverette, here is the link (https://rebornpipes.com/2013/08/11/a-peterson-dating-guide-a-rule-of-thumb-mike-leverette/)

Here is what I have found and I reproduce it verbatim from the write up:-

The Irish Free State was formed on 15 January 1922. So the Free State Era will be from 1922 through 1937. Peterson followed with a COM stamp of “Irish Free State” in either one or two lines, either parallel or perpendicular to the shank axis and extremely close to the stem.

Thus, it is confirmed that this pipe is from the period 1922 to 1937 and this has to be one of the earliest Peterson’s pipes that was in my grandfather’s rotation and probably one that was his favorite.

INITIAL VISUAL INSPECTION
The stummel is covered in dirt and grime. All that catches your eyes is the dirty darkened upper portion of the stummel something like a flume, but not quite like it!!! Closer examination confirmed my worst fears….. CRACKS!! Yes, crack with an ‘s’. There are a couple of major cracks, one to the front of the stummel in 11 o’clock direction and the second major crack is at the back of the stummel. It is from the end of this big crack that three smaller and fine lined cracks emanate creating a web of cracks at the back and extending to the sides of the stummel. These cracks appear to have been repaired at some point in the past, definitely more than 40 years back, and these repairs have been camouflaged under a blotchy coat of black stain. The exact extent of damage can be assessed only after the external surface of the stummel had been completely cleaned and under magnification. The foot of the stummel has a number of dents and dings which needs to be addressed. In spite of all the cracks and its subsequent repairs, this pipe had been in continuous use as is evidenced by the thick layer of cake in the chamber. It seems that my grandfather even took the efforts to keep the thickness of the cake to a dime, not successfully though and so unlike him!! The rim top surface is completely out of round with the cracks extending over the rim top in to the chamber. The extent of these cracks in to the chamber and damage to the walls will be ascertained only after the chamber is cleaned off the complete cake. The rim top is covered in a thick layer of lava overflow. The ghost smells are ultra-strong, I say.The mortise, shank and especially the sump are chock-a-block with old oils, tars, grime and residual flecks of tobacco. The air flow through the draught hole is laborious and will require a thorough cleaning.There being no stem with this pipe, the biggest challenge will be to find one that fits. Nonetheless, this particular pipe, though I desire to restore and preserve, I am not sure what the real condition of the stummel would be under all the dirt and grime and even if it’s worth the efforts that would be needed.

THE PROCESS
The first obvious issue that I wanted to address was to find a correct stem, preferably original P-lip stem, for the pipe. I rummaged through the parcel of estate pipe stems that had only recently reached me and I knew it contained a Pete System P-lip stem. I fished it out and tried the fit of the stem in to the mortise. Here is what I saw. Though the fit appears to be good in pictures, that is not so!! There are these following issues which are difficult to gauge from the pictures:

(a) The stem does not seat firmly into the mortise. There is a play between the tenon and the walls of the mortise; this, in spite of the rubber packing that the tenon came with. Or is this play a result of the rubber packing?

(b) The seating of the stem is too high. The tenon end does not reach anywhere near the draught hole, let alone reach slightly below it for the system to work.

(c) The stem, if pushed further in to the mortise would put additional pressure on the walls of the mortise, subsequently resulting in cracks at the shank end.

(d) The plane of the bowl and the bend of the stem are not aligned. The stem is too straight making for an awkward appearance.

With certain modifications to the stem, I feel confident that I could make the stem work efficiently in a system pipe. The saddle is deeply gouged all around. The upper and lower surface of the stem has significantly deep tooth indentations in the bite zone. The button edges are badly deformed with deep bite marks. Following pictures show the condition of the stem as I received it. The tenon is clogged with heavy accumulation of oils and tars which is seen through the tenon opening. The rubber packing cap is also covered in dirt and grime.With a sharp knife, I removed the rubber cap by separating it from the tenon end, expecting to find a chipped or badly damaged tenon. However, the tenon is intact and apart from being clogged the stem is in decent condition. After I had removed the rubber cap, I rechecked the seating of the stem in to the mortise. The seating was still loose and too high!! Next I moved ahead and reamed the chamber with a Castleford reamer head size 2 followed by size 3. With my sharp fabricated knife, I removed the cake from the chamber where the reamer head could not reach and gently scrapped away the lava overflow from the rim top surface. Thereafter, using a folded piece of 180 grit sand paper, I sanded out the last traces of cake and exposed the walls of the chamber and wiped the chamber with a cotton pad dipped in isopropyl alcohol to remove the carbon dust left behind by all the reaming and sanding process. Even though there are no heat fissures/ lines along the chamber walls where the cracks do not extend (a big solace, I say!!), the stummel cracks are a different story which I shall come to subsequently. The chamber ghosting is still significantly strong which may further reduce once I clean the sump/ reservoir and the mortise. The two major cracks (marked in red arrows) that were observed in the external stummel surface extend well in to the chamber with the old repair fills in these cracks in plain view. Further sanding and close scrutiny of the walls confirmed my gut feeling that the minor cracks originating from the major cracks will also be seen as heat fissures in the chamber walls. These have been marked in yellow arrows. As I was contemplating my further course of action to address the chamber issues, I set the stummel aside and decided to work on the stem. I cleaned the internals of the stem using hard and normal bristled pipe cleaners and isopropyl alcohol. With a pointed dental tool, I scraped out the entire dried gunk from the tenon end.I decided that I would first undertake the cleaning, both internal and external, of the stummel before proceeding with further repairs. This cleaning will not only give me a clear picture of the extent of damage but also the efforts that would be needed are justified or otherwise.

I cleaned out the internals of the shank and mortise. Using my dental tool, fabricated knife and specifically modified tool, I scraped out all the dried oils, tars and gunk that had accumulated in the draught hole, airway and sump. The amount of crud that was scrapped out and the condition of the pipe cleaners that were used leaves no surprise why the air flow through it was restricted. I finished the cleaning by running a few pipe cleaners dipped in isopropyl alcohol. I also wiped the sump with cotton buds and alcohol. I gave a final cleaning to the sump with a paper napkin moistened with isopropyl alcohol. This, however, did not address the issue of ghost smells in the stummel.I decided to address the issue of old odors in the chamber and shank by subjecting it to a cotton and alcohol bath. I wrapped some cotton around a folded pipe cleaner, keeping the tip of the pipe cleaner free of wrapped cotton as this would be inserted through the draught hole in to the chamber. This would form the wick for the shank. I tightly packed the chamber with cotton balls and filled it with 99% pure isopropyl alcohol using a syringe and set it aside. By next day, the cotton and alcohol had drawn out the all the old tars and oils from the chamber and max from the shank. With my dental tool, I further scrapped out the loosened gunk from the sump and mortise. I cleaned the external surface using a hard bristled toothbrush and Murphy’s Oil Soap. With a soft bristled brass wired brush, I removed the overflowing lava from the rim top surface and cleaned the internals of the shank with a shank brush and dish washing soap to remove what little crud remained in the shank. I rinsed it under running tap water and wiped the stummel dry with an absorbent soft cotton cloth. Fortunately for me, the blotchy coat of black stain that was applied to mask the repairs came off with use of Murphy’s Oil Soap and dish washing soap. Had this not worked, an alternative method of removing this coat would be to wipe the stummel with pure acetone and/or isopropyl alcohol on cotton swabs. With the stummel nice and clean, the damage is now all too apparent and it did not present an encouraging picture. The major cracks are quite deep and the secondary minor cracks emanating from the major crack are restricted at the back of the stummel. Here is what I saw. I shared these images with Steve and sought his opinion if this project was even worth the effort. A few minutes later, Steve responded in his characteristic manner. I reproduce the exact exchange that took place between us

Steve: What a mess

Me: What is the best way ahead? Worth the effort? Grandpa collection…

Steve: That was my question… is it worth it? With the Grandpa connection, I would probably work on it. I would thoroughly clean the inside and outside. Once that is done, I would line the bowl with J B Weld to completely bind the inside together. Once that is done, then fill and repair the outside with glue and briar dust.

Me: This is the condition of the shank and stummel joint…emotions dictate restoration while practical experience says it’s a gonner…

Steve: I have been there…go with emotions on this one…it will take time and be a real resurrection!!

Now that clarity has been established and hints for the way ahead have been spelt, I decided to complete this project.

I decided to address the stem issues first.

As noted earlier, the seating of the stem in to the mortise was loose and too high for the Pete’s famed system to work efficiently. I inserted a pipe cleaner in to the mortise and up to just below the draught hole, bending the pipe cleaner at this point to mark the depth that I desired. Next, I mark the same depth on to the saddle of the stem with a white correction pen. I wound a scotch tape along the marked white line extending towards the button end. This gave me a reference line beyond which sanding needs to be avoided. With this initial preparation completed, I next mount a 180 grit sanding drum on to my hand held rotary tool, set the speed at half of the full speed and proceeded to sand down the portion of the stem towards the tenon end. I frequently checked the fit of the stem in to the mortise to ensure a snug fit and avoid excessive sanding of the stem. Making steady progress, I was satisfied with the stem modifications at this stage. The tenon was just below the draught hole and there was no play in the seating of the stem in to the mortise. Next, using 150 grit sandpaper, I sanded the entire stem, especially being diligent around the saddle portion that was shaved off to achieve a snug fit of the stem into the mortise. Though I had to spend a considerable time, I was happy with the blending to a smooth transition at the edge which was sanded down. I wiped the stem with Murphy’s oil soap on a cotton swab to remove the sanding dust and oxidation. The stem looked good and should function as it is supposed to, making me very pleased with the fruits of my efforts at this stage.Just a word of caution here for all the first timers using the sanding drum and rotary tool; firstly, ensure that the rotary tool is set at 1/3 or ½ of the full rpm of the tool as too high a speed will fling the stem away from your grip and may result in excessive sanding of the stem surface. Secondly, keep the stem turning evenly at all times to achieve as evenly sanded surface as possible and avoid deep gouges. Thirdly, frequently check the progress being made and remember the mantra “LESS IS MORE”! Fine tuning is best achieved by eyeballing and working with hands and sandpapers.

Staying with the stem repairs, I mixed CA superglue and activated charcoal, filled all the deep tooth chatter and indentations and also over the button edges and set the stem aside for the fills to cure. I shall blend these fills and also sharpen the button edges once the fill has hardened considerably.Now with the stem set aside for the fills to cure, it was time for me to work the stummel. I topped the rim on a piece of 220 grit sand paper to even out the rim surface dents and dings and also to reduce the charred rim surface. The repairs to the cracks, marked with red arrows, are all too apparent now as can be seen in the following pictures. The rim top surface is charred and thin in 10 o’clock direction which have been marked in blue circle. The rim top repair towards the front of the bowl has resulted in thinning of the rim top. This is marked in a yellow circle. This stummel has some serious issues that need to be addressed. I preceded the stummel repairs first by coating the walls of the chamber with a slightly thick layer of J B Weld. J B Weld is a two-part epoxy Cold Weld in two tubes; hardener and steel which are mixed in two equal parts (ratio of 1:1) with hardening time of 5-6 minutes and complete curing time of 6-8 hours. I poured the contents of the two tubes and mixed it well. I applied this mix, as evenly as possible, over the entire chamber wall surface. I worked fast to ensure an even coat over the chamber walls before the weld could harden. I set the stummel aside for the application to harden and cure overnight. By the next afternoon, the J B Weld had cured and hardened considerably and will now be able to hold the stummel together as I move along with drilling counter holes, refreshing the fills in the cracks and further sanding and polishing processes. I gouged out the old fills from the cracks. I was careful not to apply too much pressure or dig deeper than absolutely necessary to remove the old fills. Using a magnifying glass and a white correction pen, I marked the points for the counter holes at the start, the turning and the end points along the extent of all the cracks seen on the stummel, and mark my words all Readers, there were plenty and then some more!! After I was done with my markings, the stummel appeared more like a mosaic of white dots!! Next, I drilled counter holes with a 1mm drill bit mounted on to my hand held rotary tool deep enough to serve as a counter hole while taking care that I did not drill a through and through hole. These counter holes arrest and prevent the spread of the cracks further. The importance of these counter holes cannot be underestimated. In fact, this pipe had been repaired previously and the repairs were solid enough, though without counter holes, that the pipe was smoked by my grandfather for many years. However, in my scant experience in pipe restoration I have seen that the extensive spread of the cracks towards the back of the stummel is a result of lack of drilling a counter hole to arrest the spread!!

I filled these cracks and counter holes with a mix of briar dust and CA superglue using the layering method (layer of superglue followed by sprinkling of briar dust and repeated it till desired thickness of fill was achieved) and set it aside for the fills to cure. I ensured that I filled the thin outer edge of rim top surface that I will subsequently sand down to match with the rest of the rim surface.While the stummel was set aside for curing, I decided to correct the geometry of the stem in relation to the plane of the bowl. The stem was too straight and was awkward to clench. After inserting a pipe cleaner through the stem, I heated the stem with a heat gun till the vulcanite became a little pliable. Holding the tip of the pipe cleaner, I gave the stem a bend, eyeballing it to suit the bowl. Once I had achieved the desired bend, I held it in place under cold running water till the stem had cooled down sufficiently to retain the shape. The stem was now comfortable to clench. Here are the pictures of the stem before (on the left side) and after (on the right side) the bend. Now that the seating of the stem into the mortise and the bend to the stem had been sorted out, I proceeded to sand/ blend the fills and impart a nice black glossy shine to the stem. With a flat head needle file, I sanded these fills to achieve a rough match. I further fine tuned the match by sanding the filled area with a folded piece of 220 grit sand paper pinched between my thumb and forefinger. I followed it up by sanding the entire stem surface using 400, 600, 800 grit sand papers and finally with a piece of 0000 grade steel wool. This serves to remove the deep seated oxidation and also reduces the sanding marks of the more abrasive sand papers. I also sharpened the button edges while sanding. I wiped the stem with a cotton swab and alcohol to remove all the oxidation and sanding dust from the surface. I applied a little Extra Virgin Olive oil over the stem and set it aside to be absorbed by the vulcanite. The stem has turned out amazing and now I felt upbeat about completing this project.I wet sand the stem with 1500 to 12000 grit micromesh pads. Next I rubbed a small quantity of extra fine stem polish that I had got from Mark and set it aside to let the balm work its magic. After about 10 minutes, I hand buffed the stem with a microfiber cloth to a nice shine. I rubbed a small quantity of olive oil in to the stem surface to hydrate it and set it aside. The stem now had a nice deep black and glossy shine.With the stem completed, I turned my attention to the stummel. In the intervening time when I worked the stem, the stummel crack fills had hardened and cured well. Using a flat head needle file, I sanded these fills to achieve a rough match with the rest of the stummel surface. I further fine tuned the fills by sanding the entire stummel surface with folded pieces of 220, 400 and 600 grit sandpapers. The stummel was now clean and even. On close scrutiny of the cleaned stummel surface, I observed a small crack which I had missed out earlier. I will need to drill counter holes to arrest the spread and extending of these cracks. Under a magnifying glass and bright light, I marked the ends of the now observed cracks with a white correction pen. I mounted a 1mm drill bit on to my hand held rotary tool and drilled counter holes. I filled these counter holes and cracks with a mix of briar dust and superglue. I also took this opportunity to touch up and refill those areas which required further fills and set the stummel aside to cure. Once the fills had cured, I went through the complete cycle of sanding with a flat head needle file followed with 220 grits sandpaper. The fills are all solid and have naturally blended in quite nicely with the entire briar surface. The rim top surface is now evenly thick and with folded piece of 220 grit sandpaper, I created a slight bevel to inner and outer edges of the rim top. I am happy with the appearance of the stummel at this stage of restoration. I polished the stummel with micromesh pads, wet sanding with 1500 to 12000 pads. I polished the freshly topped rim surface and the newly created inner rim bevel. I wiped the surface with a soft cloth at the end of the micromesh cycle. The stummel looked amazing with a deep shine and beautiful grains popping over the stummel surface. I was surprised that the rim top surface has the same deep brown coloration as the rest of the stummel surface even though the repairs to the cracks were still sticking out like sore thumbs through the shining stummel surface, I was not overly perturbed having made peace with myself regarding the repairs showing, still I shall attempt to mask them by staining the stummel subsequently. I massaged a small quantity of “Before and After Restoration Balm” with my fingers into the briar. The immediate and incredible transformation that takes place is a worthy reward for all the efforts!! I let the balm sit on the surface to be absorbed in to the briar for about 20 minutes. The bowl now looked fresh and attractive with the grains popping out any which way you look at the briar. Even the repairs to the stummel are a lot less visible what with the briar taking up a deep dark and vibrant brown hues. I polished off the balm with a soft cloth to a lovely shine. Next, with a folded piece of 150 grit sandpaper, I sanded the coat of J B Weld from the internal walls of the chamber keeping just a thin layer of coat along the walls. The coat appeared uneven at this stage but once it was coated with pipe mud, the chamber walls would become even and smooth. I decided on giving the stummel a stain wash with a Feibing’s Dark Brown leather dye. I diluted the Feibing’s Dark Brown leather dye in 99.9% isopropyl alcohol in approximate ratio of 1:4 and with a cotton swab, I dabbed the diluted stain over the stummel surface, letting it set for a few moments and thereafter wiping it off with a dry clean cotton swab. I repeated the process till I had achieved the desired coloration. I was pleased with the color of the stummel which highlighted the grains while the stummel repairs were masked nicely. This time around, even the fills had absorbed the stain and blended in nicely with the rest of the stummel. In order to ensure that the stain wash sets in to the briar, I warmed the stummel with a heat gun while being careful that I did not overheat the crack repairs/ fills.Now on to the home stretch… To complete the restoration, I re-attached the stem with the stummel. I mounted a cotton cloth buffing wheel to my hand held rotary tool, set the speed at about half of the full power and applied Blue Diamond compound to the entire pipe to remove all the minor scratches that remained. I wiped/ buffed the pipe with a soft cotton cloth to clear it of any leftover compound dust. With a cotton buffing wheel earmarked for carnauba wax, I applied several coats of carnauba wax. I worked the complete pipe till the time all the wax was absorbed by the briar. The pipe now boasted of a beautiful and lustrous shine. I vigorously rubbed the pipe with a microfiber cloth to deepen the shine and also clean away any residual wax that had been left behind. I vigorously buffed the nickel ferrule with a jeweler’s cloth and brought it to a nice shine. I was very happy with the way this beauty had turned out. The following pictures speak of the transformation that the pipe has undergone. There was only one more issue that needed to be addressed and one that could not be ignored, being a functional issue. After I had lined the walls of the chamber with a thin coat of J. B. Weld, it was necessary to prevent the walls from coming in to direct contact with the burning tobacco. I addressed this issue by mixing activated charcoal and plain yogurt to a thicker consistency, just enough that it would spread easily and thereafter applied it evenly all along the chamber walls after inserting a folded pipe cleaner through the draught hole to keep it open. Once dry and set, this will not only protect the walls but also aid in faster buildup of cake.P.S.: This project was one with many challenging issues that needed to be addressed, the first and biggest being finding an original Peterson’s system P-lip pipe stem, ensuring a snug fit in to the mortise, modifying the stem to function as it is supposed to and finally addressing, fixing and masking all those cracks. But now that the project is completed and the pipe is definitely smoke-able and gorgeous looking, I cannot but thank Steve who goaded me in to working on this pipe in the first place and for all the input/ suggestions rendered during the process to help me preserve memories of ancestor.

I wish to thank each one for sparing their valuable time to read through this write up and sharing this journey with me while I enjoyed working on this treasured inheritance.

 

Fashioning a Churchwarden as a Christmas Gift for my Son


Blog by Dal Stanton

One of the advantages of having ‘The Pipe Steward’ in the immediate family is that there’s a very good probability that his gifting patterns might reflect one of his favorite pastimes – restoring pipes!  Over the years, it has given me great joy to gift my loved ones – sons and daughters(!), with pipes that I’ve restored.  There are at least two reasons for this.  First, they receive a beautiful pipe which has been given the TLC that brings it again to a pristine condition – often better than new!  They can enjoy the composite beauty of its shape, grain formations and hues.  Additionally, understanding a pipe’s story through the research and write-up that accompanies each recommissioned pipe adds to the overall appreciation for the pipe.  The pipe itself is the first part of a growing legacy.  Secondly, the fact that the gift has passed through the care and attention of my hands, restoring the pipe’s condition, adds my personal part to the pipe’s legacy.  The ‘Giver’s’ story is added to the pipe and is then associated with the pipe by the loved one that that receives the pipe, becoming its new steward.

My son, Josiah, is coming from St. Louis to join his mother and I for Christmas here in Bulgaria.  He joins his sister, Johanna and her husband, Niko, who have come to Sofia from Nashville.  Both Josiah and Johanna, our two youngest, lived here with us when they were teens.  So, they are coming ‘home’ for Christmas and this is special for them and for us.  Two additional things add to the specialness of this Christmas reunion.  First, Josiah is bringing with him a young lady for mom and dad to meet!  They met in college and have cultivated a relationship.  She’ll be coming to meet his parents….no pressure!  Secondly, Johanna and Niko are also bringing a special gift – we just found out that they are expecting their first little one to add to our growing number of grandchildren!  Gifts are special during Christmas and they come in different ways.  The greatest gift is the reason we celebrate Christmas – God’s gift of his Son, Christ, given to a dying and broken world to bring the gift of life.

For this Christmas, a Churchwarden will be fashioned for Josiah.  I enjoy repurposing forgotten bowls to give them new life by simply mounting them to a long, flowing Warden stem.  The uniqueness of the Churchwarden is that it is not primarily the style of bowl that makes it a Churchwarden, but the length and style of the stem.  From Bill Burney’s description in Pipedia we discover this information.I found two bowls in my box that held CW potential.  A petite ‘Made in England’ Bent Billiard with the shape number 950 on the shank.  No other markings.  It’s a classic petite English pipe which is attractive by itself, but so far, no one has shown interest in adopting him from the ‘For “Pipe Dreamers” Only!’ online collection where pipe men and women commission pipes for restoration benefitting our work here in Bulgaria with women and girls who have been trafficked and sexually exploited – the Daughters of Bulgaria (Incidentally, if you go to this link you will see our daughter, Johanna, a few years ago painting a picture depicting our work with the Daughters).  I believe this bowl will serve as a gift for my son-in-law, Niko – next in queue.  The other bowl is a rusticated bowl with the sloppy stamping not fitting the smooth panel on the shank’s left flank.  Here are the candidates.As I evaluated the two, I decided on the rusticated bowl for my son, that is rustic and will give the newly fashioned CW an ‘Ole World’ feel.  I take a closer look at the ‘Rustic’s’ nomenclature.  The sloppy stamping shows ‘ERMOFILTER’ – with ‘’ER” running over onto the metal stem facing and stem, [over] ‘ORTED BRIAR’ (with the ‘IAR’ running over!) [over] ‘ITALY’, the COM.  Undoubtedly, the stamping’s aim was to reveal the name, ‘Thermofilter’ which is not found in Pipedia but Pipephil.eu has this panel of information with a ‘?’ indicating the COM.  The Thermofilter on my work desk adds Italy as the country of origin.I acquired this pipe while in the US a few years back at Madeline’s Antique Store in Manchester, Tennessee, just off Interstate 24.  It was a quick stop as we were traveling through and saw the billboard and decided to stop.  It was a very fruitful detour as I found a Dunhill in the wild and purchased it for a pittance.  In the picture below, the Dunhill (see link for this restoration: Another Wedding Trip Pick: A 1961 DUNHILL EK Shell Briar Made in England 1 4S) is visible (3rd from the bottom) and reminded me that this was on the trip when Johanna and Niko were married!  The Thermofilter is barely visible on the right edge in the pipe stand.I take some pictures of the rusticated bowl to get a closer look and to mark the start. The bowl is a perfect size for a Churchwarden, which tend to be on the diminutive side.  The half bend will provide a great sweeping trajectory for the Warden stem.  The rusticated surface is dirty and needs a thorough cleaning of the crevasses. I’m attracted to the deep burgundy red finish of the briar.  It should clean up very nicely.  To begin the project, an inspection of the chamber reveals almost no cake at all, if any.  I go directly to the Savinelli Fitsall Tool to scrape the sides and then sand the chamber using 240 grade paper wrapped around a Sharpie Pen.  To clean the chamber of debris, I wipe it with a cotton pad wetted with isopropyl 95%.After cleaning the chamber, an inspection reveals no problems with heating cracks or fissures.  Yet, I discover something strange.  On opposite sides of the chamber wall I discover stampings of numbers and perhaps some letters.  I’ve never seen this before and I decide to send a note to Steve to find out if his rebornpipes experience would lend any help. Steve’s response to my inquiry was brief:

Nope never seen that. I have seen small numbers in the bottom of the bowl. Maybe heated like a branding iron. What is the nomenclature?

With no resolution to this mystery, I move on to cleaning the external surface. I clean the rusticated surface with undiluted Murphy’s Oil Soap.  A cotton pad starts the process, but I transition to a bristled toothbrush quickly to clean in the craggy cuts of the rusticated surface.   From the worktable scrubbing, I transfer the stummel to the kitchen sink where I continue to rinse the stummel with warm water and clean the internals using long shank brushes.  With warm water, I add anti-oil dish liquid soap and scrub using the shank brushes.  After rinsing again, returning to the worktable I take the following picture of the cleaned stummel.  I notice that the finish is partially removed from the smooth briar panel holding the nomenclature.To complete the removal of the finish on the panel, I wet a cotton pad with isopropyl 95% and rub the smooth briar panel as well as the smooth briar ring circling the shank end.  This will provide a distinct contrast later during the finishing stage. What I also notice from the soiled cotton pad is that the finish color appears to be an Oxblood hue.     Moving now to cleaning the internals in earnest with cotton buds and pipe cleaners wetted with isopropyl 95%, I find that the mortise is clean!  This doesn’t happen often and I’m thankful for the shortened work!I now transition to fashioning the Churchwarden stem.  The first step is to fashion the oversized tenon of the precast Warden stem.  Using the electronic caliper – which was one of the best additions to my tool chest! – I take a measurement of the mortise diameter which is 7.86mm.  This represents the eventual sizing diameter of the tenon after sanding it down to size.The next step is to cut a starting test cut on the tenon using another great addition to my tool chest – the PIMO Tenon Turning Tool that I acquired from Vermont Freehand (https://vermontfreehand.com/).  I keep the directions on the wall in front of me for easy reference!  Before using the tool, the PIMO kit provides a drill bit to pre-drill the airway of the precast stem to fit the Tool’s guide pin.  After mounting the bit on the hand drill, I drill the airway.  Next, I mount the stem onto the PIMO tool which has replaced the drill bit on the hand drill.  Opening the carbon cutting arm to just a bit smaller than the diameter of the raw tenon, I make an initial cut of the tenon for measurement purposes.  The sizing is 9.79mm.  This is the starting point for sizing down the tenon.  Generally, it’s not a good idea to cut the tenon with the PIMO tool aiming for an exact finished target size (7.86) because of the danger of taking off too much.  It is also true that each fitting tends to be different.  So, the approach is to come to the target sizing in a more patient, conservative pace.  I add about .40 mm to the target size of 7.86 which identifies what I call the ‘fat’ target to aim for with the PIMO tool then transitioning to sanding by hand.  Adding .40mm to 7.86 results in a fat target of about 8.26mm.  This means I need to remove additionally about 1.50mm (9.79 minus 8.26) with the PIMO tool.Using the Allen wrenches to adjust the carbide cutting arm to a tighter cut, I first cut a test and measure.  I want to make sure I’m not over cutting before traversing the entire length of the tenon. And I’m glad that I did the test cut!  The test cut measured 6.72 – smaller than the target size!  The second test cut measures at 8.10mm – falling between the fat target and the target size – I go with it.  I cut the entire tenon as well as cutting into the stem facing just a bit to make sure that the edge is squared and not shouldered from the original precast stem.The cut is ideal.  The tenon is still larger than the mortise so that sanding now will ease into the fit and make it more customized.It doesn’t take too long with sanding for the mortise fully to receive the newly shaped tenon.  A coarse, 120 grade paper is used initially to do the heavy lifting then 240 follows to fine tune.  The fit is good.There is no perfect union and this picture shows the shank facing extending a bit beyond the stem facing.I wrap the shank with masking tape to provide some protection to the rusticated finish as I sand to bring the shank facing and stem into alignment.  As before, focusing on the fitting first, I start with coarse 120 and follow with 240 to sand the junction.    When the junction transitions smoothly from the shank to the stem, I transition to the stem proper.  The picture below shows the casting seam down the side of the stem.  This seam as well as the ripples that are always present in a precast stem are sanded out.After some effort, and a lot of rubber dust(!), the ripples and seams are sanded with coarse 120 grade paper.  These pictures are not easy to see detail, but if ripples remained, they would be evident with the different hues on the stem.Next, I work on the bit and button shaping.  You can see the rough condition of the button and the vulcanite excess on the slot.  The darkening of the vulcanite forming a ‘V’ in the middle of the bit shows how the surface of the precast stem dips as it flares out to the stem edge. This will be filed out and the button shaped using a flat needle file.   The following two pictures show the progress of filing.  To remove the valley dip of the surface, I file down the outside valley ridges that are higher.  At the same time, the filing sharpens the button lip.  The first picture shows the initial lateral filing to bring the bit surface into a more level state.The next picture shows the leveled bit surface after the outer quadrants have been rounded and shaped toward the stem edges.The final filing for the lower bit completed.The slot is rough.  After filing the excess vulcanite to level the slot facing, I see a small divot in the inner edge of the slot which I didn’t picture!  A round pointed needle file fits nicely into the slot allowing uniform filing of the inner slot edges – upper and lower.  With the heavy-duty sanding and filing completed. I use 240 paper to fine tune the bit and button shaping.  At this point, the button perimeter is sanded.I follow the fine tune sanding of the button by sanding the entire stem with 240 grade paper.The next picture was to remind me to remark about how nasty working in rubber dust is!  It, without question, is the least desirable part of fashioning new Churchwardens!  This Bulgarian designed work cloth will be going into the soak tonight!The Warden stem is transitioned to the kitchen sink where 600 grade paper is employed to wet sand the entire stem. During the entire sanding process, the stem and stummel remain joined so that the sanding creates a perfectly uniform union with stem and shank. Before transitioning to the micromesh phase, I file the end of the tenon where excess and rough vulcanite persists.  Using the flat needle file, it is dispatched quickly.The question in my mind is whether to bend the stem now or go directly into the micromesh phase.  By leaving it unbent at this point makes continued sanding easier, and this is what I do. Using 1500 to 2400 grade micromesh pads I wet sand the stem followed by dry sanding with pads 3200 to 4000 and 6000 to 12000.  Between each set of 3 pads I apply Obsidian Oil to condition the vulcanite.  I only show one picture of this process instead of the usual 3 because capturing the detail with the long stem is not possible. I do, however, take close-ups of the upper and lower bit. The next step is to bend the Churchwarden stem.  The goal is to bend the stem so that the end of the stem, the bit, is on a parallel trajectory with the plane of the rim of the stummel.  I sketch a template to help visualize and compare.I use a hot air gun to heat the vulcanite.  I continually rotate and move the stem over the hot air to avoid scorching the stem and to heat more evenly a section of the stem.  To begin, I focus the bend more toward the middle of the stem, where the stem is thicker.  If I heat the entire stem at once the thinner portion at the end of the stem will heat and bend first creating a sharper angle – which I am trying to avoid.  A sweeping bend is what I like best.As the stem is heated, gentle pressure is applied so I know when it becomes supple enough to start bending.  The first step focusing on the middle bend is below.  After I bend it, I hold it in place until I run it under cold water in the kitchen sink to hold the bend.  As expected, the trajectory of the end of the stem is still a little high.  The next step of heating I avoid the middle of the stem and heat the section about 3/4 up the stem – the thinner section.  After heating and bending more, again I take the stem to the sink to cool the stem with water to hold the angle.  The template shows that I’m in the sweet spot.  Notice I inserted a pipe cleaner in the end of the stem to be on the safe side – guarding the integrity of the airway as it bends.  It looks good and I move on. Next, the stummel awaits attention.  After removing the freshly bent CW stem and putting it to the side, I take a fresh look at the rusticated stummel that, to me, resembles craggy tree bark.  I like it! Before addressing the stummel, I first run the smooth briar nomenclature panel and ring around the end of the shank though the full battery of micromesh pads, 1500 to 12000. I like the craggy/smooth contrast.My aim with the stummel is to refresh the hue, which appears to be a subtle Oxblood.  Using Fiebing’s Oxblood aniline dye, I will apply it like I usually do – painting and flaming with a lit candle.  Then, during the following ‘unwrapping’ stage, I will not use Tripoli compound as I usually do.  The reason for this is that the compound will get caught in the crags and that would not be fun to remove.  I think the felt buffing wheel on the Dremel will be enough by itself to effectively unwrap and abrasively buff to remove excess crusty flamed dye.  Creating more contrast in the craggy landscape of the rusticated surface and the smooth peaks of the rustication is the aim.  At least this is my hope!  I assemble my desktop staining kit.  After wiping the stummel with a cotton pad wetted with alcohol to clean it, I warm the stummel over the hot air gun to expand the pores in the briar to help it be more receptive to the dye.  Then, using a bent over pipe cleaner, I apply the Oxblood dye in sections and flame the wet dye with a lit candle.  The alcohol in the dye combusts with the flame and sets the dye in the briar surface. After working through the entire stummel painting and flaming, I set the stummel aside to rest for several hours allowing the dye to set.Later, with a cotton cloth wheel mounted onto the Dremel and the speed set to 40% full power, I apply Tripoli compound only to the smooth briar nomenclature panel and ring around the shank end.Next, I mount a felt cloth buffing wheel onto the Dremel, setting the speed to the slowest possible, and go over the entire surface working the edges of the buffing wheel in the valleys and ridges of the rusticated surface.  The slower speed is to avoid over heating – I don’t want to start a fire with the coarser buffing wheel!I also concentrate on the upper peaks of the ridges that present very small smooth briar surfaces that are buffed.I like the contrasting effect of this process – the changing hues of the Oxblood from valleys to peaks with the smooth briar and rough briar – nice.Not pictured is mounting another cotton cloth buffing wheel onto the Dremel, setting the speed at 40%, and applying Blue Diamond compound only to the smooth briar nomenclature panel and ring around the end of the shank and to the Warden stem remounted to the stummel.  Finally, with another cotton cloth buffing wheel mounted onto the Dremel, set at the same speed, I apply carnauba wax to the entire pipe – stem and stummel. Over the rusticated surface, I increase the speed of the Dremel to about 60% full power to create more heat to dissolve the wax in the rusticated landscape.  This helps in keeping the wax from caking in the rough surface. I finish the newly formed Churchwarden by hand buffing with a micromesh cloth and brushing the stummel with a horsehair brush to raise the shine.

The Oxblood coloring of this rusticated bowl came out exceptionally well. My eyes are drawn to the contrasting of the flecks of smooth reddish briar populating the rusticated landscape.  The rustic feel of the bowl is enhanced by the ring of Oxblood smooth briar transitioning from the rough bowl to the long, black Warden stem.  The Oxblood shank ring contrasting with the stem simply pops.  Of course, the long, sweeping bend of the stem is why every pipe man or woman wants at least one Churchwarden in their collection.  This Churchwarden is heading under the Christmas tree here in Bulgaria as a gift for my son. My joy is completed knowing that in the future, when he pulls it out and fills it with his favorite blend and settles in to have some moments of reflection that he will reflect on this special Christmas in Bulgaria!  Thanks for joining me!  Merry Christmas!

Making the Best of Beautiful Pipe with an Unbelievably Rough Patch of Briar – A Giant Gold Crown Bent Billiard


Blog by Dal Stanton

The story begins when I first laid my eyes on this pipe.  It was when the box containing the ‘French Lot of 50’ arrived here in Sofia, Bulgaria, from Paris, and oh my – talk about excitement!  I was alerted to this online Lot by Romanian pipe man friend, Codruț (aka: Piper O’Beard), who had previously become the steward of an L. J. Peretti Oom Paul I had restored. I carefully and slowly unwrapped each pipe, relishing each moment. I had seen the pipes in a pile displayed by the seller on France’s eBay.  Interestingly, when I unwrapped the ‘Gold Crown Giant Bent Billiard’ now on my worktable, I went back and looked at the eBay ‘pile’ picture with the question, how could I have missed this?  I was attracted to this French Lot because of the many horn stems and several very uniquely shaped pipes – the Cutty on the top had my attention!  Yet, the Gold Crown was not visible.After unpacking and cataloging all the pipes from France, each was pictured and put online in the ‘For “Pipe Dreamers” Only!’ collection where hopeful stewards search for a pipe that speaks their name.  After all, as in Harry Potter’s wand lore, the pipe chooses the steward, not the other way around! Now, pipe man and friend, Cyrus, enters the story when he saw this pipe online in ‘Pipe Dreamers!’ collection.  He and his wife became good friends when they served here in Bulgaria with US Peace Corp for a few years.  After returning to the US, their family grew, and we stayed in touch.  Cyrus was no stranger to ‘Pipe Dreamers!’ having already commissioned and received a very nice Jarl Dublin (See: Refreshing a Jarl 1545 Made in Denmark Dublin) which benefited our work here in Bulgaria with the Daughters of Bulgaria – women and girls who have been trafficked and sexually exploited. His return to Dreamers found him drawn to the Crown Giant Billiard.  Here are pictures of the Giant Bent Billiard: The only markings on this pipe are on the gold band and the ‘tenon ring’.  I have to be honest with full confession – when I first saw this pipe, I was excited about it thinking it might have some historical value.  When it had first come out of the box, I hadn’t taken a good look at it.  When I looked at it again, it was not long after restoring another pipe from this French Lot of 50 which was a treasure.  The writeup was: Discovering the History with the Reclamation of this Petite EPC Majestic Bent Horn Stem Billiard, where my researched uncovered a long-forgotten French pipe manufacturer which resulted in my first submission to Pipedia: A. Pandevant & Roy Co..  The problem, which I have since come to realize more fully, is that one of the trademarks of this French company that disappeared in the late 1930s, based near Paris, was a trademark with the stamp ‘EP’.  The difficulty with this is that it is also now a mark stamped on metals and it simply signifies, ‘Electro Plated’.  When I pulled the acrylic stem out of the mortise and discovered the ‘tenon ring’ with ‘EP’ on it, the novelty of a ‘tenon ring’ and the ‘EP’ stamp with some sort of hallmarks created question – could this be something in line with the Petite EPC?  The gold band was stamped with a crown and a very miniscule stamped letter that I couldn’t make out for certain: GG or GP?  Probably ‘GP’ for gold plated. With questions in my mind about the ‘tenon ring’ and the ‘EP’, I sent my questions off to Steve, Master of Restoration, of rebornpipes.com and not too long after received his replies.

Dal: A strange but interesting huge Bent acrylic stem Billiard with no shank nomenclature and doesn’t appear to ever have been smoked appears to have a gold-plated band.  There are stampings on it – a crown and a very small stamp beneath.  My guess is GG or GP – but it’s so small I can’t be sure.  Then, there is a solo stamp on the opposite side of the band that appears to be the same GG or GP.  Of course, GP could signify Gold Plated.  But perhaps that’s what I want to see!  That’s the band – thoughts?

Steve: I have had gold plated bands on older Weber’s that looked the same. I concur that the GP stamp is gold plated.

 Dal: Then, on the same pipe, I was surprised that when I retracted the ample acrylic stem out of the stummel, there was a band around the tenon!  Have you ever seen anything like this?  The alignment or fit of the stem and shank isn’t great and this band is serving to expand the fit of the tenon in the mortise.  The band also has stampings which I’m assuming are faux of some sort, but the tenon band I’m assuming is an aluminum – it’s light.  I first thought it might be silver, but whoever puts anything of value around a tenon?  Thoughts?

 Steve: I have never seen this before and I can see nothing but problems with this so-called solution. The EP stamp means it is electro plated. Could be silver but looks to like nickel and definitely an aftermarket repair. It is a nice-looking pipe though.  

 It’s so much fun unpacking the package of pipes, one at a time, each one wrapped with newspaper…. Christmas over and over!

Dal

After Cyrus commissioned this pipe and it was getting closer to the worktable, I took a closer look at the pipe trying to figure out its story. The bowl is huge and quite attractive. I weigh the pipe and it comes in at a hefty, 84g. It has never been smoked. The acrylic stem is pristine but needs to be cleaned and receive a fine-tuning regarding sanding and buffing.  The pictures below show ripples where the finishing was not completed or not thorough.The chamber is virgin briar.  The rim shows some roughness – like it wasn’t finished off as well.The craftmanship is not superior. Looking down the mortise, the airway drilling isn’t straight.  Is veers off to the left so that the draft hole’s entry point is not centered, but off to the left a bit. The tenon with the ring, as Steve said, is an attempt to perfect the fit, but after taking the tenon out, I’m not able to put it back in the mortise!  The stem fit from the earlier pictures shows that it’s not good – there is a large gap on the upper side of the shank.  I pry the tenon ring off with a little effort with a pocketknife and try the fit in the mortise without the ring.  The fit is very loose – too loose for use. Carefully I rotate the gold band off the shank with no problem.  It caps the shank with a shank face overhang.  I again insert the stem to see what it looks like. The sizing of the stem is in the ballpark.Then, there’s the mysterious crop of pits and ravines on the left side of the Giant’s bowl – what’s the deal with this?  It’s not a crack or trauma but it appears to be very rough briar that emerged during the fashioning of the stummel from a block of briar – a block of briar that obviously showed great potential for the one crafting this Giant Bent Billiard.  The severity of the briar below is in such contrast to the beauty of the briar on the rest of the pipe!  Such beauty and also such despair!  So much like life….  I’m giving some thought to how to approach this. My theory is that someone, probably in France, crafted this pipe.  The block of briar is beautiful, but the shaping of the stummel revealed the imperfections – but too many to fill, but the crafter went with it anyway hoping for a good ending, attaching an attractive acrylic stem and gold band.  Yet, at the end of the day, no one wanted this pipe with the scarring it bears.  It just seems to me that the crafter of this pipe gave up on it and the fine finishing of the pipe was not worth the effort.  I’m not sure the many grain faults that are in this briar patch can be removed or repaired so that there are no lingering scars, but the beauty of the rest of the pipe can offset the imperfections and scarring – off set, probably not erase fully! It reminds me of the Daughters we work with here in Bulgaria – beautiful but also broken and of great worth and worth the effort.

I decide to address the stem fitting first.  As I looked at the fitting, the tenon ring and stem wobbling in the mortise, my first thought is to expand the acrylic tenon like a vulcanite stem.  This method is to heat the tenon by painting it with the open flame of a Bic lighter and then inserting a slightly larger drill bit end into the softened tenon resulting in some expansion. Two questions come to mind – I’m not sure if acrylic will act like vulcanite – a rubber compound.  Will it expand the same way?  I’m not sure.  The second question is, if it does expand, I’m not sure it will expand enough to de-wobble the current situation?  After puzzling more, the solution came to me after reflecting on shank repairs that both Steve has done as well as Charles Lemon of Dad’s Pipes of utilizing inserts in the airways to connect broken shanks.  The solution was staring me in the face.  The nickel band that was acting as a poor ring for the tenon, could very well serve quite nicely as an insert in the mortise.  It is already sized for the tenon correctly.  I wondered if that was the original intent of the ring, but the crafter never got around to finishing? To test my theory, I slide the ring – now an insert – partially into the mortise, and partially insert the tenon.  I believe this will work nicely. To make the insert permanent, I use BSI Maxi-Cure Extra Thick CA glue.  I place some CA on the inside lip of the mortise then spread it around the circumference using a toothpick.  I then insert the nickel ring and press it down firmly on the table top surface pushing the insert into the mortise. The end of the nickel ring is flush with the shank facing.The insert seats as hoped, but what the picture shows is the pressure of the insert creates a small crack on the shank on the upper left side.  The good news is 3-fold.  First, the crack is very small.  Secondly, the insert on the inside will not expand any further and so the crack should not have additional pressure on it.  Lastly, the gold band on the outside will help fully cover the crack cosmetically and provide additional external pressure to support the shank. To address the crack, I first drill a counter hole to keep the crack from expanding. First, using a sharp dental probe, I press a hole at the end of the crack to serve as a guide for the drill. Next, after mounting a 1mm drill bit on the Dremel, I drill a hole at the end of the crack keeping my hand as steady as possible! The counter-creep hole is good.With the drill bit still mounted in the Dremel, I decide also to drill counter creep holes at the ends of the two most distinct ravines in the rough briar grain patch topography.  While these ravines are not cracks in the sense of a trauma related problems, treating these as cracks to guard against the ravines expanding is a good thing to do it seems. I’ve numbered them below.To prepare for drilling the counter-creep holes, I place guide holes as before using the sharp dental probe.Then I drill holes at the end of each ravine.  No problems.The ravines are deep – surprisingly so!  I double check in the chamber to make sure there are no corresponding ravines!  I see none – it looks good. I make sure the crevasses are cleared of loose stuff that may have collected.  I use a dental probe to clean what I can.  I pick at the smaller grain faults as well. I finish the cleaning by wiping the ravine area and the shank crack with a cotton pad wetted with isopropyl 95%.At this point I would usually mix a batch of briar dust putty with dust and thick CA glue.  Instead, I use only regular, thin CA glue on the shank since it will be covered by the band. With the ravines and the grain faults I’ll use regular thin CA glue and sprinkle them with Briar dust building the patches in steps.  Using the thinner CA glue will allow penetration into the deeper parts of the crevasses forming a more sure foundation.  The pictures show the progress. The night is late, I set the stummel aside for the patches to cure through the night.The next morning, what’s on my mind is seeing how the stem will react to the mortise insert.  The glue will be fully cured and with the insert firmly in place, I give the stem a try.  The fit tightens with the tenon inserted about halfway into the mortise. Not wishing to force the issue, I begin sanding the fat part of the tenon down first using 240 grade sanding paper.  When the progress seemed to be stymied, I then resorted to using a flat needle file to help.After several re-tries and additional filing and sanding, the stem seated in the new insert.  It looks good.  There still seems to be a slightly larger gapping on the top, but I will wait until remounting the gold band to make a final assessment on the stem fitting.With flat needle file in hand, filing begins on the bowl patches. Since this entire area is rife with pits and crevasses, I’m not too concerned about using the needle file down to the briar surface.  Usually, I transition to 240 sanding paper when the patch is close to the briar surface using the file, but with all the sanding that will be required for this project, I use the file for sake of speed.After the filing, I finish the first round of sanding with 240 grade paper.  All the light areas in the area indicate that the briar is not smooth and that pitting remains.  The briar dust created by the sanding packs in the holes which helps to show progress, or lack!Beginning the second round of patching, I again use the probe to excavate the compacted briar dust and then I wipe the area with a cotton pad wetted with alcohol to clean.I repeat the patching process with the same, regular thin CA glue and sprinkle the patches with briar dust.In the interest of full disclosure and brevity of describing the same process repeatedly, I repeated the patching process as described above about three more time and made slow progress eradicating the pitting.  I found though, that some of the pits would resist holding the CA glue fill.  After filling with CA glue, curing and sanding, the pit would remain.  I started testing different approaches – I used CA glue, then kneaded the patch with a toothpick to release possible air pockets hindering the glue from filling and holding the crevasses.  I also utilize an accelerator before and after applying CA.The solution that I found that seemed to work the best was not using the regular, thinner CA glue but switching to an extra-thick CA glue in combination with an accelerator.  In the picture below, on this pass of patching (I’ve lost count), I’ve painted a patch of very small grain faults with the thick CA using a toothpick to spread. After using the accelerator and allowing it a few minutes to cure, I go to work on the patch with the file.  I did this method several times to fill in the grain faults as much as I could.At the end of the day, perfection is not achievable.  Yet, the lion’s share of faults have been filled and hugely minimized but some scarring remains.  After finishing the patching and filing, I go over the area with 240 grade paper followed by 600 grade paper. I think that the area is much better, and the finishing process will continue to blend and mask the rough briar patch – I hope!  I move on – finally 😊.Moving now to the top, the rim has some rough spots which are easily dispatched with the topping board.  I first place a sheet of 240 grade paper on the chopping board, my topping board.  I rotate the inverted stummel on it several times, checking as I go.  I then switch to 600 grade paper.  The rim is looking good.  Moving on. Next, using sanding sponges I continue the sanding of the stummel.  I use a coarse sponge, followed by a medium grade then finish with a light grade.  Wow, comparing the two side in the pictures below, ugh!Moving straight away to the micromesh pad regimen, with pads 1500 to 2400 wet sanding is then followed with dry sanding with pads 3200 to 4000 and 6000 to 12000.  Wow!  What a piece of briar!  Other than the area where the grains were pitted, the grain is absolutely striking on this goliath. Without doubt, if not for the rough patch of briar – that has been helped immensely, I would be applying Before & After Restoration Balm now and moving to the finer polishing processes.  But with the rough briar patch, applying a darker dye will assist in masking the many patches.  I decide to mix Fiebing’s Saddle Tan and Dark Brown – about 2 to 1 ratio.  I want a darker brown hue but with the reddish hints that the Saddle Tan will brings.  After ‘unwrapping’ the initial coat, I may decide to do a straight Saddle Tan overcoat. I assemble my desktop dyeing module.  After mixing the dyes to the ratio I described using the large eye dropper, a cotton pad wetted with isopropyl 95% is used to clean the stummel.  The end of a spring-loaded clothes pin inserted into the mortise serves as a handle. The stummel is warmed using a hot air gun to expand the briar grain helping it to be more receptive to the dye. After heated, using a folded over pipe cleaner, the dye is painted onto the stummel in swatches and then, using a lit candle, the wet dye is ‘flamed’.  The aniline dye’s alcohol base combusts and leaves the hue behind in the briar grain.  After methodically covering the entire stummel with dye and firing as I go, I then set the stummel on a cork in the candle holder to let it rest through the night.With the dyed stummel now on the sideline, I turn to the attractive acrylic stem.  As I mentioned earlier, the stem is essentially unused, but it doesn’t appear to be in a pristine state.  The finishing left ripples and some rough spots on the stem.  I take a few pictures to illustrate what I’m seeing.To address these issues, I sand the entire stem using 240 grade paper then follow by wet sanding with 600 grade paper and finish this phase by applying 000 grade steel wool.  I like the results!  The acrylic surface has cleaned up nicely. Moving on now to the full regimen of micromesh pads, starting by wet sanding with pads 1500 to 2400 and dry sanding with 3200 to 4000 and 6000 to 12000. I apply Obsidian Oil to the stem after each set of three pads. This stem is spectacular!  The shine and that acrylic translucence is eye catching.  The stem will wait till the morning for the stummel to be ready to go. The next morning has arrived and I’m looking forward to ‘unwrapping’ the dyed stummel to see how the finish came out and how well it has helped mask the rough briar patch.  I mount a felt cloth buffing wheel onto the Dremel, reduce the speed to the lowest possible and apply Tripoli compound to the bowl.  The speed is reduced to decrease the friction and heat generated.I’ve developed this technique that works very well for me.  The following pictures show the process of removing the flamed crust to reveal the grain beneath. It takes patience to move over the surface and spotting the places where dye is still thick.  Usually it looks like a dark spot on the surface.  When I apply additional rotations with the Tripoli on these areas the excess dye is removed revealing the different grain compositions – the softer wood absorbs the dye while the harder wood doesn’t – these are the lighter grains.After unwrapping the stummel, I wipe the surface with a cotton pad wetted with alcohol.  I do this to blend the new dye as well as to lighten the hue.  Lightening the hue a bit softens the finish.Next, after mounting a cotton cloth wheel and adjusting the speed of the Dremel to about 40% full power, I apply Blue Diamond to both the stummel and the rejoined stem.  Yes, I am not replacing the gold band until the end of the process.After completing the compounds, I buff/wipe the pipe with a felt cloth to remove the compound dust in preparation for the wax.  Not pictured is mounting another wheel, maintaining the speed, and applying carnauba wax to the pipe.I have two remaining mini projects before the final hand buffing.  First, to remount the gold-plated band.  I first clean the band using Tarn-X tarnish remover.  It restores a very nice shine to the metal. The band fits over the shank easily about 70% of the way, but to be on the safe side, I use the hard surface cushioned by a few cotton pads to press the band fully on the shank.  The band fit easily the rest of the way with a gentle push.With the band fully seated on the shank, I test fit the stem with disappointing results.  In the picture below the gap at the top is huge. With the band easily moving on the shank, I partially retract the band off the shank and then reengage the stem so that the stem pushes the band over the shank.  With the band pressed with the stem tenon facing, its orientation is now much more favorably aligned with the stem with the gap minimized.  This looks much better as the second picture shows.The next step is to apply some CA glue to the inside of the band and repeat the same process of reseating the band using the stem itself. Using BSI Maxi-Cure Extra Thick CA glue, I place a large drop of glue on the inside of the band and then use a toothpick to spread the glue around the circumference of the inner wall of the band.  Then, after slipping the band carefully over the end of the shank, I press the stem forward over the shank keeping the facing of the stem squarely on the band to avoid the gapping.  When the band starts to gap, I know I’m far enough.  I retract the band slightly with the stem firmly seated and essentially no gap present.  Not wanting to get CA glue on the tenon, I remove the stem and set the stummel in an egg crate to allow the glue to cure.  The results look good!While the CA glue is curing, I move to the final project.  In order to provide the virgin briar in the chamber a good foundation to build a protective cake and for aesthetics, I mix a batch of natural yogurt and activated charcoal.  This mixture is applied to the chamber wall and it hardens to provide a layer over the briar. A pipe cleaner is inserted into the airway to guard the draft hole from being blocked.  When I inserted the pipe cleaner, what I remarked about earlier regarding the off-center drilling of the air way was illustrated graphically by the angle of the pipe cleaner!  These pictures show what I’m seeing.I place a small amount of natural yogurt in a small dish and add activated charcoal to it and mix until it thickens enough not to drip off the spoon.  With a pipe nail as a trowel, I scoop the mixture into the chamber and spread it on the chamber wall with the back side of the nail. When the wall is totally covered, I set the stummel aside allowing the mixture to dry and harden.  My day has come to an end and the lights are turned off. The next morning, the gold band is solidly in place and the yogurt/charcoal coating is dry and hard.  After reattaching the stem, I give the pipe a rigorous hand buffing to raise the shine.

I’m pleased with how far this unmarked, gold band Giant Billiard has come.  The rough briar patch on the side of the bowl was a mess and took a lot of time to provide the healing that I see.  Yet, there remains some pitting from the briar faults.  The dark stain does a great job helping to mask the imperfections.  Yet, as with life, this pipe will carry with it some of the scars of its past.  However, the briar grain on this bowl is beautiful and it is huge!  I’m very pleased with the striking difference the darker brown finish provides – it changes the disposition of the entire pipe presentation.  There is now, I believe, a more striking contrast with the gold band which transition into the stem with all the same tones of color.  I like it.  Reseating the acrylic stem with the insert works well and the Crown Gold Giant Bent Billiard will sit very well in the palm of its new steward.  Cyrus saw the potential of this Giant and commissioned it.  He will have the first opportunity to claim it from The Pipe Steward Store.  Thanks for joining me!

 

Restoring and Replacing a Broken Tenon on a Scandia 263 Danish Freehand


Blog by Steve Laug

I am currently not taking on anymore restoration work from the internet or groups that I am part of on Facebook because of the large amount of estate pipes that I am working on to sell. But I have my name in at a local pipe shop here in Vancouver, British Columbia to do repair work for the shop as it comes in. there are no other pipe repairers in Western Canada that I am aware of so I feel a bit of an obligation to take care of these folks as they come. Fortunately there are not a lot of referrals but periodically they get pipemen or women stopping by with work – that is where I come in. They give them my number and email and then the repair work is between us. On Wednesday this week I received an email from one of their customers, Ron in Victoria, B.C. about a pipe that had been dropped and had a broken tenon. He described the broken stem and that left me with some questions. I had him send me photos of the broken pipe so I would be sure to have a clear picture of the issues. He said that the shank was not cracked and really the only issue was the tenon. He send the photos below so I could see what he was speaking of. Not too big an issue really – a cleanup and tenon replacement and the pipe would be good to go.After our emails back and forth he put it in the mail to me. It arrived on Friday and I took it out of the box to see what I was going to be dealing with on this pipe. Descriptions and photos are one thing but I like to have the pipe in hand to examine for myself. This is what I saw. The pipe was dirty and dull looking. There was some faint stamping on both sides of the shank. It was stamped Scandia over Made in Denmark on the left side and had the shape number 263 on the right side. There was a very uneven cake in the bowl that was crumbling. The tenon had snapped off almost smooth against face of the stem. The stem had some tooth marks and was oxidized. There was a faint SC on the left side of the saddle. It appeared that someone had tried to glue the tenon back on the stem – unsuccessfully. There was a lot of sloppy glue on the end of the stem and tenon. I took some photos of the pipe as it looked when it arrived. He had taped the broken tenon on the underside of the stem. The bowl itself was dirty with a crumbling cake about half way up the bowl from the bottom. The plateau rim top had tars and some darkening on the right top and edges. There was a large sandpit on the left side of the bowl near the rim and one on the underside of the shank that would need to be dealt with.  I removed the taped on broken tenon from the stem. I used a Dremel and sanding drum to take down the sharp edges of the old tenon remaining on the face of the stem. I wiped the face down with acetone on a cotton swab to remove the old glue. It was a sticky mess but came off quite easily with the acetone. When it was clean I used a series of drill bits to drill out the airway to accommodate the new threaded tenon. I usually start with a drill bit slightly larger than the airway and work my way up to the one that fits the tenon end. I used my cordless drill and the airway as the guide for each successive drill bit. This keeps things lined up.Once I have the airway drilled to accommodate the end of the tenon. I use a tap to thread new airway. The tenon replacements I use have a hip around the middle that I need to take down. I use a Dremel and sanding drum to smooth things out. I also rough up the threads to reduce the diameter to make room for the glue that I use to set the tenon in the stem.I used a needle file to smooth out the slight ridge at the end of the tenon. I sanded the tenon smooth to clean up the fit. I would further polish it once it was in place in the stem. I dribbled some Krazy glue on the threads and quickly turned it into the stem making sure that the alignment was correct.I took photos of the new tenon before I polished and finished it. The tenon is solid and the alignment in the shank is perfect. I set it aside to cure and turned my attention to the bowl.With the stem repaired I remembered that Ron had asked me to give him some background information on the brand so I paused at this point to gather the info. I turned to Pipephil’s site (http://www.pipephil.eu/logos/en/logo-s4.html) to get a quick overview. As expected the Scandia brand is a Stanwell second line. In this case the sandpits make it clear why it has this designation. I have included a screen capture of the pertinent section from the site.I turned then to the section on Pipedia that dealt with the Stanwell Sub-brands the Scandia pipe listed there (https://pipedia.org/wiki/Stanwell#Sub-brands_.2F_Seconds). I followed several other links listed on the article to check who designed this particular shape for Stanwell (https://pipedia.org/wiki/Stanwell_Shape_Numbers_and_Designers). Bas Stevens, a dear friend who know longer is living compiled a list of the shape numbers and their designer. The 263 was not listed there however, I remembered that the shape was actually a Stanwell shape 63. That shape was a Freehand with a plateau top and a saddle mouthpiece and was designed by Sixten Ivarsson.

To verify that my memory was correct I did a quick Google search for images of the shape 63 for comparison purposes. I include the photo below with thanks to http://www.Bollitopipe.it for the image (https://www.bollitopipe.it/en/hand-made-polished-royal-guard/18983-stanwell-royal-guard-63-bark-top.html). You can see that the shape is identical so that it is clear that the 263 and the 63 are the same shapes.With the background information gathered and summarized I turned my attention to the cleanup of the bowl. I reamed the crumbling and uneven cake out of the bowl. I left a very thin cake on the walls of the bowl. I cleaned up the small bits toward the bottom of the bowl with a Savinelli Fitsall Pipe knife. I finished by smoothing out the slight cake on the walls with a piece of 220 grit sandpaper wrapped around some doweling. I a soft bristle brass brush to clean off the debris in the plateau finish on the rim top. I was able to remove most of the darkening at the same time. While not flawless it looks significantly better.To clean the surface of the briar and remove the oils and dirt I scrubbed the briar with a tooth brush and undiluted Murphy’s Oil Soap. I rinsed off the bowl under warm water and dried it off with a soft cotton cloth. The finish looks much better with stunning grain. The sandpits are quite visible now that the pipe is clean. I repaired the sandpits with a few drops of Krazy Glue. I slightly overfill the pit with the glue as it shrinks as it cures. Once the repairs cured I sanded them with 220 grit sandpaper to blend them into the rest of the bowl. I polished the entire bowl with 400 grit wet dry sandpaper in preparation for the micromesh polishing. I polished the briar with micromesh sanding pads – wet sanding with 1500-12000 grit pads. After each pad I wiped the bowl down with a damp cloth to remove the sanding dust. The photos tell the story. I used a black Sharpie pen to darken in the deep grooves on the plateau as it would help to mask the darkening on the right and left side of the rim top and it would highlight and give depth to the finish. I rubbed the bowl down with Before & After Restoration Balm. I worked it into the surface of the plateau rim top and the rest of the briar with my fingertips and a horsehair shoe brush to clean, enliven and protect it. I let the balm sit for a little while and then buffed with a cotton cloth to raise the shine. I really like watching the Balm do its magic and bring the briar alive. With the bowl finished I turned my attention to polishing the stem. I sanded the surface of the stem with 220 grit sandpaper and 400 grit wet dry sandpaper to remove the remaining oxidation in the vulcanite and the last of the light tooth chatter.  I polished the stem with micromesh sanding pads – wet sanding with 1500-12000 grit pads. I wiped the stem down after each sanding pad with Obsidian Oil. I used some liquid paper to touch up the “SC” on the left side of the stem. I applied it and let it dry and cure. Once it had cured I scraped the excess off with a tooth pick. The “SC” looks very good.  I polished it with Before & After Pipe Stem Polish – both Fine and Extra Fine. Once I had finished the polishing I gave it a coat of a new product I am experimenting with from Briarville Pipe Repair. It is called “No Oxy Oil” and it is made to protect the stem from oxidizing. I set it aside to dry.I am happy with how this pipe looks compared to what it looked like when it arrived in pieces. It definitely has that Stanwell look to it – very Danish Freehand looking. I am excited to be on the homestretch with it and took it to the buffing wheel and polished it on the wheel with Blue Diamond to polish out the scratches in the briar and the vulcanite. I gave the bowl and the stem multiple coats of carnauba wax. I buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The pipe polished up pretty nicely. The grain really pops with the wax and polish. The shiny black vulcanite stem is a beautiful contrast to the blacks and browns of the bowl and shank. This Scandia Made in Denmark Freehand was fun to bring back to life. It really is stunning piece of briar whose shape follows the flow of the grain. The pipe is comfortable pipe to hold in the hand. The finished pipe is shown in the photos below. The dimensions of the pipe are Length: 5 ½ inches, Height: 2 inches, Outside diameter of the bowl: 1 ¾ inches, Chamber diameter: ¾ of an inch. This beautiful pipe will be going back to Ron tomorrow. If the mail is as fast as it was bringing it to me he should have it in hand by the first part of the week. I hope that he enjoys this beauty and that it serves him well. Thanks for reading this blog and my reflections on the pipe while I worked on it. This is an interesting one to bring back to life.

Life for a Republic Era Peterson’s “Sterling Silver” 68 from Bob Kerr’s Estate


Blog by Steve Laug

I am working on another pipe from Bob Kerr’s estate, another one of his Petersons. It is beautiful bent billiard with a taper stem. It is a large pipe that has some amazing grain on the briar. I have restored nine of his Peterson pipes and two of these were Peterson’s pipes made specifically for import into the Canadian market – one was a Kapruf 54 sandblast bent billiard (https://rebornpipes.com/2019/08/09/back-to-bob-kerrs-estate-another-canadian-import-petersons-kapruf-a-54/) and the other was a Kapruf 9BC 56 (https://rebornpipes.com/2019/08/09/back-to-bob-kerrs-estate-linking-petersons-kapruf-9bc-with-the-56-shape-number/). These were interesting that they had a unique numbering system designed for Petersons pipes that were specifically brought to Canada by the Canadian importer, Genin, Trudeau & Co. of Montreal, Quebec. I have included the links on that company below. (https://rebornpipes.com/2016/09/13/petersons-pipes-brochure-from-genin-trudeau-co-montreal-quebec/). I restored an English Made Peterson’s System ‘0’ 1307 bent billiard a  (https://rebornpipes.com/2019/08/17/an-english-made-petersons-system-0-1307-bent-billiard-from-bob-kerrs-estate/) and a Republic Era Peterson’s Flame Grain Bent billiard with a fishtail stem (https://rebornpipes.com/2019/08/16/a-petersons-flame-grain-x220s-bent-billiard-from-bob-kerrs-estate/).

I have been enjoying working on these Petersons particularly because Jeff has done such a thorough cleanup of them before I receive them. When I took it out of the box of the pipes that Jeff had cleaned up and sent back to me, I could see that it was stamped Peterson’s “Sterling Silver” on the left side of the shank next to the band. The right side of the shank was stamped Made in the Republic of Ireland over the shape number 68. It has some stunning grain around the bowl and shank under the thick grime. There was a thick cake in the bowl with remnants of tobacco stuck on the walls. There was a fair lava overflow on the rim. The top and edges of the rim looked good under the grime. It appears that there may be some damage on the inner edge on the left front. I think that there was a beautiful pipe underneath all of the buildup of years of use. The band is stamped Peterson’s over Dublin followed by Sterling Silver on the left side. On the underside are three hallmarks – The Hibernia stamp, the Crowned Harp stamp and finally the letter “O”. The stem was oxidized and calcified toward the end with some tooth chatter but surprisingly it did not have the deep tooth marks that I have come to expect from Bob’s pipes but the button edges were worn. Jeff took photos of the pipe before he started his cleanup work on it. Jeff took photos of the bowl and rim top to show the thick, hard cake in the bowl and the lava build up on the top of the rim and the edges of the bowl. The rim top, with the inner bevel appeared to be in good condition with a potential burn marks on the left front. The outer edges of the rim also appeared to be in good condition. Jeff took photos of the sides and heel of the bowl to show the condition of the finish. You can see the beautiful birdseye grain on the front and the heal. The flame and mixed grain on the back and sides of the bowl and shank. Even under the dirt and debris of the years it looked very good. Jeff took photos of the stamping on both sides of the bowl and shank. The vertical stamping on the left side was readable as you can see from the photos. It read Peterson’s “Sterling Silver”. The stamp on the right side read Made in the Republic of Ireland with the shape number 68 underneath and toward the bowl.The band was also stamped in the silver. Jeff took photos of the stamping. On the left side of the band/ferrule it is stamped Peterson’s Dublin. As the pipe is turned it reads Sterling Silver. Finally on the underside it is stamped with three hallmarks -1. Hibernia, 2. Crowned Harp and 3. The letter “O”. I will need to look that up during the restoration. Jeff took photos of the top and underside of the stem showing the tooth chatter, scratching and oxidation on the stem surface and wear on the edges of the button. I turned to a Peterson Catalogue that I have on rebornpipes and looked up the Classic Range Sterling Silver pipes (https://rebornpipes.com/tag/peterson-hallmark-chart/). I have put a red box around the shape 68 pipe shown in the catalogue page shown below.I turned first to Pipephil’s site to reacquaint myself with the Sterling Silver. Unfortunately there was no information to be found on this specific line. I then turned to Pipedia’s article on Peterson pipes to see what I could garner from that information. It is a great read in terms of the history of the brand (https://pipedia.org/wiki/Peterson). I have included a bit of the pertinent history here.

1950 – 1989 The Republic Era  – From 1950 to the present time, the stamp for this era is “Made in the Republic of Ireland” in a block format generally in three lines but two lines have been used with or without Republic being abbreviated.

During the 1950’s and 60’s the Kapp & Peterson company was still in the ownership of the Kapp family. However 1964 saw the retiral of the company Managing Director Frederick Henry(Harry) Kapp.

In the 1960’s Peterson hallmarked all gold mounted pipes but apparently they used their own marks on silver. This practice stopped at the end of that decade when they started to have all silver bands hallmarked.

  • With that information in hand I knew what I was dealing with in terms of the stamping on the pipe. It is a 1980 Republic Period pipe. I also wanted to be able to interpret the hallmarks on the silver band. I have captured a portion of the chart that include below that helps to clarify the meaning of each of the three hallmarks. I like the Hallmark feature on the higher end Peterson pipes with Sterling silver bands. It helps to pin down the date even further.

  • “Hibernia” seated, arm on harp represents Ireland (country of manufacture). There have been minor design changes over the years.
  • The “Harp Crowned” is the fineness mark denoting the high quality (purity) of the silver, and was used in a variety of designs until October 1992 when it was replaced by the new European Standard or Millesimal mark which gives the purity or quality of the silver in parts per thousand.
  • The Date Letter Code for the year in which the silver was hallmarked (see the chart below). In certain years a fourth hallmark is applied – for example 1966 – a Sword of Light for the 50th anniversary of the Easter Rising 1973. There were also other marks used for the fourth hallmark.

The pipe on my table had the Hibernia seated mark (Ireland) followed by the Harp Crowned signifying Sterling Silver percentage and finally in this case a lower case “o”. Each of the hallmarks was in an octagonal cartouche. The chart below helps me identify the date mark to 1980. I have highlighted the 1980 mark with a red arrow in the chart below.

I have included the entire Hallmark chart for ease of reference show any of you be looking to date the pipes that you are working on at present.I took photos of the pipe with the right stem. With over 125 pipes to clean from Bob’s estate I am very glad for Jeff’s help cleaning them. He remembers this pipe as one of the really dirty ones in Bob’s estate. He cleaned this filthy pipe with his usual penchant for thoroughness that I really appreciate. This one was a real mess and I did not know what to expect when I unwrapped it from his box. He reamed it with a PipNet pipe reamer and cleaned up the reaming with a Savinelli Fitsall Pipe Knife. He scrubbed out the internals with alcohol, pipe cleaners and cotton swabs until the pipe was clean. He scrubbed the exterior of the bowl with Murphy’s Oil Soap and a tooth brush to remove the grime and grit on the briar and the lava on the rim top. The finish looks very good with great looking grain around the bowl and shank. Jeff soaked the stem in Before & After Deoxidizer to remove the oxidation on the rubber. When the pipe arrived here in Vancouver for the second stop of its restoration tour I was amazed it looked so good. I took some close up photos of the rim top and also of the stem surface. I wanted to show what an amazing job Jeff did in the cleanup of the rim top. The rim top was burned and darkened on the left front inner edge. I also took close up photos of the stem to show the lack of tooth marks and chatter on the stem surface. It was very clean.   One of the things I appreciate about Jeff’s cleanup is that he works to protect and preserve the nomenclature on the shank of the pipes that he works on. The stamping on this one was very faint to start with so I was worried that it would disappear altogether with the cleanup. He was not only able to preserve it but it is clearer than shown in the earlier photos. I took some photos to show the clarity of the stamping. I have noticed that many restorers are not careful to protect the stamping in their cleaning process and often by the end of the restoration the nomenclature is almost destroyed. I would like to encourage all of us to be careful in our work to preserve this as it is a critical piece of pipe restoration!   I also have included a photo of the cleaned up hallmarks that were noted above.    Since this is another pipe Bob’s estate I am sure that some of you have read at least some of the other restoration work that has been done on the previous pipes. You have also read what I have included about Bob Kerr, the pipeman who held these pipes in trust before I came to work on them (see photo to the left). Also, if you have followed the blog for long you will already know that I like to include background information on the pipeman whose pipes I am restoring. For me, when I am working on an estate I really like to have a sense of the person who held the pipes in trust before I worked on them. It gives me another dimension of the restoration work. I asked Brian if he or his wife would like to write a brief biographical tribute to her father, Bob. His daughter worked on it and I received the following short write up on him and some pictures to go along with the words including one of Bob’s carvings. Once again I thank you Brian and tell your wife thank you as well.

I am delighted to pass on these beloved pipes of my father’s. I hope each user gets many hours of contemplative pleasure as he did. I remember the aroma of tobacco in the rec room, as he put up his feet on his lazy boy. He’d be first at the paper then, no one could touch it before him. Maybe there would be a movie on with an actor smoking a pipe. He would have very definite opinions on whether the performer was a ‘real’ smoker or not, a distinction which I could never see but it would be very clear to him. He worked by day as a sales manager of a paper products company, a job he hated. What he longed for was the life of an artist, so on the weekends and sometimes mid-week evenings he would journey to his workshop and come out with wood sculptures, all of which he declared as crap but every one of them treasured by my sister and myself. Enjoy the pipes, and maybe a little of his creative spirit will enter you!

Now with all of the background on the line and the background on Bob Kerr it was time to get on with the restoration of this beautifully grained Peterson’s “Sterling Silver” 68 Bent Billiard. I am really coming to appreciate the hard cleanup work that Jeff did on these pipes. They were a real mess when I sent them to Jeff and I have to tell you it was great that I did not need to clean this pipe. I decided to start the process by cleaning up the left front inner edge of the rim top. I used a folded piece of 220 grit sandpaper to smooth out the edge and give it a bevel.I polished the briar with micromesh sanding pads – wet sanding it with 1500-12000 grit pads and I wiped the bowl down after each sanding pad with a damp cloth. The bowl began to take on a finished shine.  I used Mahagony and Cherry stain pens to restain the rim top. The combination blends with the stain on the body of the bowl.I rubbed the bowl and rim down with Before & After Restoration Balm. I worked it into the surface of the briar with my fingertips to clean, enliven and protect it. I let the balm sit for a little while and then buffed with a cotton cloth to raise the shine. I really like watching the Balm do its magic and bring the briar alive. The stem was in such good condition that I could skip working on it with sandpaper and went directly to polishing it with micromesh sanding pads – wet sanding with 1500-12000 grit pads. I wiped the stem down after each sanding pad with Obsidian Oil. I polished it with Before & After Pipe Stem Polish – both Fine and Extra Fine. Once I had finished the polishing I gave it a coat of a new product I am experimenting with from Briarville Pipe Repair. It is called “No Oxy Oil” and it is made to protect the stem from oxidizing. I set it aside to dry. I used some liquid paper to touch up the P on the left side of the stem. I applied it and let it dry and cure. Once it had cured I scraped the excess off with a tooth pick. The P looks very good.I polished it with Before & After Pipe Stem Polish – both Fine and Extra Fine. Once I had finished the polishing I gave it a coat of a new product I am experimenting with from Briarville Pipe Repair. It is called “No Oxy Oil” and it is made to protect the stem from oxidizing. I set it aside to dry. As usual at this point in the restoration process I am excited to be on the homestretch. I look forward to the final look when it is put back together, polished and waxed. I put the bowl and stem back together. I polished the bowl and stem with Blue Diamond to polish out the scratches in the briar and the vulcanite. I gave the bowl and the stem multiple coats of carnauba wax. I buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The pipe polished up pretty nicely. The grain really pops with the wax and polish. The shiny black vulcanite stem is a beautiful contrast to the browns of the bowl and thick shank. This Peterson’s “Sterling Silver” 68 Bent Billiard was another fun pipe to work on thanks to Jeff’s cleanup work. The pipe almost looks unsmoked. The “Sterling Silver” has a silver Band/Ferrule that is hallmarked and works as a contrast between the stem and the briar and binds it all together. It really is another stunning piece of briar whose shape follows the flow of the briar. The pipe is comfortable pipe to hold in the hand. The finished pipe is shown in the photos below. The dimensions of the pipe are Length: 6 inches, Height: 2 inches, Outside diameter of the bowl: 1 ¼ inches, Chamber diameter: ¾ of an inch. This beautiful pipe will be going on the rebornpipes store if you would like to add it to your collection and carry on Bob’s legacy. If not, I have a lot more of Bob’s estate to work on of various brands. Perhaps one of those will catch your attention. Thanks for reading this blog and my reflections on the pipe while I worked on it. This is an interesting estate to bring back to life.

A Project  Close to My Heart;  Restoring a Dunhill from Farida’s Dad’s Collection


Blog by Paresh Deshpande

The next pipe that I have selected as my new project is a very special pipe for the following reasons:-

(a) Firstly, this pipe was in the trust of an adventurer who has been on expeditions to Antarctica, the Arctic and loved Dunhill pipes (and I happen to carry forward that trust with one of his Dunhill pipes).

(b) Secondly, is the reason why and how this pipe came to me. During one of the many Face Time chats with Steve more than a year ago, I remarked that in spite of the huge collection of British, American and Danish pipes that I had inherited, there was not a single Dunhill pipe in it and that how expensive it was to own one. Steve had then only recently acquired an estate lot that contained, amongst other pipes, seven Dunhills. We discussed each of the Dunhill and I zeroed in on one. A few days later, I received a parcel from Steve that contained the Dunhill pipe that I had selected and along with it came another Dunhill in classic Billiard shape. A call to Steve confirmed that the second pipe was not an error, but a surprise for me. He conveyed that should I decide to and thereafter be able to restore it; I could keep it!!

(c) Thirdly and most importantly, I treat this restoration as a tribute to the daughter who loves her father and desired to share that love and those memories with other pipers who wished to carry forward her father’s trust.

Well, with this as a background, the pipe on my work table once belonged to Late Mr. John Barber. His daughter, Farida had requested Steve to restore her Dad’s pipe and pass them on to others for her. Here is the link to the pipe that I had selected for carrying forward the trust of John Barber:-

https://rebornpipes.com/2018/07/07/faridas-dads-pipes-5-restoring-a-dunhill-root-briar-56-bent-billiard/

The above blog makes for a very interesting read to know the personality of Late Mr. John Barber and his adventures as conveyed by his daughter, Farida. The below picture has been picked from the above blog which Steve had done and the pipe that I had selected from Farida’s Dad collection (indicated with a yellow arrow) and the one now on my work table has been marked in blue circle.As with few other pipes from John Barber’s collection, this pipe too has very worn out and faint stampings. Under magnifying glass and bright light one is able to make out the very faint stamping on the left of the shank as “# 197” followed by “DUNHILL” over “BRUYERE”. On the right side the very faint stamping that is visible is “ENGLAND” and a circled “4” followed by the letter “A”. The high quality vulcanite stem bears the trademark Dunhill white dot.To be very honest, I am not very keen to ascertain the vintage of this pipe and lack of stampings don’t help either, since I know that all the pipes that belonged to Farida’s father are from 1950s to 1970s. Having worked on eight Dunhill pipes from my Mumbai Bonanza and researched each one, I roughly know that a Dunhill Billiard with long tapered bit with shape code # 197, similar to what I have on my work table, is from the period 1950 and 1969. This corresponds with other pipes that Steve had worked on from this collection.

I now move ahead with my initial visual inspection as it helps me chalk out a rough path or sequence that I would follow during restoration and also the processes that I would have to employ at each stage of restoration.

INITIAL VISUAL INSPECTION
This is indeed one pipe which I would have not have selected and worked on in the first place, even though it is a Dunhill, but for the provenance of this pipe and for the reasons mentioned above. The stummel is covered in dirt and grime of decades of uncared for use and storage. The stummel is very sticky to the touch and appears to be smothered in some kind of lard, could it be whale fat or fish oils from the Arctic or Antarctic expeditions that it had accompanied the previous owner? I would not know, but it is all prevalent over the stummel surface. Underneath all this lard, dirt and grime, the highest quality of the briar and solid feel in hand for which Dunhill pipes are renowned, can be seen and be felt. Beautiful cross grains along the shank bottom, front and back of the stummel await to be revealed in all their glory. Similarly, lovely bird’s eye grains on both the sides of the stummel should show up nicely when the surface is cleaned. A distinct patch on the left and right side of the stummel is prominently seen which could have been caused due melting of the lard (?) from the warmth and holding of the stummel while smoking. There is a prominent crack on either sides of the stummel extending downwards from the rim outer edge towards the heel for a few millimeters and is marked in red circle. The front and foot of the stummel is peppered with dents and dings. These should be addressed to a great extent when I sand the stummel surface to get rid of all the sticky substance and grime. Coming on to the assessment of the rim top surface and the chamber, it is immediately apparent that this is where the maximum damage lies!!!! There is an even layer of thick cake and appears to have been partially reamed before being stowed away. The rim top surface also appears to have been topped to address the severe charring to the inner edge of the rim at 6 o’clock and 12 o’clock direction (marked in red circle) and at the outer edge towards the front and back end of the stummel (marked in green semi circle). The inner edge is completely out of round and is at its thinnest in the 6 o’clock direction and along the left side of the chamber. A crack (marked with yellow arrow) is clearly visible on the left side atop the rim top surface in 9 o’clock direction which extend in to the chamber as well as to the outside as described in stummel condition above. The topped rim surface is considerably darkened and appears to have absorbed copious amounts of oils and tars. I plan to extract these oils through a salt and alcohol soaking of the chamber. The condition of the inner walls of the chamber will be ascertained only after the cake has been taken down to the bare briar. However, I envisage heat lines and fissures all over the inner walls what with the pipe being subjected to some serious use! And the smell of St. Bruno tobacco, Farida’s Dad’s favorite tobacco, is all pervading and super strong. The shank and mortise is completely clogged with accumulated oils, tars and grime and air flow is laborious to say the least. The edges of the shank end are out of round resulting in shouldering effect once the stem is seated in to the shank. The seating of the stem also appears to be a bit skewed towards the right side by a minuscule margin though not easily noticeable.The vulcanite stem has calcium depositions on either sides about an inch and a half from the button edge towards the tenon end. There are deeper bite marks on the upper and lower stem surface near the buttons in the bite zone. However, the buttons on either surface is undamaged. The tenon and horizontal slot show heavy deposition of dirt, oils and tars, adversely affecting the air flow.THE PROCESS
The restoration process started with sanding the bite zone of the stem with a folded piece of 220 grit sand paper to remove the calcium deposition and followed by internal cleaning of the tenon, stem air way and the slot with pipe cleaners and isopropyl alcohol. This was followed by cleaning the stem surface of all the oxidation by immersing the stem in “Before and After Stem Deoxidizer” bath overnight. This solution developed by Mark, pulls all the oxidation to the surface and makes the subsequent cleaning a breeze.The next morning, Abha my wife, took the stem out and cleaned all the thick sticky solution from the surface under running warm water. She blew out the solution that had clogged the airway and scrubbed out the raised oxidation with cotton pads and a piece of 0000 grade steel wool. She applied a little quantity of Extra Virgin Olive oil in to the stem to hydrate the vulcanite and set it aside. The initial sanding with a folded piece of 220 grit sand paper had evened out the minor tooth chatter and now that the stem is free of the heavy oxidation, I have a clear understanding of the damage that needs to be addressed, which by the way, is very minimal. I am pleased with the stem appearance at this stage.To raise the deeper bite marks from the upper and lower surface of the stem, I flamed the surface with a lighter flame. I went ahead and sand the raised bite mark with a 220 grit sand paper and sharpened the button edges. With a cotton swab and isopropyl alcohol, I wiped the stem surface to clean it of all the dust. I mixed superglue and activated charcoal powder and filled the bite marks and set it aside to cure. While the stem fill was set aside to cure, I worked the stummel and reamed the chamber with size 3 blade head of PipNet pipe reamer. Using my smaller sized fabricated knife, I removed all the cake from the areas which could not be reached by the reamer head. Very carefully, I removed all the charred briar from the outer and inner edges till I reached solid briar wood. With a folded piece of 220 grit sand paper, I sand the chamber walls to remove the last remaining traces of cake and wiped it with a cotton swab dipped in isopropyl alcohol. I am not very enthusiastic about the way the chamber appears at this stage. The inner edge at the rear has been pushed back significantly thinning the rim top surface. Also, the walls are peppered with numerous minor heat fissures/ lines making a web pattern. The crack, it is now clear, extends in to the chamber over the rim surface and on to the outer stummel surface. Another crack is now evident on the right side of the rim surface, but it’s superficial and not deep. Here is how the chamber appears at this stage, though not very encouraging, I say. Continuing with internal cleaning, I cleaned out the mortise, first by scrapping out the entire dried accumulated gunk with a dental tool. I further cleaned the shank internals with hard and regular pipe cleaners dipped in alcohol. Even after removing the cake from the chamber and cleaning the shank internals, the smells in the chamber are still very strong; in fact, my entire room smells of it!!Before I moved to the next stage in the process, I wanted to access the extent of charring over the outer rim edge. I gently scraped the charred briar from the outer rim edge with a sharp knife. Again not a very encouraging sight as the gaping saddle that was formed at the front and back of the stummel was anything that could be addressed by simply creating a bevel over the outer rim edge. Sad!! I have the option of addressing this issue either by topping the rim top surface or by the way of rebuilding the outer rim edge. I shall decide on the best course of action when I reach that stage.Next I decided to address the copious amounts of oils and tars that have been absorbed by the stummel giving it a considerably darkened appearance and a sticky feel in the hand. I stretched a cotton ball into a thick wick, wound it around a folded pipe cleaner and inserted it in to the shank and pushed it till it came out of the draught hole and packed the chamber, just below the rim, with Kosher salt. I topped the bowl with isopropyl alcohol using a syringe. I topped the bowl with alcohol again after 20 minutes when the alcohol level had gone down and set it aside overnight for the salt and alcohol to do its intended job. The next morning, the salt had turned a dirty and smelly brown and so was the wick and pipe cleaner in the shank. The ghost smells, the rim top dark coloration and the stickiness in the surface were still strong and hence I decided to give it a second salt and alcohol bath. This time around I used cotton balls in place of Kosher salt what with Kosher salt being more expensive and not readily available. I repeated the entire process described above and set the bowl aside overnight. By the next afternoon, the alcohol had drawn out maximum of the remaining oils and tars from the stummel surface and trapped it in the cotton balls. I am satisfied with the condition of the bowl internals with this cleaning.With the internals of the pipe cleaned and sorted, it was time to move to the external cleaning of the stummel. Using a hard bristled tooth brush dipped in undiluted Murphy’s oil soap, I very deliberately scrubbed the stummel, cleaning the surface thoroughly. I was very deliberate on the surface areas which were covered in fat-like sticky substance over which dirt and grime had accumulated over the years. I also cleaned the mortise with a shank brush and dish washing soap. I scrubbed the surface with a pad of Scotch-Brite to rid the surface of the slime. I was surprised to observe the stummel turning greasy white. This would need resorting to some heavy duty and abrasive methods to get rid of this grease from the stummel surface. Here is how the stummel appeared at this stage. I am happy that the salt and alcohol treatment had drawn out all the oils from the pores of the briar as can be seen from the cleaned up rim top surface. Next, I decided to stabilize the cracks that were observed prominently on either sides of the stummel extending downwards from the rim outer edge for a few millimeters. Under a magnifying glass, I marked the end point of the cracks and using a 1 mm drill bit, I drilled a counter hole at the base of the crack taking care that I did not drill a through hole. This ensures that the crack is stabilized and does not spread any further. With a heat gun, I warm the stummel and this expands the crack minutely. I fill this crack with clear CA superglue and firmly press the sides together. Once the superglue had sufficiently hardened, I apply a little superglue along the entire crack (rim top and side of the stummel) and press briar dust over it. This further stabilizes, strengthens and masks the fill in the cracks. I had reached that point in restoration where I had to decide on the way ahead for rim repairs. I could either top the bowl till I had a perfectly even round rim top, compromising on the shape and size or I could go for a complete rebuild. I decided on the latter as topping would significantly reduce the bowl size. Using a worn out piece of 150 grit sand paper, I completely remove the charred briar from the outer and inner rim edges in preparation for rebuilding the rim top. Using the layering technique (layer of glue followed by briar dust pressed on to this layer and repeating till the fill is over and above the intact rim surface), I completely rebuild the rim top and set the stummel aside for the fills to harden. While the rim top rebuild was curing, I decided to address the stem repairs. The stem fills had cured nicely and using a flat head needle file, I sand the fill to achieve a rough match with the surrounding stem surface. I further sand the stem surface with a folded piece of 220 and 320 grit sand papers to further blend in the repairs. However, a minor air pocket was revealed on the lower surface of the stem and I spot filled it with clear superglue and set it aside to cure and turned my attention to the stummel repairs again.The rim rebuilt surface had cured nicely. I could now proceed with reshaping the rim top and the inner rim edge to an even round. I mount a coarse 150 grit sanding drum on to my hand held rotary tool and setting a speed at half, I carefully sand off the excess fill from the rim top surface and the rim inner edge till I had achieved a rough match with the intact portion of the rim top and inner edge. I further top the rim on a 220 grit sand paper to achieve a seamless rim top surface. With a folded piece of 220 grit sand paper, I worked the inner rim to a crisp and perfectly rounded edge. I am very pleased with the rim surface rebuild at this stage in restoration. Staying with the stummel, I next decide to address the greasy white coating of whale fat or blubber or whatever fats that covered the stummel surface (remember all the Arctic and Antarctic expeditions on which this pipe must have accompanied Late Mr. John Barber!!). I sand the entire stummel surface with a piece of 180 grit sand paper. I frequently wiped the stummel with a cloth wetted in hot water to get rid of the loosened fat coating. A lot of elbow grease and few grueling hours later, beautiful bird’s eye grains and swirls began to make an appearance over the stummel surface. With renewed vigor, I completely remove the greasy white coat of fat from the stummel. I was careful not to sand the sides of the shank, but only wiping with hot water in an attempt to preserve the worn out stampings on this pipe. Though the surface has been cleaned up nicely, it appears dry and lackluster. I rub a small quantity of Extra Virgin Olive oil in to stummel to hydrate the briar and set it aside for the oil to be absorbed by the briar. The grains in the stummel now pop out and appear resplendent in their beauty. All the hard work up to this stage was well worth the effort and much more. The following pictures speak for themselves! To further smooth out the rim top, I topped the rim surface over piece of 320 grit followed by 420, 600 and 800 grit sand papers. Even though the cracks have now been exposed as a result of this topping, I am not overly worried as I am confident that the cracks have been solidly filled and stabilized.At this point I decided to work on the inner walls of the chamber. There are heat lines seen on the walls of the chamber and add to that the rebuilt inner edge using superglue and briar dust. To protect the walls and prevent the superglue and briar dust from coming in to direct contact with the burning tobacco, I plan to first coat the rebuilt part and the heat lined surface of the chamber walls with J B Weld followed by a second coat of activated charcoal and yogurt to the entire chamber which would assist in faster cake formation. J B Weld is a two-part epoxy Cold Weld that consists of two parts; hardener and steel which are mixed in two equal parts (ratio of 1:1) with hardening time of 5-6 minutes and complete curing time of 6-8 hours. I poured the contents of the two tubes and mixed it well. With a flat bamboo frond, I applied this mix, as evenly as possible, over the intended areas. I worked fast to ensure an even coat over the chamber walls before the weld could harden. I set the stummel aside for the application to harden and cure overnight. By next afternoon when I got back to working on this pipe, the J B Weld coat had completely cured and hardened considerably. With a folded piece of 150 grit sandpaper, I sand the weld coating to a smooth surface and continued till I had as thin a coat as was essential to protect and insulate the walls from the direct heat of the burning tobacco. Here are pictures of the process and the progress at this stage. Wanting a change, I decided to now tackle the stem fill which had been left curing for the last couple of days. Little did I know at this point that I was still some days away from completing the stem repairs!! I followed the golden rule of pipe restoration; “Less is more” and move ahead with sanding the fill with a piece of 220 grit sand paper without first using a flat head needle file. I followed it up with sanding the entire stem surface with 400, 600 and 800 grit sand papers. I finished the sanding regime with a 0000 grade steel wool. It was at this stage that I noticed the same dreaded air pocket and the fill was peeling out. With a dental pick, I completely removed the old fill and refilled it with a fresh mix of activated charcoal and superglue. I set the stem aside to cure overnight, third fill for the same spot!! With time still on my side before I hit the bed for the night, I decided to work on the stummel which had been set aside to absorb the olive oil. I thoroughly wiped the bowl with an absorbent paper towel to remove all the excess oils from the bowl surface. I polished the stummel, including the newly rebuilt rim top surface, wet sanding with 1500 to 12000 grit micromesh pads. I wiped the surface with a moist cloth to remove all the sanding dust left behind by the pads. I was very careful with the stamping as I desired to preserve as much of the worn out stampings as was possible. Though the rebuilt rim surface and outer rim edges stand out as sore thumb at this stage, I intend to mask the same with a dark stain. The stummel surface appears promising and I am absolutely in love the bird’s eye grains on this pipe. Next, I rub a small quantity of “Before and After Restoration Balm” in to the briar with my finger tips and let it rest for a few minutes. The balm almost immediately works its magic and the briar now has a nice vibrant appearance with the beautiful darkened grain patterns on full display. I further buff it with a horse hair shoe brush. While the stummel was set aside for the balm to be absorbed, I worked the stem fill which had cured over 24 hours. I sand the fill with a used and worn piece of 180 grits sandpaper and followed it with wet sanding the entire stem with 1500 to 12000 grade micromesh pads. I wiped the stem with a moist cloth to remove the dust and monitor the progress being made after every three grit pads. The stem polished up nicely and has a rich deep black shine to it. I applied a little Extra Virgin Olive oil to rehydrate the vulcanite and set the stem aside.Though the stummel had cleaned up nicely with a deep color to the briar, it was nowhere near the deep reddish brown coloration associated with the Bruyere line of Dunhill pipes; in fact it was much lighter. While restoring a Dunhill Bruyere from my Mumbai Bonanza (https://rebornpipes.com/2019/03/13/reconstructing-a-broken-stem-on-dunhill-bruyere-51671/), I had stained the stummel in cherry red stain and though the end results were great, it was not the original color associated with a Bruyere. The comments and suggestions received from esteemed readers of the write up pointed me in the direction of achieving this color!!! I decided to first apply a coat of DB followed by a final coat of red stain. However, when I went through my stains, I realized that I did not have Dark brown stain; the Feibing’s stain bottle had mysteriously dried out!!!!! The next best option available was the Cordovan. I consulted Steve and though he was not sure about the color, he encouraged me to go ahead and that is exactly what I did. I heated the stummel surface with my heat gun to open up the pores on the stummel so that the stain is well set while being careful that I do not overheat the fill, a lesson learned while restoring Steve’s Alexander Zavvos pipe. I dipped a folded pipe cleaner in Feibing’s Cordovan leather dye and liberally applied it over the heated surface of the stummel, flaming it with a lighter as I progressed. This helps in the setting of the stain in the grain of the briar. I set the stummel aside overnight for the stain to set. The next afternoon, I mounted a felt cloth buffing wheel on to my hand held rotary tool and proceed, as my dear friend Dal Stanton likes to say “unwrap the coat of stain to reveal the grains” on the stummel surface. Alas, there was no revelation of any sorts!! All that I saw was a dark stummel. You must understand my disappointment at this stage. I realized that the stain coat was too thick. I needed to lighten it up a bit and hence, with a cotton swab wetted in isopropyl alcohol, I wiped the entire stummel surface. Though the stain has lightened a bit, it was not the result that I desired. Here is how the stummel appeared at this stage. To further lighten the stain and “reveal” the stummel grains, I dry sand the entire stummel with 1500 to 12000 grit micromesh pads. The grains are now clearly visible. However, the trademark color of Bruyere line is still an illusion……it was browner than the reddish brown stain that I was looking for. I decided on giving the stummel a stain wash with a Cherry Red stain as suggested by Steve. I diluted the Cherry Red stain powder in 99.9% isopropyl alcohol in approx ratio of 1:4. With a cotton swab, I dabbed the diluted stain over the stummel surface, letting it set for a few moments and thereafter wiping it off with a dry clean cotton swab. I repeated the process till I had achieved the desired coloration. I am pleased with the color of the stummel which is as close as I could achieve, to the original Bruyere color. This time around, even the fills had absorbed the stain and blended in nicely with the rest of the stummel. To complete the restoration, I reattach the stem with the stummel. I mount a cotton cloth buffing wheel on to my hand held rotary tool and applied several coats of carnauba wax. I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further. This dude has definitely come a long way from the condition it was in at the start.Now that the cosmetic aspects of this pipe have dealt with, all that remained was the functional aspect that needs to be taken care of. The minor heat lines and the J B Weld coated surface needs to be protected from the direct heat of the burning tobacco and for this; I coat the complete chamber walls with a mix of activated charcoal and yogurt and set it aside to harden naturally.I shared a few pictures of the pipe with my mentor, Steve, expecting some hearty praises on this restoration!! However, his keen eyes noticed an issue which had missed mine. He very gently pointed that a sterling silver band at the shank end would mask the shouldering that was inadvertently created!! This remark of his left me shocked!! Not at the remark as such, but at the fact that I had shouldered the shank end during the restoration process. Still smarting at being chided by my teacher, I revisited all the pictures and true enough, this issue already existed and I had missed out mentioning it in my initial inspection in the write up and hence missed it out during the entire process. I made necessary amendments to the post and had to keep the pipe aside till I reached back home during my leave where my local silversmith would fabricate one such ring for me.

I revisited the small, dingy and unsophisticated shop with rudimentary tools where the craftsman had built me a Sterling Silver ring for an Alfred Massin Meerschaum cutty that I had restored two months ago (https://rebornpipes.com/2019/10/09/complicating-a-simple-restoration-of-a-cutty-meerschaum/). The craftsman at the shop made me a perfect ring for the Dunhill shank end. This ring not only masks the shouldering, it also adds a touch of class while breaking the monotony of the pipe. I refreshed the bowl coating with activated charcoal yogurt mix and completed this project with a vigorous hand buffing with a microfiber cloth. How I wish I had carried my hand held rotary tool and some carnauba wax for a final polish while on leave!!! Nevertheless, the finished pipe has received a fresh lease on life and is now all set to stay with me for the rest of my time on this earth as part of my Dunhill rotation. The repairs are solid and blended in well with the surrounding surfaces. All that now remains is to load a nice English blend and enjoy a quite peaceful smoke… P.S. This perhaps would be the longest write up that I ever have posted on rebornpipes.com!! Apart from the Alfred Massin Meerschaum pipe that I have mentioned above, this project extended over a period of two months, just for the want of sterling silver band. Nonetheless, it was one project that I enjoyed working on and hope that my Guru and mentor Steve gives me passing marks on this test project (remember that it was a sort of test put forth by Steve for me!).

The most important aspect of this restoration was being able to live up to the belief and faith that Farida had entrusted in Steve and through him, in me, to carry forth the trust of her Father. It is while working on this project that I fully comprehend and understand what and why Dal Stanton calls himself Pipe Steward!! A perfect term coined by this well read gentleman, I say.

Farida, if at all you read this write up, I wish to let you know that it has been a privilege to have been afforded an opportunity to carry forward the trust of your father. As I puffed on this Dunhill, I could conjure up images of your father and his dogs amidst all the snow and loneliness…. A MAN, HIS FAITHFUL PIPE AND HIS BELOVED DOGS!! Thank you Steve and Farida…… and the pipe has a new friend!!

The CPF Arcadia: A Pipe Out of Time


Blog by Robert M. Boughton
Copyright © Reborn Pipes and the Author except as cited
https://www.roadrunnerpipes2k.com/
https://www.facebook.com/roadrunnerpipes/
Member, North American Society of Pipe Collectors

Be careful what you wish for, you may get it.
— Anonymous, quoted in “The Monkey’s Paw,” W.W. Jacobs, from The Lady of the Barge, 1902

INTRODUCTION
Whatever inspiration led Cliff Edwards to write the lyrics to the song that became Disney’s theme, “When You Wish upon a Star” – in which one’s heart need only be in the dream for no request to be too extreme, and fate will be kind – must have been, to be gentle to all of the Mouseketeers out there, in an alternate reality to mine.  I’ve long had two rules: be careful what you ask for, lest you get it, and above all, never ask for what you deserve, because everyone has done things that should have had stiffer consequences.  I’m not being cynical.  From my experience, it’s just the way whatever Higher Power we call by various names helps us humans avoid being selfish and greedy, at least those who ask for guidance now and then if not more.

Of course, I’m not perfect, in fact, far from it.  I found myself during the past two months or so becoming more and more fixated on acquiring not just any new pipe, but one made by the Colossus Pipe Factory.  Then I began my hunt in earnest, with eBay searches and general Googling, but to no avail.  At last I got a hit with a pair of pipes titled, in a somewhat jumbled way, “Vintage Smoking Pipe Tobacco Lot of 2 Arcadia CPF London England Briar.”  From that description alone I thought maybe I was going to see something made by an Arcadia brand and a rare English CPF.  There were enough photos, however, and they were good, to determine without doubt that a big, smooth poker stamped on the right MADE IN/LONDON ENGLAND was one mixed-up part of the seller’s heading, and CPF Arcadia was the other.  The disarray of the title and the low price I paid – about $45 – told me the seller didn’t know what he had and the other bidders were not sure enough that the CPF was real to risk going higher.

Before bidding anything and after studying the pics of the alleged CPF – and I mean I really poured over every detail of them – I was certain it had to be a fake, except for the band on the shank.

From the photos that I snapped when it arrived in the mail with the poker I believe is a Ben Wade reject, the only authentic-looking parts of a CPF are the band, bone tenon and stem.  Otherwise, honestly, I could see where the basic chunk of wood could have been fashioned into a stummel long ago before some Flower Child got ahold of it and turned the bowl into a psychedelic pin cushion, but I could not imagine anyone alive more than a century ago, especially the Old World masters employed by CPF, fashioning such a monstrosity, as I saw the pipe before its comic beauty grew on me.  I even used the “m” word in an email I sent to Steve, with a link to the eBay sale, in which I more or less implored him to tell me it wasn’t real, meaning a genuine CPF.

Needless to say, I was shocked when Steve not only replied that the Arcadia was real and “very old,” an age distinction he had never before made to me, but that he had worked on a meerschaum like it a couple of years ago.  Here are some before and after shots of Steve’s meerschaum, which indeed bear a scary resemblance to my old briar.

A.F. & Co./BBB Spotted Meerschaum photos courtesy Steve Laug.

The severe chicken pox-like similarities are undeniable, and I scrutinized every word and photo of Steve’s blog in hopes of connecting the dots (I’m so sorry, that just popped out) of the definitely funky tobacco pipe specimens.  Struck by a gung-ho fit to research the abbreviation “AF&C0” in Steve’s third photo above, I interrupted my reading to find the answer before continuing and learning Steve already had done so: Adolph Frankau & Co. of England.  Steve’s work restoring the meerschaum that he also dated to 1905, thanks to great detective work tracing the unique hallmarks on the sterling silver band, was phenomenal, in particular the addition of a Bakelite stem that he not only fitted to the shank but made look as old as the original stummel.

Now, in case anyone thinks my choice of details a mere glut of disconnected trivia, I’ll make my point.  Steve took one look at the weird pipe for sale on eBay, flashed on the A.F. & Co./BBB meerschaum he gave new life and instinctively sensed a connection.  I have to say, I had doubts despite the almost genetic resemblance.  After all, there was no indication my CPF Arcadia was a Frankau import.  By the time Steve and I connected on the phone to discuss the two pipes and other matters, I had restored the Arcadia and warmed to its charms.  Although lacking any proof of the pipe’s date of manufacture such as Steve dug up for the meerschaum, certain minute observations and research led me to conclude it was created in the latter part of the 19th century.  Steve concurred.

In particular, I finally figured out that the stem was not Vulcanite but black horn, and the metal band boasted that it was “Nickel Plated.”  What kind of pipe brags about having a nickel plated band?  Nowadays, that’s the bottom of the barrel.  So I looked up nickel plating history online and learned that in 1837 the first crude electrochemical nickel plating of platinum was accomplished.  Really?  Someone thought to cover up the most precious metal with nickel?  You bet he did, and in 1869 a better process that became the industry standard for 70 years was discovered.  The purpose of nickel plating certain other metals, of course, remains nickel’s resistance to tarnishing and corrosion.  The only logical explanation for the proud “NICKEL PLATED” stamp on the band of my CPF, therefore, is that the process was still relatively new.  Given that point and the use of black horn stems being much less common in the late 19th and early 20th centuries, when amber and Bakelite predominated, I am satisfied the pipe was created in the waning years of the Victorian Era.

Returning to Steve and his inspired flash that the “knobby meer,” as he called it, and the CPF Arcadia are related, Steve told me he now questions whether the meerschaum is a real BBB, owing to certain unstated problems with the band.  Steve is the expert, but this time I have to disagree and urge him to stick with his instincts.  The notion of the meerschaum, knobs and all, being a bona fide BBB is no wilder than my briar, with its gaudy plastic bulbs and brass studs, being a genuine CPF, and I do not mean to suggest in a roundabout way that neither is the truth.  Granted the extremity of different materials used to make the pipes, and the necessity of alternate methods for achieving the knobby looks, and still further suspending disbelief because of the admitted implausibility of the idea, I nevertheless can’t help thinking that the connection is the actual crafter of the two pipes.  To be blunt, I think the same person made both of them.  Of course, I will never be able to prove the theory.  Well, isn’t that convenient, as the Church Lady used to say.

With a little more research, I was pleased to settle with much more certainty a question that nagged Steve in his blog of the unusual meerschaum: was there a connection between it and BBB?  As several of the sources below show, the link is clear.  Frankau, who started business in 1847, died in 1856.  At that time, his widow was persuaded to continue operation of A.F. & Co. under the control of Frankau’s very young assistant, Louis Blumfeld, who was then only 18.  Blumfeld started BBB (for Blumfeld’s Best Briar, later Britain’s Best Briar), the famous triangular symbol for which he trademarked in 1905 – again, the year Steve’s meerschaum was made – under the A.F. & Co. banner.  BBB seems to be the first pipe maker with a trademark.  And so the connection, if I haven’t made it obvious, is that A.F. & Co. owned BBB.

Arcadia, part of the modern-day Peloponnese, a peninsular region of southern Greece (capital, Tripoli), is also a reference to Greek mythology.  The mythological Arcadia was named for Arcas, a hunter who became king of the utopic wilderness and is best remembered for teaching the skills of baking bread and weaving.  In Arcadian myth, Pan, the god of shepherds, hunters and the wilds, is said to have roamed the region with dryads, nymphs and other spirits.  The name, therefore, is an odd one for this pipe, unless it’s a reference to the Calydonian Boar killed by the king’s daughter, Atlanta.

CPF had an ephemeral but brilliant run from 1851 to c. 1915, producing with the unparalleled skill of its Old World craftsmen some of the most astounding pipes, meerschaum and briar, ever created.  That’s all I need tell of CPF’s history, as Steve’s account in the sources below is the definitive authority.  Another link to a few of the CPF beauties in Steve’s Wonderland collection shows examples that are far closer to what I had in mind when I was wishing for a pipe of that great brand to find its way to me.

But that’s what can happen to someone who wishes for something.

RESTORATION
A few close-ups show the peculiarities and problems I found.  The first, featuring the front of the bowl, makes the little, round, plastic bulbs – which I did not yet know the means of connection to the bowl – appear red instead of their actual light brown.  Scratches all over the uneven surface that is spotted with the bulbs and brass studs presented awkwardness to remove.  The second shot, of the rim and chamber, has the correct color of the bulbs and at a glance seems the hardest part of the pipe’s repair but in fact was the easiest. The third pic made me happy the band was already spinning on the shank so I could leave it out of an early alcohol soak.  The grime and stains would come off, but I knew I could not fill in the missing patches of nickel.  Then there was the stem, top and bottom, with moderate tooth damage that would typically be no hassle to eliminate if it were Vulcanite.Before I continue, take a close look at the bowl and count the bulbs and brass studs.  There are seven bulbs and four studs, and the arrangement may seem random.  But look again, and you’ll see a very odd order: on the left side, the bulbs start on the top left to right and then down to the bottom right; the studs move diagonally from the lower left to the middle.  On the right side, the opposite is true: the bulbs go from top left down to bottom left and then bottom right, and the studs are diagonal from top right to middle.  On the front, three bulbs form a diagonal, tic-tac-toe line from top right to bottom left, or vice versa if you prefer.  Finally, the back shows all four corners with bulbs.   The person who crafted this pipe had a very playful sense of order.

Thinking the Arcadia stem was Vulcanite but knowing it would do no harm anyway, I tossed it and the one from the Ben Wade reject candidate in an OxiClean bath.  The usual old dirt and tobacco residue came off both.  The first pictures after the bath show the stem not yet fully dried, and the next three dry. This was when I snapped that perhaps the stem material was not Vulcanite and Googled black horn, although if I had ever heard of such a variety of that organic material, it was dredged up from my subconscious.  I emailed Steve somewhat stupidly without photos.  He replied that horn has striations that are visible under a magnifier, so I shot him back the above photos and asked if the last showed the kind of marks he meant.  His brief response was, “Definitely horn.”  In the meantime, I had followed up with 220-grit sanding and wet and dry micro meshing from 1500-12000.While the stem had been taking a bath, I soaked the stummel in Isopropyl alcohol.  I was worried about the possible effects of the alcohol on the bulbs, but somewhat less catastrophic in the potential result than the Trinity Tests of the atom bomb south of Albuquerque nearing the end of World War II, I took a gamble.I started the next longer part by sanding the rim with 400- and 1000-grit papers, then the rest with 1000. Smoothing the chamber with 60- and 320-grit papers, I followed up with a full micro mesh of the rim and rest of the outer stummel.I thought Fiebing’s Dark Brown leather stain would be good for the stain.I performed the retort and decided to add a coat of Fiebing’s Burgundy.  I was satisfied with the color result, but in the process of flaming and micro meshing after the latter stain, a couple of the bulbs went M.I.A. Faced with the not altogether unanticipated contingency of somehow having to replace a bulb or two, as I still considered them, I had already considered using small push pins, the kind for wall maps, and had found a couple of places online that carried close to the same shade of brown in case it became necessary.  Hoping to avoid the time waiting for them to arrive by mail, however, I scoured this wannabe big city that is lacking in so many of the amenities found in the real thing.  The best I could find was the following box of 200 map pins in every color but brown (any shade of it!).  The good news was that they only cost $2.99 minus tax at a hobby store.  I concluded it would be necessary to replace all seven of the bulbs for the sake of consistency and suppose I might have opted for a conservative dark blue or even black, but as Tom Cruise’s high school character in Risky Business put it, “Sometimes you just have to say what the @#$*!”  Besides, Christmas is coming up.  The smaller brown pin below was an original I twisted out.The one prospect I didn’t even consider until I examined the holes left by the missing “bulbs” was that some antique version of map pins might have been used when the pipe was adorned in such an unconventional way by its maker.  But when the time came to remove the bulbs that were still intact, I found out they were indeed nothing more than map pins from more than a century ago.  All I had to do was snip off the longer metal ends of the new ones and Super Glue them into the slots.  I still don’t know how the brass studs are attached because I didn’t want to mess with them.  I’m curious by nature, but I have limits.  My dad always said, if it works, don’t fix it.

And so, without further ado, here is the finished CPF Arcadia. CONCLUSION
I’ve come to love this pipe out of time that should have been made in the Art Deco period, which didn’t really get rolling until 1925 and hit its peak in the 1930s art scenes of Europe and the U.S. – or even the hippie  (or psychedelic, counterculture and what-have-you) movement of the 1960s into the ’70s).  If this restoration taught me anything, it’s that sometimes wishing for something vague can lead to a happy ending.  I’ve come to love this pipe and will happily keep it if it doesn’t sell.  And it is for sale, for the right price on my site, or a good trade.

SOURCES
https://rebornpipes.com/2017/07/30/enlivening-a-mysterious-old-knobby-oval-shank-meerschaum-bowl/
https://rebornpipes.com/2019/02/22/reflecting-on-a-few-of-my-cpf-pipes-colossus-pipe-factory-pipes/
https://rebornpipes.com/2013/04/14/some-reflection-on-the-historical-background-on-cpf-pipes/
https://www.thomasnet.com/articles/metals-metal-products/nickel-plating-history/
https://www.google.com/search?q=when+you+wish+upon+a+star+lyrics&rlz=1C1CHBF_enUS857US857&oq=when+you+wish+upom+&aqs=chrome.2.69i57j0l5.7556j0j4&sourceid=chrome&ie=UTF-8
https://www.gracesguide.co.uk/Adolph_Frankau_and_Co
https://adolphs.weebly.com/blog/adolph-frankau-tobacco-pipes
https://pipedia.org/wiki/BBB
https://trademark.trademarkia.com/bbb-71008248.html