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Restoring a 1965 Dunhill Shell Briar # 56 F/T 3/4 Bent Billiard


Blog by Paresh Deshpande

I had just finished restoring the fifth Dunhill from my Mumbai Bonanza find, a 1962 DUNHILL SHELL #196 F/T and now this is the sixth. I am left with only one Dunhill pipe to complete from the Mumbai Bonanza, a smooth finish LB.

I was fortunate enough to have heeded to the advice of my dear friend and mentor, Mr. Steve, and struck a deal with a trash collector from Mumbai. He did not know what he was selling and I did not know what I was buying as we reside in different cities!! The argument that Mr. Steve presented was that if not anything, I shall at least have some spares and this was logical. I struck a deal and here are pictures of the pipes that I received in this lot. This lot contains some very nice collectible pipes, a few well known brands and some mediocre brands. Overall, with seven Dunhills, a Preben Holm #1, a couple of “Made in England” Pete System pipes, Charatan’s, Custom-Bilt, Stanwell and other assorted pipes, I would say that I had hit a huge jack pot!! Hence, I like to call this find the “Mumbai Bonanza”.

The pipe that I decided to work on from this find is another Dunhill, a 1965 Shell Briar 3/4 bent billiard, and is marked in pastel pink circle in the picture below. It is stamped on the underside of the shank with the shape number 56 followed by F/T followed by DUNHILL over Shell Briar followed by the COM stamp Made in over England 5 (underlined) which dates it as being made in 1965. This is followed by Group size number 4 in a circle and letter S for Shell. Dunhill White Dot adorns the top of the vulcanite stem. The stampings are very slightly worn out and easily readable.In this short journey of mine in to the world of pipe refurbishing, this particular pipe has one of the deepest and beautiful sandblast patterns that I have come across. The sandblast on this pipe speaks volumes about the skills of the pipe carver. With this thought, I move ahead with the restoration of this beautiful medium sized sandblasted Dunhill bent billiard and restore it to its glory.

INITIAL VISUAL INSPECTION
The chamber is clean with a decent and even thick layer of cake. From what I can see, the chamber walls appear to be without any damage. The chamber is odorless. There is an overflow of lava on the sandblasted rim top surface. The inner and outer rim edges are undamaged. The walls appear to be thin. Is this a case of over reaming or is it because the carver decided to compromise the wall thickness for deeper sandblast patterns?The stummel boasts of some beautiful sandblast pattern of mix of straight and cross grain all around. It is dirty with grime, oils and tars filling in much of the craggy finish. The briar looks lifeless and dull. The mortise shows minor accumulation of dried tars mixed with ash and remnants of tobacco. This will have to be cleaned and refreshed. The vulcanite stem shows a minor damage to the button end with minor chatter on the lower surface. The lip edges have a few bite marks and will have to be reshaped and made crisp. The stem is oxidized; however, the quality of vulcanite is good. The white dot on the upper surface has faded in some places but is still distinctly visible. This cannot be helped and status quo has to be accepted.There are no major issues to address here on this pipe; just a little TLC and the pipe should be good to go…nah, find a place of pride on my rack!!

THE PROCESS
I start this project by tackling the stem first. I sand the stem with a folded piece of 220 grit sand paper to erase the minor tooth chatter on the lower surface, get rid of the oxidation and provide a smooth surface for the intended fill to reconstruct the button edges. I cleaned out the internals of the stem with hard bristled and regular pipe cleaners dipped in isopropyl alcohol. Once I was satisfied with the internal cleaning, I wiped the stem surface, particularly the damaged button end, with a cotton pad and alcohol to remove any traces of dirt and grime. I prepared a mix of CA superglue and activated charcoal and carefully applied it over the damaged lip and set it aside for curing over night. Before moving ahead, I would like to mention here that I had applied this mix in sufficient thickness which would help during the filing and sanding while shaping the button and achieving the correct lip edge profile.While the stem repair was set aside to cure, I moved ahead to deal with the stummel cleaning. With size 3 head of a PipNet reamer, I took the cake down to bare briar. Using a folded piece of 180 grit sand paper, I sand out the last traces of cake and expose the walls of the chamber to ascertain that there are no cracks/ heat fissures. I wiped the chamber with a cotton pad dipped in isopropyl alcohol to remove the carbon dust left behind by all the reaming and sanding process. The walls of the chamber were solid with no damage. This was followed by cleaning the mortise by scraping away at the dried gunk with my fabricated spatula and followed it up with further cleaning using cue tips, pipe cleaners and shank brush dipped in isopropyl alcohol. This eliminated all traces of old smells from previous usage. I followed up the internal cleaning with external. Using a soft brass wired brush I gently scraped away the thick lava coat in the blast of the rim. With a hard bristled tooth brush and dipped in undiluted Murphy’s oil soap, I very deliberately scrubbed the sandblast finish on the stummel and the rim top. The stummel and rim top was dried using paper napkins and soft cotton cloth and set it aside to dry out naturally. The stummel looks fresh and clean. Next, I rub a small quantity of “Before and After Restoration Balm” in to the briar with my finger tips and let it rest for a few minutes. The balm almost immediately works its magic and the briar now has a nice vibrant appearance with the beautiful contrasting hues colors that are unique to this sandblast pipe, on full display. I further buff it with a horse hair shoe brush. I set the stummel aside and turned my attention to the stem repair. The fill had cured nicely and I moved ahead and began the process of filing and shaping the button end with a flat head needle file. For a better blending, I further sand the entire stem with 220 followed by 400, 600 and 800 grit sand paper. This helps to reduce the sanding marks left behind by the more abrasive 220 grit paper. To bring a deep shine to the vulcanite stem, I went through the complete set of micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. I wiped the stem with alcohol after each pad and rubbed it down with Extra Virgin Olive oil to rehydrate the vulcanite. The repairs have blended in very well and the stem now looks shiny black and beautiful. The internals of the stem was once again cleaned out using alcohol and pipe cleaners to clear the airway of all the debris resulting due to the sanding. The finished stem is shown below. To finish, I re-attach the stem with the stummel. I mounted a cotton cloth buffing wheel to my local machine which is similar to the Dremel.  I set the speed at about half of the full power and applied White Diamond compound to the entire pipe. I wiped/ buffed the pipe with a soft cotton cloth to clear it of any leftover compound dust. I then mounted another cotton cloth wheel on to the polishing machine and applied several coats of carnauba wax. I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further.The completed pipe looks lovely, fresh and vibrant; the pictures speak for themselves. I really enjoyed working on this pipe and hope that readers too enjoyed walking with me through this restoration. If only this old warrior could share its past life with all of us…if only!! Cheers.

 

 

 

Rejuvenating the Amazing Grain of an EWA Trophee of St. Claude, France 909


Blog by Dal Stanton

Next on my worktable is another pipe I acquired from a ‘Lot of Treasures’ I found on French eBay.  This French Lot of 50 has rendered some real keepers with historic interest and collectability.  The EWA Trophee I’m now looking at is a classic Bent Billiard with a flare – the acrylic stem, banding and picturesque briar holds out great potential, but it come with some challenges as well.  Pipe man, Scott, commissioned the EWA – a friend on FB and regular contributor on different Face Book Groups, and a former US Navy man who I appreciate very much.  Scott reached out to me on FB Messenger and had been looking at the pipes available for commission in my For “Pipe Dreamers” Only! collection and there were 5 pipes he was dreaming about that he had seen, but settled on one, the EWA Trophee.  I appreciate Scott’s patience in the speed of my pipe restoration production line!  His patience is now paying off, and his commission benefits the Daughters of Bulgaria – our work here in Bulgaria helping women and girls who have been trafficked and sexually exploited.  Here are the pictures that drew Scott’s attention. I can see why this pipe got Scott’s attention.  I have worked on several French named pipes, and this was the first with ‘EWA’ stamped on the left shank flank.  Underneath and at an angle is stamped ‘TROPHEE’.  The acrylic stem also is stamped with a distinct EWA.  The right side of the shank is stamped ‘BRUYERE’ [over] ‘ST. CLAUDE’ [over] ‘FILTRE’.  Tucked on the lower side of the shank is stamped the shape number, ‘909’.  Information about this nomenclature was readily available in the Pipedia article on EWA pipes and with this being my first look at the EWA name of St. Claude, I include more of this article.

From Pipes, Artisans and Trademarks, by José Manuel Lopes

EWA is a French brand of Pipe EWA-Ets. Waille SARL. Launched in the 1970s by Michel Waille, the brand began in the Waille factory founded in 1860 by Horace Waille., and has been passed down from generation to generation ever since. He was succeeded by his son, René (1902-1932), his grandson Adré — who obtained the rank of ‘CAP de Pipier’ in 1926 and was in the company from 1920 to 1974 — and his great grandson, Michel Waille.

Michel, ‘Meilleur Ourrier de France’ but retired today, is currently President of the Pipe Club de Saint-Claude. He joined his father in 1968 and was at the head of the firm until 2002, when the brand was sold, first to Mr. Gigandet, and later to Denis Blanc, of Ad Hoc Pipe. [link is dead]

The company specialises in the production of horn, acrylic and cumberland stems, and today is the only maker in Saint-Claude producing horn and Lucite stems. It also makes the Terminus system pipes, employs half a dozen people and export 25% of its production. From site Ad Hoc Pipe [link is dead]

Horace Waille, the great-grandfather was a pioneer in the history of Pipe story of Saint Claude and created in 1860 a pipe workshop.  Rene Waille, his son, has continued the activity from 1902 to 1932 and was specialized in the initial shaping.

Andre Waille, son of Rene, obtained a “CAP de pipier” (Pipe maker degree) in 1926 and has pursued the activity of the familial company from 1932 to 1974. He is the only pipe maker, who obtained a Pipe maker degree. In 1968 Michel, son of Rene, actual Manager of EWA pipe joint the familial company and transform in 1974 the company in SARL PIPE EWA.

The information I gain from Pipedia that is useful – the Waille name is long-standing in France’s pipe center of Saint Claude.  I’m especially interested in the information that the company has historically specialized in the production and use of horn, acrylic and Cumberland stems which is relevant for the pipe on the worktable.  Pipephil.eu was my next stop and information there clarified the age of this EWA Trophee and the meaning of EWA.  The name was changed in 1979 from simply Waille to EWA from “Etablissement WAille” (English: Establishment).  So, the acrylic stemmed Billiard on my table dates at the earliest starting at 1979 with the genesis of the EWA stamp.With a better appreciation of the heritage and age of this EWA Trophee of St. Claude, I look more closely at the pipe itself.  The grain and classy acrylic stem and banding/shank ring shows promise, but there are also some issues and challenges in bringing this pipe back to a more presentable state.  I take several more pictures to catalogue the issues I see.  The fittings of the pipe have come apart.  As I disengage the stem and stummel, the 8mm filter sleeve is unattached to the stem and needs to be reattached.  The shank ring is also loose. The pipe has been heavily smoked and loved and the cake in the chamber is substantial.  By lightening the picture, you can see how the cake expands as it descends into the chamber.  There is no way to assess the health of the chamber wall until this cake is removed to allow the briar a fresh start and to inspect the wall for heat fissures or cracks.The rim corresponds to the lack of maintenance and cleaning of the chamber.  Thick lava has flowed over the rim and must be removed and cleaned to liberate the briar rim presentation.I like the grain on the stummel – very expressive.  What I don’t care for is the thick shellac finish that was used on this stummel – my classic ‘candy apple’ finish.  I love shine, but briar shine not chemical shine!  I will need to strip this stummel down to the raw briar to allow the grain I see to breathe again.There is a deep gouge on the left side of the shank that creeps toward the shank end where there is another dent next to the edge. The heel of the stummel has seen better days!  There are a few good-sized dents and divots that must be addressed.Probably the most fun will be cleaning the acrylic stem.  The external acrylic surface will not be difficult, but the discolored airway is another thing altogether coupled with the issue of not being able to use the normal cleaning attack with the use of alcohol.On close examination, my concern grows for the cleaning of the airway as I can see microscopic veins splaying from the airway – mainly at the bend of the stem. This next picture is looking into the mouth of the stem that the 8mm filter sleeve has vacated.  This needs to be cleaned thoroughly making way to reattach the filter and afterwards, the ring.We have work to do!  To begin the restoration of Scott’s choice of this EWA Trophee Bent Billiard of St. Claude, I start with the cleaning of the stummel by reaming the chamber which is nearly closed by the growth of the cake.  I take another picture to mark the start and then, starting with the smallest of the blade heads of the Pipnet Reaming Kit, I begin the cleaning process.  To help in the cleanup I first put down paper towel. The cake is hard and stubborn and takes some time and effort for the smallest blade to penetrate to the floor of the chamber.  I take a picture about three quarters of the way down the chamber. I use 3 of the 4 blades available and then switch to using the Savinelli Fitsall Tool to scrape chamber walls.  Finally, I sand the chamber with 240 grit paper wrapped around a Sharpie Pen.  To clean the chamber of the carbon dust, I wipe it thoroughly with a cotton pad wetted with isopropyl 95%.  The picture below shows the huge pile of carbon that was removed from the chamber. After inspection, the chamber appears to be in good shape.  What I notice after the reaming is complete is the rim width imbalance that is now evident after the cake was removed.  The left side of the rim (bottom in the picture) is thinning where fire was drawn over the rim during the lighting. Next, to clean the exterior surface of the stummel, I use undiluted Murphy’s Oil Soap on a cotton pad to scrub.  I also use a brass wire brush to work on the lava crusted on the rim as well as gently scraping it with a knife edge.  The cleaning helps, but the rim remains darkened from the lava and the ‘candy apple’ finish is still very much in place. To complete the stummel cleaning regimen, I use pipe cleaners and cotton buds wetted with isopropyl 95% to clean the internals. After many pipe cleaners and cotton buds, and scraping the mortise walls with a dental spatula, the color of the buds started coming out less soiled.  I decide to stop at this point – the internals were clean enough at this point.In order to strip the ‘candy apple’ finish I put the stummel in a soak of acetone. This should strip the stummel of all the old finish.  I leave it in the soak overnight. Turning to the acrylic stem, before I started on the restoration and as I was thinking about my approach, something in the recesses of my memory was ringing a warning concerning the approach to cleaning the clear, acrylic stem, but I wasn’t sure what it was. I decided to send Steve an email with the stem’s picture and my questions.  With his vast rebornpipes experience, as always, his response was helpful to help chart a course:

Hey Dal

The clear stems like that (if on a GBD are Perspex and early acrylic) are not resistant to alcohol. They can shatter or at least craze. I will often use lemon juice to start with and also liquid cleanser or soft scrub with bristle pipe cleaners or shank brushes. Sometimes you can use a needle file to work the insides. The airways are often rough inside so they need to be smoothed out. It is pretty labour intensive to clean out the stains as originally the airways were clear…

Steve

In a subsequent note he also added this:

Ok… the GBD brand was originally a ST Claude Brand. Perspex is an early acrylic. It was on GBD Prehistoric pipes… Lucite is another brand name for acrylic… both are acrylic.

I have soaked the stems and it does help some, but I have also put the cleanser on a pipe cleaner and let it soak as well. I have even used comet cleanser… big thing is no alcohol if at all possible. Too risky.

I have read of guys chucking a pipe cleaner in their drill like a drill bit and spinning it in the stem but have not tried that myself…  Anyway..,

 Enjoy

Steve

To begin the ‘enjoyment’ in tackling what proves to be a very stubborn project, I take a picture to mark the starting block.Using a sharp dental spoon, I work on digging gunk out of the slot cavity and scraping the hard stain buildup there.In Bulgaria we do not have ‘Soft Scrub’ but we have a product in the same genre called CIF that I next use to begin addressing the rough stains in the bent stem airway.  I use a bristled pipe cleaner and dip it in the cleanser and go to work.  With the pipe cleaner serving as a back drop I can see that microscopic veins are already evident in the airway lining. This is the ‘crazing’ effect that Steve mentioned in his note.  Removing stain from these will be an effort.  The veins are concentrated at the bend of the stem.To up the ante a bit, I decide to try the technique that Steve described that others had tried – to chock a pipe cleaner in a hand drill and utilize the high-speed rotation to enhance the cleaning process of the acrylic airway.  In order to increase the diameter of the pipe cleaner ‘bit’ I twist and wrap an additional pipe cleaner that I had already used.  I then insert this into the chuck and tighten it down.  I use another bristled pipe cleaner as the ‘drill’ and dip it in CIF cleanser.  I then insert the end of the pipe cleaner into the shank side of the stem and start the drill rotation gradually as I slowly insert the pipe cleaner into the airway – I haven’t done this before so I’m watching to see what happens!  It works like a charm.  As I insert the pipe cleaner, I increase the speed of the rotation and there is no wobble at all.  With the drill speed rotation engaged, I then push and draw the stem back and forth to create more cleaning movement.  I do this also with a soft pipe cleaner and cleanser.  The pictures show the pipe cleaner drilling.Well, I hoped for perfect results, but as feared, the stains in the veins remain visible and these are concentrated at the outer bend of the stem.  Because of this, it is evident that these veins have been here a while.  The rest of the airway is looking good.Next, from Steve’s suggested assault options, I squeeze lemon juice into a dish.  I will use the natural acids of the lemon to work on the airway.  I use the pipe cleaner too, but since the night is late, I settle at this point to put the stem into the lemon juice to soak through the night.  With the stummel soaking in the acetone and the stem in the lemon juice, I turn off the lights and end another day. The next morning, I use a pipe cleaner on the stem again.  The lemon soak through the night did seem to work, but the veins and the discoloration in the veins remain.  A reminder that we live in a fallen world where perfect pipes and restorations do not exist.  I accept this and decide to move on, but I decide to leave a pipe cleaner wet with CIF cleanser in the airway to continue to work on the stains while I turn to the stummel.The stummel has been soaking in acetone through the night to remove the ‘candy apple’ finish.  I fish it out of the acetone and the first appearance is that it still has the sheen showing that old finish was still present.  The finish has been greatly softened through the soak and with the gentle help of 0 grade steel wool I remove the finish without difficulty.  With the old thick finish removed, I examine the shank and the heel areas again where I saw significant dents and pits and discover that these are not as pervasive as they appeared before.  Most of the visible damage was to the thick finish and not to the briar.  Well, that’s one argument in favor of thick finishes!  The second picture below of the close-up of the grain – the bird’s eye grain is fantastic! Looking at the rim, it is thinner on the left side (bottom in the picture) and that edge is deteriorated.  The entire rim presentation needs freshening and to try to improve the width balance some. To address this, I take out the chopping board and put 240 grade sanding paper on it.  I give the stummel a minimal topping to give the rim a fresh start.After taking as much briar off the rim as will be helpful, I switch the board to 600 grade paper and rotate the stummel a few more times to smooth and blend.After the topping, the thinning on the left side of the stummel (bottom in picture above) remains thinner and more topping will not improve this because the stummel width descending in the chamber is thinned because of burning and lighting on that side.  To top until the rim width starts evening out would require too much briar real estate.  The way to mitigate against this, but not fully remove it, is to create an internal rim lip bevel.  On the ‘fatter’ side of the rim I increase the amount of bevel somewhat to help even out the round of the chamber.  I use a coarse 120 grade paper to begin, then follow with 240 and 600 grade papers.  The results I believe have improved the rounding, but again as with the stem airway, perfection is not achieved but it is looking very good none the less! Again, looking at the dent on the stummel heel and on the shank, just below the Trophee stamping, I examine the dents and how to repair them.  I go out on our 10th floor balcony, which is my ‘Man Cave’, and use the steaming method to raise the dent that’s on the heel of the stummel.  I wet a cotton cloth with water, and using my wife’s iron, I apply heat to the wet cloth.  When I do this, the moisture in the cloth evaporates and creates steam which is forced into the area of the briar compression.  The porous composition of wood expands with the forced heat and moisture and the result is the dent hopefully shrinks as the wood reclaims its original state.I apply the hot iron to the wet cloth over the dent.The results are excellent.  If I look hard at the place, I can still see an imprint but there is no longer a compression of the wood.I do the same to the small compression on the edge of the shank and the results are equally as good. To clean the entire stummel of the minor nicks and scratches, I utilize the less invasive approach of sanding sponges.  I use a coarse grade, then follow with a medium and light grade sponges.  I like using sponges because they can find the hard to get places as sponges, but they help remove the small nicks and pits in the briar surface.  The grain on this stummel is amazing – the dark grains appear almost cloudy as they cluster. Next, I take out the micromesh pads and wet sand utilizing pads 1500 to 2400. After finishing the wet sanding, I notice a fill on the underside of the shank next to the shape number that doesn’t look solid. Using a sharp dental probe, I test it and it doesn’t take much to remove it.  Before continuing with the micromesh process, I need to refill the pit left behind.I wipe the area with a cotton pad wetted with alcohol and mix a small amount of thick CA glue and briar dust.  I place a small amount of briar dust on an index card then drop some CA glue next to it.  Using a toothpick, I gradually pull briar dust into the CA glue until it thickens to the consistency of molasses. I then apply a small amount of the putty over the patch area, careful not to go over the shape number.  I put the stummel aside for the putty to cure.Several hours later, the patch has cured, and I begin the process of filing the patch down with a flat needle file.I’m careful to remain on the patch as I file avoiding collateral damage with nearby briar.After bringing the patch mound down almost to flush with the briar surface, I switch to using the sharp edge of a piece of 240 grade sanding paper to bring the patch down to the briar surface.  Again, keeping the sanding process tightly confined to the patch area.When the patch is smooth to touch, I then switch to 600 grade paper to smooth the patch and blend further.When the 600 grade has finished its work, I catch up the patch area in the micromesh process utilizing pads 1500 to 2400.With the patch completed, I continue by dry sanding using pads 3200 to 4000 and 6000 to 12000.  I love the thick grain on this stummel!There is no question in my mind about whether this grain can stand on its own!  At this point I apply Before & After Restoration Balm to the briar surface.  The B&A Restoration Balm does a great job simply deepening the richness of the natural briar.  I apply some to my fingers and rub it into the briar surface.  As I rub it in, it thickens to a wax-like consistency.  After I apply it thoroughly, I let it stand and absorb for about 20 minutes then I wipe off the excess and buff up the surface with a microfiber cloth.  I’m loving the grain!With the stummel on the side, I now turn to the clear Lucite stem. I begin by washing the stem with dish soap and warm water.  Looking closely at the bit area, the top lip of the button is compressed.  I take a picture of it but it’s not easy to see!  There is also roughness from tooth chatter.The lower bit has a tooth compression as well as tooth chatter.I apply clear CA glue to the lower tooth compression and spray the CA glue with an accelerator to hold the glue in place and to quicken the curing process.To deal with the compression on the top button lip, I simply sand it out using 240 grad paper.  I smooth out the tooth chatter as well.I then use 240 grade paper to sand and smooth the patch on the lower side as well as to remove the tooth chatter and roughness of the bit and button.  I follow the 240 sanding by wet sanding the entire stem with 600 grade paper to take out the small nicks and scratches.Following the 600 grade paper, I sand/buff the entire stem with 0000 steel wool.Following the steel would I wet sand the stem using micromesh pads 1500 to 2400 and then dry sand with pads 3200 to 4000 and 6000 to 12000.  After each set of three pads I apply a coat of Obsidian Oil to the stem. The stem is ready to go.  I take the nickel shank ring and clean it with Tarn-X.  It does a great job shining up. Now it’s time to reattach the 8mm filter sleeve.  I want to make sure its straight and seats accurately in the mortise.  I first slip the ring over the sleeve without attaching it with CA glue.  I want to simply use it as a spacer for the first step of reattaching the sleeve.  With the ring over the sleeve, I apply CA glue around the end of the sleeve that is inserted into the stem cavity. After I insert the sleeve into the cavity, before the CA glue sets up, I quickly seat the filter sleeve into the mortise with the ring compressed between the shank and stem.  I hold the stem firmly in place with proper orientation until the CA glue sets.With the sleeve properly seated, I then apply a few drops to the stem side of the ring and then reattach it, again seating the stem into the mortise.  It looks good – no gaps and a straight snug fit.To spruce up the EWA stem stamping, I apply Rub ‘n Buff European Gold.  I apply a little over the stamping and simply wipe it lightly off with a cotton pad.  The stamp is a little thin, but the Rub ‘n Buff holds well, and it looks good.Now the home stretch.  I mount a cotton cloth buffing wheel to the Dremel set at about 40% of full speed and apply Blue Diamond compound to the stem and stummel. I then separate the stem and change to another cotton cloth wheel dedicated to applying Blue Diamond to nickel and I buff up more shine on the shank ring.  After reuniting the stem and stummel again, I then wipe the pipe with a felt cloth to clean off the compound dust in preparation of the application of the wax.  I then change to another cotton cloth wheel with the same speed and apply a few coats of carnauba wax to stem and stummel and then finish with a rigorous hand buffing to raise the shine.

The unique grain cluster constellation that I see in the EWA Trophee is amazing.  The heel grain pattern shows color, swirls and vortexes that remind me of pictures of the planet Jupiter.  It is truly amazing and mesmerizing to look at.  The Lucite stem came out well – it is classy with the complimentary gold and black band ring providing a nice transition.  My only wish is that I could have purged the stem airway totally of the discoloration in the crazed veins that will remain as a reminder of this pipes battle scars from its past!  Even so, the EWA Trophee of St. Claude, is a beautiful Bent Billiard and Scott did well in seeing the potential of this pipe when he commissioned it.  As the commissioner, he has the first opportunity to acquire it in ThePipeSteward Store.  This pipe benefits the Daughters of Bulgaria – women and girls who have been trafficked and sexually exploited.  Thank you for joining me!

An Easy Sprucing up of a 1949 Dunhill Shell # 52 F/T


Blog by Paresh Deshpande

Believe you me friends, this is FUN!! Being able to work on different pipes, be able to choose your project, choose a brand you wish to work on, is an exhilarating experience for me. Prior to the Mumbai Bonanza striking me, I was restricted mostly to working on my inherited collection of pipes, each complete with its stem challenges and similar stummel condition and was getting slightly monotonous to say the least.

I was fortunate enough to have heeded the advice of my dear friend and mentor, Mr. Steve, and struck a deal with a trash collector from Mumbai. He did not know what he was selling and I did not know what I was buying as we reside in different cities!! The argument that Mr. Steve presented was that if not anything, I shall at least have some spares and this was logical. I struck a deal and here are pictures of the pipes that I received in this lot.  This lot contains some very nice collectible pipes, a few well known brand pipes and some mediocre pipe brands. Overall, with seven Dunhills, a Preben Holm #1, a couple of Made in England Pete System pipes, Charatan’s, Custom-Bilt, Stanwell and other assorted pipes, I would say that I had hit a huge jack pot!!! Hence, I like to call this find as “Mumbai Bonanza”.

The pipe that I decided to work on from this find is a smallish full bent Dunhill Shell billiard, and is marked in pastel blue circle in the picture below (the ones circled in red and yellow are completed projects). This is a beautiful deeply sandblasted billiard with a lovely tactile feel in the hand. The play of dark red brown hues on the sandblast makes for a visual treat. It is stamped on a smooth surface on the foot and the underside of the shank with the shape number 52 followed by F/T followed by DUNHILL Shell Made in England 9 (9 is underlined) 0 all in a straight line over PATENT No 417574/34 followed by an encircled 3 at the shank end. This stamping indicates that this pipe is a fishtailed group 3 sized shell and dates this pipe to being manufactured in 1949 and sold in 1950.  The Trademark Dunhill White Dot adorns the top of the vulcanite stem. The stampings are deep, crisp and clear.With this information, I move ahead with the restoration of this beautiful sandblasted Dunhill bent billiard.

INITIAL VISUAL INSPECTION
The chamber has a thick layer of even and smooth cake which indicates that the pipe has been well used but also well cared for by its previous Steward. From what I can see, the chamber walls appear to be without any damage. The chamber is odorless. There is an overflow of lava on the blasted rim top surface. The inner and outer rim edges appear to be in pristine condition. The mortise is clean and so is the shank airway. The stummel boasts of some beautiful deep sandblast pattern all around. It is dirty with grime and oils filling in much of the craggy finish. The briar, in this condition also, looks amazing. I can’t wait to see after I have worked on it. The round shank of the bent billiard flows into a bent tapered stem which has a flare, like a fish tail, at the button end and hence the stamp F/T. The vulcanite stem shows significant damage to the button end with deep bite marks on both upper and lower surface of the stem. The lip is also severely damaged and will have to be reshaped. In this project, repairs to the damaged stem will be a major challenge, however if compared to previous stem repairs, this should be a cake walk.

THE PROCESS
Since the stem has significant damage, and from my experience of stem repairs, this will be time consuming and laborious part and hence I start this project by tackling the stem first

Now that I was clear about the path to be followed, I first flame both the surfaces of the stem with a Bic lighter. The heat from the flame raises the vulcanite to the surface and takes care of the tooth chatter that was seen earlier. I sand the stem with a folded piece of 220 grit sand paper to get rid of the oxidation, have a clear idea of the areas which require fill and its extent while providing a smooth surface for the intended fill. I cleaned out the internals of the stem with hard bristled and regular pipe cleaners dipped in isopropyl alcohol. Once I was satisfied with the internal cleaning, I wiped the stem surface, particularly the damaged button end, with a cotton pad and alcohol to remove any traces of dirt and grime.To begin the stem repairs, I prepared a mix of CA superglue and activated charcoal and generously applied it over the damaged surface and set it aside for curing over night. Before moving ahead, I would like to mention here that I had applied this mix to achieve sufficient thickness which would help during the filing and sanding while shaping the button and achieving the correct stem profile.While the stem repair was set aside to cure, I moved ahead to deal with the stummel repairs. I start the reaming with a size 1 head of the PipNet reamer and progress to size 2 head. I further clean the chamber with a folded piece of 180 grits sand paper to sand out the remaining traces of cake and expose the walls of the chamber to ascertain that there are no cracks/ heat fissures. Using my fabricated knife, I gently scrapped away the lava overflow. I wiped the chamber with a cotton pad dipped in isopropyl alcohol to remove the carbon dust left behind by all the reaming and sanding process. This also eliminated all traces of old smells from previous usage. The walls of the chamber were solid with no damage. Continuing with the cleaning regime, using a soft brass wired brush I gently scraped away the thick lava coat in the blast of the rim. With a hard bristled tooth brush and dipped in undiluted Murphy’s oil soap, I very deliberately scrubbed the sandblast finish on the stummel and the rim top. The stummel and rim top was dried using paper napkins and soft cotton cloth and set it aside to dry out naturally. The stummel looks fresh and clean. Next, I rub a small quantity of “Before and After Restoration Balm” in to the briar with my finger tips and let it rest for a few minutes. The balm almost immediately works its magic and the briar now has a nice vibrant appearance with the beautiful contrasting hues colors that are unique to this sandblast pipe, on full display. I further buff it with a horse hair shoe brush. After I had applied the balm, the rim top surface appeared too darkened and unclean. I was not happy with the way the rim top looked at this stage and decided to further clean it. I scrapped the rim top surface with a brass wired brush with a bit more pressure than I normally apply. The rim surface appeared clean as can be seen in the picture below. I reapplied the balm, hoping that the surface would look clean with the sandblast patterns showing themselves proudly. But alas!! The rim top surface appeared as before, blackened and unclean. I was at my wits end when after repeated cleaning with the brass brush with increasing pressure each time, the rim top surface appeared as before, dark and unclean. Mind you readers, being a sandblasted surface, topping really was not an option that I desired to adopt. I let the rim top surface be, satisfied that it was clean and sans any old lava overflow. In my exuberance to appreciate the beautiful and rugged patterns on the stummel caused by sandblasting, I missed out on cleaning the mortise and the shank airway. This is what exactly I addressed at this stage. Using bristled and regular pipe cleaners dipped in isopropyl alcohol, I first moistened the oils, tars and gunk in the mortise. Thereafter, with my fabricated spatula, I scrapped out all the tars and oils from the mortise. As I progressed with my cleaning, eventually the pipe cleaners started coming out clean indicating that the shank internals are clean.I set the stummel aside and turned my attention to the stem repair. The fill had cured nicely and I moved ahead and began the process of filing and shaping the button end with a flat head needle file. For a better blending, I further sand the entire stem with 220 followed by 400, 600 and 800 grit sand paper. This helps to reduce the sanding marks left behind by the more abrasive 220 grit paper. To bring a deep shine to the vulcanite stem, I went through the complete set of micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. I wiped the stem with alcohol after each pad and rubbed it down with Extra Virgin Olive oil to rehydrate the vulcanite. The repairs have blended in very well and the stem now looks shiny black and beautiful. The internals of the stem was once again cleaned out using alcohol and pipe cleaners to clear the airway of all the debris resulting due to the sanding. The finished stem is shown below. To finish, I re-attach the stem with the stummel. I mounted a cotton cloth buffing wheel to my local machine which is similar to the Dremel.  I set the speed at about half of the full power and applied White compound to the entire pipe. I wiped/ buffed the pipe with a soft cotton cloth to clear it of any leftover compound dust. I then mounted another cotton cloth wheel on to the polishing machine and applied several coats of carnauba wax. I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further.The completed pipe looks lovely, fresh and vibrant. The deeply sandblasted surface proudly displays the contrasting dark brown hues which was the hallmark of Dunhill Shell pipes with a nice tactile feel in the hand. It surely is one of the best looking sandblasted pipes and will find a place of pride in my humble collection. As and when I load this pipe with my favorite tobacco (I love my English blends…) and sip my scotch, I wish this dude could tell me all about its past life!! Ah, this would be bliss…cheers!

Sprucing up another WDC: A Cased Bakelite & Briar Dublin


Blog by Paresh Deshpande

There a quite a few WDCs that I have inherited from my old man and the one on my table now is “WDC BAKELITE” in its original case. I loved the deep red color of the Bakelite shank and the fiery transparent red of the stem. Thus, no surprise here that I chose to work on this WDC Bakelite Dublin shaped pipe!!

This is the third WDC from my grandfather’s collection, WDC Bakelite in an impressive Dublin shape. The dark brown briar bowl, Bakelite base and translucent Bakelite stem looks attractive. The gold filigree at the shank end adds a classy bling, breaking the red monotony of the stem and shank.  I dare say that this pipe does not boast of only beautiful bird’s eye or cross or straight grains but nevertheless distinct swirls of grains can be seen which are eye-catching to say the least!!  The shank and stem is devoid of any stamping, however, the only stamping to identify this pipe to be a WDC is seen on the top lid of the leather covered case. The case is internally lined with a soft silky felt cloth in light green color and bears the trademark inverted equilateral triangle in red with letters “WDC” over “BAKELITE” in gold. Gold ribbons flow from either sides of the triangle and bears the words “FRENCH” on the left ribbon and “BRIAR” on the right. The quality of the case, its felt lining and the stamping simply shouts QUALITY!! I searched pipedia.com for more information on this pipe and attempt at estimating the vintage of this pipe. Though I could not find any information about this pipe in particular or a connection between WDC and Bakelite material, here is what I have found on pipedia.org about the brand:

William Demuth. (Wilhelm C. Demuth, 1835-1911), a native of Germany, entered the United States at the age of 16 as a penniless immigrant. After a series of odd jobs he found work as a clerk in the import business of a tobacco tradesman in New York City. In 1862 William established his own company. The William Demuth Company specialized in pipes, smoker’s requisites, cigar-store figures, canes and other carved objects.

The Demuth Company is probably well known for the famous trademark, WDC in an inverted equilateral triangle. William commissioned the figurative meerschaum Presidential series, 29 precision-carved likenesses of John Adams, the second president of the United States (1797-1801) to Herbert Hoover, the 30th president (1929-1933), and “Columbus Landing in America,” a 32-inch-long centennial meerschaum masterpiece that took two years to complete and was exhibited at the World’s Columbian Exposition in Chicago in 1893.

The Presidential series was the result of Demuth’s friendship with President James A. Garfield, a connoisseur of meerschaum pipes. Demuth presented two pipes to Garfield at his inauguration in 1881, one in his likeness, the other in the likeness of the President’s wife. Later, Demuth arranged for another figurative matching the others to be added to the collection as each new president acceded to the White House, terminating with President Hoover.

In early 1937, the City of New York notified S.M. Frank & Co. of their intent to take by eminent domain, part of the land on which the companies pipe factory was located. This was being done to widen two of the adjacent streets. As a result of this, Frank entered into negotiations to purchase the Wm. Demuth Co.’s pipe factory in the Richmond Hill section of Queens. It was agreed upon that Demuth would become a subsidiary of S.M. Frank and all pipe production of the two companies would be moved to DeMuth factory. New Corporate offices were located at 133 Fifth Avenue, NYC.

Demuth pipes continued to be made at the Richmond Hill plant till December 31. 1972. Then the Wm. Demuth Company met its official end as a subsidiary company by liquidation.

I came across an interesting catalog on the same page on pipedia.org which shows the exact same pipe that I am now working on. It is the same pipe as the first pipe on the left in second row. A close scrutiny of the picture confirms the following:

(a) Bakelite material was being newly introduced by WDC as WDC Bakelite line. This can be inferred from the Note on the flyer “BAKELITE IS A NEW PATENT COMPOSITION……….NOT BURN”.

(b) The pipe before me is model number 24718 and was at the time their second most expensive of all the pipes advertised in the flyer, retailing at $8!!

(c) The catalog was published by “John V Farwell Company, Chicago”. John V. Farwell & Co. was a department store in Chicago, Illinois, United States. The store’s history traces back to 1836, when the Wadsworth brothers came to Chicago to sell goods. John V. Farwell & Co. was the most successful store in the city until the 1871 Great Chicago Fire. The store continued to operate after the fire, but faced stiff competition from former partners Marshall Field and Levi Leiter. It was purchased by Carson, Pirie & Co. in 1926. (https://en.wikipedia.org/wiki/John_V._Farwell_%26_Co.) I visited rebornpipes.com and came across an interesting article on materials used in pipe making (https://rebornpipes.com/2014/08/09/hard-rubber-and-other-early-plastic-used-in-pipes-ronald-j-de-haan/)

It is here that I found the following information on “BAKELITE”:

These qualities made Bakelite the most successful synthetic material in the first half of the 20th century. From 1928 it was also produced as molded resin. Both the pressed and the molded forms were suitable for the pipe making industry. Pipes were made from Bakelite and molded phenol-resin. Complete pipes of Bakelite are very rare because of its lack of heat resistance. Phenol-resin however was frequently used for pipe mouthpieces and cigarette holders because it imitated amber.

From the above gleaned information, it is safe to conclude that the pipe now on my worktable is of 1920s and early 1930 vintage and at that point in time was WDC’s new offering retailing at $ 8!!

INITIAL VISUAL INSPECTION
The leather covered case in which the pipe was safely ensconced for many years has borne the maximum brunt of uncared for storage. The leather has weathered while being exposed to the extreme climate and has cracked at a number of places. However, the hinges and the lock mechanisms are intact and function smoothly. I shall just be giving a nice wipe with a moist cloth and applying a neutral shoe polish coat which is rich in wax content. The lining within has stained near the bowl/ Bakelite base joint and near the rim top. This needs to be cleaned up. Age definitely shows on the stummel surface!! The briar is dull and lifeless and has taken on a layer of aged patina, through which one can make out the beautiful grain patterns all around. There is a heavy overflow of lava all over the entire stummel surface. The bowl is covered in oils, tars and grime accumulated over the years of storage and is sticky to the touch. To be honest, the stummel is filthy to say the least. A thorough cleaning of the stummel followed by polish should accentuate the beautiful mixed grain pattern seen on the stummel through all the dirt. The Bakelite base of the stummel is dirty and sticky. Few scratches are also seen on close observation. The bowl (‘Real Walnut Bowl’ as specified in the flyer above!!) screws-in directly on to the Bakelite base. There is no brass or any metal separator between the bowl and the base, which is surprising. The threads on the bowl and the Bakelite base are covered in oils, tars and gunk. The bowl has one small hole at the heel through which the smoke passes in to the shank. The heel of the Bakelite base shows traces of old oils and tars. This will need a thorough cleaning.There is heavy buildup of cake with a thick layer in the chamber. The condition of the inner walls of the chamber can be ascertained only after the cake has been removed completely and taken down to bare briar. The bowl however, feels robust and solid to the touch from the outside. The rim top has a thick layer of overflowing lava. The condition of the smooth rounded inner and outer edge and rim top can be commented upon once the overflow of lava is removed and the chamber is reamed. The shank end of the pipe is clean. These issues should be a breeze to address, unless some hidden gremlins present themselves!!The diamond Bakelite stem has a rounded orifice which also points to its vintage. It is a rich reddish color that is translucent and the light really plays through. I cannot wait to see the stem clean up. Deep tooth indentations and minor tooth chatter is seen on the upper and lower surface. The pointed corner edge of the lip on the left is broken and will either have to be reconstructed or filed away to a straight profile. The lip edges have also been chewed off and greatly deformed. The screw-in tenon appears to be a Delrin tenon (or is it bone?) and is covered with dried oils and tars. The fit of the stem in to the mortise is very loose and the alignment is overturned. This will be a first for me as I have corrected metal threaded stingers, but never a Delrin or bone. The mortise does show signs of accumulated dried oils, tars and remnants of ash, greatly restricting the air flow. As I was dismantling the pipe, the gold filigree band also separated from the diamond squared Bakelite shank.The overall condition of the pipe, with the thick build-up of cake in the chamber, clogged mortises, overflowing of lava covering the entire stummel and the deep bite marks to the stem makes me believe that this would have been one of my grandfather’s favorite pipes.

THE PROCESS
As is always the case, I prefer to start my restoration with part that has the most significant damage. In this case it was the stem. I first cleaned out the internals of the airway with pipe cleaners dipped in alcohol. This was followed by cleaning the surface and the deep tooth marks with cotton pads dipped in alcohol. This helps to remove all the dirt, oils and grime from the surface before proceeding with fills. Since the tooth indentations are deep, I shall resort to the layering technique for the fills. Having cleaned the bite marks and the stem surface, I fill these with clear superglue and set it aside to dry. The fills had shrunk once the glue had cured, exposing the damage. I gave a second layer of superglue fill and set it aside to cure. I had decided to address the issue of broken corner of the lip edge by reconstructing it afresh using superglue (God, why can’t I simply straighten the edges which would have been way simpler than reconstructing the concave shaped lip edges!!). I went about this task by placing a big drop of superglue and holding the stem such that a droplet was formed at the broken edge. Once this was done, it was all about twisting, turning and blowing so that the droplet does not fall to the ground while remaining at the broken edge. After the droplet has hardened, I repeated the process till I had more than enough well cured and hardened large edge which then could be filed and shaped as required.While the stem fills were curing, I addressed the thick cake in the chamber. I started by reaming the chamber with size 2 and followed it up with size 3 and 4 head of PipNet reamer. I used a 220 grit sand paper, pinched between my thumb and forefinger, to sand the inner walls of the chamber of the pipe. Once I had reached the bare briar, I wiped the chamber with a cotton pad dipped in isopropyl alcohol. This removed all the residual carbon dust from the chamber. The walls of the chamber are nice and solid with no signs of heat fissures or cracks. I scrapped out the overflowing lava from the rim top with my fabricated knife. The inner and outer rim edges are pristine and that was a big relief.I cleaned the threads and the heel of the Bakelite base with cotton and alcohol. This was followed by cleaning the mortise and air way of the pipe using hard bristled and regular pipe cleaners, q-tips dipped in alcohol. The mortise and the draught hole were given a final clean with shank brushes dipped in alcohol. I dried the mortise with a rolled paper napkin. The shank internals and the draught hole are now nice and clean with an open and full draw.Using a hard bristled tooth brush dipped in undiluted Murphy’s oil soap and brass wire brush, I scrubbed the stummel, cleaning the surface thoroughly. I was very deliberate on the surface areas which were covered in overflowed lava over which dirt and grime had accumulated over the years. I rinsed the stummel under tap water, taking care that water does not enter the mortise or the chamber. I dried the stummel using cotton cloth and paper napkins. On close inspection, I observed a couple of minor dents and ding on the front portion of the stummel. These would need to be addressed. I also cleaned and removed the entire accumulated and now moistened gunk from the threads and base if the bowl with my fabricated dental spatula and the brass wired brush. The stummel is now clean and devoid of any grime and dirt. It is really surprising that the rim top, round edges and the stummel is in such pristine condition after so many years of storage and without a single fill. Speaks volumes about the quality of this line of pipes from WDC!! To further clean and highlight the grains, I sand the stummel with a folded piece of 220 grit sand paper followed by 600 grit sand paper. For a deeper shine and to remove the scratches left behind by the coarse grit papers, I followed it up by sanding with the micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. I wiped the stummel after each wet pad with a moist cloth to remove the resulting dust. I rub a small quantity of “Before and After Restoration Balm” in to briar and let it rest for a few minutes. The balm almost immediately works its magic and the briar now has a nice vibrant appearance. I further buff it with a horse hair shoe brush. The pipe now looks lovely with beautiful grains showing off their beauty in all glory!! While the bowl was absorbing the balm, I worked the Bakelite base. I cleaned the surface with a cotton pad dipped in acetone and with horror I realized that I could see some swirls like marks on the shank. This got me worried and I immediately conferred with Mr. Steve, my mentor. He informed me that the Bakelite needs to be cleaned only with soap water!! Ah, well, what’s done is done. He suggested that I use the balm and see if it helps and it did but not to the full extent. I bashed on regardless, going through the complete micromesh pad cycle. It was then that I realized that the so called spots were from within and not external! Whew, what a relief. The Bakelite base looks absolutely stunning with a deep red color. With the bowl and Bakelite base now nice and clean and attractive, I worked the stem of the WDC.  Just to let the readers know, that all the while that I was working the bowl and base, I was simultaneously adding layers of superglue to the tooth indentations and chatter and the broken corner edge of the lip. Once I was satisfied with the thickness of the fill (I prefer over filling which can be evened out during sanding), I began by sanding the fills with a flat heat needle to achieve a rough match with the surrounding stem surface. I sharpened the lip edges using a needle file and sand the entire stem with 220 followed by 400, 800 and 1000 grit sand paper to perfectly blend the filled surface with the rest of the stem surface. This helps to reduce the sanding marks left behind by the more abrasive 220 grit paper. By mere sanding itself, the minor tooth marks seen on stem surfaces were completely addressed. I was especially careful while shaping the broken corner edge of the lip. Finally, after long hours at the table, I was able to achieve a satisfactory reconstruction of the lip along with the proper concave around the orifice. To bring a deep shine to the Bakelite stem, I went through the complete set of micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. The only part begging for attention was also the most attractive and costly item on this pipe; the gold filigree band!! This band was easily detached from the shank end and this made the cleaning job very easy. I use Colgate tooth powder to clean all the silver and gold bands and embellishments on pipes, a trick I learned from Abha, my wife. Some readers may find it surprising, but believe you me gentlemen, please at least give a try to see if it suits you. The band cleaned up nicely. I carefully applied a very small quantity of superglue along the shank end edges and stuck the band firmly over the shank end.Before moving on to polishing and buffing, the only issue that remained to be addressed was that of the overturned tenon. I discussed with Mr. Steve who suggested that I should try using clear nail polish coat over the threaded tenon and once the nail polish had completely dried, I should try the fit. I did just that and, viola!! The fit and alignment of the stem and shank was perfect!!

To finish, I re-assembled the entire pipe. I mount a cotton cloth buffing wheel on to my local machine which is similar to a Dremel.  I set the speed at about half of the full power and polished the entire pipe with White Diamond compound. I wiped/ buffed the pipe with a soft cotton cloth to clear it of any leftover compound dust. I then mounted another cotton cloth wheel on to the polishing machine and applied several coats of carnauba wax over the bowl, Bakelite base and the Bakelite stem. I finished the restoration by giving the pipe a rigorous hand buffing using a microfiber cloth to raise the shine further. The completed pipe, with the dark brown hues of the grains on the bowl contrasting with the shining deep red Bakelite base and the translucent Bakelite stem, looks lovely, fresh and vibrant; the photographs speak for themselves. The leather covered case was cleaned and polished with wax rich neutral shoe polish. If only the pipe could tell some of my grand Old man’s stories and recount incidents witnessed while being smoked.…………… Cheers!! I am grateful to all the readers for their valuable time spent in reading this write up and joining me on this part of the journey in to the world of pipe restoration while I attempt to preserve a heritage and past memories which eternally shall remain a part of me. 

Refurbishing a Battered Dunhill Bruyere #32041


Blog by Paresh Deshpande

I had just finished restoring three pipes from my inheritance; a WDC Stratford, The Doodler and a Barling # 2639. Save for the WDC, these were easy projects and it helped that Abha, my wife, had done all the initial cleaning. I finished these pipes in real quick time.

Now I turned my attention once again to the pipes from my “Mumbai Bonanza”. I have restored three pipes; two Dunhill and a Stefano Exclusive from this lot of 30 and each one has been, well, to put it mildly a royal pain where you wouldn’t like it!!  How did I land up with this lot makes for an interesting read and about one which I have written in the restoration of the Stefano Exclusive (https://rebornpipes.com/2019/03/11/mumbai-bonanza-stefano-exclusive-restorationa-month-long-project/).

Here are pictures of the pipes that I received in this lot. This lot contains some very nice collectible pipes, a few well known brand pipes and some mediocre pipe brands. Overall, with seven Dunhills, a Preben Holm #1, a couple of “Made in England” Pete System pipes, Charatan’s and other assorted pipes, I would say that I had hit a huge jack pot!!! Hence, I like to call this find as “Mumbai Bonanza”.

The pipe that I decided to work on is from this find and is marked in a red circle in the picture below. It’s the third Dunhill from this lot, a Bruyere in a classic bulldog shape. The stummel surface boasts of some beautiful densely packed cross grain on the stummel, cap and also the shank top, bottom and side surfaces. It is stamped with “# 32041” towards the bowl and followed by “DUNHILL” over “BRUYERE” on the left side of the shank while the right side bears the COM stamp “MADE IN” over “ENGLAND” followed by underlined numeral “18”. Dunhill White Dot adorns the top of the vulcanite stem. The stampings on either side is deep, crisp and clear.The dating of this pipe is very straight forward and dates to 1978 (1960+18). Deciphering the shape code, “32041” is equally straight forward with the first digit 3 identifying this pipe as being Group size 3, second numeral, 2, identifies the style of mouthpiece as being a saddle stem and the digits 04 indicates Bulldog shape. With this information, I proceed ahead with the restoration of this handsome pipe.

INITIAL VISUAL INSPECTION
The chamber is clean with a thin layer of cake which indicates that the pipe has been kept clean by its previous Steward; however, the reaming has been done unevenly. From what I can see, the chamber walls appear to be without any damage. The chamber is odorless. It is the rim top, including the outer and inner rim edge that shows significant damage on the left side in 11 o’clock and 7 o’clock directions. This must have been caused due to hammering of the edge against a hard surface to remove dottle!! There is not even a millimeter of surface on the rim top surface which does not show signs of severe damage. All in all, it appears like this pipe’s rim top was used by the previous Steward as a hammer while giving vent to his/ her anger, and if this is true by any stretch of imagination, HE/ SHE SHOULD ENROLL FOR ANGER MANAGEMENT TREATMENT!! Darkening of the outer rim edge is also seen all along the left half of the rim top, most significantly in 11 o’clock and 7 o’clock directions. I just hope that it does not go deep in to the briar!!  Being a Dunhill, any issue of fills is never to be expected and hold true for this pipe too. However, there are a number of scratches and dents that can be seen on the stummel surface. These dents and ding are probably caused due to uncared for storage by the previous Steward and further contributed to by the trash collector who had sold the pipes to me. The stummel is covered in dirt and grime. The briar looks lifeless and dull which is nothing serious to address.I am very pleased with the condition of the stem. The diamond saddle type vulcanite stem shows minor damage to the button end and the lip edges. Light scratches can be seen extending upwards from the button end towards the saddle. The quality of vulcanite is good. These issues should be an easy fix. The mortise is clogged and will have to be cleaned. In this project, repairs to the damaged outer edge and rim top surface will be a major challenge. While restoring the Dunhill Bruyere # 51671 (https://rebornpipes.com/2019/03/13/reconstructing-a-broken-stem-on-dunhill-bruyere-51671/), I had faced difficulties in blending the repairs to the outer rim edges and these could be seen even after I had stained the stummel. Similar set of difficulties are envisaged on this pipe too!!!! I have learned my lesson and will follow the advice and suggestion received from readers of rebornpipes.com.

THE PROCESS
Since the stummel has significant damage, I start this project by tackling the stummel repairs first. I reamed the chamber with size 2 head of a PipNet reamer. The cake was thicker at the bottom and using my fabricated knife, I scraped out all the remaining cake. I further used one folded piece of 180 grit sand paper to sand out the last traces of remaining cake and expose the walls of the chamber to ascertain that there are no cracks/ heat fissures. I wiped the chamber with a cotton pad dipped in isopropyl alcohol to remove the carbon dust left behind by all the reaming and sanding process. The walls of the chamber were solid with just very fine superficial web of lines seen on one side. This was followed by cleaning the mortise by scraping away at the dried gunk with my fabricated spatula and followed it up with further cleaning using cue tips, pipe cleaners and shank brush dipped in isopropyl alcohol. With the thin sharp edge of my fabricated spatula, I cleaned in between the edges of the cap ring separating the cap from the rest of the stummel. Continuing with the cleaning regime, using a hard bristled tooth brush dipped in undiluted Murphy’s oil soap, I very deliberately scrubbed the surface of the stummel and the rim top. The original reddish dye was also washed away to some extent. The dirt and grime on the stummel surface was so stubborn that I had to resort to using a scotch-brite pad to get rid of it. While scrubbing the stummel, I paid special attention to areas where significant darkening was seen just below the rim outer edge. Thankfully, the burn marks were superficial and cleaned out nicely. However, a dark spot was revealed just below the cap ring and is marked in a red circle. The damages to the outer rim edge, uneven inner rim edge and stummel dents and dings are now clearly visible in the above pictures after the cleaning. I had a close, hard look at the darkened spot seen and marked in red. The briar on and around the spot was hard and solid with no deep heat fissures on the corresponding inner surface of the chamber. This ruled out the possibility of a burn out!!!! Phew, what a relief this was!!!! This external darkening, most probably, appears to have been caused when the pipe was placed in an ash tray alongside a smoldering cigarette butt, just a hypothesis!!! This will be addressed (hopefully!) when I sand the stummel surface to get rid of all the scratches and dents.

With the stummel now dried out, I got around to address the rim top and outer rim damage. The extent of the dip or trough caused due to banging the rim edge against a hard surface was deep and would necessitate heavy topping off of the rim surface, and I for one, absolutely wish to avoid any loss of briar!!!!! So, I decided to try out something different. I planned on first filling up the deep troughs on the rim edge using briar dust and superglue to roughly match the rim surface and some more and then topping it to achieve a smooth surface. Theoretically, this sounded logical.

I resorted to the layering method again; first I layered superglue over the damaged surfaces on the front and back outer rim edges, followed by sprinkling of briar dust, another layer of superglue followed by a final layer of briar dust. This final layer of briar dust reduces the probability of air pockets. In the last picture, you can see that the layering has been done to the level of the rim surface so that it sits evenly on a flat surface without showing any gaps. I set the stummel aside to cure. While the stummel fill was being set aside to cure, I tackled the stem repairs by first flaming the surface with a Bic lighter flame to raise the bite marks to the surface. This was followed by sanding the stem surface with a folded piece of 220 grit sand paper. This step has a twofold purpose; firstly, it helps to roughly blend the raised bite marks with the rest of the stem surface and brings to fore the spots which require filling and secondly, it helps to rid the oxidation from the stem surface which helps subsequently in better finish after polishing. I cleaned out the surface with a cotton pad dipped in alcohol to remove all the dirt and grime. Once the surface was clean, the lip edges and the bite marks were filled with a superglue and activated charcoal mix and set aside to cure overnight. The fill repair to the outer rim edges had cured by this time and with a flat head needle file, I roughly sand the fills to match the surrounding surface. Using a folded piece of a 220 grit sand paper, I further blended the outer filled edges with the rest of the edge and created a slight bevel to mask the uneven inner rim edges. The rim top surface was topped on a piece of 220 grit sand paper to further blend and even out the rim top, checking frequently the progress being made. Personally, I prefer to avoid topping as I do not appreciate loosing even one mm of briar estate, but in this instance, I was left with no recourse but to top the rim. I lightly top it on 600 grit sand paper to reduce the sanding marks left behind by the 220. However, a few air pockets revealed themselves (marked in red-orange circle) at this stage which necessitated reapplication of briar dust and super glue. Sorry, missed out taking pictures of this stage!! While the second fill to the rim outer edge was curing, I turned my attention to work on the cured stem fills. Using a flat head needle file, I roughly matched the fills with the rest of the stem surface. For a better blending, I further sanded the entire stem with 220 followed by 400, 600 and 800 grit sand paper. This helps to reduce the sanding marks left behind by the more abrasive 220 grit paper. To bring a deep shine to the vulcanite stem, I went through the complete set of micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. I wiped the stem with alcohol after each pad and rubbed it down with Extra Virgin Olive oil to rehydrate the vulcanite. The repairs have blended in very well and the stem now looks a shiny black and beautiful. The internals of the stem was cleaned out using alcohol and pipe cleaners. The finished stem is shown below. The next evening, the repairs to the edge had completely cured and I move ahead by filing and rough shaping with a flat head needle file. I further fine tune the blending by sanding it down with 220, 320, 600 and 800 grit sand papers. Here is how the repaired area appears at this stage. I am very pleased with the way this repair progressed. I sand the entire stummel using 220, 400, 600 and 800 grit sand papers. The little dents and dings that remained on the stummel and outer rim edge were also evened out under this sanding process. This was followed by polishing with micromesh pads. I wet sand the stummel with 1500 to 2400 grit pads and follow it up by dry sanding with 3200 to 12000 grit pads. I wiped the surface with a moist cotton cloth after every wet pad to check the progress. The repaired rim edge appears, in picture, as though it is patchy with air pockets. However, that is not the case. The fill is smooth and solid and should get masked after I have stained it. I rub a small quantity of “Before and After Restoration Balm” in to the briar with my finger tips and let it rest for a few minutes. The balm almost immediately works its magic and the briar now has a nice vibrant appearance. I further buff it with a horse hair shoe brush. I had hoped that the balm would work its magic on the filled area and help in blending it a bit, and that did happen!! I am very pleased with the way these repairs have turned out. And now on to staining and polishing… After Mr. Steve had uploaded my write up on the Dunhill Bruyere Horn shaped pipe (https://rebornpipes.com/2019/03/13/reconstructing-a-broken-stem-on-dunhill-bruyere-51671/), the feedback and responses were very educative and I had decided to incorporate these suggestions while working this project. Mr. Roland Borchers brought out that the original color of Bruyere was achieved by first staining with Dark Brown stain followed by Cherry red stain. Mr. Steve also concurred and then there was no turning back!! I stained the stummel in DB stain first. I use the powder variety of stain and mix it with 99% isopropyl alcohol. I heated the stummel surface with a heat gun and applied the stain with a folded pipe cleaner. As I paint the stummel with stain over sections at a time, I burn the dye using a Bic lighter that combusts the alcohol in the aniline dye and sets the dye pigmentation in the wood.  After fully saturating the stummel and covering the whole surface, including the rim top, I set the stummel aside to rest for several hours. By next evening, the stain had set nicely. I mount a cotton cloth buffing wheel (because I do not have felt cloth buffing wheels!!) on the Dremel and set the speed at about 40% of full RPM and apply white compound to the stummel. This does help in revealing the grains gradually. This time around, the repaired area had blended very nicely in to the rest of the stummel surface. Here is another lesson that I have learned; it is advisable to use white compound after staining and not red Tripoli as I used to, for the reason that the red Tripoli compound is more abrasive and does not make sense to use after polishing by 12000 grit micromesh pad!! I followed this polish by re-staining the stummel with Cherry red stain. I set it aside to let the briar pores absorb the stain pigments. To finish, I re-attach the stem with the stummel. I mounted a cotton cloth buffing wheel to my local machine which is similar to a Dremel, set the speed at about half of the full power and applied White Diamond compound to the entire pipe. I wiped/ buffed the pipe with a soft cotton cloth to clear it of any leftover compound dust. I then mounted another cotton cloth wheel on to the polishing machine and applied several coats of carnauba wax. I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further. The completed pipe looks lovely, fresh and vibrant; the photographs in this case, do not do justice to the appearance of this beautiful pipe. I cannot thank enough my friends and gentlemen who painstakingly identified my mistakes and suggested remedial measures after reading the write up for helping me to hone my skills while gaining experience.

Restoring the 3rd of Jennifer’s Dad’s Pipes – A 1960 Dunhill Tanshell 589 Zulu


Blog by Steve Laug

Time to get back to Jennifer’s Dad’s pipes. The next pipe on the worktable is from the estate of George Rex Leghorn. You may not have read this so I will retell the story. I received an email from Jennifer who is a little older than my 64+ years about whether I would be interested in her Dad’s pipes. My brother Jeff and I have been picking up a few estates here and there, so I was interested. Here is the catch – she did not want to sell them to me but to give them to me to clean up, restore and resell. The only requirement she had was that we give a portion of the sales of the pipes to a charity serving women and children. We talked about the organization I work for that deals with trafficking and sexual exploitation of women and their children and she decided that would be a great way to carry on the charitable aspect of her Dad’s character. With some great conversation back and forth she sent the pipes to Jeff and he started the cleanup process on them. Once he had finished cleaning them all he sent them to me to do my work on them.

The third pipe I chose to work on from the lot was another craggy looking Dunhill. This one was a Tanshell Zulu shaped pipe. It had a beautiful sandblast on the bowl sides and shank. It had the Dunhill Tanshell rich tan brown stain but it was dirty and hard to see the colour well. The stem was badly oxidized with tooth marks and chatter on the top and underside near the button. The transition to the button was worn to almost an angle. There was a thick cake in the bowl and it had overflowed with lava was dirty and tired looking. It had been sitting in boxes for a lot of years and it was time to move ahead with the restoration. Jennifer took photos of the pipes she was sending. I have included three she included from this pipe. When the box arrived from Jennifer, Jeff opened it and took photos of each pipe before he started his cleanup work on them. This rugged looking Dunhill Zulu appeared to be in good condition underneath the grime and oxidation on the bowl and stem. The finish looked intact under the grime. The bowl had a thick cake that had hardened with time. The lava overflow on the rim could very well have protected the rim from damage. We won’t know what is under it until Jeff had cleaned it off. It had a Sterling Silver band on the shank that probably was a repair band to deal with a crack in the shank. The stem was worn looking with a lot of deep oxidation and some tooth chatter and deep bite marks on both sides at the button. As mentioned above the button was worn. Jeff took photos of the bowl and rim top to show the cake in the bowl and the lava build up on the edges of the bowl. It was thick and hard but hopefully it had protected the rim and edges from damage.The sandblast grain around the bowl sides and heel was quite beautiful. Lots of interesting patterns in the blast that would clean up very nicely. It was a beautiful pipe.Jeff took photos of the stamping on the underside of the shank. The stamping was clear and readable. It read 589 on the heel of the bowl – the shape number which is a bit of a mystery as I cannot find that number. That was followed by Dunhill over Tanshell. Next to that it read Made in England with a superscript 0 after the D making this a 1960 pipe. I am guessing that there may have been a circle 4 followed by a T which gave the size of the pipe and the fact that it is a Tanshell Briar but it is covered by a sterling silver band.Jeff took photos of the stem – first the White Spot on the top side of stem and then the top and underside of the stem at the button. You can see the tooth damage to the stem surface and the wear to the edge and top of the button. I am once again including the tribute that Jennifer consented to her Dad for the blog. She is also sent some photos of her Dad and her step mom. Note the pipe in his hand in both photos. She also included some things that her Dad wrote for Jeff and me to be able to get a feel for him. In the meantime I asked her to also send me an email with a brief tribute that I can use until then. Here is her email to me.

Steve, I want to thank you again for accepting my dad’s pipes.  They were so much a part of my dad’s life that I could not simply discard them. But as his daughter, I was not about to take up smoking them either. *laughing* I think my dad would like knowing that they will bring pleasure to others.  I know that I do.

I’m not sure what to say about his pipes. I always remember Daddy smoking pipes and cigars.

First a bit about my dad. Though my father, George Rex Leghorn, was American (growing up in Alaska), he managed to join the Canadian Army at the beginning of WWII, but in doing so lost his American citizenship.  He was fortunate to meet a Canadian recruiting officer who told him the alphabet began with “A” and ended with “Zed” not “Zee”, and also told him to say that he was born in a specific town that had all its records destroyed in a fire.  When the US joined the war my dad, and thousands of other Americans who had made the same choice*(see the link below for the article), were given the opportunity to transfer to the US military, and regain their citizenship.

After WWII, my dad, earned his degree at the University of California Berkeley and became a metallurgist. There is even a bit about him on the internet.

He loved taking the family out for a drive, and he smoked his cigars on those trips. (As a child, those were troubling times for my stomach.)

I most remember my father relaxing in his favorite chair with a science fiction book in one hand and a pipe in the other… Sir Walter Raleigh being his favorite tobacco… and the pipes themselves remind me of him in that contented way.  If I interrupted his repose, he’d look up, with a smile on his face, to answer me.

It seemed he smoked his Briarwood pipes the most, though he had others.  At the time, it was only the Briarwood I knew by name because of its distinctive rough shaped bowl.  And it was the Anderson Free Hand Burl Briar, made in Israel, which I chose for his birthday one year, because I thought he might like that particular texture in his hand.

At least two of his pipes, he inherited from his son-in-law, Joe Marino, a retired medical laboratory researcher (my sister Lesley’s late husband)… the long stemmed Jarl (made in Denmark), and the large, white-bowled, Sherlock Holmes style pipe.  I believe Joe had others that went to my dad, but Lesley was only sure about those two.

The Buescher, corncob pipe my older sister Lesley bought for Daddy while on one of her travels around the States.

A note on the spelling of my sister’s name… My dad met my mother, Regina, during WWII and they married in Omagh, Ireland.  My mother was English and in the military herself.  The English spelling of Lesley is feminine, and Leslie masculine, in the UK… just the opposite of here in the United States.  I guess my mom won out when it came to the spelling of the name.

I’ll send you photos of my dad soon, along with his WWII experience story.

Jennifer

*https://www.thestar.com/news/world/2013/10/22/the_americans_who_died_for_canada_in_wwii.html

Once again Jeff cleaned the pipe with his usual penchant for thoroughness that I really appreciate. He reamed it with a PipNet pipe reamer and cleaned up the reaming with a Savinelli Fitsall Pipe Knife. He scrubbed out the internals with alcohol, pipe cleaners and cotton swabs until the pipe was clean. He scrubbed the exterior of the bowl with Murphy’s Oil Soap and a tooth brush to remove the grime and grit on the briar and the lava on the rim top. The sandblast was rugged and beautiful. There was still some darkening and burn marks on the rim top and also a dark spot on the heel of the bowl. There were some white paint flecks in the grooves of the briar. The band on the shank was rough on the stem edge. He soaked the stem in Before & After Deoxidizer to remove the oxidation on the rubber. When the pipe arrived here in Vancouver for the second stop of its restoration tour it looked very good. I took photos before I started my part of the work. I took some close up photos of the rim top and stem surface. I wanted to show what an amazing job Jeff did in the cleanup of the rim top but remaining darkening and burn damage. I also took close up photos of the stem to show the tooth marks and chatter in front of the button on both sides. I also took a photo of the stamping on the pipe – to capture the stamp in one photo. It read as noted above. The next photo shows some of the damage to the band on the left side of the photo. There is also a small crack on the bottom part of the shank that can be seen in the photo above.To clean up the paint specks on the blast and to work on the darkening on the rim top I used two different brass bristle brushes that I use at time like this – a coarse one and a fine one and isopropyl alcohol. I also worked over the dark spot on the heel of the bowl. I was worried that it might be a potential burn through but the briar was solid both inside and outside the bowl. It looked as if the pipe may have been set down in an ashtray and bumped against a burning cigar or cigarette. I worked some Before & After Restoration Balm into the briar with my fingertips to clean, enliven and protect it. I worked it deep into the sandblast finish with a horsehair shoe brush. I find that the balm really makes the briar come alive again. The contrasts in the layers of the blast really stand out. I let the balm sit for a little while and then buffed with a cotton cloth to raise the shine. The pipe really looks good at this point. I am very happy with the results. The band was loose so I took it off and cleaned up the rough edge on the topping board with 220 grit sandpaper. I smoothed out the edge with a flat blade screw driver. Once I had it reshaped I glued it in place on the shank.This is when I should have called it a night and stopped working on the pipe. But I didn’t and fiddled with the fit of the stem against the band. All was going really well and the fit was better than it looked in the photos above. I was getting excited about the pipe starting to look pretty good. I slowly turned the stem to remove it and there was a sickening pop! If you have worked on pipes long enough you know that sound and the sinking feeling that you get when it happens. The tenon snapped off tight against the stem and was stuck in the shank. After my initial sick feeling and a response of wanting to chuck the pipe across the room I settled down and started to look at what I had done! I used a screw to pull the broken tenon out of the shank and took a photo of the damages. Now I needed to replace the tenon! Frustration galore.I flattened the tag end of the broken tenon on the stem with my Dremel and sanding drum, being careful to not make more work for myself in the process. I took out my cordless drill and got started drilling out the end of the stem for a new tenon. I started with a bit slightly larger than the airway and worked my way up to the size of the insert.I used the Dremel and sanding drum to reduce the diameter of both ends of the tenon – the insert end to fit the stem and the mortise end to fit the mortise. It was slow going but worked well. I used a slow drying super glue to anchor the tenon in the stem and checked the fit in the shank. It was as close as I was going to get it so I set it aside to dry.Once the new tenon was set I turned to address the multiple tooth marks on the stem surface of both sides. Surprising the button surface itself was ok and free of tooth marks (I would also need to build up the slot and button edges but I would get to that soon enough). I called it a night and set the stem aside while I went to sleep.In the morning the repair had cured and I used a needle file to smooth out the repaired spots and also reshape the sharp edge of the button. I sanded the repairs and the rest of the stem with 220 grit sandpaper to blend the fills in and to remove some of the oxidation. I followed that by sanding with 400 grit sandpaper to start the polishing process. Now I needed to address the damage to the slot and the button. The slot was too far to the left side of the stem and looked like there was missing material on that side of the button. I used a needle file to open the slot to the right side and then built up the left edge of the button with super glue and charcoal powder. It took a process of layering until I go the flow and shape just right. I shaped it with files and sandpaper until the shape worked for me. I shaped the button and polished the stem with micromesh sanding pads – wet sanding it with 1500-2400 grit pads and dry sanding it with 3200-12000 grit pads. I wiped the stem down with Obsidian Oil after each pad and set it aside to dry. I put the stem back on the bowl and polished the bowl and stem with Blue Diamond polish on the buffing wheel. I gave the bowl multiple coats of Conservator’s Wax and the stem multiple coats of carnauba wax. I buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The Tanshell sandblast finish on this briar is quite beautiful and the shine on it makes the variations of colour really pop. The pipe polished up really well. The wax and the contrasting stain on the bowl made the grain just pop on the briar. The polished black vulcanite seemed to truly come alive with the buffing. The pipe feels great in my hand and when it warms with smoking I think it will be about perfect. Even though it is far from flawless there is still a lot of life left in this old timer. Have a look at it with the photos below. The dimensions are Length: 6 inches, Height: 2 inches, Outside diameter of the bowl: 1 1/2 inches, Chamber diameter: ¾ of an inch. This is one that will go on the rebornpipes online store shortly. If you want to carry on the pipe trust of George Leghorn let me know. Thank you Jennifer for trusting us with his pipes. Thanks to each of you who are reading this blog. Remember we are not pipe owners, we are pipemen and women who hold our pipes in trust until they pass on into the trust of the next pipeman or woman.

A Challenging Restoration of my Grandfather’s WDC Stratford Pipe


Blog by Paresh Deshpande

This is the third pipe which I received from Abha, my wife, which has been cleaned, reamed and with no “before” pictures!!

I have inherited a large collection of my grandfather’s pipes; a few of them are unique and quite collectible. There are many WDC pipes in this collection and the one now on my work table is a “WDC STRATFORD” in its original case (in fact there are quite a few pipes in their original cases!). This smallish bent billiards displays gorgeous densely packed straight grain all round the stummel, including the shank and a sterling silver band adorns the shank end. It is stamped on the left side of the shank as “STRATFORD” in sentence case over the trademark “WDC” in an inverted equilateral triangle. The sterling silver band bears the American hallmarks of a STAR, EAGLE AND LETTER ‘D’ over “STERLING”. There are no other stampings visible on the entire pipe. The leather case, though worn by age and weather, is still solid and the inner golden hued felt lining is intact. This lining is stamped in deep red square with black border on the lid as “WDC” in a triangle and “STRATFORD”.INITIAL VISUAL INSPECTION
This pipe is third pipe that Abha, my wife had sent me after she had reamed the cake back to the bare briar and cleaned the stummel exterior and rim top surface with Murphy’s oil soap. She had also cleaned the sterling silver band using Colgate toothpowder. She followed it up with cleaning the mortise and the shank using regular and hard bristled pipe cleaners dipped in isopropyl alcohol. The felt lining inside the case was painstakingly cleaned up by repeated wiping with a cloth and warm soap water. The cleaned up pipe on my work table now, can be seen in the following pictures. It really feels nice to work on a clean pipe; I must admit and cannot help but thank her for doing all the dirty work. Unfortunately, she did not click any pictures of the condition of the pipe before she worked her magic on them. When I enquired about the condition before she had cleaned it, her one line reply was “it was in the worst of condition of all the pipes seen till date!!!” For those who have been reading my previous write ups would recollect that my grandfather never really believed in cleaning his pipes, he would rather buy new ones when the old pipes clogged up and became unsmokable.

The cake was so thick that even her little finger would not go in and there was heavy and sticky overflow of lava all over the stummel and shank. This lovely little pipe must have been his favorite and has been extensively used. There are a few issues which are immediately noticed. Firstly, the stem is shorter than the case and does not sit flush in the mortise. The tenon end of the stem appears to be unevenly cut. Secondly, the brass tenon, though it fits snugly in to the mortise, is clearly not original to the stem. The tenon end is also uneven (circled in violet).Thirdly, there are two dings on the right side of the stummel and this will have to be addressed. There is not a single fill on the entire stummel.Fourthly, the bowl is completely out of round with the left side of the rim and chamber wall thinner than the right side. Topping the bowl rim surface should address this issue to an extent. As regards the comparatively thin wall on the left side, I shall decide once I reach that stage of restoration.Fifthly, the vulcanite stem has a round slot which is correct for the vintage of this pipe. However, from the shortened length, the brass tenon and the fact that the stem does not sit flush with the shank end are all pointers to the fact that the stem has undergone extensive repairs at some point in its existence. My assumption is that this pipe must have fallen down on a hard surface and the tenon must have broken at an odd angle. While fitting a new brass tenon, the repairman had to cut a small portion of the stem at the tenon end, drill a new hole for the shaft of the tenon and fix it afresh. Even though the cut to the stem is not a clean one, the repairs are solid. This, and the assumption that this pipe was my grandfather’s favorite, is evident from the damage to the upper surface of the stem. There are two large gaping holes, one near the lip edge (which is understandable and attributed to clenching) and the other is nearly half way down the stem towards the tenon end (and can neither be explained at this stage!!). The stem is oxidized. THE PROCESS
Since in this project, the stem has the most number of issues to be addressed, it is where I start the restoration. I flamed the surface of the stem with a Bic lighter to raise the tooth indentations and scratches on the stem. The heat from the flame of Bic lighter causes the vulcanite to expand and regain its natural shape, reducing the marks. I wiped the stem surface clean with a cotton pad dipped in alcohol to remove all the dust and dirt from the surface. I had a closer look at the tenon and its fit in to the mortise. I realized that the length of the tenon is slightly longer than the mortise and that is the reason why the stem did not sit flush with the shank end. Also the tenon end was uneven as can be seen in the above pictures (circled in violet). I addressed this issue by grinding the tenon end on a grinding disk, frequently checking the seating joint of the stem and the shank end. Before proceeding with any further stem repairs, I decided to run a pipe cleaner through the stem to clean out the fine dust left behind due to grinding of the tenon end and it was then that I understood the possible reason for the second hole on the stem upper surface. The pipe cleaner did not pass through the airway cleanly!! There seems to be some kind of protrusion in the airway. On further close scrutiny, I realized that the tenon end inside the stem airway was thicker than the airway and thus obstructing the passage of the pipe cleaner through it causing repeated slamming of the pipe cleaner on the stem upper surface. That explained the probable cause of the second hole!!

I decided to smooth out the inside of the tenon to match the stem’s airway. Using a drill bit which was slightly larger than the tenon opening, I increased the tenon bore. With a round needle file, very carefully I filed the tenon end inside the stem till the pipe cleaner passed through it very easily. This was followed by sanding the stem surfaces with a folded piece of 220 grit sandpaper to remove the oxidation. I again cleaned the internal and external surface of the stem and proceeded to reconstruct the damaged upper surface of the stem. Once I was satisfied with the internal cleaning, I wiped the stem surface, particularly the damaged area, with a cotton pad and alcohol to remove any traces of dirt and grime. To begin the stem repairs, I smeared a pipe cleaner with petroleum jelly and inserted it in to the stem airway. I prepared a mix of CA superglue and activated charcoal and generously applied it over the gaping hole in the button of the stem and set it aside for curing overnight. While the stem repairs were curing, I decided to address the two dings on the stummel. I wiped the area with a moist cloth to remove the dust from the surface and spot filled it with a mix of briar dust and super glue. I use the layering technique, first fill with briar dust followed by super glue and again a layer of briar dust. I use this method since the moment super glue comes in contact with briar dust, the mix hardens instantaneously. I set the stummel aside to cure overnight and call it a day!!Once the filling of charcoal and CA superglue had cured, using a needle file, I sand the fill to match the surface of the stem. For a better blending, I further sand the entire stem with 220. At this stage, I observed air pockets in both the fills. This is the most dreaded observation for me as addressing this issue costs me more time and repeat of the entire process. Nevertheless, I again coat the damaged surface with clear super glue. While the fill was curing, with a flat needle file, I sand the stummel fill to achieve a rough match with the rest of the stummel surface. I further blend the fill with a 220 grit sand paper. This fill turned out satisfactory. I shall completely blend this fill during the micromesh cycle.Next issue to be addressed was the out of round rim top and the comparatively thin left side of the chamber wall. I approached this issue by first topping the rim on a 220 grit sand paper. This process also addressed the thinning of the rim observed on the left side to some extent. To further even out the inner rim edge, I created a bevel using a 220 grit sand paper. I am pretty satisfied with the way the rim surface appears at this stage. The uneven thickness on the left side is still apparent and to address this I had an option of increasing the thickness by lining the chamber wall with J B Weld followed by coating with a mixture of activated charcoal and yogurt. However, since I am not going to smoke this pipe ever, I decided to keep the appearance as it is, which incidentally does not look as glaring as it appears in the description.The next step in the process was to bring out the shine and highlight the beautiful grain on the stummel. I had an option of using more abrasive 220 grit sandpaper followed by micromesh pad cycle and loose the patina or straight away go to the micromesh cycle. Using the more abrasive sand paper, minor dents and dings would be further addressed but I would lose out the old sheen which the briar has taken over the years.  I decided on keeping the old sheen and went straight for the micromesh cycle. I wet sand the stummel with 1500 to 2400 grit pads and follow it up by dry sanding with 3200 to 12000 grit pads. The stummel, at this stage, looks absolutely stunning with the straight grain popping out from every inch. The natural finish and hues on this pipe is something that I have not seen before on any pipes. The very dark brown hued straight grains contrast beautifully with the dark browns on the rest of the stummel giving it a very antique appearance. I rub a small quantity of “Before and After Restoration Balm” in to briar and let it rest for a few minutes. The balm almost immediately works its magic and the briar now has a nice vibrant appearance. I further buff it with a horse hair shoe brush. In my enthusiasm to finish this project, I forgot to take pictures of the results at this stage.

Once the second filling of charcoal and CA superglue had cured, using a needle file, I sand the fill to match the surface of the stem. This time around the results were much more disastrous!!!! The entire filling collapsed in to airway, leaving the same gaping holes on the stem surface. I was so frustrated that I just did not have the heart to take pictures. To cut the rambling, I again repeated the procedure and made a fresh filling for both the holes and set it aside for curing. Once cured, I file the fillings with a needle file. For a better blending, I further sand the entire stem with 220 followed by 600 and 800 grit sandpaper. This helps to reduce the sanding marks left behind by the more abrasive 220 grit paper. To bring a deep shine to the vulcanite stem, I went through the complete set of micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. I wiped the stem with alcohol after each pad and rubbed it down with Extra Virgin Olive oil. The internals of the stem was cleaned out using alcohol and pipe cleaners. The finished stem is shown below. To finish the restoration, I re-attach the stem with the stummel. I mounted a cotton cloth buffing wheel to the Dremel (actually it is not the brand machine, but a local machine which is similar).  I set the speed at about half of the full power and applied White Diamond compound to the entire pipe. I wiped/ buffed the pipe with a soft cotton cloth to clear it of any leftover compound dust. I then mounted another cotton cloth wheel on to the polishing machine and applied several coats of carnauba wax. I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further.The completed pipe looks fresh, vibrant and ready for its next innings with me. This piece of briar will find a place of pride in my collection, if not as part of rotation, as a part of the memories left behind by my grand old man. If only it could tell me stories it had witnessed and why did my grandfather love this pipe so much?!! PS:  There is one contentious issue which I have deliberately raised and left it open for discussion. I would like to encourage the readers to express their views in a frank manner as it will help me in understanding the minds of the esteemed readers while clearing my own thought process. The issue that I am talking about is my decision (temporary!!!!) to let the unequal thickness of the chamber wall on the left side to remain addressed to the extent I have managed and not address it completely as well as the way I had thought of completely addressing it, if at all I decide to do so. Cheers……….!

RESTORING MY GRANDFATHER’S PIPE; “THE DOODLER”


Blog by Paresh Deshpande

The early Transition Era Barling #2639 that was recently restored was a breeze to work on and finished in real quick time, including the write up. The next pipe now on my work table has a lot of similarities to the Barling #2639; it is cleaned and spruced up by Abha, comes from my inheritance of pipes, has no serious issues to address (apparently) and in this instance too, she has not taken pictures before she commenced her cleaning regimen!!

“The Doodler” pipe on my work table is definitely not a looker by any stretch of imagination!!!! It is a simple straightforward billiard with a vulcanite saddle stem. What is unique though, is its design contribution in the ever progressing quest in the pipe world for a cool smoke and the man behind its design and development. The characteristic features of this pipe are a Custom-Bilt like worm rustications on the heel and shank, even and equally spaced out drilled holes and vertical slats which can be seen through the three rings of briar. From the design itself, it is apparent that all these features that have been incorporated in construction is with one and only purpose and that is to increase the dissipation of heat from the chamber while providing a nice cool smoke. The only stamping seen on this pipe is “THE DOODLER” in fancy block letters over “IMPORTED BRIAR”, on the right side of the shank. The saddle straight vulcanite stem is devoid of any logo.While restoring one of the 5 (or 6) Custom-Bilt from my inherited pipes, I had read about the legendary pipe maker from America, Mr. Tracy Mincer and his second innings after Custom-Bilt, The Doodler!!! To refresh my memory, I revisited rebornpipes.com and pipedia.org. These sites have all the information that one is looking for on “THE DOODLER”. Here are the links from these sites; https://rebornpipes.com/2013/05/22/a-unique-piece-of-pipe-design-history-doodlers-by-tracy-mincer/

https://pipedia.org/wiki/The_Doodler

From both the above articles, it is amply evident that the pipe that is on my work table is from the 1953 to 1960s era and is an integral part of history in mankind’s eternal quest for a cool smoke!!!!

INITIAL VISUAL INSPECTION
This pipe is another that Abha, my wife had sent me after she had reamed the cake back to the bare briar and cleaned the stummel exterior and rim top surface with Murphy’s oil soap. She had also cleaned out all the nooks and crevices resulting from the design of the pipe. She followed it up with cleaning the mortise and the shank using regular and hard bristled pipe cleaners dipped in isopropyl alcohol. The cleaned up pipe on my work table now, can be seen in the following pictures. It really feels nice to work on a clean pipe; I must admit and cannot help but thank her for doing all the dirty work. Unfortunately, she did not click any pictures of the condition of the pipe before she worked her magic on them. When I inquired about the condition before she had cleaned it, her one line reply was “surprisingly different from his (grandfather’s) other pipes!!!” For those who have been reading my previous write ups would recollect that my grandfather never really believed in cleaning his pipes, he would rather buy new ones when the old pipes clogged up and became unsmokable. However, in this case, there was a very thin layer of cake and the stem was in good condition. From the present condition of the pipe, there are only two issues that I would need to address on the stummel; a heat fissure on the wall of the chamber and the heel has thinned out (or so it appears to me). To err on the positive, I intend to coat the chamber wall and heel with a mix of activated charcoal and yogurt. This coat will not only protect the chamber wall from direct heat, but will also aid in faster build up of the cake.

The vulcanite stem is surprisingly clean with only a slight damage to the lip on the upper surface. This issue should not be a major headache to address. The lip edge on both sides is distinct but will have to be sharpened. Also, the upper surface of the slot has thinned out. Why, I fail to comprehend!! The quality of vulcanite is good. The fit of the tenon in to the mortise is slightly loose. This is usually observed in pipes where the mortise wall has dried out due to non usage for a long time. THE PROCESS
Since in this project, the stem has the most number of issues to be addressed, it is where I start the restoration. I wiped the stem surface clean with a cotton pad dipped in alcohol to remove all the dust and dirt from the surface. To address the issue of thinned out upper surface of the slot, I layered the upper lip edge with a mix of activated charcoal and clear CA superglue and I set it aside to cure overnight. I applied a layer of this mix to the lower lip edge to ensure an even thickness on both surfaces.Once the filling of charcoal and CA superglue had cured and I was satisfied with the thickness, using a needle file, I sand the layers of the fill to match the surface of the stem. For a better blending, I further sand the entire stem with 220 followed by 600 and 800 grit sandpaper. This helps to reduce the sanding marks left behind by the more abrasive 220 grit paper. To bring a deep shine to the vulcanite stem, I went through the complete set of micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. I wiped the stem with alcohol after each pad and rubbed it down with Extra Virgin Olive oil. The internals of the stem was cleaned out using alcohol and pipe cleaners. The finished stem is shown below. I rub a small quantity of “Before and After Restoration Balm” in to briar and let it rest for a few minutes. The balm almost immediately works its magic and the briar now has a nice vibrant appearance. I further buff it with a horse hair shoe brush. To finish the restoration, I re-attach the stem with the stummel. I mounted a cotton cloth buffing wheel to the Dremel (actually it is not the brand machine, but a local machine which is similar).  I set the speed at about half of the full power and applied White Diamond compound to the entire pipe. I wiped/ buffed the pipe with a soft cotton cloth to clear it of any leftover compound dust. I then mounted another cotton cloth wheel on to the polishing machine and applied several coats of carnauba wax. I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further.The completed pipe looks fresh, vibrant and ready for its next innings with me. This piece of briar will find a place of pride in my collection, if not as part of rotation, as a part of history of pipes. If only it could tell me stories it had witnessed and why did my grandfather not smoke it as heavily as his other pipes?!!!! Thank you for having the patience to reach this far while reading the write up. PS:  The only issue that needed to be addressed was that of the thin line of heat fissure. I mixed activated charcoal and yogurt to a consistency where the mix is thin enough to spread evenly but thick to the point that it is not runny at all. Using my fabricated bamboo frond, I apply an even coat all along the chamber wall and drop a thick blob of the mix over the heel. I tap the foot of the stummel with my fingers to ensure an even spread of the mix over the heel and expel air bubbles.

 

The Restoration of the First of Jennifer’s Dad’s Estate Pipes – A Comoy’s Deluxe 78


Blog by Steve Laug

The next pipe on the worktable came from the estate of George Rex Leghorn. I received an email from his daughter Jennifer who is a little older than my 64+ years about whether I would be interested in his estate. My brother Jeff and I have been picking up a few estates here and there, so I was interested. Here is the catch – she did not want to sell them to me but to give them to me to clean up, restore and resell. The only requirement she had was that we give a portion of the sales of the pipes to a charity serving women and children. We talked about the organization I work for that deals with trafficking and sexual exploitation of women and their children and she decided that would be a great way to carry on the charitable aspect of her Dad’s character. With some great conversation back and forth she sent the pipes to Jeff and he started the cleanup process on them. Once he had finished cleaning them all he sent them to me to do my work on them.

The first pipe I chose to work on from the lot was a Comoy’s De Luxe 78 Military Bit Apple. It had some amazing grain on the bowl sides and shank. It had a Sterling Silver ferrule on the shank end that was oxidized and blackened. It had a badly oxidized stem with tooth marks and chatter on the top and underside near the button. There was a thick cake in the bowl and it was dirty and tired looking. It had been sitting in boxes for a lot of years and it was time to move ahead with the restoration. Jennifer took photos of the pipes she was sending. I have included the three she included from this pipe. When the box arrived from Jennifer Jeff opened it and took photos of each pipe before he started his cleanup work on them. This Comoy’s was a real beauty underneath the grime, tarnish and oxidation on the bowl and stem. The finish looked intact under the grime. The bowl had a thick cake that had hardened with time. The lava overflow on the rim could very well have protected the rim from damage. We won’t know what is under it until Jeff had cleaned it off. The silver work was tarnished but still looked classy on this old timer. The ferrule was undamaged with no dents of dings that are often found on these pipes. The stem was worn looking with a lot of deep oxidation and some tooth chatter and bite marks on both sides at the button. The overall look of the pipe made me think seriously about adding it to my own collection. Jeff took photos of the bowl and rim top to show the cake in the bowl and the lava build up on the edges of the bowl. It was thick and hard but hopefully it had protected the rim and edges from damage.The grain around the bowl sides and heel was quite beautiful. Lots of cross grain and birdseye that would clean up very nicely. It was a beautiful pipe.Jeff took photos of the stamping on both sides of the shank. The left side was stamped Comoy’s De Luxe and the right side had the Comoy’s COM stamp and shape number. The COM stamp is a circle with Made and London arching around “in” in the centre. Underneath it read England. The shape number is 78. I am not overly familiar with this line of Comoy’s and will need to do some work to get an idea of both age and value in the hierarchy of the lines.He also took photos of the stamping on the ferrule and the three circle inlay of the C on the left side of the stem. The ferrule read HC in a box over STERLING LONDON. There were no hallmarks on the silver so I could not use those to help date the pipe. The C inlay looked very good and did not show damage to any of the three circles. Jeff did not take photos of the stem at this point. It is so easy to miss some photos in the processing of pipes.Jennifer consented to write a short tribute to her Dad for the blog. She is also sending along some photos and an article that her Dad wrote for Jeff and me to be able to get a feel for him. When it arrives I will post the photo with the other blogs on his pipes and will add it to this one as well. In the meantime I asked her to also send me an email with a brief tribute that I can use until then. Here is her email to me.

Steve, I want to thank you again for accepting my dad’s pipes.  They were so much a part of my dad’s life that I could not simply discard them. But as his daughter, I was not about to take up smoking them either. *laughing* I think my dad would like knowing that they will bring pleasure to others.  I know that I do.

I’m not sure what to say about his pipes.   I always remember Daddy smoking pipes and cigars.

First a bit about my dad. Though my father, George Rex Leghorn, was American (growing up in Alaska), he managed to join the Canadian Army at the beginning of WWII, but in doing so lost his American citizenship.  He was fortunate to meet a Canadian recruiting officer who told him the alphabet began with “A” and ended with “Zed” not “Zee”, and also told him to say that he was born in a specific town that had all its records destroyed in a fire.  When the US joined the war my dad, and thousands of other Americans who had made the same choice*(see the link below for the article), were given the opportunity to transfer to the US military, and regain their citizenship.

After WWII, my dad, earned his degree at the University of California Berkeley and became a metallurgist. There is even a bit about him on the internet.

He loved taking the family out for a drive, and he smoked his cigars on those trips. (As a child, those were troubling times for my stomach.)

I most remember my father relaxing in his favorite chair with a science fiction book in one hand and a pipe in the other… Sir Walter Raleigh being his favorite tobacco… and the pipes themselves remind me of him in that contented way.  If I interrupted his repose, he’d look up, with a smile on his face, to answer me.

It seemed he smoked his Briarwood pipes the most, though he had others.  At the time, it was only the Briarwood I knew by name because of its distinctive rough shaped bowl.  And it was the Anderson Free Hand Burl Briar, made in Israel, which I chose for his birthday one year, because I thought he might like that particular texture in his hand.

At least two of his pipes, he inherited from his son-in-law, Joe Marino, a retired medical laboratory researcher (my sister Lesley’s late husband)… the long stemmed Jarl (made in Denmark), and the large, white-bowled, Sherlock Holmes style pipe.  I believe Joe had others that went to my dad, but Lesley was only sure about those two.

The Buescher, corncob pipe my older sister Lesley bought for Daddy while on one of her travels around the States.

A note on the spelling of my sister’s name…

My dad met my mother, Regina, during WWII and they married in Omagh, Ireland.  My mother was English and in the military herself.  The English spelling of Lesley is feminine, and Leslie masculine, in the UK… just the opposite of here in the United States.  I guess my mom won out when it came to the spelling of the name.

I’ll send you photos of my dad soon, along with his WWII experience story.

Jennifer

*https://www.thestar.com/news/world/2013/10/22/the_americans_who_died_for_canada_in_wwii.html

I turned to my usual sources for information about the De Luxe line of Comoy’s and found nothing on the pipephil website. On the Pipedia site there was nothing clearly written identifying the brand but there was a page from a Comoy’s Catalogue advertising Specialty pipes from Comoy’s that included the De Luxe (https://pipedia.org/wiki/File:Comoy-Specialty.jpg). I have included a screen capture of the page for you to have a look.It describes the De Luxe as being available in 14 Army styles in walnut and sandblast finishes. These fine pipes have their beauty enhanced by heavy gauge sterling silver bands hand fitted by silversmiths. It is also available in Blue Riband and London Pride on special order. So it seems that it is a specialty item and a beautiful one at that. Does anyone know anything else about the line?

Jeff cleaned the pipe with his usual penchant for thoroughness that I really appreciate. He reamed it with a PipNet pipe reamer and cleaned up the reaming with a Savinelli Fitsall Pipe Knife. He scrubbed out the internals with alcohol, pipe cleaners and cotton swabs until the pipe was clean. He scrubbed the exterior of the bowl with Murphy’s Oil Soap and a tooth brush to remove the grime and grit on the briar and the lava on the rim top. He was able to get most of the oxidation off of the silver ferrule as well. He soaked the stem in Before & After Deoxidizer to remove the oxidation on the rubber. When the pipe arrived here in Vancouver for the second stop of its restoration tour it looked very good. I took photos before I started my part of the work. I took some close up photos of the rim top and stem surface. I wanted to show what an amazing job Jeff did in the cleanup of the rim top and the great condition it was in under the thick lava coat. I also took close up photos of the stem to show the tooth marks and chatter in front of the button on both sides.I also took some photos of the stamping on the pipe – both sides of the shank and the Sterling ferrule. You can see the three part C in the stem as well. The ferrule is loose and will need to be glued in place again. You can see in the third photo below that it is on the top of the shank instead of aligned on the left side with the stamping on the briar.I decided to repair the tooth marks on the top and underside of the stem so it could be drying while I worked on the bowl. I cleaned the tooth marks with a cotton swab and alcohol and dried it off. I filled in the deep divots with black super glue and set the stem aside so the repairs could cure.I turned my attention to the bowl. I painted some white all-purpose glue on the shank end and carefully pressed the ferrule onto the end of the shank. I turned it on the shank to align the HC Sterling London stamp on the ferrule with the Comoy’s stamp on the briar shank. I let the glue dry on the ferrule and once it had set I polished the briar with micromesh sanding pads. I wet sanded with 1500-2400 grit pads and dry sanded it with 3200-12000 grit pads. I wiped the bowl down after each pad with a damp cloth. The grain really began to stand out. I worked some Before & After Restoration Balm into the briar with my fingertips to clean, enliven and protect it. I find that the balm really makes the briar come alive again. The grain shines through and really stands out. I let the balm sit for a little while and then buffed with a cotton cloth to raise the shine. The pipe really looks good at this point. I am very happy with the results. I used some silver polish to remove the remaining oxidation on the Sterling Silver ferrule. I rubbed it in with a cotton pad and polished it once it had dried. It took some time to polish out the scratches in the silver and give it a shine. I followed that up by polishing the ferrule with a jeweler’s polishing cloth. The photos show the shine.I set the bowl aside at this point and turned back to address the cured repairs on the stem surface. I sanded the stem with 220 grit sandpaper to blend the repairs into the surface of the rubber and also to remove the oxidation that remained after Jeff’s cleanup. I polished it with 400 grit sandpaper to smooth out some of the scratching that was left behind by the earlier sanding.I polished the stem with micromesh sanding pads – wet sanding it with 1500-2400 grit pads and dry sanding it with 3200-12000 grit pads. I wiped the stem down with Obsidian Oil after each pad. I polished it with Before & After Pipe Stem Polish – both Fine and Extra Fine polishes. I wiped it down with a final coat of Obsidian Oil and set it aside to dry. I put the stem back on the bowl and polished the bowl and stem with Blue Diamond polish on the buffing wheel. I carefully worked around the Sterling Silver ferrule so I would not damage it. I gave the bowl and the stem multiple coats of carnauba wax. I buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The grain on this briar is absolutely beautiful and the shine on it makes the grain really shine. The pipe polished up really well. The wax and the contrasting stain on the bowl made the grain just pop on the briar. The polished black vulcanite seemed to truly come alive with the buffing. Comoy’s really captured this shape in a way that no one else has in my opinion. The pipe is perfect in my hand and when it warms with smoking I think it will be about perfect. Have a look at it with the photos below. The dimensions are Length: 5 1/2 inches, Height: 1 3/4 inches, Outside diameter of the bowl: 1 1/4 inches, Chamber diameter: ¾ of an inch. This is one that will remain in my collection. Once I figure out the value of the pipe I will make a donation on behalf of Jennifer’s Dad to the organization that I work for. It is a pipe like no other Comoy’s that I have seen before. I want to carry on the pipe trust of George Leghorn. Thank you Jennifer for trusting us with his pipes. Thanks to each of you who are reading this blog. Remember we are not pipe owners, we are pipemen hold our pipes in trust until they pass on into the trust of the next pipeman or woman.

Renewing a Classic Bari Shape – A Bari Opal 8443


Blog by Steve Laug

The next pipe on the table is from one of the unsung pipe makers that I really enjoy working on. It is a Bari pot shaped pipe with a rectangular shank and tapered vulcanite stem. This has some stunning straight and flame grain around the bowl and shank with birdseye on the top of the bowl and the heel. It showed a lot of promise even in its filthy condition. The rim top was quite wide and had a slight bevel on the inside rim edge. The pipe is stamped on the topside of the shank Bari over Opal and on the underside Made in Denmark over the shape number 8443. Lately we have been picking up some really dirty pipes and this pipe was no exception. It was very dirty with a thick cake in the bowl and a layer of lava overflowing on to the rim top. It was thick enough to have some wrinkles in the surface that looked almost like cracks. It was hard to know what the inner edge of the rim looked like because of the lava and cake. From the photos it appeared that the inner edge was in good condition. Other than being dirty the finish also appeared to look very good. The stem was lightly oxidized and the button surface on both sides was worn down from tooth damage. There was chatter on both sides of the stem. Jeff took some photos of the pipe before he started working on it. He took photos of the rim top to show the thick cake in the bowl and the overflow of lava. The cake is thick and hard and the lava overflow is a thicker toward the back of the beveled rim. The bowl and the rim are a real mess. This must have been a great smoking pipe.He took a photo of the right side and heel of the bowl to show some of the grain and the condition of the pipe. There is one small fill at the top of the bowl that will need to be dealt with but otherwise it is a pretty pipe.Jeff took photos of the stamping on the top and underside of the shank to capture the clarity of it even under the grime. It is clear and legible.The vulcanite stem was worn at the button with the sharp edge of the button worn down with tooth marks. The stem also had a lot of chatter both sides and some oxidation.Jeff had already cleaned up the pipe before sending it to me. He had reamed the bowl with a PipNet pipe reamer and cleaned it up with a Savinelli Fitsall Pipe Knife. He scrubbed the exterior with Murphy’s Oil Soap and a tooth brush to clean off the grime off the finish and the heavy overflow of lava on the rim top. He cleaned up the internals of the shank, mortise and stem with pipe cleaners, cotton swabs and alcohol to remove all of the oils and tars in the pipe. When it arrived here in Vancouver it was a clean pipe and I knew what I had to work with. I took photos of it before I started my part of the restoration. I took photos of the rim top and the stem to show their condition. Jeff was able to clean up the thick cake and lava overflow that was shown in the rim and bowl in the earlier photos. He was also able to get rid of the grime and grit in the surface of the briar. The rim top looked a lot better than when he started. There was still some pitting and darkening on the surface of the inward bevel but it should clean up very well.I decided to work on the scratches in the surface of the briar first. I polished the surface with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I wiped the rim down with a damp cloth after each pad. I was able to polish out the scratches without damaging the finish on the bowl or the rim. The finish looked very good once I was done polishing it. On the right side of the bowl there was a fill that stuck out. I touched it up with a black Sharpie pen and buffed it by hand. I used a Maple stain pen to touch up the area around the fill and the lighter areas on the shank end. The finish on the rest of the bowl was in excellent condition. After I was finished with the stain pens and polishing the restained areas I rubbed the bowl and shank down with Before & After Restoration Balm to deep clean the finish on the bowl and shank. The product works to clean, enliven and protect the briar. After it sat for a little while I wiped it off and buffed it with a soft cloth. The briar really began to have a rich shine. I took some photos of the bowl at this point to mark the progress in the restoration. It is a beautiful bowl. I set the bowl aside and worked on the stem at this point in the  process. The stem may well be a replacement one but it is hard to know for certain. It is well made and fits perfectly to the shank. I decided to start by repairing the deep tooth marks on the button and the stem. I filled them in and built up the surface of the button with clear super glue and set the stem aside while I went to lunch.I used a needle file to cut a sharp edge on the button on both sides of the stem. I worked it until there was a definite sharp edge. I sanded the button and the stem with 220 grit sandpaper and 400 grit sandpaper to remove the scratches. I polished the stem with micromesh sanding pads – wet sanding with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. I wiped the stem down after each pad with Obsidian Oil to remove the sanding dust. I polished Before & After Pipe Stem Polish – both Fine and Extra Fine. I gave it a final hand buff with some Obsidian Oil and laid it aside to dry. I put the stem back on the pipe and the pipe to the buffer. I worked it over with Blue Diamond to polish out the remaining small scratches in the briar and the vulcanite. I gave the bowl and the stem several coats of carnauba wax and buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. I love the way that the buffer brings a shine to the pipe. I was happy with the look of the finished pipe. The photos below show what the pipe looks like after the restoration. I have worked on quite a few Bari’s over the years and I am always pleased with the way the shape and the grain work together.  The shape and the look is uniquely Bari and are very elegant. The polished black vulcanite stem looks really good with the contrasting browns of the briar. The dimensions of the pipe are Length: 5 inches, Height: 1 3/4 inches, Outside diameter of the bowl: 1 3/4 inches, Chamber diameter: 7/8 of an inch. This pipe will soon be added to the rebornpipes online store. If you are interested in adding it to your collection let me know. This one should be a great smoker. Thanks for walking through the restoration with me on another beauty!