Tag Archives: topping a bowl

A Picadilly Brand Genuine French Rustique Briar Pipe


Blog by Steve Laug

The second box that was labeled Picadilly Brand Genuine French Rustique Briar Price $15 had one lonely pipe left in it after I had combined the pieces in the first boxed set and cleaned up the Berkeley Club billiard. This one was the only one that actually belonged in the set. It is marked as the others had been on the left side of the shank. It reads Real Briar in script over Made in France stamped in a smooth part of the shank. This one had been smoked, though lightly. The bowl had a light cake and the rim top was covered in tar and oils with a slight build up. The stem had tooth chatter on the Redmonal/Bakelite top and bottom sides near the button. The alignment was perfect on this one. Real1I took some photos of the pipe before I cleaned it up to show the condition it was in when I started. It was a really clean pipe compared to many of the ones that I work on. It would be an easy cleanup.Real2 Real3I took a close up photo of the rim top to show the cake and the build up on the rim. I also took some close up photos of the stem to show the tooth chatter and the metal tenon on this pipe.Real4 Real5I scraped out the light cake with a Savinelli Pipe Knife.Real6Rather than top the bowl and start over with the finish I used a medium grit sanding block to remove the tarry build up on the rim top. I scrubbed it down with a cotton pad and alcohol and then followed that by sanding the top with a 1500 grit micromesh sanding pad.Real7 Real8I touched up the stain on the rim with a dark brown stain pen.Real9I cleaned out the mortise and the airway in the shank and the stem with a cotton swabs, pipe cleaners and alcohol.Real10I sanded the stem with 220 grit sandpaper to remove the tooth chatter and marks on the top and the bottom sides. I wet sanded it with 1500-2400 grit micromesh sanding pads to begin polishing them I gave it a coat of Obsidian Oil. I dry sanded it with 3200-4000 grit pads. I gave it another coat of oil. I finished sanding it with 6000-12000 grit pads, gave it a final coat of oil and set it aside to dry.Real11 Real12 Real13 Real14I gave the bowl and stem several coats of Conservator’s Wax and buffed it with a shoe brush. I lightly buffed the bowl and stem with a clean buffing pad. I hand buffed it with a microfibre cloth. I put the pipe back in its case while I continue to look for the rest of the set to complete a second boxed set. The finished pipe is shown in the photos below. It is a beauty. Thanks for looking.Real15 Real16 Real17 Real18 Real19 Real20

Another for the strange but true hunt for a Cooler/Drier Smoker Collection


Blog by Steve Laug

My brother sent me the links to this sale on EBay and I was hooked. It is probably the oddest pipe contraption I have seen in the many pipes that formed the pipeman’s dream of a cooler, drier smoke. There have been many over the years that vied for the oddest looking contraption but to date this one takes the prize. I have a few in my own oddity collection that would give this one a fair run for its money but I think this one is still by far the strangest. The T shaped look of the pipe is one thing but once it taken apart it is even odder. The only normal part of the pipe is the vulcanite stem. The Bakelite shank ends in a dropped down base that is part of the shank. It is as big as the briar bowl on the top.Filt1Inside the base is a metal canister contraption that has six wedge shaped holes around the edges and a single hole in the crowned centre. The crowned centre meets the hole in the bottom of the threaded briar bowl which is indented to hold the contraption in place.Filt2The Bakelite shank on the pipe is the only part of the pipe that bears any identification marking. It reads Filtre T with PAT. to the left of the name and PND. to the right. Thus the stamping is Filtre T Patent Pending. The Bakelite base is quite thick with threads extending into it to hold the bowl in place. The diameter of the opening is ¾ inches and the exterior 1 inch. The length of the base and stem is 5 1/8 inches. With the bowl in place the height is 2 ½ inches tall. The hang down base is 1 ¼ inches. The bowl itself is 1 ¼ inches. The filter canister is stamped with the same stampings as the shank PAT. over FILTRET over PND. and is made of aluminum.Filt3I did some hunting for a Patent on the US Patent site and found a written patent. The pipe seems to have been made by FILTRET Inc. of Seattle, Washington and the patent filed by George E. Baldwin, President on May 5, 1930. I cannot find the attached specimens mentioned in the document but this at least identifies the name and gives me a base date.

Filt43

When the pipe arrived in Idaho my brother took some photos of it. The stem was slightly oxidized and it was stuck in the shank. It was underturned to the left and could not be straightened out. The rim was dirty with a tar build up and there was a cake in the bowl. The bowl itself was slightly out of round. The briar had a few small fills in it and the finish was dirty.Filt4 Filt5 Filt6When my brother Jeff took the bowl off the base the interior of the base was very dirty with tars and oils. The metal basket was also covered with debris of tars, oils and saliva. It looked to me that the way the pipe worked was that the air was drawn through the single hole in the top of the canister and then it came out through the wedges and into the airway in the shank.Filt7 Filt8 Filt9This pipe was a pleasure to work on because Jeff did the lion’s share of work on it. He reamed and cleaned the bowl. He cleaned out the stem with pipe cleaners and alcohol and the base with cotton swabs and alcohol. He flushed out the canister with alcohol and then water. He flushed it until it was clean. He scrubbed the bowl with Murphy’s Oil Soap and removed the finish and the debris from the surface of the bowl. He was able to remove much of the tar and oil on top of the bowl. The next set of four photos show the way the pipe looked when I unpacked it this afternoon. Thanks Jeff this was an easy clean up.Filt10 Filt11I took a close up photo of the rim top to show the damage to the inner edge of the rim. It is darkened and also has some burned areas on the top and inner edge.Filt12I also took a close up photo of the stem – it was stuck tight in the shank and it was underturned to the left. I tried to heat it with hot water to try to loosen it. It would not move. After taking this photo I put it in the hot water to soak and see if it would loosen the tars and oils in the shank that were holding it tight.Filt13I turned my attention to the bowl and the base while the stem soaked. I cleaned out the airway in the bottom of the bowl with a cotton swab and alcohol to remove the “gunk” that was clogging the airway and reducing the air flow.Filt14I topped the bowl on a topping board with 220 grit sandpaper. I topped it until I had removed the damaged areas on the rim surface.Filt15I rolled a piece of 220 grit sandpaper to sand the bowl and the inner edge to clean up the damaged inner edge and bring it back to round.Filt16I sanded the bowl and rim with a medium and a fine grit sanding block to remove the scratches in the briar. Once it was clean of scratches I stained it with a dark brown stain thinned by half with alcohol. I flamed it and repeated the process.Filt17I wiped the bowl down with cotton pads and alcohol to make the stain more transparent and to make the grain show through.filt18I took the stem and base out of the hot water and wiggled it until the stem turned. I removed the stem so that I could clean the inside of the shank and base.Filt19I used a dental spatula inside the tube of the shank to scrape away some of the thick build up on the walls of the shank. I then scrubbed it down with alcohol, cotton swabs and pipe cleaners until they finally came out clean. I also scrubbed down the inside of the base with them to remove the grime in the base.Filt20I used the micromesh sanding pads to polish the Bakelite base and the shank. I sanded it with 1500-12000 grit pads and then wiped it down with some Obsidian Oil.Filt21I scrubbed out the canister one more time and found that it was very clean. I dropped it in place in the base.Filt22With the canister in place I screwed the bowl onto the base and took some photos.Filt23 Filt24 Filt25It was ready to buff with Blue Diamond so I took it to the wheel and buffed the bowl and the base. I gave bowl several coats of carnauba wax and then buffed it with a clean buffing pad to raise the shine. Once I finish the stem I will give it several more coats of wax.Filt26 Filt27 Filt28I cleaned out the airway in the stem with alcohol, cotton swabs and pipe cleaners. After heating it with the hot water to loosen the stem a lot of grime came loose in the shank and ran down the stem.Filt29The stem had some tooth chatter along with the oxidation that I brought out with the hot water bath. I sanded it with 220 grit sandpaper to remove both the chatter and the oxidation. I wiped it down with Obsidian Oil.Filt30I wet sanded the stem with 1500-2400 grit micromesh sanding pads and rubbed it down with Obsidian Oil. I dry sanded it with 3200-4000 and gave it another coat of oil. I finished sanding it with 6000-12000 grit pads and gave it another coat of oil. I buffed it on the buffer with Blue Diamond polish and gave it a final coat of Obsidian Oil and set it aside to dry.Filt31 Filt32 Filt33I put the pipe back together and gave it a final buff with Blue Diamond and then gave it multiple coats of carnauba wax. I buffed it with a clean buffing pad and then by hand with a microfibre cloth to deepen the shine. The finished pipe is shown in the photos below. It is a true oddity but the more I worked on it the more I am intrigued with it. I wonder how the contraption works in real-time. Well, I may have to give it a try one day soon. Thanks for looking.Filt34 Filt35 Filt36 Filt37 Filt38 Filt39 Filt40 Filt41 Filt42

A Berkeley Club 7118 Billiard that turns out to be Sasieni Made


Blog by Steve Laug

Inside the first boxed set of Picadilly Brand Genuine French Rustique Briar pipes that my brother picked up was a straight billiard that did not bear the markings that were on the bent billiard or on the other complete set of Picadilly pipes. This one had a familiar finish to me but I could not put my finger on it and identify it. It was stamped on the underside of the shank with the following: 7118 over Berkeley Club over London Made. The bowl end of the smooth bottom of the shank it was stamped England in an arch. The finish on the bowl sides was very clean. The rim was a bit beaten. The front edge of bowl had been knocked out on a hard surface repeatedly and left a rash. The entire top of the rim was also beaten up and pitted. It was the only part of the bowl that was in rough shape. The stem had some tooth chatter and some light tooth marks on the top and bottom sides near the button. There was some oxidation and a faded stamp with what looked like a B partially circled by a C.Berk2 Berk3I took a close up photo of the bowl and rim to show the cake on the bowl and the damage to the rim surface. I also took a close up photo of the stamping on the underside of the shank.Berk4I went online to Pipephil’s site Logos and Stampings (http://www.pipephil.eu/logos/en/logo-b4.html) and found the brand and the reminder that had niggled at the back of mind. The Berkeley Club with this stamping was made by Sasieni. The photo below came from that website and shows the same finish and the same stamping on both the shank and the stem.Berk1With that in mind I took the pipe apart to have a look at it. I was expecting the pipe to have an inner tube in the tenon. I looked in the bowl and the point extended into the bowl showing a glint of metal. However when I took the pipe apart there was no inner tube. I shined a light down the mortise and airway in the shank and sure enough the tube had broken off in the airway leaving the mortise unobstructed. I looked at the stem and saw the same – broken off slightly inside the tenon leaving it also unobstructed.

I decided to work on the rim top damage by topping the bowl with 220 grit sandpaper on a topping board. It took some work to remove the damaged portion of the rim. The second photo shows the initial sanding and the third photo shows the finished topping. You can also see the chips in the cake at 12 o’clock in the third photo.Berk5I used the Savinelli Pipe Knife to clean out the cake in the bowl and work on the inside edge of the rim. I was able to remove all of the cake and smooth out the rim edge while keeping it in round in the process.Berk6With that completed I decided to drill out the broken inner tube in the shank of the pipe. I used a drill bit almost the same size as the airway in the inner tube. I increased the size of the bit until it was the same size as the airway and drilled out the broken tube. I never use a power drill when I am doing this – rather I use a cordless drill sans battery (I don’t want to inadvertently hit the trigger and regret it). I turned the shank onto the drill bit until it grabbed onto the tube and I was able to pull it out on the end of the bit. While I was pulling I also used the end of the Savinelli Pipe Knife to push on the end of the inner tube in the bowl. It takes patience but the result leaves behind no damage to the airway or the bowl.Berk7I scrubbed the rustication on the bowl with a tooth brush and Murphy’s Oil Soap until it was clean. I rinsed it under running water to remove the soap and the debris. I dried it off with a soft cotton towel.Berk8I took some photos of the cleaned and dried pipe to get an idea of what I needed to do with the finish on the bowl and shank. The pipe looks really good other than the top of the rim that I will need to restain and polish.Berk9 Berk10I cleaned out the mortise in the shank and the airway in the shank and the stem. The airway was quite clean thanks to the broken inner tube. The mortise had some tars and oils that took a few cotton swabs, pipe cleaners and alcohol to remove. The stem was dirty on the inside and took considerably more pipe cleaners than the shank. I used pipe cleaners and alcohol to clean out the stem airway.Berk11To match the stain on the bowl sides I used a black Sharpie Marker and a dark brown stain pen to restain the rim top and the outer edges of the bowl.Berk12I cleaned up the inner edge of the bowl with a piece of sandpaper wrapped around my finger to smooth out the rough edges of the inner rim. It took a few passes to smooth out the edge but when it was done it looked much better.Berk13I gave the bowl a coat of Conservator’s Wax and buffed the bowl with a shoe brush to bring up the shine.Berk14I used the same method that I spelled out above – a stationary drill and drill bits to remove the broken tube in the tenon. I drilled until the bit caught a hold of the tube and then pulled the tube out of the tenon.Berk15I used some European Gold Rub ‘n Buff to fill in the logo on the stem. I applied it with a cotton swab and then rubbed off the excess. The finished logo is shown in the photo below.Berk16I wet sanded the stem with 1500-2400 grit micromesh sanding pads. I rubbed it down with Obsidian Oil. I dry sanded it with 3200-4000 grit pads and gave it another coat of oil. I finished sanding with 6000-12000 grit pads. I gave it a final coat of Obsidian Oil and set it aside to dry.Berk17 Berk18 Berk19I buffed the stem with Blue Diamond polish on the buffing wheel and then gave it multiple coats of carnauba wax. I buffed the bowl and the stem with a clean buffing pad to raise the shine and polish the wax. I buffed it again by hand with a microfibre cloth. The finished pipe is shown in the photos below. It came out looking really good. This one will eventually be listed for sale on the store. You can send me an email or a message any time if you would like to add it to your collection. Thanks for looking.Berk20 Berk21 Berk22 Berk23 Berk24 Berk25 Berk26

Another ‘Hole in the Wall’ Find – BBB Banker Bent Volcano


Blog by Dal Stanton

Last April, during one of my earlier visits to what I have affectionately named, ‘The Hole in the Wall’ antique store near the Zhenski Pazar (Women’s Market) in downtown Sofia, Bulgaria, my eyes locked on to a very handsome pipe that called out to me resolutely – “Take me home!”  The pipe was a slightly bent volcano shape, brandishing a broad flattened oval shank and stem that drew my attention.  In my small collection of pipes then, and even today, I have nothing like it.  After taking in the unique shape, the briar grain, obscured by layers of grime and old wax, gave me an internal ‘wow!’ that I carefully kept hidden from the shop owner who would see my excitement as potential greater profit for him – so I played it cool.  I looked at how the grain moves horizontally across the bowl and shank giving the appearance of a tiger pattern looking down on the shank.  Looking straight at the bowl the grain looked like horizontal flames terminating on the sides of the bowl with Birdseye patterns – I was anxious to work on this pipe.  The top of the shank was imprinted with the classic BBB diamond mark over Banker.  Underneath the shank had London, England over 739.  The stem top also had the white diamond BBB mark.  I also spied another pipe in the basket that looked like a good candidate to bundle with the BBB Banker, a French Jeantet Fleuron 70-7 which helped me negotiate 30 Bulgarian Leva for the pair – about 16US.  Not a bad deal at $8 a pipe!  The first picture is the Jeantet followed by the BBB Banker after I arrived home from the ‘Hole in the Wall’ with my newest acquisitions:Bank1 Bank2 bank3 Bank4 Bank5 Bank6 Bank7 Bank8 Bank9I found a lot on the internet about the BBB name.  The small blurb in Pipehill describes the evolution of the BBB moniker:

BBB: ” Best British Briar” is now a brand of the Cadogan Company (Oppenheimer group). American rights to use the brand name were sold to Wally Frank in 1980.

Founder of the brand in 1847: Louis Blumfeld. The oldest pipe brand name in the UK has been registered in 1876 (Blumfeld Best Briar).

Steve also posted a blog on the history of BBB pipes a few years ago using the French article:

https://rebornpipes.com/2012/08/05/history-of-bbb-pipes/

I discovered that there are many BBB collectors and enthusiasts in my research.  Unfortunately, I could find nothing helping me to date or place my BBB Banker except some informed guesses comparing to the BBB stamps (pictured below) depicted in the French article Steve posted above which would probably date the Banker at the earliest in 1989 when the Cadogan Company consolidated manufacturing its various pipe lines at Southend-on-the-Sea, but more likely in the 2000s – not a terribly old pipe (Can anyone help me on that?):Bank10The condition of the Banker is generally good.  There is some cake build up in the chamber but I still want to ream the bowl down to the briar for a fresh start and to be able to make sure there are no problems lurking beneath – which I really don’t expect.  The rim has light grime and lava on it, but a significant wearing down of the front lip so that bare briar is exposed.  The stummel looks to be in good shape – I detect one fill underneath but it looks to be solid and will blend well.  The stummel grain is dulled and obscured by grime and oil build up.  The stem is in good shape – showing almost no oxidation, but has a tooth dent on the lower side of the bit.  I take a fresh close up of the rim to mark the progress.  I begin with reaming the bowl with my Pipnet reaming kit.  As I’ve become accustomed, I try to do the dirtier part of the cleanup on the 10th floor balcony adjoining our bedroom where my work-station is here in Sofia, Bulgaria.  Sometimes I wish I had a basement work area, but we do what we must!  I use only the two smaller blades of the four blades available to ream the cake down to the briar.  I follow the use of the reaming blades with 120 grit sanding paper to clean the cake further and finish with 240 grit on the chamber wall.  The bowl looks good.  True confession – while I was reaming the bowl my thoughts drifted off to a Savinelli reaming knife – on the eBay block, that I’ve had my eye on – one like Steve often employs.  There are still a few days left in the auction and I’m hopeful that I might add it to the arsenal!  I’ll let you know!  In order to get a better idea of the rim’s condition, I clean the external stummel with Murphy Oil Soap and work on the grime covering the rim.  I use cotton pads with undiluted Murphy’s.  I also employ a brass brush to work on the rim.  After the cleaning, I take the stummel to the sink and rinse it with cool tap water.  The pictures show the progress.Bank11 Bank12 Bank13 bank14Ok, for you who have years of restorations under your belts, here are some newbie musings – your patience appreciated!  At this point I realize I need to top the bowl to repair the front lip of the rim – it won’t take much but it is needed.  When one takes the rim down to the bare briar, I’ve learned that one also must have a plan for matching the hue of the old stain if one desires to keep the old stain tone matching the bowl.  I like the color scheme of the BBB Banker and I desire to keep it.  To keep it, I need to match the rim color tone with the rest of the stummel AND I need to address the very minor scratches and wear marks on the stummel surface BUT NOT sand it aggressively to remove the stain.  It is in some ways much easier to take the briar down to the wood with acetone and sanding and then apply new stain and voila!  New surface and color all blended and ready to go.  I know this situation calls for use of polishing compounds and such, which is a more passive approach to dealing with the surface – more opportunity to learn new things!  So, I move forward with topping the bowl with the aim of maintaining the current rich, deep red tones – we’ll see how it goes.  I took the BBB Banker to the topping board – 240 grit paper on a chopping block and rotated it on the paper in a gentle clockwise circle not applying too much pressure – letting the grit do its work.  To make sure I wasn’t leaning into the damaged lip area as I rotated, I eyeballed that the damaged area was untouched during the early rotations which meant the topping was true – I took a picture at this point (second picture).  I took off only enough to clear out the front lip problems.  I think it went well and the bowl looks perfectly round.  As I often like to do, to add a classy touch to the rim I bevel the inside lip.  I make the initial cut of the bevel with 120 grit sanding paper followed by 240 grit.  I’m satisfied with the bevel – not too much but just an accent.  I use micromesh on the rim from 1500-12000 to complete the rim repair preparing it for stain later.Bank15 Bank16 Bank17 Bank18 Bank19Now, the stummel surface.  I have questions rolling through my mind regarding how aggressive I can be to remove small scratches and wear blemishes but maintain the original patina of the briar as it came to me.  I elect to micromesh the stummel surface and leave the small blemishes.  I do not start with the coarsest pad (1500) but at 2400 – gentle approach (though the first picture below shows the 1500 it was not used).  I’m not sure this is the best plan but I can always back up to a more aggressive posture if I’m not satisfied with the results.  After a quick email with Steve, I feel better about the course of action.  I continue on the stummel with micromesh pads 3200-4000 and 6000-12000.  I am loving the briar grain popping out through the micromesh process – one of God’s small creations each piece of briar.  The pictures show the progress:Bank20 Bank21 Bank22As I put the stummel aside to work on the stem, I realized that I was so involved in working on the externals that I forgot that I hadn’t cleaned the internal of the stummel nor stem.  Before working on finishing the stem I decide to use the retort to clean the internals.  Last time I used the retort, an alcohol saturated cotton ball was launched from the bowl during the process.  I was gun-shy of the retort to begin with when I first acquired it – the launch didn’t help.  Notwithstanding, I unwrap the retort, get out the vodka, and proceed to let the retort do its work.  The pipe was surprisingly clean.  After two retort cycles, I finished off with cleaning the internals of stummel and stem with Qtips and pipe cleaners dipped in alcohol.  I think it’s better to clean internals earlier in the process….Bank23 Bank24 Bank25Now to the stem externals.  Earlier, I applied black super glue to two significant tooth dents on the underside of the bit (visible in picture above).  I use 240 grit sanding paper to remove the excess super glue removing traces of the dents as  well as file marks after using a needle file to fine tune the shape of the button. There was very little oxidation on the stem or teeth chatter so I proceed to wet sand with micromesh 1500-2400 and apply Obsidian Oil to the stem.  I follow by dry sanding using 3200-4000 micromesh pads and then the same with 6000-12000 and apply Obsidian Oil and set the stem aside to dry.  I’m pleased with the vulcanite ‘pop’ – that wet reflective look is great.Bank26 Bank27 Bank28 Bank29Well, I mentioned earlier that I was hopeful to add a Savinelli pipe knife to my tool box.  Steve speaks highly of this tool and has increasingly put it to good use in his restoration work.  He also posted a blog describing it when it arrived on his work table in Vancouver.  When I saw one on the block in the eBay’s estate pipes in tobacciana listings a few days ago, I decided to watch the auction and see if I could snag it – it seemed to be calling out to me: “I want to live in Bulgaria!”  As you would guess, others were watching too.  I’m thankful that my bid was sufficient and my new Savinelli pipe knife will be delivered to my daughter and son-in-law who live in Denver.  They will carry it with them to Bulgaria (along with some other supplies I’ve ordered including 32 oz. of Lane BCA Cavendish tobacco which I discovered with great enjoyment on my last trip to the US) when they visit in September!  My son-in-law had no problem agreeing to find space in the suitcases when I bribed him with sharing bowls together of the Lane BCA!  So, I’ll look forward to their arrival for the additional reasons that they will be packing new supplies and my new pipe knife!Bank30The BBB Banker slightly bent volcano is now in the home stretch.  After topping and sanding the rim with micromesh, I left the rim the bare wood until I finished the sanding of the stummel. I did this so that the stain I would eventually apply to the rim would be more closely matched.  Using an Italian brand stick, I applied a dark Mahogany stain to the rim and before it dried, lightly wiped it with a dry cotton pad to remove uneven stain application – the first two pictures below show before and after application of the stick.  I’m very satisfied with the match up of stummel and rim and am anxious to finish the stummel.  Living on the 10th floor of a former Communist block apartment building and with my work station in my bedroom (shared with my gracious and understanding wife!) space is at a premium.  My Dremel high speed tool is my workhorse when it comes to the polishing wheel.  Starting with a felt wheel, I first purge the engaged wheel by using the flat edge of the Dremel’s metal tightening wrench against it.  This softens the wheel and rids it of residue Tripoli caking from previous jobs.  With the newly purged wheel, I begin the final polish of the BBB Banker applying Tripoli to the surface addressing the minor pits and scratches on the bowl surface that I did not sand out aggressively to guard the beautiful patina of this piece of briar.  Bank31 Bank32 Bank33Finished with the Tripoli and Blue Diamond, I change to a cotton cloth wheel for the Dremel and apply several coats of carnauba wax.  I use the slowest setting for the Dremel and keep a continuous circular rotation over the briar surface – oh my, does the grain pop!  I cannot say exactly when this pipe was made, but if it’s been since 1989, someone employed by Cadogan Company’s Southend-on-the-Sea pipe making plant did an amazing job with the choice of this piece of briar and the volcano shape it became.  The grain is beautifully showcased in horizontal movements laterally across the stummel so that one can see the horizontal flame grain facing the stummel straight on and then move to the sides of the stummel and see the grain emerge in Birdseye perspective and swirls.  In the beginning I described the top-down view of the broad, flattened oval shank as reminiscent of tiger fir to me – now as I look at it zebra also comes to mind.  Another example of the beautifully showcased briar grain in the Volcano shape is the broad landscape of its underside – from across the broad shank to the front lip of the volcano base, runs a robust dissecting flow of grain that is majestic from my vantage point.  Yes, I confess, I’m a briar grain junkie.  Its beauty reminds me of its Maker.  With my last application of carnauba wax on stem and stummel, I change to a clean cotton cloth wheel and buff the entire stummel and stem.  Then I give the BBB Banker bent volcano a brisk buffing with microfiber cloth to bring out the richness of this briar even more.  I’ve enjoyed this restoration and look forward to loading the BBB Banker with its first bowl of tobacco in my hands.  Thanks for joining me!Bank34 Bank35 Bank36 Bank37 Bank38 Bank39 Bank40 Bank41 Bank42

 

Restemming and Restoring a Made in Denmark Apple


Blog by Steve Laug

I got an email from a fellow in Dawson Creek, British Columbia asking if I would be willing to work on a pipe that he had that was one of his favourites. It was an apple that he really liked and he liked the patina on it as well. This is what he wrote to me: Sir, I have a pipe in need of your skills. I was visiting City Cigar on a trip to Vancouver and William recommended you. I’ve inherited a pipe from my dad that needs to be refurbished. I wish to add a new curved stem. The old stem’s very loose. I will mail, or ship the pipe to you, as I live in Dawson Creek, BC. Once we discuss price & details. After leaving City Cigar, I was left with the impression that you’re “the guy” for the job.” 

I asked him to send some photos of the pipe and give me a look at the pipe. The next two photos are the ones that he sent to me. The saddle stem looked like a replacement to me. I had him send the pipe to me for a closer look.apple1When it arrived I could see that my assumption about a replacement stem was correct. Whoever had added the new stem had sanded the shank and removed half of the stamping on the shank. I could read that it said Made in Denmark and that there were no other stampings. The shank was significantly lighter in colour than the bowl. The rim was dirty and had a chip out of it and its top was damaged. There was some concrete rash on the back side below the chip where the bowl had been knocked on concrete.apple2 apple3I took a close up photo of the bowl top to show the extent of the damage and the uneven cake on the bowl sides. I also took photos of the stem and shank junction to show how the shank had been sanded to meet the stem diameter.apple4

I also took a photo of the back side of the bowl showing the horizontal line across the bowl. That line was a large fill that bulged and stuck out the surface of the bowl.apple5The bowl was covered with a thick grime and sticky material. I wiped it down with a cotton pad and alcohol to remove the grime and get back to the finish. The grain really began to shine through once I had removed the gummy buildup. The left and right sides of the bowl showed some nice birdseye. The front and back showed cross grain that ran along the top and bottom of the shank. The birdseye ran along both sides of the shank.apple6I topped the bowl on a piece of 220 grit sandpaper to remove the damaged portions of the rim.apple7I sanded the backside of the bowl to smooth out the bulging fill that ran across the bowl.apple8I sanded down the outer edge of the rim to remove the rim damage and also the burn and darkening on the edges. I scrubbed the bowl down with acetone and cotton pads to remove the finish so that once it was clean I could blend in the lighter portions with the rest of the bowl.apple9 apple10The owner wanted a new stem for the pipe so I went through my can of stems until I found one that would fit. He wanted a taper stem and the one I found would suit the bill. He also wanted it to have a slight bend in the end. This sharply tapered stem would make that an easy fit and fix. The stem was slightly larger in diameter than the shank so I would need to reduce it to match.apple11I took off the excess vulcanite with a Dremel and sanding drum. I worked on it until it match the shank diameter.apple12 apple13I took it back to the work table to hand sand it. I used 180 grit sandpaper and took back the excess stem material.apple14I sanded the stem further with 220 grit sandpaper until the transition between the stem and shank was smooth to the touch. I heated water in the microwave until it was boiling and put the stem in the water to soften it enough to put the bend in it. I bent it just enough to give it a jaunty look.apple15 apple16I used the medium and the dark stain pen to touch up the shank. The combination of colours matches the rest of the bowl colour.apple17 apple18I wet sanded the stem with 1500-2400 grit micromesh sanding pads to begin polishing it and to begin to remove the scratches. I rubbed it down with Obsidian Oil. I dry sanded it with 3200-4000 grit pads and gave it another coat of oil. I finished sanding it with 6000-12000 grit pads and gave it a final coat of Obsidian Oil. I set it aside to dry.apple19 apple20 apple21I buffed the bowl and stem with Blue Diamond on the buffing wheel and polished the briar and the stem. The polishing took out the last of the scratches in the vulcanite stem. The fill on the back of the bowl blends in perfectly now and it is smooth to the touch. The transition from the stem to the shank is also smooth. The slight bend in the stem works well with the pipe. It is finished and ready to go back to Dawson Creek. Hopefully the owner will enjoy the new stem and the virtually “new pipe”. It still carries with it the memories of his dad giving it to him. It still as some of the marks of its story but the look and the feel of the pipe are better than when we began the journey. Thanks for looking.apple22 apple23 apple24 apple25 apple26 apple27 apple28 apple29

Doing Shaping Work on a Comoy’s Grand Slam Pipe 66


Blog by Steve Laug

Recently I traded the Simpson Sandblast Billiard that I restored with a reader of the blog for a Comoy’s Grand Slam 66. It is stamped on the left side of the shank Comoy’s over Grand Slam over Pipe. On the right side it has the classic Comoy’s Circle Made in London over England Com Stamp and further along with the shape number 66. The finish was in decent shape though there was some sticky dirt buildup on the sides. The right side of the bowl had a small divot on the bottom front of the bowl. On the left side of the bowl there was a ring or a small trough that was indented in the bowl from the left rear of the bowl to left front of the bowl. It looked like a dent in the briar. It is very clearly shown in the second and the third photos below. The stem had some oxidation and three deep tooth gouges on the top of the stem and one on the button top. There were also some deep tooth marks on the underside of the stem and the button. The C stamp on the stem is a newer stamp in the vulcanite that is painted with a white paint.Comoy1 Comoy2 Comoy3I measured and studied the side of the bowl before I decided what to do with it. I was not sure if the trough was caused by and issue inside of the bowl so my brother and I both cleaned and checked that out and could see nothing. I turned to look at the outside of the bowl and noticed that the bowl actually bulged above and below the line. That line itself actually was the same height as the rest of the bowl apart from the bulge. The bulge was thus briar that needed to be removed rather than the line a dent of missing briar. I breathed a sigh of relief and began to work on restoring it to normalcy.

I sanded the side of the bowl with 220 grit sandpaper to try to minimize the groove in the bowl side. The photos below show the progress of the repair. The first photo shows the first sanding on the bowl side. With the initial sanding you can see length of the groove on the side of the bowl. I sanded the bowl side on both sides of the groove until the groove disappeared. I was actually surprised that I was able to remove the damage to the bowl without making the bowl any thinner in the process. It was almost as if when the bowl was turned in the factory the cutting head that turned the bowl slipped and left a hump above and below the groove. Thus the groove itself was actually level with the rest of the bowl other than the humps.Comoy4 Comoy5 Comoy6 Comoy7In the next photo you can see the slight divot at the 11 o’clock position at the top of the photo. It was a deep cut in the briar that must have happened when the pipe was dropped somewhere along process. I sanded it smooth and filled in the divot with clear super glue and briar dust. Once the repair cured I sanded it smooth with 220 grit sandpaper to smooth out and blend in the repair. I sanded it with a medium and a fine grit sanding block to remove the scratches in the briar.Comoy7a Comoy8The rim on the bowl had a light buildup of tars so I lightly topped it on the topping board to remove the buildup. I topped it against 220 grit sandpaper then against a medium and a fine grit sanding block.Comoy9 Comoy10 Comoy11 Comoy12I stained the bowl with a dark brown aniline stain thinned with alcohol to match the colour of the existing finish. I applied it to the surface and flamed the stain. I repeated the process until I had a good even coverage on the bowl sides.Comoy13 Comoy14I wiped the bowl and shank down with alcohol on cotton pads to even out the colour of the stain and make it more transparent. Once that was done, the finish of the bowl looked really good to my eye.Comoy15 Comoy16 Comoy17 Comoy18The stem was a newer style Comoy’s as noted above because of the style of the logo. It was stamped into the vulcanite and then painted. There were some significant bite marks on the stem that needed attention. The lighter tooth marks I was able to sand out with 220 grit sandpaper and remove them. There were others that were quite deep. I cleaned the surface of the stem and used a thick black super glue to fill in the tooth marks. Comoy19I sanded the repaired spots with 220 grit sandpaper and cleaned up the sharp edge of the button with a needle file. I was pleased with the overall look of the stem once the repairs had been sanded smooth.Comoy20I wet sanded the surface of the stem with 1500-2400 grit micromesh sanding pads to begin the process of polishing the stem. I rubbed it down with Obsidian Oil.Comoy21Before proceeding further with the micromesh I decided to touch up the “C” stamp. I used a fine bristle brush and white acrylic paint to fill in the letter. I sanded off the excess with the 1500 grit micromesh pad and went over that section with 1800-2400 grit to match the rest of the stem.Comoy22I dry sanded the stem with 3200-4000 grit pads and gave it another coat of Obsidian Oil. I finished sanding it with 6000-12000 grit pads, gave it a final coat of oil and set it aside to dry.Comoy23 Comoy24I polished the pipe and the stem on the buffing wheel with Blue Diamond polishing compound and gave the entire pipe several coats of carnauba wax. I buffed it with a clean buffing pad and then by hand with a microfibre cloth. The finished pipe is shown in the photos below. The adjustment to the left side of the bowl worked well to smooth out the bulges and crease and the pipe looks as it should have when it left Cadogan. Thanks for looking.Comoy25 Comoy26 Comoy27 Comoy28 Comoy29 Comoy30 Comoy31

Marxman Jumbo Lovat


Blog by Aaron Henson

Several years ago when I was first getting into our hobby, I stopped into a local antique store looking for practice pipes.  This particular store did not have much and what few they did were dirty, heavily caked and $25 each. The dirt and the heavy cake didn’t bother me but dropping 25 clams on an old briar pipe for practice was not going to happen.

A few weeks ago, one of my jobs happened to take me past this same store. It had been two years since I had been in so I thought it might be time for another look.  After my last visit I wasn’t expecting much.  When I asked the gentleman behind the counter about pipes he directed me to the same old display case at the back of the store.  The same pipes were on display but this time the price tag had been changed.  Clearly the pipes had been in inventory too long and he wanted to move them because now they were two for $10.   Not one to pass on a deal this good, I selected four large bowl pipes including the Marxman below (shown second from the top) as well as a large caliber Emperor and an unmarked Custombilt look-alike. L1The Marxman is a truly large pipe (and not the largest of the three) with a bowl diameter of 1 1/2”, chamber diameter of 1” and a depth of 1 5/8”.  The shank is a whopping 7/8” in diameter and the bit is that same width. The following page from a 1946 ad for Marxman calls the large size a “Jumbo” but I do not have any way of telling what letter size it might be.L2For background, Marxman only made pipes from 1934 until 1953 before being bought out by Mastercraft.  But Bob Marx’s short run made an impact on Hollywood and on US pipe makers in general. Pipedia has a short article on Marxman.L3Taking the pipe to the work bench I started by cataloging the things that needed to be done.  The bowl had a thick cake built up. So much so that I had to start with the smallest head on my Castleford reamer (and the largest head was too small to be effective to finish reaming the bowl).  The rim had a significant buildup of tars and a couple burn marks.  The outside of the stummel was grimy and had some dents but nothing too devastating.  On the bottom of the bowl there were two dark burn marks.  They were located on the bottom side of the shank which made me think they were not burn-outs but with the bowl cake so thick I could not be sure.  When I removed the stem, I could see that the end of the tenon, the stinger and the inside of the shank were all coated with a heavy tar.  This was going to be an arduous cleaning job. L4 L5For as much build up as there was in the stummel there was little in the way of tooth chatter or marks on the stem.  One small tooth dent on the top side of the stem was all. The button was quite small but the slot was nicely formed. Aside from some oxidation, all in all the stem was in great shape.

I set the stem to soak in an Oxiclean bath to loosen the oxidation and the tar build up in the air way and turned my attention to the stummel. First I reamed the cake out of the bowl. I could not believe just how much there was!  I took it back to clean briar to make sure there was no burn through. After the largest reaming head, I still needed to finished off the chamber with 80 grit sand paper wrapped around a dowel. There was a slight loss of briar about half way down the bowl but no burn through. If I had to guess, the previous owner may have been in the habit of half loading the pipe early in its life.

I shaped a soft wood stir stick into a narrow spatula shape and used it to clean out the caked gunk in the shank. I also need a short piece of wire coat hanger to open the air way. I finished scrubbing the internals of the shank with bristled pipe cleaners dipped in alcohol and cotton swabs until they came out clean.

Now that the insides were clean I turned to the outside of the pipe.  The rim was heavily coated with crusted tar/lava.  I had hoped to clean up the rim without needing to top the bowl but that was not the case. There were some burn marks in the rim under the tar build up that were best removed at the topping board. When topping a bowl, I use 100 grit paper on a smooth flat surface and work the bowl in a circular motion. I have recently started rotating the bowl a quarter turn every 10 passes. This helps me keep the topped bowl level by ensuring I don’t put too much pressure on one side of the bowl all the time.L6I started cleaning the outside of the pipe by wiping down the briar with acetone. This removed the wax and grime build up. I had hoped that the burn marks on the bottom of the shank were superficial and would be removed with a light sanding but I was mistaken.  I am not sure what happens to the pipe but it appeared to have been exposed to a significant heat source because the burns were deep. The wood was not damaged, that is to say there was no charring.  After a significant amount of sanding with 220 grit I had removed as much of the burn as possible without significantly impacting the shape of the pipe. I was careful to sand the entire area around the burn to blend, or feather, the repair.  Even so, it did not completely remove all of the burn mark.L7Next I steamed out dents by wrapping the bowl with a wet terrycloth rag and applying a clothes iron. The important thing here is to keep your fingers away from the steam and the iron away from any stamping.

I finished the bowl by sanding the outside with 1500 – 3200 micro mesh pads. I also took the liberty of beveling the inside of the rim which I thought gave the large bowl some visual character.L8Even though I sanded the chamber back I could still smell some ghosts of the old tobacco so thought I would give the pipe a salt and alcohol soak. I let sit for 24 hours but there was still a residual odor.  Before I was done with the restoration, I had to run three tubes of grain alcohol in a retort through the pipe before the pipe was truly clean (sorry no pictures). L9

The original finish was very light colored, almost a natural. To hide the remnants of the burn I decided to go with a light brown stain and contract the worm grooves with a slightly darker stain to make them stand out.  This would also help hide the burn.L10The stem was an easy clean for a saddle bit. The Oxiclean bath had loosened the crud in the airway and a few passes with bristled than soft pipe cleaners took care of the internals. The outside I sanded with 1500 grit micro mesh then added a small drop of black super glue to the one small tooth mark and a another dent that I didn’t want to sand out. I had tried to raise both with heat first but with little success hence the super glue.  Continued sanding with micro mesh pads up through 12,000 grit. I kept the pipe assembled during this process in order to keep the shank-stem connection flush.L11

With sanding and polishing complete I coated the entire pipe in mineral oil and let sit overnight. The mineral oil seems to help hydrate the briar and vulcanite of the stem.L12After 12 hours I wiped off any remaining oil and took the pipe to the buffer.  I went over the whole pipe with red diamond then applied multiple coats of carnauba wax.  As a finishing touch I decided to apply a bowl coating to the chamber.  I wiped the inside with maple syrup then add a table spoon of charcoal powder.  Placing the heel of my palm over the rim I shake the pipe until the charcoal evenly coats the inside.  I let the pipe dry for a week before dumping out the excess charcoal.

Now it’s time to “Relax with a Marxman”.  Thank you for taking the time to look.L13 L14 L15

 

Restoring ‘The Professor’ – WDC Milano Hesson Guard


Blog by Dal Stanton

This pipe was gifted to me in 1980 while a seminary student.  I was Professor Freundt’s student assistant and I spent much time with him in his office which was a virtual jungle of books, papers and journals – heaped in piles here and there yet the professor knew where to find the most obscure minutia.  Added to the smells of old books and leather covers were the tobacco and smoke that regularly provided an upper layer haze in his work space.  The Professor introduced me to the art and enjoyment of smoking pipes – now some 36 years ago.  I was young and eager, soaking in the ambiance of academia at a post-graduate level and pipes I discovered, were very comfortable partners in this environment.  Professor Freundt gave me the Hesson Guard, showed me how to pack its first bowl in my hands, and I smoked it, adding my offerings to the perpetual haze.  After these days, pipe smoking was put aside until last fall when Steve reintroduced me to it.  At this point, 3 pipes made up my collection: a corncob I also bought during those seminary days to use while fishing and duck hunting, a Willard I received after my grandfather’s passing (a future restoration), and the WDC Milano Hesson Guard that I had tucked away in drawers over the past three and a half decades.   Anxious to put a pipe back into service last fall, I grabbed the Hesson Guard, to clean it and do what I thought then were needed repairs….  I made a mess of the pipe – cracked the shank, reamed out the mortise so that the metal tenon was too loose – sloppy repair with super glue….  I’m anxious now to return to ‘The Professor’ (its given name) and try to make amends for the rough treatment he received last fall!

The right side of the shank is stamped with the well-known WDC inverted triangle next to Milano over Real Briar.  The left side holds Hesson Guard.  The bottom of shank had PAT. 1855800 which enabled me quickly zero in on the dating of the pipe.  The patent application was submitted by the inventor of the special internals, William W. Hesson, in 1930 and granted two years later.  An excerpt from the patent documentation describes the essence of the design:

The principal object of the invention is to provide a pipe which will eliminate contamination of the natural aroma of the tobacco through noxious secretions and which will remain sweet and clean.  A further object is to devise a construction of pipe which will be simple and inexpensive to manufacture and which. will be devoid of pockets to harbor noxious elements.  The principal feature of the invention consists in the novel arrangement of a tubular resilient member surrounding and embracing a metal stem which extends from the pipe bowl to the mouth piece and forming a seal to prevent the seepage of moisture around the metal stem.

(https://www.google.bg/patents/US1855800?dq=1855800&hl=en&sa=X&ved=0ahUKEwibqa2KsOjNAhUFVBQKHZ1DAvMQ6AEIGjAA)

I was curious to compare my Hesson Guard with the patent diagram which essentially is a long metal tenon meeting up with a metal sleeve at the base of the bowl and shank junction.  This design, along with many other designs, was to eliminate the moisture build up, gurgle and gunk.  Figure 1 (below) is followed by my overlay comparison picture – the tube inserts quite a way according to the 1930 design.  Following are pictures telling the current story of The Professor:H1 H2 H3 H4 H5 H6 H7 H8 H9 H10 H11The pipe is attractive and has a good feel in my hand.  The free-hand sculpting on the bowl gives the appearance of flames rising and is showcased in 3 paneled murals around the bowl. I notice that one of the panel dividers has been damaged at the top by cutting the briar.  It looks like they were seeking to connect the panels – not sure.  That will need to be filled in.  The rim will also need some gentle repair to what appears to be nicks created by wear and tear.  The cracked shank will need repair to keep it from growing and cleaning up the metal tenon and creating a good fit with the mortise might be a challenge.  The bit has very mild tooth chatter.  The last picture above captures not only the crack in the shank but the metal sleeve deep in the mortise that the chamfered tube/tenon docks with to create a dryer smoke – according to the patent information.  Before any cosmetic restoration takes place I first must deal with the major issues of the shank crack repair and the tenon/mortise fit.  I start the crack repair by drilling a small hole at the end of the crack to keep the crack from creeping up the shank.  I use my Dremel tool and a 1.5mm drill bit to make the hole. I utilize a magnifying glass to trace the crack which had become a ‘hairline’. I’m careful not to drill too far and breach the mortise wall.  Next time, I want to use a 1mm drill bit to leave less of a footprint.  Next, after inserting the tenon into the mortise to expand the crack area for glue penetration, I create a mixture of briar dust and CA Instant Glue filling the hole and running a line of glue along the crack.  I then sprinkle briar dust over the entire area and wait to dry.  The timing worked out well as my wife just called me for lunch!  After lunch, I work on cleaning up the tenon removing the old superglue with fingernails, Winchester knife, brass brush and 240 grit sanding paper – back in pristine shape. H12 H13 H14Well, after about a week, I return to the Milano Hesson Guard after my wife and I take advantage of the summer opportunities at the Black Sea coast.  We enjoy some days at the beach near our favorite coastal fishing town, Sozopol. While at the beach, I thought about the Milano and how best to approach the overly loose tenon/mortise fit.  Instead of applying clear nail polish around the metal tenon, which is what I did before, I attempt to rebuild the mortise wall by applying a very gentle coat of superglue on the inner wall of the mortise, rotating it as I applied superglue to achieve, what I hope, will be an even texture around the mortise wall.  Amazingly, this seems to have worked!  After drying, I gently reach into the mortise to remove some superglue ‘bumps’ with a needle file and I use a tightly rolled piece of 240 sanding paper carefully to smooth things down.  I don’t want to inadvertently remove too much of the restored mortise wall! I also give the crack repair a light, strategic sanding with 240 grit paper, careful to guard the stampings. I refit the stem and to my relief, a snug fit was restored.H15 H16 H17With the stem refitting correctly and inserted, I return to the shank crack to finish sanding it to remove the excess superglue – I do this with stem in so as to not create unevenness between the mortise and stem shoulder.  Satisfied with the shank crack repair and rebuilding the mortise wall, I put the stem in an Oxyclean bath for a soak to soften up the moderate oxidation buildup. I move my attention to the bowl to ream the mild cake down to the briar and then move to rim repairs and then to the panel repair.  I want to have all these completed before looking at the general stummel cleanup and refinishing. I move out to the 10th floor balcony adjoining my bedroom work station with Pipnet reaming kit to minimize the airborne cake soot – maximizing happy wife status!  I started with the smallest reaming blade moving to use 3 of the 4 blades available to remove the moderate cake in the bowl.  I finished the reaming by employing 120 grit paper on the chamber wall to remove remaining cake and smoothing the wall.  I took a close up of the chamber and rim to show progress and to get a good idea of how to approach the rim repair.  Inspecting the rim, I place a drop of superglue on one particular ‘dent’ that reached significantly down the external side of the bowl.  I’m hoping that this small fill will enable me not needing to take as much off during the bowl topping to repair the rim.H18 H19 H20 H21After the superglue sets up on the rim dent fill, I top the bowl using 240 grit sanding paper on top of a chopping block.  Since the day is beautiful, I again move to the 10th floor balcony to do the work. With the rim having no burns, I expect the surface to plane off evenly without pulls toward softer burned areas of the rim.  I rotate in a clockwise circular even motion and take off only as much as needed to remove the damaged area of the rim.  As I like to do, I create a small bevel on the inner wall of the rim to give a more finished, classier look.  I use 120 grit paper to form the initial bevel angle followed by 240.  I also decide to give the outer rim edge a slight sanding to round off the lip which seems to be consistent with the original Milano design.  Again, I make the initial cut on the lip with 120 grit paper and finish off with 240.  I have grown to appreciate more the rim presentation in finished pipes.  To me, the rim, it’s nuances, are the first thing the eye is drawn to when looking at a pipe – much like the first thing one sees when looking a person are the eyes, then one follows by taking in the general appearances.  The following pictures show the Milano’s rim progress.H22 H23 H24 H25You can see in the immediate preceding picture the rim superglue fill spot at the 11 o’clock position of the rim and the ongoing panel repair just below it (to the left in the picture).  Before moving to the stummel finishing, I now need to resolve the panel repair. I realize at this point with all the stummel repairs (cracked shank, topping and panel line), I will be removing the finish and refinishing the surface in order to achieve an even briar tone appearance.  Now, continue to ‘heal’ the panel cut – earlier I applied superglue to it to build it up.  I take a close up of the panel as it is now in order to know what I have. In order to blend more, I rough up the original superglue with a Dremel stone sander instrument. I apply on top of it a thick mixture of superglue and briar dust to form the restored surface that will join the side briar panel with the solid ring around the top of the bowl. I use toothpicks to mix, spread and tamp the mixture into place. I want this briar dust putty to setup well so I put the stummel aside for the time and turn to the stem which has been soaking in Oxyclean.H26 H27 H28The Oxyclean bath did the job of bringing the oxidation to the stem surface. I attack this initial layer with 000 steel wool and then use 240 grit paper to address the minor tooth chatter – I take pictures of bit top and bottom before starting to show progress. In order to have a good match between the mortise and the stem, I want to eyeball what the fit looks like before I proceed further.  As I suspected, with all the superglue applied to the mortise area, the fit between mortise end and stem was not flush.  I took the stummel back to the topping board and gently rotated the shank end on the board to regain a flush docking between stummel and stem.  After a few rotation cycles and testings to eyeball things, I am satisfied.H29 H30 H31 H32 H33 H34Before starting the micromesh cycles for the stem finishing, I need to remove the lip that I discovered with the shank end over the stem.  With the topping of the shank end, I enlarged the circumference of the end just a bit so that it was a bit larger than the circumference of the stem shoulder – primarily on the lower side of the shank.  I use 240 grit paper to even out the difference between the shank and stem – leaving the stem in place to assure a good, smooth transition! I am careful to use my thumb to cover and protect the nomenclature as I move around the shank with the sanding paper.H35Now to the panel repair below the rim. Using 240 grit sanding paper I bring the hardened superglue and briar dust mixture down to the bowl surface careful to maintain a rounded surface and not to flatten out the area of sanding focus.  The pictures show the progress.H36Dal

I like the panel patch and it will blend with a darker stain.  On a roll, I launch into the clean-up of the stummel and especially the ‘flame murals’ which are filled with grit and dust.  I use a tooth brush with Murphy’s Wood Soap undiluted and work over the entire stummel with special focus in the fire sculpting to remove the surface finish.  I follow this with rubbing down the stummel using cotton pads and tooth brush with acetone to remove the finish deep in the grain of the briar.  I finish my clean-up of the surface by picking the carved crevices with a dental tool.  Using micromesh sanding pads, I sand the high points of the stummel.  Using 1500-2400 I wet sand.  Following, 3200-4000 dry sand and finishing dry-sanding with 6000-12000.  The pictures show the progress – I’m liking the briar grain the micromesh process is bringing out.H38 H39 H40 H41 H42At this point, I have two questions about how to proceed before staining the stummel.  First, I need to clean out the ‘flame’ sculpting and use a black fine tipped permanent marker to darken the flames to give more contrast after the stain is applied.  The other question was how do I treat the stampings of the WDC Milano – Hesson Guard?  Do I protect it from the stain?  Do I cover them with Vaseline?  What? Upon closer inspection, I notice that the left side stamping, Hesson Guard, appeared to have gold left over in the ‘Hesson’ lettering – the rest having worn off (picture below) after the crack repair.  After a quick email to Steve, his input revealed that both sides would have originally born the gold lettering.  So, from my model kit (I’ve been involved in a project for several years building the USS Constitution sailing ship) I discover a bottle of Testors Gold Enamel Model Paint and my wife finds a small brush which I trim with my knife to create a more distinct point.  With Steve’s counsel stored in my mind, I applied the paint over the lettering and wiped off the excess.  To my relief and joy, the gold paint adhered to the crevices of the lettering and the overflow came off with the paper towel.  My first stamping restoration with paint worked well!  Steve also said that there was no need to worry about the new lettering during staining – that the gold paint would repel the stain.  Careful to avoid the new gold lettering, I clean the bowl with isopropyl using a tooth brush to get rid of the residue from the sanding and then I move to highlighting the flame sculpts to bring greater definition to the paneled murals in the finished pipe.  The pictures tell the story.   H43 H44 H45 H46 H47Time to stain and I decide to use a mixture of an alcohol-based Italian stain I found here in Bulgaria with a color description of dark nut.  I want this as the base, but I mix it with a mahogany color water based stain to bring out a slightly more redish tone in the briar.  I think the red will work with the flame sculpting motif and I think this will look good – but of course the briar does what it will with the hues!  After mixing the stains in the shot glass, I apply the mixture to the stummel mounted on the cork and candle stick with cotton balls making sure to cover everything and getting a good thick coverage.  After applying stain, I use the butane lighter to flame the stain.  With the mixture that I made, the alcohol content was too low to ‘flame’ so I evenly moved the lighter flame across the surface to evaporate the alcohol setting the dye in the grain of the briar.  I repeated the process again and set the stummel aside to dry.H48With the stummel put aside, I turn again to the stem.  I re-inspect the button area after the earlier sanding to remove the teeth chatter.  I decide that the button needed a little more attention.  I use 240 grit sanding paper and a needle file to fine-tune the shape of the button before starting on the micromesh cycles.  I wet-sand the stem using 1500-2400 and complete the cycle by applying Obsidian Oil.  While still wet from the oil I continue to dry sand with 3200-4000 micromesh pads, again concluding the cycle by applying Obsidian Oil. The final cycle, 6000-12000 is used and a final coat of Obsidian Oil and I put the stem aside to dry.  I love watching the shine of the stem progressively make it to the surface getting that final wet, reflective look in the stem.  Nice!  The stem pops.  The pictures capture the progress!H49 H50 H51 H52For me, beginning the process of finishing the stummel after the staining dries, is like opening a Christmas present.  The anticipation is to see what actually is under the crust of flamed stain and what the briar grain will reveal.  With the Dremel tool, I begin to remove the ‘wrapping’ using a felt wheel.  Also with a felt wheel I polish beginning with Tripoli and then move to Blue Diamond.  I focus on bringing out the contrast of briar ‘flames’ showcased in the three panels.  I switch to a cotton cloth wheel and apply carnauba wax to both stummel and stem.  After several coats of carnauba, I complete the job by giving the pipe a clean cotton cloth wheel buff followed by a rigorous buffing with a micro-fiber cloth to bring out the deep tones of the briar.H53 H54I’m pleased with the revitalization of ‘The Professor’, WDC Milano Hesson Guard.  I think Professor Freundt, if he were alive today to comment, would agree.  The rich dark tones of the briar, with the hints of deep reds, reminds me of the myriads of leather bindings and books that filled his hazy office.  I’m pleased with the results.  Thanks for joining me!H55 H56 H57 H58 H59 H60 H61 H62

 

Cleaning up a no name Vineyard Meerschaum Billiard


Blog by Steve Laug

I received a second meerschaum pipe in a leatherette or vinyl covered case. This one was a straight billiard. The bowl was lightly carved with grape vines and clusters of grapes all around the bowl. There were two rings carved around the top of the bowl to set off the vines and grapes. The bowl has begun to colour – especially around the shank and on the lower portion of the bowl. The rim had some dark marks and a coat tar that was stuck on the top. The stem is made of a dark acrylic and has some tooth marks and chatter on the top and the bottom sides near the button. The nylon/Delrin threaded tenon has some darkening but is in excellent condition. The stem sits perfectly on the shank. The case is lined with white satin like material.G1 G2 G3 G4I took a close-up photo of the rim top to show the damage. There was darkening and tar but there were also some nicks in the surface that had retained the oil. I also took some photos of the top and bottom side of the stem to show the tooth chatter and tooth marks.G5 G6I wiped down the surface of the meerschaum with soft scrub to remove some of the marks and oils from handling that were on the bowl sides, front and back.G7I scrubbed the bowl top with the soft scrub and wet sanded the rim top with 1500-2400 grit micromesh sanding pads. I followed that up with 3200-4000 grit sanding pads. I wiped the top of the bowl down with the cotton pad. I was able to remove all of the damage and all of the buildup.G8I scraped out the light cake with the Savinelli Pipe Knife. I did not want any cake build up in the bowl. I wiped the bowl down on the inside with a damp cotton pad.G9I scrubbed out the shank and the airway in the tenon and the shank with pipe cleaners and cotton swabs and light alcohol. I was surprised that the internals were not too dirty. I scrubbed out airway in the stem with alcohol, cotton swabs and pipe clean cleaners. I worked on the area that the tenon screwed into in the stem.G10I sanded the tooth marks and tooth chatter with 220 grit sandpaper until they were no longer visible. I wet sanded it with 1500-2400 grit micromesh sanding pads and rubbed it down with Obsidian Oil. I dry sanded it with 3200-4000 grit sanding pads and gave it another coat of oil. I finished sanding it with 6000-12000 grit pads. I gave it a final coat of Obsidian Oil and set it aside to dry.G11 G12 G13I buffed the stem with Blue Diamond and hand buffed bowl. I gave the stem several coats of carnauba wax and buffed it with a clean buffing pad. I hand buffed the entire pipe with a microfibre cloth. The finished pipe is shown in the photos below. This one is also available for anyone who is interested in adding it to their rack. Just send me a message on Facebook or leave a message in the response box below the blog. Thanks for looking.G14 G15 G16 G17 G18 G19 G20 G21

What a mess – a Georgetown Made in London, England Canadian


Blog by Steve Laug

The grain on this old Georgetown Canadian really spoke to me when I took it out of the box of pipes from my brother. The mix of diagonal cross grains on the sides of the bowl and the birdseye on the front and back of the bowl and the top and bottom of the bowl and shank are really quite stunning. The bowl itself was incredibly dirty and the finish had rubbed and baked in grime all over. The rim was thickly caked with an overflow of lava the came from a bowl that was so caked that there was hardly room for any more tobacco. The stem was oxidized and there was a thick white build up of what I call calcification that comes from saliva and use. The slot in the end of the button was almost closed off with merely a small space mid slot. It was truly a mess that caused me to wonder what I would find once I cleaned and reamed the bowl.Geo1 Geo2I took some close up photos of the rim and bowl as well as the stem to show the extent of work that would have to be done to clean it up.Geo3 Geo4I also took a photo of the stamping on the shank to try to capture how it looked. It read MADE IN LONDON on the top line and under that ENGLAND. Stamped high and touching the bottom of the letters of the England stamp is the GEORGETOWN stamp.Geo5I reamed the bowl with the PipNet reamer starting with the smallest cutting head and working up the third head. The cake was harder toward the bottom of the bowl so I worked on smoothing it out with the Savinelli Pipe Knife and finished with the third cutting head of the reamer. You can see the rim damage on the inner edge of the rim at the back of the bowl in the photo below.Geo6I topped the bowl on the topping board until the damaged areas were minimized on the rim surface and the thick hard lava build up was gone. You can see the out of round areas on the inner edge of the rim in the second photo below.Geo7I scrubbed the surface of the bowl with acetone and cotton pads to remove the grime and the waxes on the finish. If you look closely at the pipe you will see a multitude of fills that are well placed in the grain of the pipe and barely visible.Geo8 Geo9I worked on smoothing out the damage to the inner rim by beveling it with the Dremel and sanding drum and then sanding it with a folded piece of 180 and 220 grit sandpaper. I smoothed out the scratches with 1500-2400 grit micromesh sanding pads.Geo10I started cleaning out the shank and the airway with pipe cleaners, cotton swabs and alcohol but found that I would need to use too many of them to be effective. I put the stem in place on the shank and set up the retort to boil alcohol through the pipe. I used five test tubes of alcohol before finally I was able to get one that was clear after boiling it through.Geo11 Geo12 Geo13I cleaned out the airway in the shank and the stem as well as the mortise with a few pipe cleaners and cotton swabs to remove the remnants of alcohol and debris left behind by the retort. I used the light brown stain pen to touch the area on the rear side of the bowl where I had done some light sanding and repair as well as the area around the shank stem junction that was lighter.Geo14I wet sanded the stem with 1500-2400 micromesh sanding pads and gave the stem a coat of Obsidian Oil. I dry sanded it with 3200-4000 grit pads, gave it another coat of oil and finished sanding with 6000-12000 grit pads. I gave it a final coat of Obsidian Oil and set it aside to dry.Geo15 Geo16 Geo17I buffed the pipe with Blue Diamond on the buffing wheel and then gave the bowl and stem multiple coats of carnauba wax. I buffed it with a clean buffing pad to raise the shine and then hand buffed it with a microfibre cloth to deepen the shine. The finished pipe is shown in the photos below. I am still trying to figure out who made the pipe. I know that the Made in London, England stamp was used by Barling and in the pre-Cadogan era by GBD. If anyone can give me more definitive information regarding the maker of these pipes for the Georgetown Tobacconist please contact me in the comment section. Thanks ahead for your help and thanks for journeying with me on this refurb. Geo18 Geo19 Geo20 Geo21 Geo22 Geo23 Geo24 Geo25