Tag Archives: article by Paresh Deshpande

A Tribute to an American Pipecarver – “John L. Lakatosh”


Blog by Paresh Deshpande

In my last blog on Boswell ’96 pipe restoration, I had confessed my growing admiration for pipes made by American pipe carvers after having worked on a number of pipes like Tracy Mincer, Custom-Bilts, Kaywoodies, John Bessai, J M Boswell etcetera. I realized that American pipe carvers are artistic, technologically inventive and that the pipes they made are robust, life lasting with a nice feel and heft and of very high quality. However, my liking for freehand pipes has remained undiminished. So now I have on my work table, three freehand pipes made by an iconic American small time pipe carver, who passed away in March this year. The carver that I am mentioning is Mr. John Lakatosh.

The three pipes currently on my work table are large sized freehand which were hand carved by John Lakatosh. The first is a large bent freehand billiard carved in 4-81; the second is a large sized triangular freehand pipe with a nice heft and hand feel, carved in 1-83 while the third is a sitter Saxophone (or should I call it a Ballerina!!!!!) carved in 5-85, the first digit indicating the month and later two digits denoting the year in which they were carved. All these pipes bear the stamping “HANDMADE” over “LAKATOSH” over the “MONTH AND YEAR” in which they were made. These stamps are in engraved in a script hand on the shank end of each pipe. I was keen to know more about John Lakatosh, the carver, his pipe making techniques and philosophy. I searched pipedia.com and there is a very brief write up on him. I reproduce the information available on pipedia.com for a quick read.

John Lakatosh was a carver from New Columbia, Pennsylvania. He made pipes in his home workshop in the Susquehana Valley up above Sunbury. John made pipes during the week and sold most of them at craft fairs in Central and Southern Pennsylvania. He retired from carving, to go back to bus mechanic work after the tobacco industry took a decline. He now lives with his wife in Lewisburg Pennsylvania, where he now crafts furniture for family and friends. He recently passed on March 8th 2018. (Primary/Familial Source)

As I was surfing the net for more information on Mr. John Lakatosh, I came across his obituary. Here is the link (https://www.heffnercare.com/obituaries/obituary-listings?obId=3010702)

INITIAL VISUAL INSPECTION
The stummel surface of all three pipes boasts of beautiful straight and flame grains all along the stummel surface. The 4-81 carved pipe has three hand rusticated patches, one on either sides of the bowl and one on the front side. The front of the stummel on the one carved in 1-83, has a beautiful and delicate sliver of rustication extending from top left side of the rim and extends to half way down towards the heel on the right side. The sitter carved in 5-85 has smooth surface with no rustications.  The stummel is relatively clean and has a few dents and dings likely due to uncared for storage. The briar is dull and lifeless and has taken on a layer of aged patina, through which one can make out the beautiful grains all round. All three pipes should clean up nicely. Apart from the pipe 4-81 which appear to have been smoked maybe once or unsmoked, the other two pipes have seen considerable use and have a decent layer of cake. The condition of the inner walls of the chamber on both used pipes can be ascertained only after the cake has been removed completely and taken down to bare briar. Both the bowl feels robust and solid to the touch from the outside. This issue should be a breeze to address. The plateau rim top has darkened on the 1-83 and 5-85, more so on the later due to frequent lighting, on the back side of the rim. This can be seen in above pictures. The plateau rim top of the 4-81 is pristine. The condition of the inner edge and rim top can be commented upon only once the rim has been cleaned. The plateau shank ends of all three pipes are clean and without any accumulation of dirt and grime. However, the mortise does show signs of accumulated dried oils, tars and remnants of ash, greatly restricting the air flow.The 1-83 and 5-85 have green and brown acrylic stem respectively. The 4-81 has a vulcanite stem. The acrylic stems have beautiful swirls of contrasting light and dark colors. The green stem has significant damage in the form of deep bite marks on both the upper and lower stem surface near the edge of the lip. The brown acrylic stem has tooth chatter on both surfaces of the stem, also near the edge of the lip while the vulcanite stem is devoid of any tooth chatter or bite marks, but is heavily oxidized. There is some damage to the stem in form of cuts, on the flared edge towards the tenon. The tenons on both the green and brown acrylic stem are covered in dried oils and tars and so is the airway. The air flow through the stems is laborious to say the least. The fit of both these stems in to the mortise is very loose, which will loosen further after the mortise and tenon have been cleaned. These issues will need to be addressed. THE PROCESS
I started this project by reaming the chambers of 1-83 and 5-85 with size 3 head of PipNet reamer. I used a 220 grit sand paper, pinched between my thumb and forefinger, to sand the inner walls of the chamber of all three pipes. Once I had reached the bare briar, I wiped the chamber with a cotton pad dipped in isopropyl alcohol. This removed all the residual carbon dust and also rid the chamber of all ghost smells. I followed up the reaming by cleaning the mortise and air way of all three pipes, using hard bristled and regular pipe cleaners, q-tips dipped in alcohol. The mortise and the draught hole of 5-85 was so chock-a- block with all the dried tars, oils and gunk that I had to use my fabricated spatula and the drill bit from the Kleen Reem pipe reamer!!!! I gave a final clean with shank brushes dipped in alcohol and dried the mortise with a rolled paper napkin. The shank internals and the draught hole are now nice and clean with an open and full draw.I cleaned out the internals of the stem using hard bristled and regular pipe cleaners dipped in alcohol. I scraped the dried oils and tars from the tenon with the sharp edge of my fabricated dental spatula. The deep bite marks on the green stem of 1-83 were cleaned with cotton pad dipped in alcohol and spot filled with clear superglue. I set the stem aside to cure the fill. Now, it was the turn of the stummel of all three pipes to get cleaned up. Using a hard bristled tooth brush dipped in undiluted Murphy’s oil soap, I very deliberately scrubbed the stummel, cleaning the surface thoroughly. Special attention was paid to scrub out all the dirt and dust from the crevices in the rustication on the sides and front of the stummel on 4-81. I cleaned the plateau rim and shank end too. The stummel, plateau shank end and rim top were dried using paper napkins and soft cotton cloth. The cleaning of the stummel revealed three dents on the stummel of 5-85. I decided to raise these dents to the surface using the steaming method. I heated my smaller fabricated knife over a candle. Once the knife was hot, I placed a soaked Turkish towel over the dent and placed the heated knife over it. The steam generated pulled out two of the three dents. I spot filled the remaining dent with clear superglue and set it aside to cure overnight. Once the fill had cured, using a flat head needle file, I blend the fill with the surrounding briar and further sand it with a piece of 220 grit sand paper to achieve finer match. I wanted to highlight the grains seen and further blend all the repairs carried out to the stummel. To achieve this aim, I sand down the three stummel using micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. The three stummel now have a deep shine with grains popping out with magnificent contrast. Though this part of restoration is the second most time consuming and laborious, the end results are also the most satisfying. The play of grains, the contrast and the smooth surface are well worth the efforts. I rub a small quantity of “Before and After Restoration Balm” in to briar and let it rest for a few minutes. I took some extra efforts to work the balm in to the hand carved rustication on the bottom of the bowl. The balm almost immediately works its magic and the briar now has a nice vibrant appearance. I further buff it with a horse hair shoe brush. With the stummel nice and clean and attractive, I worked the stems of all three pipes. The fill on the green acrylic stem had cured nicely and I sand it down with a flat head needle file. I sharpened the lip edges using a needle file and sand the entire stem with 220 followed by 400, 800 and 1000 grit sand paper. This helps to reduce the sanding marks left behind by the more abrasive 220 grit paper. By mere sanding itself, the minor tooth marks seen on stem surfaces of the brown stem of 5-85 were addressed completely while this process eliminated the deep oxidation seen on the vulcanite stem of the 4-81 pipe. To bring a deep shine to the vulcanite stem as well as the green and brown acrylic stems, I went through the complete set of micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. I wiped the stem with alcohol after each pad and rubbed it down with Extra Virgin Olive oil. The internals of the stem was cleaned out using alcohol and pipe cleaners. The pictures of the process and final results are shown below. To finish, I re-attach the stem with the stummel. I mount a cotton cloth buffing wheel on to my local machine which is similar to a Dremel. I set the speed at about half of the full power and applied White Diamond compound to each of the three pipes. I wiped/ buffed all the pipes with a soft cotton cloth to clear it of any leftover compound dust. I then mounted another cotton cloth wheel on to the polishing machine and applied several coats of carnauba wax over the stummel and the stem of all three pipes. I finished the restoration by giving all the pipes a rigorous hand buffing using a microfiber cloth to raise the shine further. The completed pipes, with the dark brown hues of the stummel contrasting with the shiny black stem, looks lovely, fresh and vibrant; the photographs speak for themselves. The beauty, size and shapes of all these pipes make it one of my favorites and will find a place of pride in my modest collection. If only the pipe could tell some of the stories and techniques used by Mr. John Lakatosh while carving pipes.… Cheers!!

Restoring a Pipe Carved by an American Living Legend – “J.M. Boswell”


Blog by Paresh Deshpande

I shall be honest with you; I love vintage English made pipes! I love vintage British bikes and own a couple; I love vintage British fountain pens and have a decent collection of the same. It is something about the simplicity yet unique British craftsmanship, robustness and reliability factor of British made products that I find most appealing. However, after having worked on a number of pipes made by various pipe carvers from USA like Tracy Mincer, Custom-Bilts, Kaywoodies, John Bessai etc, I realize that American pipe carvers are artistic, technologically inventive and the pipes they made are robust, life lasting with a nice feel and heft and of very high quality. Am I gravitating towards American pipes? May be……. The next pipe on my work table is a 22 years old and completely handmade freehand full bent billiard made by an iconic pipe maker from Pennsylvania, USA. Yes, I am working on a pipe made by J M Boswell from the year 1996.

This is a large sized full bent billiard freehand pipe with a nice heft and hand feel. The shape of the pipe is unique in that the proportionate shank has a sudden taper towards the shank end and this size is carried forward on to the saddle of the stem, tapering a bit along the stem before flaring out at the stem end. Wow!!!! That was one hell of a description which has left me exhausted and brain drained!!!! The stamping on the left side of the shank was clear and readable. It read “Boswell” in script signature over “96 USA”. The pipe was made in 1996.The saddle stem bears no stampings.I was keen to know more about J M Boswell the carver, his pipe making techniques and philosophy. I searched rebornpipes.com and sure enough, Mr. Steve has worked on a Boswell before!!! As is his habit, he has thoroughly researched this carver and has included valuable information in his write up. Therefore, instead of reinventing the wheel, here is the link to this write up for detailed information; (https://rebornpipes.com/2017/07/19/refurbishing-a-boswell-2003-spiral-twist-bent-billiard/). Do give it a read.

Is there not a single brand that this gentleman has not worked on before??? Is there never going to be an opportunity for me to research and contribute one pipe make on rebornpipes??? Well, I have just started on my journey as against his decades of dedicated hard work and as Robert Frost wrote in his poem “……..and miles to go before I sleep”. The quest for excellence and contribution continues!

INITIAL VISUAL INSPECTION
The stummel surface boasts of beautiful straight grains on the right side and most of the front while the left side has lovely swirls of grain interspersed with bird’s eye. The bottom of the shank has unique hand carved rustication which taper towards the right side and extends in a thin and straight line towards the rim on the right side. Lovely bird’s eye can be seen on the top of the shank surface with straight grains on either side of the shank.  The stummel is covered in oils, tars and grime from the overflowing lava. The crevices in the rustication are filled with dirt, dust and grime. The briar is dull and lifeless and has taken on a layer of aged patina, through which one can make out the beautiful grains all round. This one should clean up nicely. This pipe has seen heavy use and the chamber has a nice thick consistent layer of cake, about the size of dime, as is recommended. The cake has been regularly reamed to maintain correct thickness. This seems to be a well cared for pipe. The condition of the inner walls of the chamber can be ascertained only after the cake has been removed completely and taken down to bare briar. The bowl feels robust and solid to the touch from the outside. However, the mortise does show signs of accumulated dried oils, tars and remnants of ash, greatly restricting the air flow. This issue should be a breeze to address.The rim top is covered in a thick overflow of lava from the chamber. This is the only part of the stummel which appears to be neglected. The condition of the inner edge and rim top can be commented upon only once the rim has been cleaned. However, I have a feeling from looking at the appearance, that the right side of the inner edge in 3 o’clock direction may be charred from frequent lighting. Well, we’ll see about it later. Thankfully, the outer edge is pristine and shows no signs of damage!!The vulcanite stem is without any bite marks or tooth chatter. The upper and lower lip does show one bite mark each. The stem was apparently used with a rubber bit as can be seen from the calcification marks on the stem (Come on!! One does not have to be a Sherlock Holmes for this deduction!!). The saddle stem is heavily oxidized. The tenon is covered in dried oils and tars and so is the airway. The air flow through the stem is laborious to say the least. The fit of the stem in to the mortise is very loose, which will loosen further after the mortise and tenon have been cleaned. These issues will need to be addressed.THE PROCESS
I started this project by reaming the chamber, starting with size 2 head of PipNet reamer and moving on to size 3 head. I used a 220 grit sand paper, pinched between my thumb and forefinger, to sand the inner walls of the chamber. Once I had reached the bare briar, I wiped the chamber with a cotton pad dipped in isopropyl alcohol. This removed all the residual carbon dust and also rid the chamber of all ghost smells. Using a sharp knife, I gently scraped the rim top to remove the lava overflow. I followed up the reaming by cleaning the mortise and air way using hard bristled and regular pipe cleaners, q-tips dipped in alcohol. The mortise and the draught hole was chock-a- block with all the dried tars, oils and gunk that I had to use my fabricated spatula and the drill bit from the Kleen Reem pipe reamer!!!! I gave a final clean with shank brushes dipped in alcohol and dried the mortise with a rolled paper napkin. The shank internals and the draught hole is now nice and clean with an open and full draw.I cleaned out the internals of the stem using hard bristled and regular pipe cleaners dipped in alcohol. I scraped the dried oils and tars from the tenon with the sharp edge of my fabricated dental spatula.Now, it was the turn of the stummel to get cleaned up. Using a hard bristled tooth brush dipped in undiluted Murphy’s oil soap, I very deliberately scrubbed the stummel, cleaning the surface thoroughly. Special attention was paid to scrub out all the dirt and dust from the crevices in the rustication on the bottom of the shank and right side of the bowl. I cleaned the rim too. The stummel and rim top was dried using paper napkins and soft cotton cloth. I was not happy with the way the rim top had cleaned up. There were darkened areas on the rim top, which kept drawing my attention, as well as very light, almost negligible damage to the outer edge in the form of dents. For the sake of my own satisfaction, I decided to address these blemishes. I topped the rim top on a 220 grit sand paper. I was careful to avoid excessive topping and frequently checked the progress. It was at this stage that I realized that the left inner edge has a slight char in 8 o’clock direction. And all this while I had anticipated this damage to be on the right!! So much for playing Sherlock Holmes!! I address the issues to the inner and outer edge by creating a slight bevel using a 220 grit sand paper pinched between my thumb and forefinger. It’s looking good now, I say, save for a black spot on the left side!!! I wanted to highlight the grains seen and further blend all the repairs carried out to the stummel. To achieve this aim, I sand down the stummel and rim top using micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. The stummel now has a deep shine with grains popping out with magnificent contrast. Though this part of restoration is the second most time consuming and laborious, the end results are also the most satisfying. The play of grains, the contrast and the smooth surface are well worth the efforts. I rub a small quantity of “Before and After Restoration Balm” in to briar and let it rest for a few minutes. I took some extra efforts to work the balm in to the hand carved rustications on the bottom of the bowl. The balm almost immediately works its magic and the briar now has a nice vibrant appearance. I further buff it with a horse hair shoe brush. With the stummel nice and clean and attractive, I worked the stem. I sharpened the lip edges using a needle file and sand the entire stem with 220 followed by 400 and 800 grit sand paper. This helps to reduce the sanding marks left behind by the more abrasive 220 grit paper. By mere sanding itself, the minor tooth marks seen on both stem surfaces were addressed completely. To bring a deep shine to the vulcanite stem, I went through the complete set of micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. I wiped the stem with alcohol after each pad and rubbed it down with Extra Virgin Olive oil. The internals of the stem was cleaned out using alcohol and pipe cleaners. The pictures of the process and final results are shown below. To finish, I re-attach the stem with the stummel. I mount a cotton cloth buffing wheel on to my local machine which is similar to a Dremel.  I set the speed at about half of the full power and applied White Diamond compound to the entire pipe. I wiped/ buffed the pipe with a soft cotton cloth to clear it of any leftover compound dust. I then mounted another cotton cloth wheel on to the polishing machine and applied several coats of carnauba wax. I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further. The completed pipe, with the dark brown hues of the stummel contrasting with the shiny black stem, looks lovely, fresh and vibrant; the photographs speak for themselves. The beauty, size and shape of this pipe make it one of my favorites and will find a place of pride in my modest collection. If only the pipe could tell the story of its journey till date…………… Cheers!! PS: The last functional aspect which I addressed at this stage was the protection of the walls of the chamber against the possibility of a developing serious heat fissures. I mix activated charcoal and yogurt to a consistency which allows for an easy and even spread and evenly apply it on the inner walls and set it aside to dry out naturally. This coating helps in protecting the wall surface and assists in quicker formation of a cake.

Restoring a Rare “Zeus” U.S. Pat # 2.158.897


Blog by Paresh Deshpande

I am really privileged to have inherited a large collection of pipes that once were actively smoked by my grandfather for nearly 40 years, from 1930s to mid of 1970s!! This eclectic collection has a large variety of pipes of various origins; British, Denmark and US makers being in larger numbers. As I am researching and restoring each pipe, I have come to realize that there are actually quite a few that are a part of pipe history!! The one that is now on my work table is one such. It’s a “ZEUS”!!

This an oddly shaped Apple with a very wide shank which extends for about an inch before it is joined by an aluminum oval tube. An oddly shaped stem, something similar to a mermaid’s tail, fits into the end of the metal tube. The stummel surface boasts of beautiful flame grains along the sides of the stummel, while cross grains adorn the top and bottom of the shank. The left hand of the shank is stamped with “U.S. PAT.” in block capital, over the patent number “2.158.897”. The uniquely shaped twin bore Cumberland stem bears three stars on top surface of the stem, one at the top over “ZEUS” and two stars below. The lower surface of the stem bears the stamp “MADE IN” over “U.S.A.”In order to research any pipe that I am working on, the first place I visit is rebornpipes.com!! There is a wealth of information that Mr. Steve has collated in one place. There is a write up on a “ZEUS” which has been restored by Mr. Steve and he has painstakingly collated all the relevant information on this model of pipe which was made by LH Stern Inc. Instead of reinventing the wheel, here is the link to the write up which all pipe enthusiasts and collector may like to read to know more on this ultra rare pipe (https://rebornpipes.com/2015/05/10/a-unique-piece-of-pipe-history-a-zeus-system-filter-pipe/).

INITIAL VISUAL INSPECTION
Overflow of lava is seen on the rim top and also on the stummel surface, more so at the joint where the shank and the stummel meet. Through all this dust, dirt and grime, beautiful flame grains can be seen all around on the stummel. There is not a single fill that can be seen through the grime on the stummel. Maybe after a clean, a few gremlins will show up. The aluminum shank extension is without any dents and dings, which is a surprise of course, and is securely fixed over the shank. I do not intend to disturb the geometry of the pipe by attempting to separate it from the shank. The briar is dull and lifeless and has taken on a layer of aged patina, through which one can make out the beautiful grains all round. This one should clean up nicely. There is a thick and uneven layer of cake in the chamber which makes it difficult to ascertain the condition of the walls of the chamber. From the thin rim surface, it appears that the walls on upper portion of the bowl are thin and thickens down towards the heel as the bowl flares outwards, giving it the classic Apple shape. I really pray that I do not encounter the chamber condition akin to what I had encountered while working on the “SON”!!! The thin rim top is covered with overflow of lava. The inner edge appears uneven and so does the rim top. The outer edge is covered in overflow of lava and its condition will be ascertained after the rim has been cleaned.There are two spikes on the shank end which extend in to the aluminum shank extension. These spikes and the insides of the shank extension are filled with oils, tars and grime. The mortise is clogged and restricts the flow of air. These issues will need to be addressed.The twin bore Cumberland stem is the first that I shall be working on. The twin bore stem moved toward a single airway in the thinner portion towards the end of the stem. It formed a Y. The twin bores were quite large as can be seen in the photo. The airway appeared clean and would require a routine cleaning with pipe cleaners and alcohol. There a few very light bite marks near the end of the stem. There are small bite marks on the lower and upper lip edges. It is nice, dark, and smooth. These issues should not be a major headache to address. The tenon is clean and flow of air through the airway is full and smooth. THE PROCESS
I started this project by cleaning the chamber using size 4 head of the PipNet pipe reamer as the chamber is very wide. I used a 220 grit sand paper, pinched between my thumb and forefinger, to sand the inner walls of the chamber. Once I had reached the bare briar, I wiped the chamber with a cotton pad dipped in isopropyl alcohol. This removed all the residual carbon dust and also rid the chamber of all ghost smells. I gently scrapped the rim top with a sharp knife to remove the entire lava overflow. The process had revealed a web of very thin superficial lines which looked like the beginning of heat fissures. To make sure, I ran a toothpick along the lines. If these were the beginning of heat fissures, there would be some give in the lines as the charred briar would fall out. Luckily, this was not the case here. However, to be on the safer side I shall give the inner walls of the chamber a coating of activated charcoal and yogurt.Once the chamber and the rim top were cleaned, I realized that the inner edge of the rim was uneven and the bowl was badly out of round. However, the outer edge of the rim was in pristine condition. I worked on the inner edge of the rim with a 220 grit sand paper. I realized that nicks to the inner edge were larger than anticipated and also the thin rim surface had some blackened surfaces. The uneven thickness of the rim was also an eye sore!! I addressed these issues by topping the rim on a 220 grit sand paper. This completely addressed the issues of nicks and blackened surface on the rim. Though the issue of uneven rim thickness was addressed to a great extent, the rim is slightly thinner on the right side in 4 o’clock direction. To maintain the profile of the stummel and not lose too much briar, I let it be. Now, it was the turn of the stummel to get cleaned up. I sand the stummel surface with a used piece of 220 grit sand paper and got rid of all the overflow of lava. I was careful around the stamping on the shank, lest I sand it off completely!I cleaned the internals of the mortise, shank extension, tenon chamber and the stem air way using hard bristled/ normal pipe cleaners and q-tips dipped in alcohol. I followed up the cleaning of the internals of the pipe by external cleaning of the stummel with a hard bristled toothbrush and undiluted Murphy’s oil soap. I wanted to highlight the grains seen on the stummel. To achieve this aim, I sand down the stummel and rim top using micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. The stummel now has a deep shine with grains popping out with magnificent contrast. I also sand the caramel colored aluminum extension with the micromesh pads to bring out the luster of the dark golden brown. I rub a small quantity of “Before and After Restoration Balm” in to briar and let it rest for a few minutes. The balm almost immediately works its magic and the briar now has a nice vibrant appearance. I further buff it with a horse hair shoe brush. Next, I worked on the stem. I sharpened the lip edges using a needle file. I sand the entire stem with 220 followed by 400 and 800 grit sand paper. This helps to reduce the sanding marks left behind by the more abrasive 220 grit paper. To bring a deep shine to the vulcanite stem, I went through the complete set of micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. I wiped the stem with alcohol after each pad and rubbed it down with Extra Virgin Olive oil. The pictures of the process and final results are shown below.To finish, I re-attach the stem with the stummel. I mount a cotton cloth buffing wheel on to my locally procured machine which is similar to a Dremel.  I set the speed at about half of the full power and applied White Diamond compound to the entire pipe. I wiped/ buffed the pipe with a soft cotton cloth to clear it of any leftover compound dust. I then mounted another cotton cloth wheel on to the polishing machine and applied several coats of carnauba wax. I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further. The last functional aspect which I addressed at this stage was the protection of the walls of the chamber against the possibility of a developing serious heat fissures. I mix activated charcoal and yogurt to a consistency which allows for an easy and even spread and evenly apply it on the inner walls and set it aside to dry out naturally. This coating helps in protecting the wall surface and assists in quicker formation of a cake.The completed pipe, with the dark brown hues of the stummel complemented by golden caramel colored aluminum extension and the Cumberland stem, looks lovely, fresh and vibrant. In fact, the finished pipe looks more beautiful and unique in person than in photographs!! The rarity, beauty and shape of this pipe make me feel fortunate to have inherited such unique pieces of pipe history…………… Cheers!! PS: While discussing this pipe with my guru and mentor, Mr. Steve, he remarked that this is only the second “ZEUS” that he has come across to this day, the first being in his personal collection!! And this comes from a gentleman who is working and collecting pipes for decades!!

This pipe was worked on at different place, both by Abha and self at different points in time and pictures were clicked on different backgrounds as available to us using different phone cameras! Hence there is a variation in the background and difference in picture quality. And I am still struggling and experimenting with best background and angles for taking photographs which will accentuate the beauty of the completed pipe!

Restoring a Beautiful “Edwards #712- L”


Blog by Paresh Deshpande

One of the first restorations that I had undertaken was an Edward’s # 784 quarter bent Zulu. It was a very clean pipe to begin with and only required cleaning and shining of the stem and the stummel. There was not a single fill on that pipe and the feel of the stummel in the hand, briar, the grains and the stem oozed superior quality. I really liked that Zulu. The next pipe on my work table is an Edward’s # 712-L. This large sized bent billiard has a fantastic heft to it and fills the palm nicely, and I do have fairly large hands!! There are two minute fills on this huge stummel but, nevertheless, it is one handsome and robust looking pipe!!

The stummel surface boasts of beautiful swirls of grains interspersed with bird’s eye along the sides of the stummel, while cross grains adorn the top and bottom of the shank extending to the back of the stummel. The left hand of the shank is stamped as “Edward’s” in cursive hand. The right side of the shank is stamped as “ALGERIAN BRIAR” in block letters over “712- L” which probably is the shape and the letter denoting the large size. The bottom of the shank bears “# 7” near the shank end which in all probability is the model number. The fancy stem bears no stampings.I searched pipedia.org for information and background of this brand and also attempt to date. I did not get the complete details that I was looking for, however the interesting information that I collected from this site was enough to convince me that the pipe I am currently working on is a no-push-over and can hold itself against some of the more known brands commanding a premium!! Here is the link to the information on pipedia.org (https://pipedia.org/wiki/Edward%27s).  For those who prefer immediate results without wasting time, here is an important piece of information from the website:-

“All of Edward’s pipes are Algerian Briar – a fact very few pipe companies can claim, and all are oil-cured utilizing natural finishes – no strange concoctions are used to interfere in your tastebud’s dance with the briar. Algerian, Calabrian, Sardinian, Corsican – take your pick, but Algerian Briar is generally considered the finest smoking briar ever used. When combined with oil-curing, Algerian takes on a magical quality that even Alfred Dunhill recognized as far back as 1918 as the choice for both his Bruyere and Shell.”  

I searched pipephil.eu in my attempt at dating this large handsome dude. Though I did not succeed in my endeavor, but I did get some interesting information like that Randy Wiley got his start at Edward’s!!!!!! Here is the link for those interested (http://www.pipephil.eu/logos/en/logo-e1.html). Even though this may not be a vintage pipe, but it definitely is of high quality and capable of holding itself up against some of the best in business!!!

INITIAL VISUAL INSPECTION
As I had noted earlier, this large bent billiard pipe was in great condition when I started restoring it. There were only two small fills on the shank, one on the left side near the bowl and shank joint and the other on the top surface of the shank, about an inch from the shank end. There is a small superficial chip in front of the bowl on the right side. The stummel is free of any spilled oils, tars or grime from the chamber. However, the briar is dull and lifeless and has taken on a layer of aged patina, through which one can make out the beautiful grains all round. This one should clean up nicely. The pipe appears to have been smoked a few times and there is a very thin layer of cake in the chamber. The chamber walls are nice and thick with no apparent damage. There is a minuscule amount of lava overflow on the rim surface. There are two small dents on the inner rim edge in 3 o’clock direction. The outer rim edge is slightly damaged in 12 o’clock direction, the result of likely being banged against a hard surface. The mortise is as clean as can be and the airflow through it is free and smooth. These issues should be a breeze to address. The vulcanite stem is without any bite marks or tooth chatter. There are small bite marks on the lower and upper lip edges. It is nice and dark, but not smooth. The roughness is due to oxidation of the top surface. These issues should not be a major headache to address. The tenon is clean and flow of air through the airway is full and smooth.THE PROCESS
I started this project by cleaning the chamber. Since there was a very thin layer of carbon, I used a 220 grit sand paper, pinched between my thumb and forefinger, to sand the inner walls of the chamber. Once I had reached the bare briar, I wiped the chamber with a cotton pad dipped in isopropyl alcohol. This removed all the residual carbon dust and also rid the chamber of all ghost smells. I worked on the inner edge of the rim and on the rim surface with a 220 grit sand paper. I realized that the nicks to the inner edge were larger than anticipated and also the rim surface had some blackened surfaces. I addressed these issues by topping the rim on a 220 grit sand paper. This addressed all the issues on the rim, including the damage to the outer edge of the rim.Now, it was the turn of the stummel to get cleaned up. Using a hard bristled tooth brush dipped in undiluted Murphy’s oil soap, I very deliberately scrubbed the stummel, cleaning the surface thoroughly. I cleaned the rim too. The stummel and rim top was dried using paper napkins and soft cotton cloth. I gouged out the old fills on the shank and the chipped portion on the front of the bowl with a pointed knife and wiped the area clean with a cotton swab dipped in isopropyl alcohol. I spot filled these with clear CA superglue and set it aside to cure. While the stummel was drying, I worked the stem. I sharpened the lip edges using a needle file. I sand the entire stem with 220 followed by 400 and 800 grit sand paper. This helps to reduce the sanding marks left behind by the more abrasive 220 grit paper. To bring a deep shine to the vulcanite stem, I went through the complete set of micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. I wiped the stem with alcohol after each pad and rubbed it down with Extra Virgin Olive oil. The internals of the stem was cleaned out using alcohol and pipe cleaners. The pictures of the process and final results are shown below. The fills on the stummel had cured. Using a 220 grit sand paper, pinched between my thumb and forefinger, I sand the fills and the entire stummel to match each other. I wanted to highlight the grains seen and further blend all the repairs carried out to the stummel. To achieve this aim, I sand down the stummel and rim top using micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. The stummel now has a deep shine with grains popping out with magnificent contrast. I rub a small quantity of “Before and After Restoration Balm” in to briar and let it rest for a few minutes. The balm almost immediately works its magic and the briar now has a nice vibrant appearance. I further buff it with a horse hair shoe brush. To finish, I re-attach the stem with the stummel. I mount a cotton cloth buffing wheel on to the Dremel (actually it is not the brand machine, but a local machine which is similar).  I set the speed at about half of the full power and applied White Diamond compound to the entire pipe. I wiped/ buffed the pipe with a soft cotton cloth to clear it of any leftover compound dust. I then mounted another cotton cloth wheel on to the polishing machine and applied several coats of carnauba wax. I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further. The completed pipe, with the dark brown hues of the stummel contrasting with the shiny black stem, looks lovely, fresh and vibrant; the photographs speak for themselves. The beauty, size and shape of this pipe compel me to wonder how anyone could let go of such a robust and beautiful looking pipe! If only the pipe could tell the story of its journey till date…………… Cheers!

Restoring my Inherited, Long Oval Shank “SON” ¼ Bent Pot


Blog by Paresh Deshpande

I had set my eyes on this pipe’s restoration for a long time, but was delayed for some reason or the other. Finally, it is now on my work table and I am looking forward to finishing this pipe. This is one of the two “SON” pipes from my inherited collection, the other being an un-smoked sandblasted bent brandy in its original sock.

The stummel boasts of lovely straight grains rising from the heel of the stummel towards the rim while the long oval shank displays beautiful cross grains all round. The heel of the stummel has some fabulous swirls interspersed with bird’s eye!!!! The pipe is stamped on the bottom of the long oval shank end as “SON” over “HAND MADE” over “DANMARK”. The long ¼ bent saddle stem is devoid of any stamping.During my previous two restorations of Nording pipes, I had searched the internet and had come to know about the association between Mr. Nording and Mr. Skovbo and the first pipes that they made together were named “SON”! After the split, Mr. Nording continued to make pipes under this name before changing the company name to “Nording” in mid 1960s. Here is the link for more detailed information and reading interest; https://pipedia.org/wiki/Nørding. You may also like to read the write up on rebornpipes.com for abridged details; https://rebornpipes.com/2017/12/06/breathing-new-life-into-a-son-freehand-an-early-nording-pipe/

From the above information, I can safely claim that this pipe was made during the 1960s.

INITIAL VISUAL INSPECTION
Most of the pipes in my grandfather’s collection show signs of heavy usage with heavy build up of cake in the chamber and overflow of lava over the rim. The stem is also generally in dire state. I have always thought that my grand old man believed in a “use and throw” policy! This pipe is no exception to this general observation.

The stummel is covered in oils, tars and grime to such an extent that the bowl is very dull to look at with all the grains hidden and the surface sticky to the touch. This will need a thorough cleaning. There are a number of dents, dings and chipped surfaces over the entire stummel. Whether to sand the bowl with micromesh pads to bring to fore the lovely grains will be decided later. The bowl is heavily caked and has large amounts of lava overflow on top of the rim. The internal condition of the bowl and rim will be ascertained only after the cake has been completely reamed out. There is always a fear of possibility of charred rim edges or burn fissures or charred briar inside the chamber of pipes in this condition. However, the entire stummel appears solid to touch from the outside reducing the probability of any of the above issues being present.The rim top has an inward slope towards the chamber and will make topping impossible without compromising the rim profile, should the need arise. The heavy overflow of lava over the rim top also hides any damages to the inner edge of the rim and also atop the rim surface. However significant damage, in terms of chipped surface, is seen to the outer edge of the rim on the right side in 3 o’clock position and minor dents are seen along the entire outer rim edge. This will have to be taken care of.When I took some close up pictures of the heel of the pipe, I thought I could see a very small and thin crack dead in the center of the heel. My fears were confirmed when I shared pictures of this with my mentor, Mr. Steve, and he concurred with my assumptions. The exact extent of the damage, whether it’s a through crack or just a superficial external crack, can only be known after the cake has been completely reamed back to bare briar. Addressing this issue will be a first for me on my journey!As expected from the condition of the pipe, both the mortise and stem airway is clogged and air flow is restricted.The long ¼ bent saddle stem is heavily oxidized with heavy tooth chatter on both surfaces near the button end. The oxidation is heavier about an inch from the lip. The edges of the lip are worn and will need to be reconstructed and reshaped.THE PROCESS
Since I had noticed a small hairline crack on the exterior surface at the bottom of the bowl, I wanted to investigate it further and that is where I start my restoration work. I ream the chamber with head size 2 of the PipNet reamer and progress to size 3 head. To smooth out the inner surface of the chamber and completely remove the last traces of remaining cake, I sand the inner surface of the chamber with a 220 grit sand paper. With a sharp knife, very gently I scrapped the surface of the rim top and removed the accumulated tars, oils and grime. I further clean the chamber with a cotton swab dipped in isopropyl alcohol.Once the chamber was cleaned, I was relieved that the hairline crack seen on the heel of the stummel was restricted to the external surface. However, the walls of the chamber have the markings of the beginning of burn out on the lower half of the chamber walls on the left, front and above the draught hole. I further sand the chamber walls with a 180 grit sand paper. With a fabricated thin and sharp knife, I gently remove all the charred briar from the walls and also from the bottom of the chamber. What was revealed really blew my sock away!!!! The extent of damage was something that I had not seen in 50 odd pipes that I have restored/refurbished to date. The gouges left behind were huge and the bottom surface was severely undulated. I shared these images with my Mr. Steve, who immediately responded and confirmed that the bottom had significantly thinned out and the walls have sustained significant damage. He suggested that the present condition necessitates coating with JB Weld to make it smokable and if that is not available, Plaster of Paris could be used as a substitute. But neither is available to me here in this remote area. I decided to proceed with further restoration while being on a look out for JB Weld! I clean out the mortise and the shank with a fabricated spatula, hard bristled and regular pipe cleaners dipped in isopropyl alcohol. To further clean and open out the drought hole, I had to use the shank cleaning tool of the KleenReem reamer. The amount of gunk, hardened oils and tars that was scooped out was astounding to say the least! After some efforts, I was finally able to clean out the mortise and airway of all the filth. The airflow is now open, full and free. Now, it was the stummel’s turn to be cleaned up. Using a hard bristled tooth brush dipped in undiluted Murphy’s oil soap, I very deliberately scrubbed all the stummel surfaces, cleaning them thoroughly. I cleaned the rim too. This cleaning and scrubbing revealed a new fissure/crack/fill towards the front of the bowl, on the left side. I checked the alignment of this crack with the heat fissures on the walls of the chamber as I feared a through burn out. Luckily, this fill was nowhere near the damaged portion of the chamber walls. The stummel and rim top was dried using paper napkins and soft cotton cloth. I set the stummel aside to dry out naturally. Next I decide to address the issue of damaged outer rim edge. I raised the chipped surface of the outer edge using the steaming method. I heat my fabricated knife and placing a wet Turkish hand towel over the damaged rim edge, placed the hot knife over it. The steam raised the chipped surface to a great extent. I followed the steaming process with sanding the entire stummel and shaping the rim outer edge with a 220 grit sand paper. I sand the rim surface and edge such that the profile of the inward slope of the rim top is maintained. It was a painstaking and time consuming process, but the end result was a smooth and even stummel, rim top and edges. I was very satisfied with the results of the effort. The superficial crack that was revealed on the front of the bowl after the cleaning of the stummel and the thin superficial crack seen on the heel of the stummel were addressed next. I gouged out the dead and dried briar from the crack with a thin and sharp knife, cleaned it with a cotton swab dipped in alcohol and filled it with clear CA superglue. There was a small nick on the right side of the shank end. This too was filled with superglue. Using a magnifying glass and a whitener pen, I marked the start, turning and end points along the extent of the crack. I next drilled holes using a 1mm drill bit (this was the smallest sized drill bit I could lay my hands on!!!) fitted on to my local Dremel machine, taking care that I did not drill a through and through hole. This helps in preventing further spreading/ progression of the existing crack. I cleaned the crack with a toothpick and spot filled clear CA superglue in to the drilled holes and over the crack. I set aside the stummel for the glue to cure. While the repairs to the stummel were curing, I addressed the repairs to the stem. Using a Bic lighter, I flamed both the surfaces of the stem. This helped in raising some of the tooth chatter and bite marks to the surface as vulcanite has a property to regain its original shape on heating. The high quality of the vulcanite ensured that maximum of tooth chatter was raised to the surface and what little remained, would be addressed subsequently during the sanding process. I used a 220 grit sand paper to sand out the oxidation. I used a flat head needle file to sharpen and reshape the lip edge and rubbed a little Extra Virgin Olive oil in to the stem surface. I wiped the stem again and worked on it with micromesh sanding pads – wet sanding it with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. Between each set of three pads I rubbed the stem down with extra Virgin Olive Oil and also gave it a final rubdown after the 12000 grit pad. I cleaned the stem airway with pipe cleaners dipped in isopropyl alcohol. I set the stem aside to dry while I worked on the bowl. I sand the fills on the stummel with a flat head needle file and further match these fills with the stummel surface by sanding it with a 220 grit sand paper. Once I am satisfied with the match, I progress to polishing the stummel with micromesh pads going through the entire cycle. Due to the light, natural hues of the briar, these fills are still visible, but overall, the pipe looks amazing. I intend to stain it with a darker shade, but as you guessed it right, I don’t have the material and wherewithal to carry out the staining. I rub a small quantity of “Before and After Restoration Balm” into briar with my fingers and let it rest for a few minutes. This balm enlivens and protects the briar. The balm almost immediately works its magic and the briar now has a nice vibrant appearance. I further buff it with a horse hair shoe brush. To finish, I re-attached the stem with the stummel. I mounted a cotton cloth buffing wheel on to the Dremel (actually it is not the brand machine, but a local machine which is similar).  I set the speed at about half of the full power and applied White Diamond compound to the entire pipe. I wiped/ buffed the pipe with a soft cotton cloth to clean it of any leftover compound dust. I then mounted another cotton cloth wheel on to the polishing machine and applied several coats of carnauba wax. I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further. The completed pipe looks lovely, fresh and vibrant; the photographs speak for themselves. Thank you for having the patience to reach this far while reading the write up. It is always heartening when I receive comments on the write up, good or bad, either way is encouraging, but the real happiness and maximum satisfaction is derived from knowing that someone has dedicated his/ her precious time in reading your write up. PS: There are two issues which are yet to be addressed; one is the coating of the chamber for protection of the walls (functional necessity) and the second is staining the stummel in darker hues (cosmetic necessity). I do not have necessary materials and equipment to carry out these works as I pursue this hobby as a non earning pursuit. But I am gradually and step by step purchasing the equipment and materials necessary for reaching the standards that I have set myself. I shall keep you updated on this beauty as and when I address both the above issues. Cheers and wish me luck!!

Restoring a Beat up “Mini Woodart” Pipe #856


Blog by Paresh Deshpande

The fourth and the last pipe that I worked on simultaneously was another pipe that I had purchased on eBay along with the Rolex vest pipe. I was attracted to its vase like shape and through all the dirt and grime some beautiful bird’s eye grains peeked and beckoned me for help. The shank end flares out and the chunky, short and broad, 1/4 bent saddle stem with a conical tenon end makes for a very interesting appearance to the overall pipe. The appearance of this beauty was beat, the rim appeared to be damaged and there were a few prominent fills which appeared like blistered wounds. But, nevertheless, it is one handsome, more like cute, looking pipe!!!!

The stummel surface boasted of beautiful swirls of grains interspersed with bird’s eye along the sides of the stummel and shank, while contrasting cross grains adorn the top and bottom of the shank extending to the back and bottom of the stummel. The left hand of the shank is stamped as “MINI” over “WOODART” over “FRANCE”. The bottom of the flared out shank end bears the model number “# 856”. The saddle top of the stem bears the logo of “W” in an oval. This stem logo was revealed later after the stem had been soaked in hydrogen peroxide solution.I could not find any information about this brand on Pipedia.com or rebornpipes or anywhere on the internet. However Pipephil.eu does make a mention of this brand and even has a picture of a pipe with similar stampings (http://www.pipephil.eu/logos/en/logo-w3.html#woodart), but no further information was available!

INITIAL VISUAL INSPECTION
As I had noted earlier, this little pipe was in a sorry and battered state. There is not a single surface on the stummel which does not have either a dent or a fill or a chipped surface. The stummel is covered in oils, tars, sticky grime and dust, through which one can make out the beautiful grains all round. The overflow of lava has not only covered the area between the narrow top portion and rest of the bowl, but has spilled over to the back of the bowl and accumulated in the area where the shank meets the bowl. There are a large number of dents, dings and scratches prominently seen on the edge below the neck of the vase like stummel shape. There are a few major fills in the stummel, the most prominent ones being to the right side on the shank. These will need to be addressed. The bowl is narrow and tapers down towards the draught hole. The chamber has a thin layer of cake, but the appearance indicates that there may be issues with the walls of the chamber. The mortise is full of oils, tars and gunk and restricts air flow. The rim top is where maximum damage is seen through the overflowing lava. The inner and outer edge of the rim is peppered with dings, dents and chips, a result of striking the rim edge against a hard surface while cleaning after a smoke. The bowl is completely out of round with undefined rim edges. This will have to be taken care of without losing too much of briar estate and will be a challenge to achieve desired results. The vulcanite stem is so heavily oxidized that it appears brown in color!!!! The upper surface of the stem has very light tooth chatter towards the button end while the lower surface has a few deep bite marks with damage to the lip edge. This issue should not be a major headache to address. The tenon is filled with oils and tars, restricting flow of air through the airway.THE PROCESS
I started this project by flaming both the surfaces of the stem with a Bic lighter to raise the tooth chatter and bite marks to the surface. I followed it by immersing the stem in to the solution of hydrogen peroxide and hot water. Within 20 minutes the stem color changed to greenish brown, a sign indicating that the oxidation has been pulled to the surface. This also revealed the stem logo of “W” encircled in an oval, on the top surface.After the oxidation was raised to the surface, I removed the stem and wiped it with paper napkins. I ran a couple of pipe cleaners through the airway to clean it. Once I was satisfied that the internals of the stem are clean, with a 180 grit paper, I sand the stem surface to get rid of the raised oxidation. I followed it by filling the deeper bite marks and lip damage with a mixture of activated charcoal and CA superglue and set it aside to cure. While the stem was curing, I worked on the stummel. The small size of the chamber dictated that I could only use my smaller sized fabricated knife to remove as much cake as possible. I further sand the chamber walls with a piece of 150 grit sand paper wound on a thin but dry bamboo twig (which are abundant in the jungles in this part of my country) attached with a rubber band. This was followed by 220 and 400 grit sand paper and now we have a smooth and even surface on the walls of the chamber. This process exposed the walls of the chamber and confirmed my initial apprehensions. The chamber walls show a number of heat fissures on both the front wall as well as above the draught hole. I shall address this issue at the end by coating the chamber wall with a mixture of activated charcoal and yogurt. I wiped the insides of the chamber with a cotton pad dipped in isopropyl alcohol. I cleaned the mortise using hard bristled and regular pipe cleaners, dental spatula and shank brush dipped in isopropyl alcohol. I continued with the cleaning of the chamber by giving it a salt and alcohol treatment. I packed the chamber, just below the rim, with cotton balls. I stretched a cotton ball into a thick wick, tapering at one end, and inserted it in to the shank and pushed it as far inside as I could using a straightened paper clip. I find that cotton balls work just fine in drawing out all the tars and smells from the mortise and the bowl. I topped the bowl with alcohol again after 20 minutes when the alcohol level had gone down and set it aside overnight for the cotton and alcohol to do its intended job. The next day, the cotton and alcohol had fulfilled its intended task. I removed the cotton balls and ran pipe cleaners through the mortise to clean out all the loosened tars and gunk. The internals of the stummel is now clean and fresh. I set the stummel aside to dry out. While the stummel was drying, I worked the stem. I covered the stamping on the stem with whitener using a whitener pen. The filling of charcoal and CA superglue had cured and using a needle file, I sand the filling to match the surface of the stem. For a better blending, I further sanded the entire stem with 220 followed by 400 and 800 grit sand paper. This helps to reduce the sanding marks left behind by the more abrasive 220 grit paper. To bring a deep shine to the vulcanite stem, I went through the complete set of micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. I wiped the stem with alcohol after each pad and rubbed it down with Extra Virgin Olive oil. The internals of the stem was cleaned out using alcohol and pipe cleaners. The finished stem is shown below. With a sharp, thin knife I removed the entire old and loosened fills and cleaned the surface with alcohol. These are now ready to take on a fresh fill. Now, it was the turn of the stummel to get cleaned up. Using a hard bristled tooth brush dipped in undiluted Murphy’s oil soap, I very deliberately scrubbed the stummel, cleaning the surface thoroughly. I cleaned the rim too. However, the grime, oils and tars covering the stummel and rim surface was so stubborn that I could not get rid of it completely.  The stummel and rim top was dried using paper napkins and soft cotton cloth. I mixed briar dust and CA superglue and filled all the major gashes while the minor ones were filled with clear CA superglue. I set the stummel aside to dry the filling.After the filling had dried out overnight, I sand the filling with a flat head needle file to match the surface of the stummel.Before sanding the entire stummel to match the fills and clean the stubborn grime, I decided to address the out of round and charred rim top by topping the rim top on a 220 grit sand paper. I was careful not to sand too much to maintain the original profile of the stummel. Topping also helped in reducing the dents and chipping to the outer edge of the rim. The rim top, after topping, looks much better.However, the inner edge profile was still uneven giving the bowl an out of round appearance. Also the outer rim edge had a few dents, chips and scratches. I addressed these issues by creating a bevel on the inner and outer edge of the rim. The results are pleasing to the eye.The issue of damaged rim was addressed to a great extent at this stage. However, the issue of addressing the large number of dent, dings and scratches prominently seen on the edge below the neck of the vase-like stummel shape still remains. I decided to reduce/ eliminate, if possible, these dents and dings by steaming them out. I heated my fabricated knife over the flame of a candle, placed a wet Turkish hand towel over the marked areas and steamed out the dents by placing the heated knife over the towel. Though some dents were still visible, these were greatly reduced when compared to before steaming.Thereafter began the arduous, painstaking and time consuming process of matching the repairs by sanding the entire stummel with 220 followed by 400 and 800 grit sand papers. I was able to match all the repairs and dents and dings on the lower edge of the stummel by upward sanding motion while moving up from heal and downward motions while moving down from the rim top. I was satisfied with the appearance of the stummel after this sanding. I wanted to highlight the grains seen and further blend all the repairs carried out to the stummel. To achieve this aim, I sand down the stummel and rim top using micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. The stummel now has a deep shine with grains popping out with magnificent contrast. I rub a small quantity of “Before and After Restoration Balm” in to briar and let it rest for a few minutes. The balm almost immediately works its magic and the briar now has a nice vibrant appearance. I further buff it with a horse hair shoe brush. To finish, I re-attach the stem with the stummel. I mount a cotton cloth buffing wheel on to the Dremel (actually it is not the brand machine, but a local machine which is similar).  I set the speed at about half of the full power and applied White Diamond compound to the entire pipe. I wiped/ buffed the pipe with a soft cotton cloth to clear it of any leftover compound dust. I then mounted another cotton cloth wheel on to the polishing machine and applied several coats of carnauba wax. I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further.The completed pipe looks lovely, fresh and vibrant; the photographs speak for themselves. The beauty, size and shape of this pipe compel me to wonder if this pipe could once have been nestled in the hands of a lovely lady in Paris. If only the pipe could tell the story of its journey till date…Cheers!! PS: – Once I had finished with all the buffing and polishing, only one issue remained to be addressed; heat fissures on the walls of the chamber. I coated the walls of the chamber with a mixture of activated charcoal and yogurt. Once dried, this will speed up the formation of cake and protect the chamber from a burn out.

Sprucing up a Sparingly Used “Rolex” Vest Pipe


Blog by Paresh Deshpande

The third pipe that I worked on simultaneously is a small folding “Rolex” vest or pocket pipe which I had purchased on eBay. I generally avoid making purchases on eBay as I am not sure as to what I shall land up with. I know there are all kinds of checks and balances on the site to prevent fraudulent transactions and various guarantees protecting the buyer, but still the fear of unknown prevents me from making purchases. However, in this case, I found the pipe interesting with the asking price to my liking and the seller had advertised it as rarely used and from the pictures, it appeared so. I decided to add it to my collection and made the purchase.

A long wait of 43 days followed and finally the pipe was received by my wife as I was away at my duty station. She immediately gave me a call to confirm receipt and sent me pictures of the pipe. She confirmed that the received pipe was indeed in excellent condition and would not require much work. This coming from her allayed all my fears about the overall transaction. A few months later, I went on some well earned leave and on return bought it with me to restore.

This round and flattened pipe has vertical thinly wired rustications running from the heel of pipe to the rim. The right side of the surface has a smooth surface in the center which bears the only stamping seen on this pipe. It is stamped as “ROLEX” over “BRUYERE” over “ITALY”. The bottom of the smooth surface has a stamp picturing a gnome. There is no other stamp on the stummel or the stem.I searched the internet for some information on this pipe and also on dating this pipe. I visited Pipedia and learnt that Rolex vest pipes were made by Brebbia of Italy. However, I hit a jackpot when I visited rebornpipes which really has a wealth of information on nearly every pipe ever made and served on a platter!!! It is here that I became aware that it is the picture of a gnome that adorns this pipe and that the gnome was the logo Brebbia used to put on its pipes from 1953 to 1956 (https://rebornpipes.com/2016/08/24/an-interesting-brebbia-silver-as1-square-shank-brandy/). Thus, is it possible to assume that this Rolex vest pipe was made between the years 1953 to 1956?????

INITIAL VISUAL INSPECTION
As is commonly seen on rusticated or sandblasted pipes, the crevices in these will be filled with dust, dirt, oils, tars and grime from all the years of smoking and storage. This Rolex vest pipe is no exception to this observation. The tight vertical rustications are filled with dust. The fact that the vertical rustications are dirty and filled with dirt is accentuated more due to a very dark reddish brown stain on the smooth patch on the stummel which bears all the stampings seen on this pipe. The briar is looking nice and a little TLC will further enhance its appeal.The bowl is oval and pinched at either end along the length of the pipe. The chamber is filled with a thin layer of cake which should make for an easy clean. However, the shape of the bowl and chamber will prevent the use of a regular pipe reamer. I would not be able to even sand it with a sand paper pinched between my fingers. Improvisations will have to be made to remove the cake build up. The short mortise is relatively clean and air flow is open and free. The rim top has the same thin wired rustications and is filled with dirt and dust. The inner and outer edge of the rim is in pristine condition with no dings or dents. The full bent vulcanite stem is so heavily oxidized that it appears greenish brown in color!!!! There are two major bite marks on the lower surface of the stem. The upper surface has a little debris stuck near the bottom of the lip. These issues should not be a major headache to address. The lip edge on both side is crisp and without any damage. The quality of vulcanite is good.THE PROCESS
As I had written in my write-up on John Bessai, I had learnt the use of Hydrogen Peroxide and hot water solution to raise the stem oxidation to the surface. Since I had decided to use this method, I had immersed stem of this pipe along with the stems of the John Bessai and Mini WoodArt pipes to make maximum use of the solution. Before I immersed this stem in the solution, I flamed both the surfaces of the stem with the flame of a Bic lighter. This helped in raising the deep bite marks on the lower side of the stem to the surface. The result of this flaming was so fantastic, that there were little or no traces of any tooth indentation on the lower and upper surface. This was followed by immersing the stem in to hydrogen peroxide solution. Within 20 minutes the stem color changed to greenish brown, a sign indicating that the oxidation has been pulled to the surface.I used a 180 grit sand paper to sand out the raised oxidation and rubbed a little Extra Virgin Olive oil in to the stem surface. I wiped the stem again and worked on it with micromesh sanding pads – wet sanding it with 1500-2400 grit pads and dry sanding with 3200-12000 grit pads. Between each set of three pads I rubbed the stem down with extra Virgin Olive Oil and also gave it a final rubdown after the 12000 grit pad. I set the stem aside to dry while I worked on the bowl. I cleaned the stem airway with pipe cleaners dipped in isopropyl alcohol. I removed the cake from the chamber by scraping it with my smaller sized fabricated knife. I found the chamber to be solid and without any heat fissures or cracks. To finish the chamber, I wound a piece of 150 grit sand on a thin but dry bamboo twig (which are abundant in the jungles in this part of my country) attached with a rubber band, and used it to sand the inner walls. This was followed by 220 and 400 grit sand paper and now we have a smooth and even surface on the walls of the chamber, ready for taking on a fresh layering of carbon cake!! This was followed by cleaning the short mortise with qtips, pipe cleaners and shank brush dipped in isopropyl alcohol. This further eliminated all the traces of old smells from previous usage.

Now, it was the turn of the stummel to get cleaned up. Using a hard bristled tooth brush dipped in undiluted Murphy’s oil soap, I very deliberately scrubbed through all the vertical rustications, cleaning them thoroughly. I cleaned the rim too. The stummel and rim top was dried using paper napkins and soft cotton cloth. I set the stummel aside to dry out naturally. I started work on the stummel which has dried by now. I rub a small quantity of “Before and After Restoration Balm” in to briar and let it rest for a few minutes. The balm almost immediately works its magic and the briar now has a nice vibrant appearance. I further buff it with a horse hair shoe brush. To finish, I re-attach the stem with the stummel. I mounted a cotton cloth buffing wheel to the Dremel (actually it is not the brand machine, but a local machine which is similar). I set the speed at about half of the full power and applied White Diamond compound to the entire pipe. I wiped/ buffed the pipe with a soft cotton cloth to clear it of any leftover compound dust. I then mounted another cotton cloth wheel on to the polishing machine and applied several coats of carnauba wax. I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further.The completed pipe looks lovely, fresh and vibrant; the photographs speak for themselves. Thank you for having the patience to reach this far while reading the write up.

Decking out my Grandfather’s Battered Pre-transition Barling # 1354.


Blog by Paresh Deshpande

In one of a first, I had decided to work on four pipes simultaneously. Well, honestly, it was a decision which was forced on me due to extraneous circumstances that I had created for me. It so happened that after having discussed with my mentor, Mr. Steve, I decided to work on a John Bessai creation from my Grandfather’s collection. As I was turning the John Bessai in my hands, I felt that there were not very many major issues involved in its restoration and the small Barling’s, also from my old man’s collection, appeared to be a straight slam dunk of a restoration. Thus, I decided to work on both simultaneously, which appeared doable. However, things turned in to a challenge when I was just surfing YouTube on pipe restoration topics. In one of the videos, Hydrogen Peroxide and water solution was used to raise the oxidation to the surface and subsequent cleaning of the same was a breeze. I decided to try out this method and in order to make max use of the solution; I dunked stems of two more pipes in to it. Now I have four pipes in line to restore. I can still manage the restorations; it is the write ups that are a huge challenge for me as Mr. Steve will vouch for the delayed submissions.

The Barling’s Make pipe on my work table is a quaint little billiards with beautiful and very tightly packed birdseye grains on either side of the bowl and shank, extending over to more than half of the front of the stummel. Equally tightly packed cross grains are seen on the front left and back of the bowl and also on the upper and bottom surface of the shank. It is stamped on the left side of the shank as “BARLING’S” in an arch with block capital letters over “MAKE” in a straight line over the numeral “1354”. The right side of the shank bears the spaced out stamp “S M” towards the bowl shank junction. The vulcanite saddle stem bears the trademark Barling stamped in cross on the upper surface of the saddle and “Barling” over “Design” in a cursive hand on the lower surface of the saddle.  Even though there are quite a few Barling’s in grandfather’s collection, this beauty is the first of the Barling’s that I am trying to restore. To know more about the brand, the lines offered by the maker and attempt to date this pipe, I visited Pipedia which has a wealth of neatly cataloged heading-wise information on Barling’s pipes. Here is the link and the snippets of relevant information that I picked up https://pipedia.org/wiki/Barling#Model_Numbers:

Model Numbers:

Also according to Tad Gage, the only four-digit number that denotes a Pre-Transition piece begins with “1,” which was used for pipes sold in England. Any other four-digit Barling pipe is a Transitional piece– (Tad Gage in P & T magazine).

Model numbers were occasionally stamped below the logo as early as the late 1920’s.

Other Nomenclature:

The “MADE IN ENGLAND.” stamp was in use in the 1930’s thru 1962. As with all things related to Barling nomenclature there are variations. Sometimes there is no “MADE IN ENGLAND.” stamp. Examples exist with a “MADE IN LONDON” over “ENGLAND” stamp. And, there are examples with “MADE IN ENGLAND” with no period after the word “ENGLAND”.

Size Stampings:

Up to 1926 and possibly beyond, Barling used specific, completely unrelated, model numbers to designate the various sizes of a specific shape. They produced pipes in three sizes, small, medium, and large.  

Barling’s published price lists show that they continued to offer pipes in only three sizes, small, medium, and large until 1941. That’s it, small, medium, and large. So when someone claims that they have a 1930’s EL, EXEL, or other size, they are mistaken.
In 1941 the published range of sizes expanded. Going from the smallest to the largest, they are SS, S, S-M, L, EL, EXEL, and EXEXEL. There is no “G” for giant. Giant pipes, or magnums, which are oversized standard billiards, were not stamped “G” but are commonly identified by collectors as such because they are obviously large relative to even EXEXEL pipes, and carried no size stampings (Gage).

Size stamps were rare before WW2, but we do an example from 1925 that we will discuss later as it is part of a forgotten class of Barling pipes.

Patent Stamps:

In addition to the stampings on the briar, Barling stems had stampings that relate to specific periods. In 1935 Barling received a patent for a stem design that radically improved airflow as well as cooling of the smoke.

Pipes made in 1934-5 may have the words “Reg’d Design” on the underside.

Following the granting of the patent in 1935, Barling stems featured the following patent numbers:

REG’D 98 046 – US patent number – 1936 – 1949 • REG’D 42/8968 – WW2 production – 1942 – 1950 • REG’D 754 068 – WW2 production • Barling Design – 1950 – 1962

 Not all pipes have this stamping on the underside of the stem, but its presence is a good indicator for the period of manufacture, assuming that the stem is original.

Throughout their history Barling continued to innovate in the area of stem and bit design.

From the above information, it is conclusively assumed that this piece is from the Family era/ Pre- transition period and was made somewhere during 1950s to 1960s. The minimalist stampings indicate that this pipe was intended to be sold in the local markets.

INITIAL VISUAL INSPECTION
The chamber shows a nice even build up of a thick cake which makes it difficult to comment on the condition of the inner walls of the chamber. There is a thick overflow of lava and completely covers the rim top and further spills over on to the stummel surface. The condition of the inner edge of the rim and rim surface will be ascertained only after chamber has been reamed down to its bare briar. The outer rim, however, is damaged and has a number of chips and dents, probably caused due to hitting the bowl against a hard surface to remove the dottle! Criminal, to say the least! The surface of the stummel is covered by the overflowing lava, which in turn has attracted a lot of dirt and grime over a period of time. The stummel surface is peppered with numerous dents and dings, more so towards the heel of the bowl, probably caused due to careless and uncared for storage for the last 40-45 years!!!! It will be a big decision whether to address these dents and dings by abrasive sanding method and loose the patina which has developed on the surface, or let them be. Well, I shall cross the bridge when I reach it. The mortise is surprisingly clean and air flow through it is open and full. The vulcanite stem is heavily scratched, but not oxidized. Some light tooth chatter is seen on both surfaces of the stem towards the lip with one deep bite mark on the upper surface. This issue should not be a major headache to address. The lip edge on both sides is crisp but lightly damage. The quality of vulcanite is good.THE PROCESS
I did not soak the stem of this pipe in the Hydrogen Peroxide solution as I was not sure how it would affect the stamping and so decided to play it safe. I flamed the stem surface of the stem with a Bic lighter to raise the tooth indentations and scratches on the stem. The heat from the flame of Bic lighter causes the vulcanite to expand and regain its natural shape, reducing the marks. The tooth bite marks which were visible after the flaming were filled with a mix of activated charcoal and clear CA superglue and I set it aside to cure overnight. I reamed the chamber with size 1 head of a PipNet reamer and followed it with a size 2 reamer head. To reach the areas where the PipNet reamer could not reach to remove the carbon cake, I used my smaller fabricated knife and scraped out all the remaining cake. I further use a folded piece of 180 grit sandpaper to sand out the last traces of remaining cake and expose the walls of the chamber to ascertain that there are no cracks/ heat fissures. I wiped the chamber with a cotton pad dipped in isopropyl alcohol to remove the carbon dust left behind by all the reaming and sanding process. The walls of the chamber were solid with no damage. I gently scraped the rim top surface with a sharp knife to remove the lava overflow. This was followed by cleaning the mortise with cue tips, pipe cleaners and shank brush dipped in isopropyl alcohol. This further eliminated traces of old smells from previous usage. The old smell was still prevalent, though greatly reduced. To completely eliminate the smell, I decided to resort to alcohol bath. I packed the chamber, just below the rim, with cotton balls. I stretched a cotton ball into a thick wick, tapering at one end, and inserted it in to the shank and pushed it as far inside as I could using a straightened paper clip. I topped the bowl with isopropyl alcohol using a syringe. I know that it is generally a practice to use Kosher salt for this procedure, but since Kosher salt is not easily available here, and when available, it’s very expensive, I use cotton balls. I find that cotton balls work just fine in drawing out all the tars and smells from the mortise and the bowl. I topped the bowl with alcohol again after 20 minutes when the alcohol level had gone down and set it aside overnight for the cotton and alcohol to do its intended job.The next day, the cotton and alcohol had fulfilled its intended task. I removed the cotton balls and ran pipe cleaners through the mortise to clean out all the loosened tars and gunk. The internals of the stummel is now clean and fresh. Now, it was the turn of the stummel to get cleaned up. Using a hard bristled tooth brush dipped in undiluted Murphy’s oil soap, I very deliberately scrubbed the surface of the stummel. I cleaned the rim too. The stummel and rim top was dried using paper napkins and soft cotton cloth. I am not very happy the way the rim top appears at this stage with all the charring and uneven inner and outer rim edges. This needs to be addressed. I set the stummel aside to dry out naturally. While the stummel was drying, I worked the stem. I covered the stampings on the stem with whitener using a whitener pen. The filling of charcoal and CA superglue had cured and using a needle file, I sand the filling to match the surface of the stem. For a better blending, I further sanded the entire stem with 220 followed by 400 and 800 grit sand paper. This helps to reduce the sanding marks left behind by the more abrasive 220 grit paper. To bring a deep shine to the vulcanite stem, I went through the complete set of micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. I wiped the stem with alcohol after each pad and rubbed it down with Extra Virgin Olive oil. The internals of the stem was cleaned out using alcohol and pipe cleaners. The finished stem is shown below. After cleaning the rim top with Murphy’s oil soap, I had observed that the rim top surface was charred and the inner edge was uneven, presenting a very sorry appearance. I topped the rim on a 220 grit sand paper, checking frequently till I was satisfied that the charred surface was greatly reduced. The inner edge is still uneven, though much better than before topping, it will need to be addressed.Next, I decided to address the dents and dings on the stummel surface and on the rim outer edge. Using a whitener pen, I marked all the major areas with dents and dings as I had decided to leave the minor ones as they were. I heated my fabricated knife over the flame of a candle, placed a wet Turkish hand towel over the marked areas and steamed out the dents by placing the heated knife over the towel. Though some dents were still observed, these were greatly reduced when compared to before steaming.The steaming method had raised to the surface all the major dents and dings. However, the outer and inner edges of the rim were still uneven. I took a piece of used and worn 180 grit sand paper, folded it and pinching it between my thumb and forefinger, created a slight inner bevel on the inner edge of the rim. Using the same technique, I created a light bevel on the outer edge. Now the rim surface and both its edges appear clean, even and well rounded.Steaming out the dents and dings from the stummel surface had necessitated that the surface of the stummel be evened out by sanding. I had an option of using more abrasive 220 grit sand paper followed by micromesh pad cycle and loose the patina or straight away go to the micromesh cycle. Using the more abrasive sand paper, minor dents and dings would be further addressed but I would lose the old sheen which the briar has taken over the years.  I decided on keeping the old sheen and went straight for the micromesh cycle. The old patina and the minor dents and dings would add to the vintage look of the pipe, which it was. I wet sand the stummel with 1500 to 2400 grit pads and follow it up by dry sanding with 3200 to 12000 grit pads. I rub a small quantity of “Before and After Restoration Balm” in to briar and let it rest for a few minutes. The balm almost immediately works its magic and the briar now has a nice vibrant appearance. I further buff it with a horse hair shoe brush. To finish, I re-attach the stem with the stummel. I mounted a cotton cloth buffing wheel to the Dremel (actually it is not the brand machine, but a local machine which is similar).  I set the speed at about half of the full power and applied White Diamond compound to the entire pipe. I wiped/ buffed the pipe with a soft cotton cloth to clear it of any leftover compound dust. I then mounted another cotton cloth wheel on to the polishing machine and applied several coats of carnauba wax. I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further.The completed pipe looks lovely, fresh and vibrant; the photographs in this case, do not do justice to the appearance of this beautiful little pipe. Thank you for having the patience to reach this far while reading the write up.

A Fresh Breath of Life for a Unique Creation by “John Bessai”


Blog by Paresh Deshpande

The next pipe that I decided to work on, and duly approved by Mr. Steve, is a pipe that was carved by an iconic pipe carver from USA who had carved pipes in the back room of his tobacco shop by hand. This pipe carver was lost to history, being marginalized and lost to the world, since his creations were in very small numbers and restricted to local sales only. This pipe carver is an integral part of American pipe making history and is now being revisited and revived by some experienced and knowledgeable pipe restorers and pipe collectors, notably Mr. Andrew Hross, who has carried out a detailed mapping of the pipe maker, his creations, dating his pipes based on stamping and pipe models. Mr. Steve has himself worked on a couple of these rare pipes and has included them in his personal collection!!!! Well, I think I have been able to rouse enough curiosity regarding this pipe carver in the minds of the reader and now to reveal the name……… The carver that I have been rambling about is John Bessai!!

Since having completed the restoration of an antique 1902-20’s era GBD with Albatross wing bone extension and horn stem from my Grandfather’s collection, I reverted back to Mr. Steve for selection of my next project. I have realized that he always suggests the most unique pipe, from the ones presented to him, for my next project and this time around he selected this John Bessai Rhodesian pipe with a suggestion that I should first read the blog on a couple of pipes from the same maker that he had previously worked on. I did exactly that and I realized that I have in my possession a rare and collectible pipe to work on.

This pipe has the classical Rhodesian shape with a cap which is differentiated from the rest of the stummel by a double ring. It has beautiful sandblast pattern all over the stummel and over the round shank, save for a small smooth portion on the right side of the shank which bears all the identification marks of this pipe, and on the rim top which looks amazing. It is stamped on the right side of the shank as “…BESSAI”, the initial part of the stamping is unclear, over bull’s eye symbol. The shank end is adorned by ½ inch hand rusticated Sterling silver band, which has developed a patina with age. It is stamped as “STERLING” in block capital letters, on the right side, in-line with the shank stampings. It would look classic once cleaned up. The stem is devoid of the trademark “JB” logo. Mr. Steve has researched this pipe maker and would make an interesting read for anyone, even remotely, interested in pipe history. Here is the link to his write ups: https://rebornpipes.com/2014/07/14/restemming-and-restoring-a-john-bessai-special-diamond-shank-bent-brandy/

This is the link to his second John Bessai project: https://rebornpipes.com/2012/08/21/reworking-a-john-bessai-pipe/

These write ups not only helped me in gaining knowledge about the pipe maker that John Bessai was, but also helped me know about dating the pipes that he had created. I have produced relevant extracts, though there is a wealth of information, from Mr. Steve’s write ups which include facts about dating as researched by Mr. Andrew Hross.

John Bessai was a long time pipemaker, repairman and tobacco shop owner who operated his pipe shop at the “Old Arcade” in Cleveland, Ohio. The shop was opened in approximately 1898. It was a small 2-room shop where he hand-crafted his own pipes in the back room and could work when customers were not there. Like so many other shop made brand, John Bessai’s limited production was quickly acquired by regular customers and thus his craftsmanship remained little known outside of Ohio and the Midwest. While his name is known by pipe collectors in the Midwest, his work is seldom seen elsewhere! He died before 1969. Nevertheless, John Bessai left behind a small number of classic shaped pipes; all were made on-site. They are praised worthy of collecting and reflecting skills well beyond most American pipe makers. John Bessai’s logo “JB” appeared as one letter as the “back” of the “J” and the “back” of the “B” share a single line. The logo was stamped on the stem and on the left side of the shank. His son Herb Bessai took over the business and also continued making pipes. He closed the shop in about 1978.

Pipes offered by John Bessai Pipe Clinic:
Most of the pipes that were offered by the John Bessai Pipe Clinic were fairly standard in shape… I would say most of the pipes Bessai offered were smooth pipes. My assessment would be 90% smooth and 10% rusticated / sandblasted…

Stampings and rough dating of John Bessai Pipe Clinic Pipes:
Which pipes did John make and which ones did Herb make/finish? All Bessai pipes carry his standard large JB stamp either on the stem or shank or both. Typically the JB on the stem is within a circle.

All pipes created by John Bessai’s hands reportedly contain the miniscule ‘jb’ stamp on the shank or body of the pipe. I have older pipes in my possession that do not contain this stamp (condenser, old stamps, etc) that were clearly shop made pipes. I feel he started using the tiny ‘jb’ stamp in the 50s to early 60s.

Dating / Circa era Bessai Pipes:
If the pipe carries a stamp stating Cleveland, O U.S.A. it’s considered an older production pipe (pre1960s). I’ve not seen any newer pipes with that stamp.

Bullseye stamping usually indicates an earlier pipe as that stamp seems to have been abandoned pre1960 as well.

Thus, from the above information, it is safe to suggest that the pipe presently on my work table is fairly rare as only 10% of the pipes made by John Bessai were rusticated or sandblasted and was made prior to 1950s as this one too does not have the famed “JB” stamp and bears the “Bull’s-eye” stamp on the shank.

INITIAL VISUAL INSPECTION
The bowl is nicely rounded and wide at the rim with a depth of about 1 1/5 inches. The chamber is so filled with cake that I am unable to reach the bottom of the bowl with my little finger. The build-up of the cake is more heavy on the bottom half of the bowl. The condition of the inner walls of the chamber can be commented upon after the cake has been taken down to the bare briar.The mortise is full of oils, tars and gunk and air flow is restricted. The rim top is also rusticated which can be seen through the overflowing lava. The inner and outer edge of the rim appears to be in pristine condition with no dings or dents. However, exact condition can be ascertained only after further cleaning. As is commonly seen on rusticated or sandblasted pipes with some serious age on them, the crevices in these are always filled with dust, dirt, oils, tars and grime from all the years of smoking and storage. This one is no exception to this observation. The grooves of the sandblast are filled with dust while the small smooth right side of the shank which bears the stamping is covered in dust and grime. The fact that the grooved patterns are dusty and filled with dirt is accentuated more due to a very dark reddish brown stain on the stummel and the shank. The briar is looking lifeless and bone dry and has taken on black hues. The twin bore, ¾ bent vulcanite stem is so heavily oxidized that it appears brown in color!! Some heavy tooth chatter is seen on both surfaces of the stem towards the lip with one deeper bite mark on the upper surface. This issue should not be a major headache to address. The lip edge on both sides is badly chewed off with heavy bite marks and would need to be reconstructed and reshaped. However, the quality of vulcanite is superior to other vulcanite stems that I have handled before.The hand rusticated sterling silver band has developed a patina due to oxidation. This will have to be addressed.

THE PROCESS
During one of my YouTube surfing sessions on pipe restoration techniques, I came across a video which showed the use of Hydrogen Peroxide and hot water solution as an alternate method to tackle oxidation on a vulcanite stem. I decided to adopt this method to tackle heavy oxidation seen on this stem. Before proceeding with this method to get rid of the oxidation, I wanted to raise the tooth chatter and bite marks to the surface. Using a Bic lighter, I flamed the surface of the stem. This helped in raising some of the tooth chatter and bite marks to the surface as vulcanite has a property to regain its original shape on heating. The remaining tooth chatter and bite marks would be addressed subsequently.I mixed Hydrogen Peroxide and hot water in the ratio of 1:2 in a plastic bowl and immersed the stem of this pipe along with two other stems of the pipes which are in line for restoration. Within two minutes, the color of the stem changed to a dirty greenish brown color indicating that the oxidation is being pulled to the surface. I removed the stems from this bath and scrubbed it clean with “MagiClean” sponge. I followed it up by cleaning the internals of the stem. I used 220 grit sandpaper to sand the stem and removed all the oxidation that was raised to the surface. This step further reduced the tooth chatter and bite marks present on the stem. I addressed the deeper tooth chatter and bite marks by filling them up with a mix of activated charcoal and CA superglue. I applied a slightly thick layer over the lip which I will later sand down to create a defined edge. Once I had applied the mix, I set it aside to cure overnight. While the stem filling was left aside for curing, I worked on the stummel by first reaming the chamber with size 2 of PipNet reamer head, followed by size 3 head. I further scraped the chamber walls with my fabricated knife to remove the remaining carbon deposits. Once the cake was reamed back to the bare briar, I used a 150 grit sand paper followed by 220 grit sand paper to remove all the traces of remaining cake and also to smooth the inner walls of the chamber surface. Finally, to remove the carbon dust, I wipe the chamber with a cotton pad wetted with isopropyl 99%. This was followed by cleaning the mortise with cue tips, pipe cleaners and shank brush dipped in isopropyl alcohol. This further eliminated traces of old smells from previous usage. However, I must admit that I was still not very happy with the internal cleaning of the stummel and shank. The old smell was still prevalent, though greatly reduced. To completely eliminate the smell, I decided to resort to alcohol bath. I packed the chamber, just below the rim, with cotton balls. I stretched a cotton ball into a thick wick, tapering at one end, and inserted it in to the shank and pushed it as far inside as I could, using a straightened paper clip. I topped the bowl with isopropyl alcohol using a syringe. I know that it is generally a practice to use Kosher salt for this procedure, but since Kosher salt is not easily available here, and when available, it’s very expensive, I use cotton balls. I find that cotton balls work just fine in drawing out all the tars and smells from the mortise and the bowl. I topped the bowl with alcohol again after 20 minutes when the alcohol level had gone down and set it aside overnight for the cotton and alcohol to do its intended job.The next day, the cotton and alcohol had fulfilled its intended task. I removed the cotton balls and ran pipe cleaners through the mortise to clean out all the loosened tars and gunk. The internals of the stummel is now clean and fresh. Now, it was the turn of the externals of the stummel to get cleaned up. Using a hard bristled tooth brush dipped in undiluted Murphy’s oil soap, I very deliberately scrubbed through all the grooves of the sandblast, cleaning them thoroughly. I cleaned the groove in between the cap ring with a sharp knife tip. The stummel was dried using paper napkins and soft cotton cloth. I set the stummel aside to dry out naturally. While the stummel was drying, I worked the stem. The fill had cured and with a flat head needle file, I worked on the filling till I had achieved a rough match with the surrounding surface. For a better blending, I further sand the entire stem with 220 followed by 600 and 1000 grit sand paper. This helps to reduce the scratch marks left behind by the more abrasive 220 grit paper. To bring a deep shine to the vulcanite stem, I went through the complete set of micromesh pads, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. I wiped the stem with alcohol after each pad and rubbed it down with Extra Virgin Olive oil. The finished stem is shown below. Once I was satisfied with the stem restoration, I started work on the stummel which had dried by now. When I had another look at the stummel after it had dried, I was not very pleased and satisfied with the way the rim top had cleaned up. I again cleaned it with Murphy’s oil soap and scotchbrite pad till the rim top was nice and clean. I rubbed a small quantity of “Before and After Restoration Balm” in to briar and let it rest for a few minutes. The balm almost immediately works its magic and the briar now has a nice vibrant appearance. The only surface on the stummel that remained to be spruced up was the Sterling silver band at the shank end. Abha, my wife, had suggested that I should try using Colgate toothpowder to bring back the shine on the Sterling silver band. She had tried this on her jewelry with amazing results. I rubbed the silver band with Colgate toothpowder and the results are truly amazing.I mounted a cotton cloth buffing wheel to the Dremel (actually it is not the brand machine, but a local machine which is similar).  I set the speed at about half of the full power and applied White Diamond compound to the entire pipe. I wiped/ buffed the pipe with a soft cotton cloth to clear it of any leftover compound dust. I then mounted another cotton cloth wheel on to the polishing machine and applied several coats of carnauba wax.I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further. The finished pipe is shown below. This is indeed a beautiful pipe which feels great to hold in your hand and the classy looks add to its overall appeal. I was wondering how my grandfather, who had never traveled to US, let alone to Ohio, ended up with one of John Bessai’s creations????? If only this pipe could recount and narrate its story from Ohio to India…Thank you for your read and as usual, any suggestions/ comments are always welcome. They help me progress on my journey into the pipe world.

The Challenge Continues… Restoring a Vintage Era GBD


Blog by Paresh Deshpande

As I had remarked earlier in my write up on the late 1850s era FIRST CHOQUIN, A METZ (https://rebornpipes.com/2018/11/17/a-challenging-restoration-of-vintage-era-first-choquin-a-metz/),I could not contain my curiosity to open the third, and the last, box of my inherited pipes. In addition to the regular collection of Barlings, Charatans,Comoys and other assorted collection, I came across two pipes which caught my fancy!!!!!

The pipe on the left bears a football stamp that reads “CHOQUIN” over “A METZ” and the one on the right side simply reads “GBD”  (there are other stampings on the silver ferrule, details of which will be highlighted when it comes up for restoration). Both of these pipes looked vintage and unique enough that I immediately Facetimed with Mr. Steve of rebornpipes. His admission that he is willing for a trade off with me for these two pipes was an indication enough for me to know and understand their uniqueness!!! Thus these two pipes moved to the top of my unorganized and chaotic list of restoration. 

Having now restored the CHOQUIN and experienced the challenges that these vintage pipes pose, I was faced with a dilemma of whether I should consider restoring the GBD or take a break and restore another unique and interesting pipe. Mr. Steve suggested the latter and hence I decided to undertake the restoration of the GBD amidst my hectic schedule.  

This GBD is a long and large pipe with a fairly large and deep smooth briar bowl and a steeply raking shank, the end of which is adorned by a sterling silver ferrule.The horn stem is connected with the shank by a long and hollow Albatross wing bone extension having sterling silver end caps at either end, most probably to strengthen it. The stem attaches itself to the wing bone extension by screw-in type tenon which is attached to this extension. The bowl is stamped on the left side of the shank as “GBD” in an oval encirclement and is the only stamping seen on the stummel. The Sterling silver ferrule at the shank end bears the oval stamp of “GBD” over “M R C LTD”,all in separate squares, over a rhombus which in all likelihood, enclosed the faded number “925” for Sterling silver. For its age, the stamping is crisp and clear.

The large bowl shows beautiful, densely packed birdseye grain on the right side and extending to the front of the bowl,while a combination of tightly packed straight and cross grain adorns the left side and back of the bowl. The shank on the bottom surface appears to be divided into two exact halves, the right side with closely packed birdseye while the left side has tight straight grains. These grains on either side of the shank extend neatly in a straight line to the front of the bowl dividing the grains in symmetrical equal halves.

I searched Pipedia for information on this brand and this model in particular. Even though I could neither find any pictures or mention of this particular pipe that I was working on, I did find some important snippets of information which helped me making an intelligent guess as to the vintage of the pipe. I have reproduced the information that I had gleaned from Pipedia:

A HISTORY OF GBD

In 1850 three gentlemen got together in Paristo establish a firm dedicated to the fabrication of Meerschaum pipes – a courageous step in politically restless times. Ganneval probably came from the area of Saint-Claude where he had learned making wooden pipes. Bondier’s family obviously came from Paris and had immigrated in 1789 to Geneva. He himself had worked as a wood turner in the clay and china pipe industry in and around Saint-Claude making stem extensions etc. Donninger was an Austrian or Swiss and had worked in Vienna, the world’s center of the Meerschaum pipe. They agreed on the acronym GBD selecting the initials of their surnames.

There is a very simple explanation for GBD’s program to turn more”British”: GBD became a British company soon after the turn of the century! In 1902 Marechal and Ruchon sold GBD to A. Oppenheimer & Co.in London.

The business relation to GBD in Paris began as early as 1870. Being the most important customer in the English speaking world, Oppenheimer & Co. were designated as sole distributor for Great Britain, the USA and Canada in 1897.Especially Adolphe Oppenheimer had a burning interest in the pipe business, and Louis’ son James Adler shared that. He should play the most important role in the amicable merger of GBD. A. Marechal, Ruchon and Cie. in Paris was now Marechal, Ruchon & Co. Ltd. (see Marechal Ruchon & Cie. page) – a British firm with four directors: Adolphe Oppenheimer and James Adler had their seat in the head office in London while Auguste Marechal and Ferdinand Ruchon went on leading the GBD factory in the Rue des Balkan in Paris, which was considerably extended and modernised. Ruchon acted as CEO.

Marechal Ruchon & Cie. was a company owned by Auguste Marechal and Ferdinand Ruchon (“& Cie” is the french equivalent of “& Co”) which owned the GBD brand from the end of the 19th century until 1902 when they sold Marechal, Ruchon & Cie. to Oppenheimer Pipe,which in turn changed the name of the company to Marechal, Ruchon & Co., Ltd. Upon the creation of Cadogan, however, the brand was no more, remembered only in the name of the GBD Marcee pipes made until just after the Second World War.

Cadogan Investments Limited is a subsidiary of A. Oppenheimer& Co. Limited. It was formed by Oppenheimer Pipe in 1920 as a holding company for its many recent acquisitions, including BBB,Loewe & Co.,two pipe factories in St. Claude and others. It continued to acquire pipe brands and makers for decades, adding GBD and others to their marquee.

It is from the last two paragraphs above, that I can judge that this pipe was made somewhere between 1902 and 1920!!!!!!

INITIAL VISUAL INSPECTION

The large, deep chamber shows a decent amount of cake build up with overflow of tars and tobacco oils on the surface of the rim top. The condition of the inner walls of the chamber will be ascertained once the cake has been reamed back to the bare briar. The inner and outer edges of the rim show a few odd minute dings. Once I have scraped the lava overflow from the rim top, I shall decide on the method to tackle them and may even decide to let them be. I do not envisage any major surprises inside the chamber as the bowl feels solid to the touch from outside.Air flow is laborious and constricted through the shank and will improve once the internals are cleaned.

The surface of the stummel is covered in oils and tars from the overflowing lava and is sticky to the touch. There are a few dings to the surface of the stummel, more particularly near heel of the bowl and bottom surface of the shank. Should I address them by sanding, I am not sure, as I fear losing the patina during the abrasive process of sanding with sandpaper.

While I was handling the stummel, I realized that the sterling silver ferrule at the shank end had come loose. I removed the ferrule and what was revealed turned my stomach inside out. The glue was hard and dry and the briar had totally dried out and the shank end opening was uneven. I could even make out one small crack running down from the lip of the shank opening. Talk about challenges!!!! This will have to be addressed without fail.

The Albatross wing bone extension is dirty and covered in dirt and grime. There are two superficial cracks on either side near the shank end. I        know these cracks are superficial as the bone surface around it is solid and without any give. These cracks will have to be addressed. The sterling silver end cap towards the tenon end has a flared out rim which is uneven. This causes the bone stem to sit unevenly on the rim. Air flow through the shank extension is clean and full.

The horn stem shows some minor tooth chatter on both the top and underside, but more prominently on the top surface. This should be taken care of by sanding with a 220 or higher grade sand paper. All in all, the stem appears to be pretty solid. The edge of the lip on both upper and lower surface is slightly damaged and will need to be sharpened. Air flow through the stem is open and full.

The sterling silver ferrule and bone shank end caps are deeply oxidized and show the patina normal for its age. Once they are cleaned and shining they will add a class to this pipe.

THE PROCESS

I started the process of restoration by reaming the chamber with size two of the PipNet reamer head and progressing through to size three. I followed up the reaming with scraping the remnants of the cake from the walls of the chamber and the rim top surface with my fabricated knife.Once the cake was reamed back to the bare briar, I used a 150 grit sand paper followed by 220 grit sand paper to remove all the traces of remaining cake and also to smooth the inner walls of the chamber surface. Finally, to remove the carbon dust, I wiped the chamber with a cotton pad wetted with isopropyl 99%. I gently scraped the rim top surface with a sharp knife. Removing all the cake from the chamber and rim top revealed that firstly, the rim was well rounded with no charring and only a minor chip and secondly, as I had anticipated,there was no damage to the inner walls of the chamber.

With 220 grit sand paper, I cleaned the internal and the external surfaces of the shank end opening, which until now was covered by the sterling silver ferrule, to remove all the carbon build-up, oils, tars,grime, dried briar wood and the dried glue. This process results in even more dried briar crumbling off, leaving behind a gaping hole. This needed to be restored as the damage is to that portion which supports the Albatross wing bone extension where it sits in to the shank. I conferred with Mr. Steve and it was decided to reconstruct the damaged portion by layering the gap with superglue and briar dust as the glue hardened immediately on coming in contact with the briar dust.

Before beginning the reconstruction of the broken shank end, I cleaned the internals of the shank, using hard bristled and regular pipe cleaners, q-tips, shank brushes, all generously dipped in isopropyl alcohol. The pipe cleaners would not pass through the mortise airway and the draught hole and so had to resort to more invasive methods. I straightened a paper clip and curving it, probed the insides of the mortise and the airway. After some efforts, I was able to dislodge the block. I scraped the inner walls of the mortise with a fabricated dental spatula. I gave a final cleaning with pipe cleaners dipped in isopropyl alcohol till the pipe cleaners came out, well, clean!!!  The heap of pipe cleaners and q-tips that are seen in these pictures are just the proverbial tip of the iceberg. I must have gone through an entire packet of 50 of both types of pipe cleaners, in addition to the q-tips and brush cleaning!!!!!

I, thereafter, began the process of reconstructing the broken portion of the shank end. I folded a pipe cleaner to fit snugly in to the opening of the shank end. Once I was satisfied with the fit, I smeared the pipe cleaner with Vaseline jelly and inserted it in to the opening.I applied first layer of superglue and pressed a little briar dust over it and let it set for a few minutes. This is followed by another layering and continued this process till I was satisfied with the reconstruction. I set the stummel aside overnight for the reconstruction to cure.

As the shank end reconstruction was curing, I initiated the repair and clean up of the Albatross wing bone extension and the horn bone stem. I cleaned the internals of the wing bone extension and the horn stem with bristled and normal pipe cleaners dipped in isopropyl alcohol.Once the internals were clean, I cleaned the external surface of the extension with cotton swabs dipped in Acetone and finely applied superglue over the superficial crack. This was done primarily to stabilize, strengthen and prevent further spreading of the superficial crack and obviate any chances of air escaping from these cracks in future. I set the wing bone extension to cure overnight along with the shank end repair.

As I had remarked during my initial visual inspection, I felt that the tooth chatter on the lower and upper surface of the horn bone stem should be taken care with sanding it down with a 220 grit sandpaper. How wrong was I! After sanding the upper and lower surfaces of the horn stem, I realized that the tooth chatter was deeper than I had anticipated and would have to be addressed with a fill of clear superglue. And so I filled these tooth chatters with superglue and the stem too joined the ranks of the shank end repair and wing bone extension on the rack for curing overnight.

The next evening, after a hectic and tiring day in office, I decided to work on the shank end reconstruction. I filed the external repaired area with a flat head needle file and carefully matched the profile of the fill with that of the surrounding area so as not to adversely affect the fit of the ferrule at a later stage. I frequently checked the progress by fitting the ferrule over the shank end. I achieved a perfect profile match by sanding the shank end with a used 150 grit sand paper. Once the external profile was matched, I worked on the internal adjustment of the reconstruction to match the seating of the wing bone extension in to the mortise using a round needle file. I frequently checked the seating of the extension in to the mortise and making necessary adjustments by filing till I was able to achieve a perfect fit. To be honest, it was not as easy as it appears while reading it.The amount of time and concentration required cannot be described in words.

Staying on the stummel restoration, I cleaned the external surface of the stummel and the rim top surface with undiluted Murphy’s oil soap and a hard bristled toothbrush and rinsed it under running tap water, taking care that water does not enter the chamber and the mortise. I dried the stummel using paper towels and soft, absorbent cotton cloth and set it aside to dry out naturally. The beautiful grain really stands out at this stage with the symmetrical division of grains on the lower surface of the shank, more distinct and clear. It is easily one of the best grained pipes that I have in my collection. Somehow, I was not satisfied with the way the rim top surface had cleaned up and I again sought the advice of my mentor, Mr. Steve, and received his reply, in his peculiar style, as “I would”, that’s all he had remarked!!!!!!

And so my initial plan for not topping the rim top was shelved and I decided to carefully top the rim surface. This would also help to address the one single chip on the rim’s top surface and also to remove traces of lava overflow. I topped the rim surface with 220 grit sand paper.Though it is recommended to have a wooden board with the 220 grit sand paper firmly fixed over it, I just keep the sand paper on a flat table top, holding it firmly with my left hand and rotating the stummel rim top over it with my right hand. I have come to realize that this set up gives me lot more freedom of movement, better control and convenience of storage. The single chip was addressed to a great extent, but was still an eye sore. Using a folded 150 grits and paper pinched between my thumb and forefinger, I created a very light bevel to mask the chip. Though the bevel is not easily discernible, it helped address the issue of the chipped rim inner edge.

I followed it up by micromesh polishing pads,wet sanding with 1500 to 2400 grit pads. Again, I wiped the bowl with a moist cotton cloth after each pad. I used the 3200 to 12000 grit pads to dry sand the stummel to a nice shine. It was at this stage that DISASTER struck!!!!! The stummel slipped from hands and crashed to the ground, shattering the reconstructed shank end and sustain a big ding to the heel of the stummel. Oh my!!! What agony it would be to reconstruct,re-profile the exterior and readjust the seating of the extension in to the mortise. But at this stage of restoration, I was left with no recourse but to reconstruct.

 This time around, I slightly tweaked the process. I wound a cotton rag around the complete stummel, less area to be repaired, so that the glue and briar dust does not spill over rest of the stummel and create more work for me. I completely sanded the earlier reconstructed portion and applied a layer of superglue and let it cure for a few minutes. Once the glue had hardened, I applied second layer of super glue and pressed some briar dust over it. I repeated this process of layering till I had achieved a matching top surface. I applied a final layer of superglue over the complete reconstruction and set it aside to cure overnight.

The next evening, I worked on the wing bone extension and the horn stem. I sanded the fills on the shank extension and the stem with a 220 grit sand paper. I sharpened the edges on the lip with the help of a flat head needle file and a folded piece of 220 grit sand paper. When the fills were matched with rest of the surface, I progressed to micromesh polishing, wet sanding with 1500 to 2400 grit pads and dry sanding with 3200 to 12000 grit pads. I wiped the shank extension and the stem with a moist cloth after every pad and rubbed a little extra virgin olive oil on the surface after every three pads. The Albatross wing bone extension and the horn stem is nice, smooth and clean. The wing bone extension has retained its natural coloration and there is nothing one can do anything about it. I finished the restoration of the wing bone extension by polishing the sterling silver end caps with cigar ash. At this stage, the entire assembly of the extension and screw-in type of bone stem looks beautiful, smooth, shiny and classic. I call it a day and decide to work on the stummel the next evening.

I start work on the stummel by filing the external surface with a flat head needle file and go through the entire process described earlier to match the exterior and internal surface with the sterling silver ferrule and seating of the Albatross wing bone extension respectively. I was extra careful this time around while working the stummel. You may find it amusing, but I sat on my double bed while I worked on the stummel!!!! Such a fright this incident had caused.

Then there was the issue of a dent near the heel in the stummel surface. Mr. Steve suggested adopting the steaming method to address this dent. Though theoretically I was well conversed with this method, I had never attempted it before and now to attempt it on a pipe of such vintage, beauty and value, had me in doubts. Added to this, I did not have any electric iron in my room as all the laundry, including ironing, is done by the washer man (I do enjoy certain privileges that come at my seniority in my organization). But seeing no other way out, I decided to give it a go. I improvised a bit and heated my trusted fabricated knife on a candle flame, soaked a thick Turkish hand towel and placed it on the dent. When I felt that the knife was sufficiently hot (well, I got it nicely hot!!!), placed it over the hand towel and over the dent. When there was a nice sizzling sound and a thick whiff of steam, I immediately removed the knife away from the surface and with a thumping heart, removed the hand towel to inspect the results, and boy was I pleased!!! The dent was reduced to nothing with the briar expanding nicely to lift the dent due to the steam, but it did leave behind a stark discoloration around the area. After a brief discussion with Mr. Steve and exchange of pictures, he suggested to rub some ‘Before and After’ balm in to the affected area to see if this would help in addressing the issue. Fortunately, it did!!!!Since I had attempted this steaming method for the first time, I was too preoccupied and missed out on taking pictures, my sincere apology to all those who were looking forward to these pictures.

To match the repaired surface with the rest of the stummel, I went through the complete micromesh polish cycle again.

At the end of 12000 grit pad, I rubbed a little quantity of ‘Before and After’ restoration balm in to the stummel with my fingers and set it aside for 10-15 minutes while I polished the sterling silver ferrule. The transformation in the briar is amazing to say the least!!!!! I buffed the stummel with a soft cotton cloth. I finish this stage of restoration by re-attaching the nicely polished and shining sterling silver ferrule over the shank end using super glue.

To finish the restoration, I mounted a cotton cloth buffing wheel to the Dremel (actually it is not the brand machine, but a local machine which is similar).  I set the speed at about 40% full power and applied White Diamond compound to the entire pipe.  Afterwards, I wiped/buffed the pipe with a soft cotton cloth to clear it of any leftover compound dust. I then mounted another cotton cloth wheel to the polishing machine,maintaining 40% speed and applied several coats of carnauba wax.

I finished the restoration by giving the entire pipe a rigorous hand buffing using a microfiber cloth to raise the shine further. The completed pipe looks lovely, fresh and vibrant. Thank you for having the patience to reach this far while reading the write up. Your comments are of utmost importance to me for improving my skills in restoration process as well as writing about it. Cheers!!!

PS. During the journey of restoring this beauty, my Guru and mentor, Mr. Steve was always around with his words of wisdom and encouragement to egg me on towards completing this project. It felt like he was holding my hand and helping me take my first baby steps around towards completing this restoration. Thank you once again, Mr. Steve.