Daily Archives: January 11, 2026

Repairing and Restoring a Charatan’s Make Executive Extra Large Dublin


by Steve Laug

The next pipe on the table is another one that came to us from the seller in Caldwell, Idaho, USA on 07/12/2025. It is a large Dublin bowl with a lip on the front. There is a large scar on the left side of the bowl. I would need to examine it and see the details of the problem. It is in dirty but in good condition other than that as can be seen in the photos below. The sides of the shank are clearly stamped and readable. The left side is stamped Charatan’s Make [over] London.England [over] Executive. To the left of the stamping it had a cursive L in a circle that tells me that the pipe is a Lane era pipe. On the right side it is stamped Extra Large in script [over] Made by Hand. That helps to date this to the time after the patent was filed in 1970.The stamping is clear and readable. It has rugged rusticated finish that is very tactile on both the shank and the bowl. The shape works very well with the grain. The finish was dusty and dirty with grime deep in the finish but grain really stands out. The bowl had a moderate cake and there was tobacco debris in the bowl. The rim top had a lava coat on the rim top and edges. The Double Comfort vulcanite stem is lightly oxidized and has tooth marks and dents on the top and underside of the stem. There is a faint CP stamping on the left side of the stem and on the right is stamped REG.NO. 203573. I took photos of the pipe to show what it looked like before I started working on it. I took a closer photo of the rim top and bowl to show the condition of the bowl and rim. You can see the light cake in the bowl and the darkening and lava on the top and damage to the inner edge.The stamping on the sides of the shank is clear and readable as noted above. I took a photo of the pipe with the stem removed to give a sense of the proportions of the pipe. Even with the deep gouge in the left side of the bowl it is a real beauty. To try and figure out the era of the Charatan’s pipe I was working on I turned to the pipephil website on Logos and Stampings. There is some really helpful information on each of the lines of Charatan’s Make pipes that entered the market. Here is the link to the section of the site that I turned to, http://www.pipephil.eu/logos/en/logo-charatan.html. There is an alphabetical listing of the lines including the Executive. The site did give a short history of the brand. I quote the portion that is most pertinent.The brand was founded in 1863 by Frederik Charatan. When his father retired in 1910, Reuben Charatan took over the family business. All the pipes were handmade until 1973. The brand name has been overtaken by Dunhill in 1978 and sold in 1988 to James B. Russell Inc. (NJ, USA). During the period 1988-2002 Charatans were crafted by Butz Choquin in St Claude (France). Dunhill re-purchased Charatan brand name in 2002 and Colin Fromm (Invicta Briars, Castleford) followed up on freehand production.

I turned to Pipedia to see if I could find more information on the brand and possibly a link to the Executive line (https://pipedia.org/wiki/Charatan) but once again in the general article it was not listed.  It did give a little more historical information and is worth reading. I am including a few sections from the site.

In 1863 Frederick Charatan, a Russian/Jewish immigrant, opened a shop in Mansell Street, located in the borough of Tower Hamlets, London E1, where he began to carve Meerschaum pipes. These pipes got very popular soon, and thus Charatan moved to a bigger workshop in Prescot Street, just around the corner. Here he began to make briar pipes which should make the name famous the world over. Charatan was the first brand to make entirely hand-made briars from the rough block to the finished pipe including the stems. The nomenclature “Charatan’s Make” refers to this method of production and was meant to differ Charatan from other brands who “assembled” pipes from pre-drilled bowls and delivered mouthpieces.

Being the undisputed No. 1 in English pipemaking, Charatan was approached by Alfred Dunhill who was unsatisfied with the quality of the pipes he imported from France. During 1908 – 1910 Dunhill bought pipes from Charatan paying exorbitant prices to ensure he had some of the very best pipes for sale in England. In 1910 he lured away Joel Sasieni, one of Charatan’s best carvers, and opened his own small pipe workshop on 28 Duke Street. On the retirement of his father in 1910 Reuben Charatan took over the family business…

…The pre-Lane period (prior to 1955) and the Lane era pipes (1955 to until sometime between 1979 – 1984) are of primary interest the collector. The Lane era is often quoted as beginning about 1950… Charatan records are almost non-existent before Lane due to a factory fire, making it difficult to date pre-Lane pipes. Charatan used 4 basic grades prior to 1950: Supreme, Selected, Executive, and Belvedere. After 1950 Herman Lane’s influence began, and the grades started to expand. In 1955 Lane took over sole distributorship of Charatan in the US. In 1957 he introduced the Supreme S. Most of his other introductions were from the 60’s and early 70’s…

The section called Miscellaneous Notes had some interesting information.

Charatan records indicate the DC (Double Comfort) bit was introduced in the 50’s, but some report seeing them in earlier production. Still others indicate they were introduced by Lane in 1960. Regardless, the DC bit is not an accurate way to date a pipe because many Charatan’s were made with regular and saddle type bits throughout the “Lane Era”…

…The Lane Trademark serif and circled L indicates the pipe is from the “Lane Era” (approx. 1955 to 1979 -1984?), however it appears that both the English factory or Lane themselves sometimes, or perhaps even often forget to stamp the L on a pipe. The Charatan factory was known for inconsistencies, especially in stampings. Therefore, although an L on the pipe definitely defines it as a Lane Era pipe, the lack of it could simply mean the pipe missed receiving the stamp from the factory. The lack of the trademark could also mean the pipe was destined for the European market.

…Generally, when the pipe is stamped with the BLOCK letters “MADE BY HAND” it means the pipe was probably made between 1958 and 1965”

Generally, block letters “MADE BY HAND” and some of the other nomenclature in script (i.e. City of London or Extra Large next to the MADE BY HAND) means the pipe was made sometime between 1965 and the mid 1970’s. The total script nomenclature “Made by Hand in City of London” evolved over this period of time, so many pipes had variants, such as Made By Hand in block letters and City of London in script, or some other variation of the terms or stampings. The Charatan Logo (CP) on the pipe bit was changed over the years.

From all of the historical data I could work through this Charatan’s Make Executive was one of the higher grade pipe from the mid 1970’s Lane era. I continued digging further into the dating of the pipe, but what I had found was a good start for me. If some of you would like to try your hand at dating it more accurately as to the time period it came out you might want to check out the article on Pipedia on Dating Charatans (https://pipedia.org/wiki/Dating_of_Charatans). I had enough for me to start working on the pipe itself and see what lay beneath the heavy tars and oils.

I began working on the pipe by addressing the deep gouge in the left side of the bowl. The first picture shows the gouge in the bowl side. It is quite deep and could easily be hiding a crack in the bowl side. I wiped the damaged area down with alcohol on a cotton pad. I filled in the gouge with clear CA glue. I pressed briar dust into the super glue and let it dry. I used a wooden sphere and 220 grit sandpaper to clean up the inner edge of the bowl and the rim top. I used a folded piece of 220 grit sandpaper to remove the darkening on the inner edge of the bowl. I sanded the repaired side of the bowl with 220 grit sandpaper to smooth out the repair. I used a Cherry Stain Pen to restain the sanded area of the bowl side. I reamed the bowl with a PipNet reamer. I used the third and fourth cutting heads to clean out the cake. I cleaned up what remained in the bowl with a Savinelli Fitsall Pipe Knife and scraped it back to bare briar. I finished by sanding the inside of the bowl with a dowel wrapped in sandpaper. The inside walls are free of burn damage or checking so the gouge does not go all the way through. I cleaned out the inside of the shank and the airway in the stem with alcohol, cotton swabs and both bristle and regular pipe cleaners.I scrubbed the bowl and shank with a tooth brush and some undiluted Murphy’s Oil Soap. I rinsed it off with warm water to remove the dust and soap from the finish. I dried it off with a soft cloth and it looked much better. I sanded the bowl with 320 – 3500 grit 2×2 inch sanding pads and wiped it down after each sanding pad with a damp cloth to remove the sanding debris. I polished the bowl with 1500-12000 grit micromesh sanding pads. I wiped the bowl down with a damp cloth to remove the dust and debris. The pipe began to look very good. The gouge in the bowl was repaired and looked better. I rubbed the briar down with Before & After Restoration Balm. I worked it into the briar with my fingertips to work it into the finish. The product works to clean, enliven and preserve the briar. I let it sit for 10 minutes then I buffed it with a cotton cloth to deepen the shine. The briar really comes alive with the balm. I set the bowl aside and turned my attention to the stem. I ‘painted’ the surface of the stem with the flame of a lighter to lift the tooth marks. I was able to lift almost all of them. I sanded the surface of the stem with a folded piece of 220 grit sandpaper to clean up the oxidation and tooth chatter on both sides. I sanded the stem with 320-3500 grit 2×2 inch pads to further adjust the fit of the stem to the shank. I wiped the stem down with an Obsidian Oil cloth after each sanding pad.I polished the vulcanite with micromesh sanding pads – 1500-12000 grit pads. I wiped it down with Obsidian Oil after each sanding pad. I used Before & After Pipe Polish – both Fine and Extra Fine to further polish the stem. With the stem polished I put it back on the Charatan’s Make Executive Extra Large Made by Hand Lane Era Dublin and lightly buffed the bowl with Blue Diamond. I buffed the stem with a more aggressive buff of Blue Diamond. I gave the bowl several coats of Conservator’s Wax and the stem several coats of carnauba wax and buffed the pipe with a clean buffing pad to raise the shine. I hand buffed it with a microfiber cloth to deepen the shine. The repaired gouge looked better but now looks like a fine line across the bowl side. The pipe polished up pretty nicely. The finished pipe is shown in the photos below. This Charatan’s Make Executive Extra Large Dublin will soon be on the rebornpipes store in the British Pipe Makers Section if you want to add it to your rack. The dimensions are Length: 6 inches, Height: 2 inches, Outside diameter of the bowl: 1 ½ inches, Chamber diameter: 1 inch. Thanks for walking through the restoration with me as I worked over this Charatan’s Make.

Cracking the Mystery of an Alluring Gourd Calabash


by Kenneth Lieblich

This is a wonderful gourd calabash with a long history, and I hope that one of you will fall in love with it. There is an elegance to the lines of this pipe, with its swan-like curves. It is a classic, and looks (and feels) satisfying in one’s hand. It had been well-loved by its previous owner, and understandably so. This calabash hid a big secret and it was my job to uncover and repair it. Sometimes I bite off more than I can chew and this might be one of those times. Maybe this should have been called Kenneth’s Krazy Kalabash Kure. No markings at all on this pipe, but no matter. Let’s take a closer look at it. The gourd has a deep, rich colour that I really like. The size is really pleasing too. It is more modestly sized than most calabashes – and that’s a positive. I bought this pipe in an auction and, because the auction was away from my home, I didn’t get to inspect the pipe closely beforehand. Boy, was I in for a surprise! The pipe was in dirty but decent condition. The vulcanite stem had quite a bit of wear: lots of tooth marks, oxidation, calcification, etc. The acrylic shank extension was dirty, but otherwise fine. The gourd, similarly, was dirty, but in good shape. BUT, as soon as I removed the meerschaum bowl from the gourd, I saw the problem. At some point in the past, the bowl had cracked in half: northern and southern hemispheres, if you like. That’s a big deal! This was a tough repair, but I am pleased with the results and the pipe is good to go now.As the photo above shows, the bottom part of the bowl was embedded into the gourd. I gave a preliminary and somewhat half-hearted attempt to pry it out with a dental tool. That didn’t work and it’s probably just as well. In attempting to pry it out, I was quite concerned about either cracking the gourd or cracking the bowl further – or both. I ended up heating the gourd and bowl with my heat gun – hoping that ancient tars were holding it in place. And that did the trick: I was able to extract the bottom bowl chunk (plus a few fragments) safely from the gourd without causing further damage to either. You can see the results below.At this point, I figured that I would restore the stem while I thought about what to do with the bowl. I used a disposable lighter and ‘painted’ the stem with its flame. The gentle heat of the flame can cause the dents in the vulcanite of the stem to expand back into shape. In this case, some improvement occurred – but not a lot. The stem’s calcification was quite substantial. I used an old butter knife and gently scraped some of the thicker accretion off. Doing this now helps later in removing the oxidation. I used isopropyl alcohol on a few cotton rounds and wiped down the stem to provide an initial cleaning of filth before moving on to the next steps. The primary cleaning came next. I disinfected the inside of the stem with both pipe cleaners and cotton swabs dipped in lemon-infused 99% isopropyl alcohol. I scrubbed thoroughly to make sure the interior was very clean. The goal of the next step is the removal (or minimization) of oxidation. Going to my sink, I used cream cleanser, cotton rounds, and a toothbrush, and scoured the stem to remove as much surface oxidation as possible. As the photos show, the result was a hideous, ochre-coloured mess – but better off the stem than on it.Once the stem was reasonably clean, I soaked it overnight in some Briarville Stem Oxidation Remover. This solution works to draw oxidation in the stem to the surface of the vulcanite. This is a major aid and an important step in ensuring a clean stem. The following day, I drew out the stem from its bath and scrubbed the lingering fluid with a toothbrush. Due to the severity of the oxidation, I then repeated the scrubbing with the cream cleanser for maximum effect.While the stem was soaking, I also cleaned the acrylic shank extension. I followed the same cleaning procedure as with the stem. It took a while, but I got it clean.As the stem was now clean and dry, I set about fixing the marks and dents in the vulcanite. This was done by filling those divots with black cyanoacrylate adhesive, impregnated with carbon and rubber. I left this to cure and moved on.The penultimate step for the stem is sanding. First, with my set of needle files, I reduced the bulk of the cyanoacrylate repairs. I removed the excess adhesive as near to the surface as possible, without cutting into the vulcanite. Following that, I used all nine of the micromesh sanding pads (1,500 through 12,000 grit) to sand out flaws, even out the vulcanite, and provide gentle polishing of the finished surface. I also applied pipe-stem oil while using the last five micromesh pads. There was a wonderful, deep black shine to the stem when I was done. I did the same with the shank extension. I moved on to the gourd. I cleaned the exterior of the gourd with some pH-neutral detergent and some distilled water, on a few cotton rounds. I cleaned inside of the gourd gently by scraping with my reaming knife, tube brushes, and some other tools. I was pleased with the results. I gave the gourd a thorough going-over with some beeswax polish and let that sit. I buffed it with a microfibre cloth and then, much later, I rubbed some LBE Before & After Restoration Balm into the gourd and let it sit for 30 minutes or so. I then buffed the gourd again with a microfibre cloth. On to the bowl. Meerschaum is too fragile for a proper reamer, so I used 220-grit sandpaper on the end of a wooden dowel to clean out the bowl and it turned out well. One of the frustrations of cleaning meerschaum is that once smoked, the stains never go away – and this pipe was heavily smoked. However, I did what I could and it definitely improved.Now with the stem, shank extension, gourd, and meerschaum cleaning done, it was time to put Humpty Dumpty back together again. Before repairing the separated chunks of the bowl, I needed to secure the two hemispheres together. This was not intended to be the critical attachment point, but just a solid method of marrying the two pieces. I used an adhesive for ceramics and clay – not because meerschaum is ceramic or clay (it isn’t) – but it does mimic certain characteristics of those insofar as it is very porous. This adhesive worked perfectly – it did exactly what I wanted it to. I was also able to attach the small shards of meerschaum that were left over (as seen in photos above).Now to go ‘all in’ on the repair of those missing chunks. I taped off the areas of the bowl that I didn’t want affected by the repair medium. This was a long and challenging repair and went through several failed attempts (which I won’t bore you with). Some failures included plaster of Paris, amalgams involving primarily calcium carbonate, and other ingredients (like leather dye). In the end, I came up with a good solution that maintains the integrity of the bowl shape, gives an incredibly resilient (and hard) repair, is resistant to high temperatures, and is completely inert when cured. After much trial and error, I settled on a particular type of epoxy mixed with a combination of the aforementioned calcium carbonate and briar dust. You might reasonably ask, ‘Why calcium carbonate?’ Good question. It is a material that best acts as a repair medium for meerschaum and I encourage you to read an important article I wrote about the issue here. You may also ask, ‘Why briar dust?’ Also a good question. This provided a slight brownish tint to the epoxy and CaCO3 mixture. Matching the surrounding colour was always going to be an impossibility, but I wanted to do the best I could.

I mixed my concoction and applied it liberally to the affected areas. During this process, the epoxy mix was much less viscous than I had hoped it to be. This was a big problem as it was oozing in ways that I didn’t want it to! However, like the trooper I am, I fiddled and fixed and floundered until I got it just right. It needed a full 24-hour cure and I was only too happy to leave the frustrating thing alone for a while!In the meantime, I glued the shank extension back into place in the gourd. Looks great.On the morrow – no surprise – the bowl was pretty darn ugly, but I can fix ugly. I donned a tight-fitting dust mask and went to work. My goal, of course, was to sand down excess epoxy and bring it to the level of the surrounding meerschaum, while simultaneously not reducing the bulk of the meerschaum. This took a lot of hard and careful work (plus a few touch ups), but we got there in the end. I am satisfied with the results, since the repair was never going to look invisible. The benefit of this pipe is that the repair is hidden from view, below the rim of the gourd. I then sanded down the entire piece of meerschaum with my Micromesh pads. I also rubbed two different beeswax polishes into the meerschaum. Then I let it sit for 20 minutes, buffed it with a microfiber cloth and then repeated the beeswax process. Worked like a charm! Before I went off to the buffer, I gave the meer and the gourd another going over with Clapham’s beeswax rub. This really worked well. I only took the stem to the buffer, as meerschaum and gourds don’t tolerate those high speeds very well!

This gourd calabash was a delightful can of worms right from the start and its beauty only increased through the restoration process. I am pleased to announce that this pipe is for sale! If you are interested in acquiring it for your collection, please have a look in the ‘Calabash’ pipe section of the store here on Steve’s website. You can also email me directly at kenneth@knightsofthepipe.com. The approximate dimensions of the pipe are as follows: length 6½ in. (165 mm); height 4½ in. (115 mm); bowl diameter 2⅛ in. (54 mm); chamber diameter ⅞ in. (21 mm). The weight of the pipe is 2⅜ oz. (68 g). I hope you enjoyed reading the story of this pipe’s restoration as much as I enjoyed restoring it. If you are interested in more of my work, please follow me here on Steve’s website or send me an email. Thank you very much for reading and, as always, I welcome and encourage your comments.